ML20207B094
| ML20207B094 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 07/15/1986 |
| From: | Stello V NRC OFFICE OF THE EXECUTIVE DIRECTOR FOR OPERATIONS (EDO) |
| To: | Asselstine, Roberts, Zech NRC COMMISSION (OCM) |
| References | |
| CLI-85-09, CLI-85-9, NUDOCS 8607170414 | |
| Download: ML20207B094 (2) | |
See also: IR 05000289/1985097
Text
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JUL 151986
MEMORANDUM FOR: Chairman Zech
Commissioner Roberts
Commissioner Asselstine
Commissioner Bernthal
FROM:
Victor Stello, Jr.
Executive Director for Operations
SUBJECT:
SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)
FOR TMI-1
The Commission in its Memorandum and Order CLI-85-09, which lifted the immedi-
ate effectiveness of the 1979 Shutdown Orders on TMI-1, directed the staff to
perform Performance Appraisal Team (PAT) inspections and Systematic Appraisal
of Licensee Performance (SALP) inspections at the end of six months of opera-
tion and again at the twelve-month mark.
The enclosed SALP report documents
the results of the six-month assessment covering the period from restart
'
through April 30, 1986. We have incorporated in this report the staff's prior
'
appraisal of the restart effort, referred to herein as an Interim SALP.
Although 1ot required by Commission directive, the Interim SALP allowed us to
focus solely on the transition from the shutdown mode through the planned GPUN
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restart program which ended January 10, 1986.
The six-month PAT inspection,
I
which was forwarded to you on May 23, 1986, was one of the primary inputs into
the enclosed SALP.
The next SALP will evaluate performance from May 1,1986 to October 31, 1986
and will include insights from the second PAT Inspection. The report will be
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provided to the Commission by January 15, 1987.
Origir.al signegg ,
ylctor Stellqp >*
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Victor Stello, Jr.
Executive Director for Operations
Enclosures:
As stated
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION
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REGION I
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KING OF PRUSSIA, PENNSYLVANIA 19406
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10 JUL 1986
Docket No. 50-289
GPU Nuclear Corporation
ATTN: Mr. H. D. Hukill
Director, TMI-1
P. O. Box 480
Middletown, PA 17057
Gentlemen:
Subject: Systematic Assessment of Licensee Performance (SALP); Report
No. 50-289/85-97
The NRC Region I SALP Board conducted a review on June 6,1986, and evaluated
the performance of activities associated with the Three Mile Island (Unit 1)
Nuclear Generating Station.
The results of this assessment are documented in
-
the enclosed SALP report, which covers the period September 16, 1985, to
April 30, 1986. The Interim SALP which covered the period from September 16,
1985 to January 10, 1986 is also enclosed for completeness. We will contact
you shortly to schedule a meeting to discuss the report.
At the meeting, you should be prepared to discuss our assessment and any plans
'
you may have to improve performance further. Any comments you may have regard-
ing our report may be discussed at the meeting. Additionally, you may provide
written comments within twenty days after the meeting.
)
Following our meeting and receipt of your response, the enclosed report, your
response, and summary of our findings and planned actions will be placed in the
NRC Public Document Room.
Your cooperation is appreciated.
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Sincerely,
Thomas E. Murley
Regional Administrator
Enclosure:
As stated
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10 JUL 1986
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cc w/encis:
R. J. Toole, Operations and Maintenance Director, TMI-1
C. W. Smyth, Manager, TMI-1 Licensing
R. J. McGoey, Manager, PWR Licensing
E. L. Blake, Jr.
TMI-1 OTSG Hearing Service List
Pubile Document Room (PDR)
Local Public Document Room (LPOR)
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Nuclear Safety Information Center (NSIC)
NRC Resident Inspector
Commonwealth of Pennsylvania
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U. S. NUCLEAR REGULATORY COMMISSION
REGION I
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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
INSPECTION REPORT 50-289/85-97
GENERAL PUBLIC UTILITIES NUCLEAR CORPORATION
THREE MILE ISLAND NUCLEAR GENERATING STATION
1
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ASSESSMENT PERIOD:
SEPTEMBER 16,1985 - APRIL 30,1986
BOARD MEETING DATE: June 6, 1986
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TABLE OF CONTENTS
Page
I.
INTRODUCTION
A.
Purpose and Overview. . . .
1
. . . . . . . . . . . .
B.
SALP Board Members. . . . . . . . . . . . . . . . . 2
C.
Background. . . . . . . . . . . . . . . . . . . . . 3
II.
CRITERIA . . . . . . . . . . . . . . . . . . . . . . . .
5
III.
SUMMARY OF RESULTS
A.
Facility Performance. . . . . . . . . . . . . . . .
7
B.
Overview. . .
7
. ..................
IV.
PERFORMANCE ANALYSIS
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A.
Plant Operations. . . . . .
9
. . . . . . . . . . . .
B.
Radiological Controls . . . . . . . . . . . . . .
12
C.
Maintenance . . . . . . . . . . .
15
. . . . . . . . .
D.
Surveillance. . . . . . . . . . . . . . . . . . .
18
E.
Startup Te s ti ng . . . . . . . . . . . . . . . . .
20
F.
Emergency Preparedness. . . . . . . . . . . . . .
21
G.
Security and Safeguards . . . . . . . . . . . . .
23
H.
Technical Support . ...............25
I.
Training and Qualification Effectiveness. . .
28
. . .
J.
Assurance of Quality. . .
31
. . . . . . . . . . . . .
K.
Licensing . . . . . . . . . . . . . . . . . . . .
33
V.
SUPPORTING DATA AND SUMMARIES
A.
Investigations and Allegations Review . . . . . .
35
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B.
Escalated Enforcement Actions . . . . . . . . . .
35
C.
Management Conferences. . . . . . . . . . . . . .
35
D.
Licensee Event Reports. . . . . . . . . . . . . .
35
E.
Reactor Trips / Forced Outages. . . . . . . . . . .
36
TABLES
Table 1 - Inspection Report Activities . . . . .
T1-1
. . . . . . . .
Table 2 - Inspection Hours Summary .
T2-1
. . . . . . . . . . . . . .
Table 3 - Enforcement Summary.
T3-1
.................
Table 4 - Enforcement Data . . . . . . . . . . . . . . . . . . .
T4-1
Table 5 - Licensee Event Reports . . . . . . . . . . . . . . . .
T5-1
Table 6 - Unplanned Reactor Trips and Forced Outages . . . . . .
T6-1
__ Table 1 - Licensing Actions. . . . . . . . . . . . . . . . . . .
T7-1
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Table 8 - Radiological EffTUent Releases . . . . . . . . . . . .
T8-1
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I.
INTRODUCTION
A.
Purpose and Overview
The Systematic Assessment of Licensee Performance (SALP) is an
integrated NRC staff effort to collect available observations and
data on a periodic basis to evaluate licensee performance. The SALP
process is supplemental to the normal insp6ction processes used to
ensure compliance with NRC rules and regulations.
It is intended to
be sufficiently diagnostic to provide a rational basis for allocating
NRC resources and to provide meaningful guidance to the licensee's
management in order to improve the quality and safety of plant
operations and modifications.
This report is the SALP Board's assessment of the licensee's perfor-
mance at TMI-1 Nuclear Generating Station for the period September
16, 1985, through April 30, 1986. The summary findings and conclu-
sions reflect a 7h-month period.
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This SALP is termed SALP I since it is the first of two SALPs
directed by the Commission in its restart order.
It includes the
period (September 16, 1985, to January 10,1986) covered by the
interim SALP (NRC Inspection Report No. 50-289/85-98), which is
attached for completeness. The purposes of the interim SALP were:
(1) to assist in the preparation for the Performance Appraisal Team
(PAT) I, (2) to verify performance during the transition from a
long-term shutdown condition to commercial power operation, and (3)
to determine the allocation of NRC resources for future inspections.
However, for those functional areas addressed in the interim SALP,
the details of the performance analysis from the interim SALP period
will not be repeated unless they also apply to licensee performance
during the period January 10, 1986 to April 30, 1986.
The previous SALP period covered the period from February 1984 to
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January 1985.
The licensee's performance from February 1985 to
,
September 15,1985, in 10 of the 11 functional areas were not con-
sidered since the plant was not operating during that period and,
therefore, the results would not be as meaningful.
In the licensing
functional area, performance from February 1, 1985 to September 15,
1985, was included in the period for the SALP I report. An NRC SALP
Board, comprised of the staff members listed in Section B, met on
June 6, 1986, to review the collection of performance observations
and data to assess the licensee's performance in accordance with the
guidance in NRC Manual Chapter 0516, " Systematic Assessment of
Licensee Performance." A summary of the guidance and evaluation
criteria is provided in Section II of this report.
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B.
SALP Board Members
Chairman
R. Starostecki, Director, Division of Reactor Projects, RI
Members
R. Bellamy, Chief, Radiation Protection Branch, Division of Radiation
Safety and Safeguards (DRSS), RI (Part Time)
R. Blough, Chief, Reactor Projects Section No. lA, Division of Reactor
Projects (DRP),RI
R. Conte, Senior Resident Inspector (TMI-1), DRP, RI
S. Ebneter, Director, Division of Reactor Safety (DRS), RI
W. Kane, Deputy Director, DRP, RI
H. Kister, Chief, Projects Branch No.1, DRP, RI
J. Stolz, Director, Project Directorate No. 6 (PD No. 6), NRR (Part Time)
J. Thoma, Operating Reactors Project Manager (TMI-1), PD No. 6, NRR
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Other Attendees
J. Callan, Chief, Performance Appraisal Section, Office of Inspection
and Enforcement
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J. Durr, Chief, Engineering Branch, DRS, RI
R. Weller, Section Leader, Project Directorate No. 6, NRR
F. Young, Resident Inspector (TMI-1), DRP, RI
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C.
Background
1.
Licensee Activities
Section I.C.1 of the interim SALP summarizes licensee activities for
the period of September 16, 1985, to January 10, 1986. Below is a
summary for the period of January 10, 1986, to April 30, 1986.
The licensee operated the facility at full power during this period,
except for approximately five weeks.
Throughout the period and
during the power operation periods, routine operations, surveillance,
and maintenance (including preventive maintenance) were conducted.
At the beginnir.g of the period, the licensee completed certain startup
tests for the 100 percent power plateau. These tests were scheduled
for completion during the startup test program in December, 1985, but
could not be completed at that time due to a power limitation of about
88%.
Between January 27 and February 3, 1986, the licensee placed the
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plant in cold shutdown in order to repair leaking pipe expansion
bellows on the eighth stage extraction steam lines inside the main
condenser.
From the return to power operation on February 3,1986 to March 21,
1986, the licensee operated TMI-1 at full power, except for the
reactor trip of March 15, 1986. This reactor trip resulted from a
turbine trip, which was caused by a low main turbine lubricating oil
pressure that occurred during the transfer of inservice coolers for
the main lube oil system.
Between March 21 and April 20, 1986, the reactor was shut down with
the reactor vessel drained down to support eddy current testing (ECT)
of a sample of the steam generator tubes.
Initial bubble and drip
tests showed no visible indication of leaking tubes. Based on
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subsequent ECT results, twenty-five tubes were plugged before
startup.
Two significant events occurred during the initial stage of tf+ ECT
outage. There was a noble gas release during reactor coolant system
(RCS) degasification on March 22, 1986, which resulted in the declara-
tion of an Unusual Event. Also, there was a buildup of radioactive
iodine in the Reactor Building on March 24, 1986, with the RCS vented
to the Reactor Building atmosphere.
2.
Inspection Activities
Section I.C.2 of the interim SALP summarizes NRC inspection activi-
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ties for the_ period September 16, 1985, to January 10, 1986. Below
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is a summary for the period of JanuaFy 10, 1986 to April 30, 1986.
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On March 31, 1986, Region I assigned two additional resident inspec-
tors to the facility, bringing the resident staff to one senior
resident inspector and three resident inspectors.
As directed by the Commission, a Performance Appraisal Team (PAT)
inspection was conducted to provide additional insights into licensee
performance. This inspection covered the following functional areas:
plant operations; maintenance; surveillance; technical support;
training; and assurance of quality.
In distinction to the previous SALP periods (prior to restart), this
SALP does not evaluate fire protection and housekeeping as a separate
functional area. These aspects of facility operation are covered in
several appropriate functional areas.
In the future, fire protection
will be evaluated as a separate functional area only when extensive
new information is generated on performance, such as when an Appendix
R team inspection has occurred.
In reference to Table 2, the total inspection hours for the 7h-month
7
period was 6,461 or approximately 10,338 hours0.00391 days <br />0.0939 hours <br />5.588624e-4 weeks <br />1.28609e-4 months <br /> on an annual basis.
Of that total, 61 percent occurred during the period covered by the
interim SALP and 12 percent occurred during the PAT inspection.
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II. CRITERIA
Licensee performance was assessed in selected functional areas significant
to nuclear safety and the environment. Assessment areas were selected
based on facility status of startup testing followed by normal operations.
Consequently, SALP I includes typical SALP functional areas for an operat-
ing plant.
For the interim SALP a special category of startup testing was
included.
One or more of the following evaluation criteria were used to assess each
functional area.
1.
Management involvement and control in assuring quality
2.
Approach to resolution of technical issues from a safety standpoint
3.
Responsiveness to NRC initiatives
4.
Enforcement history
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5.
Report and analysis of reportable events
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6.
Staffing (including management)
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7.
Training effectiveness and qualification
This report also discusses " Training and Qualification Effectiveness"
and " Assurance of Quality" as separate functional areas. Although these
topics, in themselves, are assessed in the other functional areas, through
their use as evaluation criteria, a synopsis of these two area is provided.
For example, quality assurance effectiveness has been assessed on a day-
to-day basis by resident inspectors and as an integral aspect of specialist
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inspections. Although quality work is the responsibility of every employee,
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one of the management tools to measure this effectiveness is reliance on
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quality assurance inspections and audits. Other major factors that in-
fluence quality, such as involvement of first-line supervision, safety
committees, and worker attitudes, are discussed in each area.
Based upon tha SALP Board assessment, each functional area evaluated is
classified into one of three categories. The definitions of these perfor-
mance categories are:
Category 1.
Reduced NRC attention may be appropriate.
Licensee manage-
ment attention and involvement are aggressive and oriented toward nuclear
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safety; licensee resources are ample and effectively used so that a high
level of performance with respect to operational safety or construction is
being achieved.
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Category 2.
NRC attention should be maintained at normal levels.
Licensee management attention and involvement are evident and are con-
cerned with nuclear safety; licensee resources are adequate and reasonably
effective so that satisfactory performance with respect to operational
safety or construction is being achieved.
Category 3.
Both NRC and licensee attention should be increased.
Licensee management attention or involvement is acceptable and considers
nuclear safety, but weaknesses are evident; licensee resources appear to
be strained or not effectively used so that minimally satisfactory perfor-
mance with respect to operational safety or construction is being
achieved.
Normally, the SALP Board assesses each functional area to compare the
licensee's performance during the last quarter of the assessment period to-
that during the entire period (normally one year) in order to determine
the recent trend for each functional area.
Because of the short period
covered by this SALP, the SALP board evaluated performance for discernible
trends in the last one-to-two months of the SALP period. The SALP trend
e
categories are as follows.
Improving:
Licensee performance has generally improved over the last
part of the SALP assessment period.
Consistent:
Licensee performance has remained essentially constant over
the last part of the SALP assessment period.
Declining:
Licensee performance has generally declined over the last
part of the SALP assessment period.
Notwithstanding the allowance permitted by a Category 1 rating to reduce
NRC attention, NRC oversight at TMI-1 will be maintained at a high level
because of (1) plant restart following a shutdown of over six years, and
(2) extraordinary sensitivity to TMI-1 among various government agencies
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and the public. Due to the nature and scope of activities at TMI-1, it is
NRC policy that close scrutiny be provided for the first two years of
operation from restart similar to that provided for a plant receiving its
initial full power license. Subsequent SALP evaluations (beyond SALP II)
are currently planned for a 12 month frequency.
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III. SUMMARY OF RESULTS
A.
Facility Performance
Interim
Recent
SALP I
Trend
Functional Area
(9/16/85-1/10/86) (9/16/85-4/30/86) (Last 1-2 Mos.)
1.
Plant Operations
2
2
Consistent
2.
Radiological Controls
1
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Declining
3.
Maintenance
2
2
Consistent
4.
Surveillance Testing
1
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Consistent
5.
Startup Testing
1
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Note 1
1
Consistent
7.
Security and Safeguards
Note 1
2
Consistent
8.
Technical Support
Note 1
3
Consistent
9.
Training and Qualifi-
1
1
Consistent
cation Effectiveness
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10.
Assurance of Quality
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2
Consistent
11.
Licensing
Note 1
1
Consistent
Note 1: This functional area was not assessed as a' specific area in the
.
interim SALP.
B.
Overview
Overall, the licensee continued to operate TMI-1 in a competent and
safe manner.
Clear and well defined programs are in place which
provide the necessary direction and guidance for assuring that the
various functions are integrated and controlled.
Licensed operator
performance continued at a high level.
Some problems were
identified with non-licensed staff training. Although control room
operators performed well, a number of events and violations were
attributable to personnel error.
In some cases this was aggravated
by procedural deficiencies. The concern in the interim SALP regarding
an apparent general disregard of workers for equipment protection in
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the operating spaces was not observed during this period indicating
that the licensee's corrective actions have been effective. Plant
equipment remained in good material condition evidencing a generally
strong ar.d aggressive preventive and corrective maintenance program.
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Six unplanned reactor trips and shutdowns occurred during this
period, five of which were attributed to secondary plant problems.
Unnecessary challenges to safety systems and operators continues to
be a concern. More attention to preventive maintenance and in some
instances secondary plant design could result in fewer failures of
susceptible balance of plant features that result in challenges to
the reactor protection system.
Although technical support for startup activities was good, increased
attention to the overall technical support area is warranted. As
previously mentioned, programs are strong but implementation is lack-
ing. A number of examples of improperly prepared / installed modifi-
cations reflected the lack of a thorough design review both at the
peer / supervisor level and at the regulatory-mandated technical review
level. This was further supported by problems observed by licensee-
initiated review groups subsequent to the normal review process.
A recurring theme in a few areas is the staff's observation that
_
some activities r'e performed in a hurried manner to meet schedules
and that this sometimes results in problems.
For example, some
unplanned exposures and radiological releases are attributed to the
higher pace of activities.
In this regard the SALP Board attributes
this partially to a conflict between upper management's expressed
goals for achieving a high level of performance and middle
management's emphasis on meeting schedules. We believe that this
conflict has not yet been effectively dealt with and is responsible
for many of the problems discussed in this SALP. Similarly, the
degree of supervisory oversight in the review of routine procedures
and their implementation was-found to be lacking.
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IV. PERFORMANCE ANALYSIS
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A.
Plant Operations (3528 hours0.0408 days <br />0.98 hours <br />0.00583 weeks <br />0.00134 months <br />, 54%)
The interim SALP period rated the licensee's performance as
Category 2.
The NRC found the licensee displayed excellent overall
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control of the plant; management established their presence and
involvement during all shifts; and, management exhibited conservatism
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in resolving technical issues in an adequate, but not aggressive,
manner.
Implementation of procedures for significant evolutions was
adequate.
For the most part, procedures were technically sound but,
individual procedure step inadequacies challenged personnel in
strictly adhering to those procedures for routine activities.
Licensed operator performance continued to be oriented toward
nuclear safety. Operators conducted themselves in a professional
,
manner.
Shift turnovers and pre-briefings for major evolutions were
thorough and detailed. Depth of knowledge of plant anomalies,
current plant conditions, and on going evolutions by operating crews
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was excellent. This is partially attributed to licensee training of
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operators.
In general, the licensed operators' positive attitude
toward operating the plant in a safe manner is one of the major
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factors in contributing to good performance of the plant.
1
Licensee personnel maintain the control room and conduct related to
business in a manner to avoid disruptive activities and to present a
posture of overall control of operations. Operations staff is
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segregated from other personnel by an entrance barrier made up by a
panel, bookcases, and an entranc.e gate.
Routine business and requests,
including pre-shift briefings, are conducted across that bookcase
section to avoid unnecessary personnel in the control room proper
area. No radios, televisions, and unrelated reading material are
permitted; and, for the most part notebooks, procedures, and manuals
are properly stored. A dress code continues to be implemented. Main .
control board overhead annunicators that are normally lighted are
relatively few and the licensee has administrative controls to track
alarms that periodically change status or come on and stay lighted
beyond one shift. With additional effort by licensee technical sup-
port personnel, a condition where no anunciators are routinely lit is
achievable. Overall, a professional atmosphere is maintained in the
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control room.
Despite upper management directives to adhere to procedures, a proce-
dure adherence problem persists and it is related to attention to
detail in complying with procedures. Moreover, it also appears to
be precipitated by middle management attempting to maintain schedules
of activities and their ineffectiveness in communicating the expressed
upper management intention in this area.
In several instances during
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the startup from the ECT outage, inattention to detail and'communi-
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cation problems along with.the fast pace of activities led to -
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improper procedure implementation.
Examples include:
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.
.
-
10
shift SR0 in control room for 1/4 hour with the plant above 200 F;
improper deboration valve alignment; and failure to properly respond
to a waste gas first alarm (alert) during a routine gas release.
In
other minor cases: completed procedures requiring steps to be signed
off or initialed as being completed were not done; out-of-specifica-
tien log readings continued for long periods of time; and some opera-
ting crews performed only minimum documentation of plant evolutions,
plant anomalies, or surveillance / maintenance activities in their logs
(representing minimal compliance with related administrative controls
on logs and record-keeping).
From a control viewpoint, the two management directives to meet
schedules and adhere to procedures can coexist. Overall, control of
special evolutions and testing has been quite good; but, in several
operational instances, as noted above, dealing with routine activi-
ties, licensee personnel (from management down to the worker) have
not properly implemented procedures. This demonstrates that the
conflict between the expressed procedure adherence policy and the
desire to meet established schedules has not yet been effectively
e
resolved.
Technical adequacy of station procedures was sufficient; however,
some weaknesses continued to be noted.
For example, a reactor trip
was partially attributed to weak procedures associated with the main
turbine lube oil system.
Lifting of a relief valve during a plant
degasification evolution demonstrated the need for a clearer proce-
dure. The QA monitoring of plant operations on all shifts aided the
licensee in identifying these plant operational problems.
An assessment of the licensee's safety and technical reviews organi-
zation found the system was operating in accordance with the mecha-
nism stated in the technical specifications.
Each department thus
achieves this requirement independently in diverse ways using differ-
ent procedures and initiatives. Because of this independence, many
-
overview / analysis reports on the procedure review process are diverse
and for the most part, they are not diagnostic with respect to the
nature of problems in the program. As a result cognizant vice pres-
idents are missing the opportunity to assess problem areas and take
appropriate corrective action. An exception to this is in the Nuclear
Assurance Department, where reports do lean toward evaluative summaries
for these reports.
The plant is generally kept clean and free of transient combustibles.
Daily involvement by management has been aggressive with respect to
fire prevention and housekeeping as evidenced by their frequent
tours, including a daily backshift tour. However, a poor practice
permitted fire service water to be routinely used as a source of
back-flushing water for other systems and equipment on a continuing
__
-
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_ _ _
~
_
_ basis ^which had the potential for degrading the fire service water
i
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.
-
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.
.
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. . . .
.
-
__ - ._
__
_ _ _ _ -
__-__-
.
.
-
11
.
,
system.
Further, with respect to fire protection training and prac-
tices, the licensee program meets the minimum requirements but, in
some instances, it lacks thoroughness-in implementation to assure
meaningful training.
The quality of training during fire drills was
noted to be limited due to the large number of participants which
resulted in a lack of realism in the training.
,
Licensee Event Reports (LERs) from TMI-1 are generally reported with-
in the required time period following the occurrence. Reporting is
accurate and appropriate corrective action generally is planned or
taken.
The four unplanned reactor trips from power operation, which occurred
in the 7-month report period, equates to a rate of approximately
seven trips per year. Several reactor trips were the result of turbine
or generator problems with the protection systems responding as expected.
Additional management attention is warranted in reducing secondary
plant upsets during startup and routine operations.
r
Overall, the licensee's programs are strong in the area of adminis-
trative controls and licensed operator performance.
For the most
part, procedures were technically adequate but individual procedure
step inadecuacies persist. The licensee continued to experience
difficulty in providing the proper balance between schedular consid-
erations and the expressed policy on procedure adherence. This was
particularly evident when middle managers inserted themselves directly
and accelerated the pace of work activities.
Licensee management
needs to review their routine conduct of operations to see if competing
factors are precluding the achievement of the goal to adhere to
procedures.
Conclusion
Category 2, Consistent
.
Recommendations
Licensee: See text and summary of Section IV.J, Management
Assurance of Quality.
~
-
-
~-
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,
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.
.
_
_
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12
B.
Radiological Controls (389 hours0.0045 days <br />0.108 hours <br />6.431878e-4 weeks <br />1.480145e-4 months <br />, 6%)
Analysis
During the interim SALP period, the licensee's performance in this
area was Category 1.
Program elements were noted to be sound and
thorough.
Minor problems were identified in the area of radiological
work planning where better planning could have prevented releases of
radioactivity and personnel contamination.
Problems of this type
continue and are discussed in this section.
The licensee's radiation protection organization contains sufficient
technical expertise and an appropriate level of staffing to adequate-
ly implement the program. Thorough and well-defineo radiation worker
and radiological controls technician training programs are in place
and are effectively implemented by the licensee. An additional
cyclic training program is provided for radiation protection techni-
cians and would appear to establish a method for communicating recent
procedural modifications to the technicians. However, lapses in
,
communication of recent procedural changes do occur.
Fcr example, a
change in licensee policy regarding dosimeter placement inside
anti-contamination clothing when face shields were worn was observed
to be neither clearly understood nor uniformly implemented in the
.
field.
I
Audits by QA of the radiation protection program were conducted as
required and appeared to be of adequate technical depth and scope.
Although the overall audit plan'in this area is formalized and
carried out in accordance with a schedule, no tracking system is in
place to ensure all individual program elements within this area are
periodically reviewed.
Wel'-defined procedures are established to control radiation protec-
tion program activities.
Radiation protection personnel appeared
.
familiar with and conversant on all procedural requirements.
The licensee typically demonstrates a strong commitment to ALARA and
planning for the radiological aspects of the March 1986 steam genera-
tor outage was initiated in a timely manner. Judicious scheduling of
technician training and qualification boards allowed the licensee to
effectively staff outage operations without reliance on a large
contractor HP technician work force.
The licensee's use of the radiation work permit (RWP) system to
control radiological work activities was generally very effective.
Pre-job surveys were always taken and were of appropriate scope for
evaluating radiological hazards. No violations of RWP requirements
,
_
were noted during this assessment. However, there was an instance
1
)
_
.
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9
1
l
,
_
__
_
.
.
-
13
when middle management became intimately involved in steam generator
ECT work setup and this resulted in their personal contamination.
Poor
communication and weak RWP extremity protection requirements were
contributing factors to these events.
Housekeeping and radiological posting in the work areas reflects a
management commitment to keeping workers well informed as to radio-
logical conditions.
Survey information is prominently displayed at
the HP control point and at the access to cells and cubicles. The
licensee has been responsive in implementing NRC guidance to limit
posting to the appropriate' area surrounding the radioactive source,
rather than simply posting large areas at the doorways. The licensee
has also implemented a system to serialize all posted " hot spots" to
allow tracking and re-surveying by the HP staff. However, inatten-
tion to detail on the part of personnel was the root cause of a
violation which was a failure to properly post a radiation area.
Overall, a programmatic problem does not appear to exist in this
area.
_
~
The recent steam generator eddy cur rent testing performed during
March and April represented the licensee's first post-critical outage
work in several years. During this outage, a failure to perform timely
surveys for airborne radioiodine during steam generator operations
led to a late identification of reactor building airborne radiciodine.
This resulted in the unplanned uptake of radioiodine by a substantial
number of workers. Communication problems between shifts and staff
preoccupation with a concurrent noble gas problem aggravated the delay
in the licensees identification of, and response to, the radioiodine.
Licensee corrective action, once the situation was identified, was
appropriate and mitigated further consequences. Additionally, licen-
see staff contained sufficient technical expertise for performing
followup whole body counting and dose assessment.
Licensee response towards both NRC and licensee-identified deficien- .
cies is timely and thorough. Additionally, the radiological controls
organization often takes the initiative in identifying engineering or
design deficiencies which may adversely affect radiological condi-
tions.
For example, the radiological staff initiated an investiga-
tion of sampling and floor drain flow paths in the auxiliary and fuel
handling buildings which were contributing to a noble gas airborne
problem in those buildings.
One inspection of licensee radioactive waste organization and trans-
portation activities was conducted during this assessment period.
Organizational structure and staffing of the Unit I radwaste group
appeared adequate to support the group's activities. Generally,
training for the radwaste group appeared to be timely and comprehen-
sive with one exception.
Specifically, a radwaste supervisor did not
_
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6
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'
1
14
receive the biennial retraining as required by licensee commitments.
A review of licensee audits of the radioactive waste management area
indicted that appropriate program elements were audited.
The licensee has a well-organized and smoothly-functioning effluent
monitoring and control program.
Licensee documentation of effluent
releases was found to be thorough and complete.
Effluent monitors
were calibrated at a frequency more conservative than the technical
specification r,equirement. An LER received during this assessment
period transmitted notification of the isolation of the condenser
offgas radiation monitor during power operation. This inadvertent
isolation was promptly discovered by the licensee and adequate
corrective actions have been taken.
The licensee's organizational structure, with direct reporting to the
Vice President, Radiological and Environmental Controls, provides for
added measures of independence. Quality assurance and audit activi-
ties were conducted as required and licensee response to identified
deficiencies was timely.
In general, procedures were technically
e
adequate.
However, implementation problems did occur. Although
certain pre-job planning efforts and job performance could have been
<
enhanced by better communications and less direct middle management
involvement, jobs involving significant radiological hazards were
conducted in a safe manner and they were oriented toward ALARA.
Conclusion
Category 1, Declining
Recommendations
None
.
l
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_.
_ _
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15
C.
Maintenance (426 hours0.00493 days <br />0.118 hours <br />7.043651e-4 weeks <br />1.62093e-4 months <br />, 7%)
Analysis
The interim SALP rated the licensee's performance as Category 2.
Overall performance of maintenance activities was good and reflected
a safety conscious mode of operation.
Problem areas existing during
this period were a general overall lack of awareness concerning the
fact that the plant was now in an operating mode which requires
greater sensitivity to adverse work in safety-related areas. Engi-
neering support / coordination was also a weak area, along with proper
job planning, incorporating operations and radiological control input
to assist safe accomplishment of maintenance activities.
Many positive elements of the maintenance program noted in the
interim SALP continued to be exhibited. The same level of knowledge,
staffing, scheduling, and completion of work items was maintained.
Management concern and participation continued to be evident. The
corrective maintenance trending report developed every three months
e
was used to identify problem areas on a system and component basis.
Several problems continued to be exhibited and were specifically
identified by the PAT inspection. One problem was adequacy of
procedures and practices related to the emergency feedwater system.
The procedure for repacking the EFW pumps was generic and not specif-
ic enough to resolve special problems with the particular character-
1stics of these pumps. This apparently contributed to a failure of a
pump packing gland during post-maintenance testing.
There was a lack
of preventive maintenance on check valves for the EFW instrument air
system. Another problem dealt with the adjustment of limit switches
and torque switches on motor-operated valves (MOVs). The specific
switch settings were not always defined or documented, and changes
were not always reviewed for impact on valve operation. An aggressive
effort was exerted during the ECT outage for the motor-operated valve -
testing program and it has resolved a majority of problems with switch
settings. The continuation of the program for all safety-related
valves, other than those identified in Bulletin 85-03, is desirable
and is planned for future outages. Overall, maintenance procedures
are adequate, but these examples point out a continuing need for
attention to detail in the procedure review process.
Maintenance conducted during the eddy current outage was an ambitious
effort to work on several existing problems, along with the major
effort of steam generator tube exan.ir.ition.
Effective control of
vendor activities was exhibited during the eddy current activities.
The testing was accomplished with " state of the art" equipment and
applicable requirements were followed.
The EFW flow nozzle thermal
,
sleev3_ cracking problem _and associated extensive activities that were
.
_
_
-
_
_ _
_
_
.
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.
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I
16
'
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I
not initially planned were completed in a safe manner, although formal
evaluation of the nozzle failure method is yet to be resolved.
For
'
these major evolutions, procedures were properly implemented.
The safety-related systems reviewed by NRC during this assessment
period continued to evidence the effects of good preventive and
corrective maintenance. Of particular interest was the replacement
of the "A" vital battery bank - a modification conducted by the
maintenance department in accordance with the licensee's modification
,'
control program.
The procedures used for this effort reflected
,
current industry standards for station storage batteries procurement
'
,
!
and installation. Testing confirmed that the battery replacement was
accomplished satisfactorily with no major maintenance problems
4
,
I
evidenced in the testing and checkout process (see Surveillance
j
section on the adequacy of periodic testing of battery banks).
However, several instances were noted in which minor plant modifica-
tions were conducted using the maintenance mechanism without proper
-l
review and approval in accordance with the modification control program.
In addition to PAT I findings in this area, the most notable incident
,
1
was the licensee discovery that the high voltage power supply for a
l
channel of nuclear source range instrumentation was not connected to
,
the detector during deboration to criticality; This was directly
related to a technician switching cable connectors in a containment
4
penetration in accordance with an outdated controlled drawing.
The
i
penetration configuration was changed based on previous maintenance
,
work which did not use the established modification control program.
j
Based on previous SALP findings, these improper minor modifications
are repetitive.
Enhanced management attention to this area is
,
!
warranted.
I
l
y
Maintenance personnel appear to have shown increased sensitivity
j
to existing plant conditions when planning and conducting maintenance
activities. No plant trips or major equipment damage have occurred
.
!
as a direct result of maintenance activities during this assessment
2
period. However, certain secondary plant transients / trips could be
J
related to maintenance practices. A number of instances continued to
indicate poor maintenance planning with respect to radiologically
3
3
controlled system work.
!
Engineering and technical support was evaluated as a problem area in
i
the interim SALP period. The licensee is working on corrective
!
actions, but problems continue to occur.
It was not apparent that a
formal evaluation on the EFW nozzle cracking would be conducted.
i
Also, NRC staff questioning apparently caused organizational review
-
I
of the leakage associated with Decay Heat System check valves. On
the~other hand, for significant or visible issues, such as the diesel
blower problem and the steam generator tube.pluggi.ng,; effective actions
were planned and implemented by the licensee.
-
.
1
-
3
.
._
_
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&
.
. _ , - .
. , -
- , - - _ - - -
- -
.
. , - _ - - - - -
. . - - - -
_.
.
.
17
Housekeeping activities continued to be a strong point in maintenance
activities. No problems were identified in routine activities or
during the extensive eddy current outage activities. No fire hazards
were observed during these intensive work activities.
Overall, the maintenance program is properly established, imple-
.
mented, and staffed. However, several instances reflect weak
implementation despite management involvement.
Personnel attitudes
relevant to respect for plant equipment appear to be improving. The
t
ability to control extensive maintenance activities in short outage
situations and react to changing problem areas was evidenced in this
period.
Procedure adequacy and technical support problems cortinue
to be noted.
Conclusion
Category 2, Consistent
,
_
Recommendations
Licensee:
See text and summary of Section IV.J, Management
Assurance of Quality.
,
.
. --
g
e
6
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.
s
_
18
D.
Surveillance Testing (339 hours0.00392 days <br />0.0942 hours <br />5.605159e-4 weeks <br />1.289895e-4 months <br />, 5%)
Analysis
The interim SALP rated the licensee's performance as Category 1.
This was due to a strong surveillance ~ program with quality assurance
(QA) involvement, ample staffing, well-kept records, and proper
procedure adherence. Minor problems that surfaced were few and did
not adversely affect plant safety.
The licensee continued to properly implement their surveillance
program throughout the assessment period.
The computerized
scheduling system continues to be used effectively to ensure that
surveillance tests are accomplished in a timely manner with minimal
effort on plant operations.
Surveillance procedures were followed,
personnel were knowledgeable, and problems were documented. However,
a missed surveillance on a fire door in the diesel generator building
resulted from a poorly coordinated review / approval of several sur-
veillance procedure revisions.
,
With respect to proper problem identification and documentation, poor
understanding by personnel of the proper use of exception and defic-
iency (E&D) forms persisted. The interim SALP identified poor hand-
ling of the Power Operated Relief Valve (PORV) E&D's. During this
period, weekly and monthly surveillance for the new "A"
battery bank
were incomplete because personnel thought all fluid levels had to be
at a specific mark (high level indicator) for corrected specific
gravity. With the incomplete data, personnel classified the problem
only as an " exception." This precluded operations department review
of the anomaly. Technical support personnel were slow to respond to
correct "the deficiency." Subsequently, the results of a review by
the licensee indicated that level correction was not needed and the
battery bank was operable. However, the problem reiterated another
example of weak technical support and the need for plant-wide training.
in the use of the new E&D system.
In general, technically-adequate surveillance procedures were noted
during NRC review of the RB spray system, containment local leak rate
tests, station batteries tests, and emergency feedwater system tests.
However, certain weaknesses were noted. The PAT I identified that
emergency feedwater pump discharge check valves were not being tested
for proper seating and ability to prevent back flow because the test
lineup isolated the idle pump check valves from pressure when the
,
other pumps were being tested,
l
During this appraisal period the "A" battery bank was replaced.
Although periodic surveillance testing requires a capacity test in
accordance with Technical Specific _ations, the licensee did not
~
-
~
propose to conduct future periodic duty. jesting after conducting one
such test.
-
.
-
.
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_
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-
-
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-
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.
19
.
Latest industry standards suggest such testing and in light of the
apparently early end of life for the previously installed battery
bank, such a practice seems appropriate. The licensee is not
specifically required to follow this edition of the standard but
this incident reflects either (1) a lack of awareness / understanding
of current industry standards or (2) a lack of initiative to adopt
industry practices beyond those imposed by NRC. Although an
isolated event, it does adversely reflect on the licensee's
commitment to excellence.
Overall, the surveillance program is adequate and is aggressively
implemented. Additional training is needed in the proper processing
of test problems. The above-noted procedural weaknesses warrant
further licensee management attention with respect to overall
adequacy of the licensee's review process.
Conclusion
Category 1, Consistent
,
Recommendation
Licensee:
See text and summary of Section IV.J, Management
Assurance of Quality.
.
1
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-
.
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-
,
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-
.
20
E.
Startup Testing (561 hours0.00649 days <br />0.156 hours <br />9.275794e-4 weeks <br />2.134605e-4 months <br />, 9*4)
This area was evaluated in the interim SALP (see attached) and the
startup testing program was completed on January 10, 1986.
,
Conclusion
Category 1
Recommendations
Licensee - none
NRC - Assure that existing periodic surveillance tests are
sufficient in the long term to measure battery reliability.
'
-
,
.
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.
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.
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-
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,
-
.
. - - .
. .
. - .
.
.
21
<
F.
Emergency Precaredness (242 hours0.0028 days <br />0.0672 hours <br />4.001323e-4 weeks <br />9.2081e-5 months <br />, 4%)
This area was not addressed in the interim SALP.
During the prior
assessment period (February 1,1984 - January 31, 1985), no signifi-
cant weaknesses were identified and this area was rated Category 1.
During this assessment period, a full-secle emergency exercise, which
included NRC participation, was held on November 20, 1985. The licen-
see's execution and participation in the exercise demonstrated thorough
planning and a strong commitment to emergency preparedness.
Examples
of thoroughly planned activities observed by NRC team members included
timely staff briefings in each emergency response facility, adequate
interface with NRC Incident Response Team members, and demonstration
by emergency personnel of familiarity with emergency duties and use
of Emergency Plan Implementing Procedures (EPIPs).
The licensee's
performance demonstrated that it could implemen,t the emergency pisi
and EPIPs in a manner that would adequately provide protective measures
for the health and safety of the public. Minor weaknesses noted
included a large number of personnel in the control room, information
e
flow, and development of protective action recommendations.
Positive
corrective action by management from the previous drill was noted
where a weakness was identified.
For example, significant items
observed in the 1984 exercise did not recur.
Licensee management is
taking the initiative in this area to further improve their emergency
response capabilities.
Radiological control personnel in the control room perform dose
assessment and in plant health physics functions. This results in a
larger number of people with an attendant increase in background noise
level.
Consequently dose assessment information in the EOF is obtained
from a communicator and this arrangement is not as effective in
supporting the emergency support director in the EOF once it has been
activated.
Similarly, in plant health physics functions need to be
communicated to the Operational Support Center where workers are
-
dispatched to deal with problems in the plant. Although no specific
deficiencies can be directly associated with this arrangement,
experience at other sites shows performance can be enhanced with
alternative options.
The licensee took the initiative by consolidating the three unit
emergency plans (TMI-1, TMI-2, and Oyster Creek) into one corporata
plan. This consolidation is to help standardize approaches at all
three plants. Another noteworthy initiative was the licensee permit-
ting the local area fire fighters to use their " burn building" for
training.
This and other licensee support of these local companies
has made a positive contribution to local fire fighter preparedness
to support an emergency at TMI.
--
- - --
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22
In summary, the licensee performs well in the emergency prepared-
'
ness area and continues to successfully demonstrate this
during drills and annual exercises.
Conclusion
Category 1, Consistent
Recommendations
Licensee:
Assess the effectiveness of dose assessment and in plant
health physics functions in emergencies dealing with longer term
scenarios where the EOF and OSC are fully operational.
1
1
9
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e
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,
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,
. . .
. -
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-
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.
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.-
.
.
-.
-
- - _ . - .
_-
.
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23
I
l
G.
Security and Safeguards (79 hours9.143519e-4 days <br />0.0219 hours <br />1.306217e-4 weeks <br />3.00595e-5 months <br />,1%)
i
Analysis
l
This area was not assessed separately in the interim SALP. The
previous SALP period (February 1,1984 - January 31,1985) rated the
I
licensee performance as Category 1.
No major security program issues
I
were identified.
'
i
i
During this assessment period, one unannounced physical protection
inspection was performed by a region-based security inspector.
Routine resident inspections continued throughout the assessment
period.
Corporate management's interest in the program was exhibited by the
,
continued involvement of the Director of Security in the day-to-day
security activities on site. That involvement appears to have
further opened communication chann,els between site and corporate
management and has resulted in increased appreciation by corporate
e
management of program needs. Monthly meetings held on site between
corporate and site security management continue to enhance the
program by demonstrating strong corporate support for the program and
by allowing potential problems to be surfaced and resolved before
they can have an adverse impact.
Onsite security management is competent and knowledgeable of the
-
requirements and objectives of nuclear plant security. They are also
effective in directing the program.
I
Staffing of the program is adequate and management remains attentive
i
to human factors. This is evidenced by the continued high morale and
!
professionalism of members of the security force and the stability in
i
the force.
Further, the training and qualification /requalification
]
program continues to be managed by a competent staff whose sole
'
i
responsibility is training.
Few personnel errors were attributable
i
to the security force during the assessment period. However,
security personnel apparently were not aggressive in enforcing badge
controls (as discussed later in this section) -- training on
i
program / policy changes needs strengthening. Training facilities are
well maintained and indicative of the importance management places on
security force training.
"
The licensee's security audit program, which consists'of an annual
corporate audit and quarterly audits by site personnel, is well
,
planned a..)ci comprehensive. Audit reports are disseminated to appro-
priate levels of management and are generally promptly responded to
'
with effective actiorts. A recent licensee initiative, involving
semi-annual self-inspections conducted in conjunction with security
-
-
personnel from the licensee's Oyster Creek facility to review and -
~
,
compare program implementation, is further evidence of a positive -
-
-
-
management attitude toward the-security program.
It also provides
.
1
y
- ~
-_. _ - - . , .
__
_..,_
-.- .
.
.
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24
for an exchange of experiences and problem solving between the
facilities.
This program appears to be effective in providing
yet another perspective concerning program implementation.
While correction of problems identified by NRC staff was generally
adequate, some problems were noted during this period. Safeguards
licensing issues, e.g., perimeter intrusion detection system (PIDS),
remained outstanding for about two years despite on going dialogue
with NRC staff. The staff's frustration in resolving these issues
resulted in a letter to the licensee in March 1986, identifying those
issues which were still outstanding. Management attention is required
to resolve these long-standing issues.
Further, a security badge
control violation resulted because of ineffective licensee corrective
action subsequent to an NRC staff concern regarding personnel not
effectively controlling their badges and key cards.
Initially,
security implementing procedures were weak in this area. After the
procedures were strengthened, personnel failed to properly implement
these procedures and licensee management was lax in enforcing them.
When brought to their attention, licensee management exhibited a lack
e
of understanding of the issue and refuted the violation by expressing
apparent futility in how to avoid future violations.
Based on sub-
sequent discussions with licensee representatives and on actual
observations in the plant, it now appears that effective corrective
actions have been taken.
In summary, the licensee has a well-established program and, in
general, it is properly implemented.
Positive measures should be
taken to resolve the PIDS deficiencies.
Conclusion
Category 2, Consistent
Recommendations
-
None
>
~
~~
~~
-
- , _
_
_
.
,
pm
9
-
-
._
-
-
'
_ _
. .
._.
_.
-
.
-
-- -.
. _ - -
- _ . _ _
-
___ .__
.
.
-
1
25
H.
Technical Support (127 hours0.00147 days <br />0.0353 hours <br />2.099868e-4 weeks <br />4.83235e-5 months <br />, 2% - not including PAT inspection)
i
Analysis
'
l
The interim SALP did not specifically evaluate this functional area
4
"
because of the operational / test emphasis for that period. However,
'
comments were made in each of the functional areas with a conclusion
~;
in the overview section. Technical support was considered adequate
but not aggressive. Specifically, licensee engineering personnel and
,
management demonstrated an apparent lack of inquisitiveness for a
4
complete understanding of technical problems.
In their response to
that SALP, licensee management claimed that this was due to the heavy
4
burden on their engineering staff from questions by oversight groups,
including NRC staff, but they committed to enhance their attention to
this area.
,
!
j
For the remainder of the SALP period, some improvements were noted
i
but problems continued to be exhibited in other areas (see mainte-
_
nance and surveillance sections).
However, as found by PAT I, there
~
does appear to be a problem, despite a well-established program, with
the thoroughness and completeness of design reviews for engineering
plant modifications. This leads NRC staff to believe that the
3
'
symptoms manifested during restart by licensee engineering personnel
j
and management were indicative of a more fundamental problem as
addressed later in this section.
The licensee's modification control program is well established.
The
Technical Functions procedures are quite detailed; and they are
organized well enough to give personnel a good understanding of what
the system is and what their responsibilities are. This system
brought on a marked improvement in the quality of the licensee's
4
safety evaluations. The program is in place to assure that
safety grade design criteria are applied to plant modifications.
'
However, for various reasons, full implementation of the program
-
has not been achieved.
,
The PAT I identified a number of examples where modifications or
,
temporary modifications were improperly prepared and/or installed.
They included:
lack of 10 CFR 50.59 evaluation for temporary shield-
ing installation; lack of thorough and complete review to assure EFW
2-hour backup air supply bottles met single failure criteria; lack of
thorough and complete review to assure cycle 6 remote shutdown panel
and safety grade signal conditioning cabinet met electrical isolation
l
criteria; weak documentation of design input and lack of documenta-
tion to su'pport design assumptions and calculations; lack of complete
design verification; and, inconsistent and uutdated drawings avail-
able for design and operational use.
Some of these issues are
i
exampleslof failure to properly implement the licensee modification r
_ _ _
control program procedures. These findings demonstrated that
._
_
_~
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v.
..-q.-.
,
-,- .-
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, . _ . .
.,...,m
- , _ . ,
, . _
_ - - _ _ _
, , . ~ .
. - - . - ,
.
.
. .
_
26
l
licensee personnel, including first-line supervisors, and the
independent technical and safety review process were not sufficiently
thorough and comprehensive in performing their activities and lacked
the attention to detail in properly following procedures.
The environmental qualification area is another example of poor
engineering project implementation.
The PAT I identified that the
licensee did not complete a review, specific for TMI-1, for use of a
certain cable type in safety related applications.
Further, NRC
staff questioning identified another cable type (different vendor)
that was not included in the TMI-1 plant-specific file. Substantia-
tion of terminal block qualification was weak in that comparative
samples were not available for traceability markings and similarity
of kind markings. The results of a walkdown inspection by the
licensee further disclosed that the Reactor Building fan motor power
cable qualification could not be substantiated. This resulted in a
delay to the startup from the ECT outage because of last minute work
to replace the connectors. Once the connectors were replaced, QA
identified a need for rework in that splicing material conditions
e
were not within the bounds of the qualified splice. Errors were
made in the establishment of the TMI-1 EQ file due, in part, to a
lack of a thorough and comprehensive independent review. The under-
lying causes of these problems appear to have been a lack of under-
standing of the equipment qualification process and the need for
technically comprehensive reviews.
These problems also affect performance in the licensing area in that
they lead to errors in information presented to NRC staff in licensing
correspondence. Examples include:
non-EQ equipment for emergency
feedwater system (EFW); single failure susceptibility of the EFW
instrument air system; and lack of electrical isolation between a
safety grade signal conditioning cabinets and control room panels.
On the other hand, for startup activities there was good technical
.
support to the site. Several initiatives were exhibited as noted in
the performance of generically applicable special natural circulation
testing. Site staffing from the corporate engineering division has
increased and is taking on more responsibility for processing minor
modifications.
---
__
_ _ __
_
@
m m
m
.N
e
e
op
6
y..y
-
.-,-:+,
,,
.
.
-
-
27
During the recent outage work, licensee management involvement was
adequate in maintaining positive control of all work being performed.
This was exhibited in the unplanned outage for main condenser work
in February 1986.
Further, to alleviate the administrative burden
on the licensed operating crew during the ECT outage, the licensee
assigned an offshift qualified senior reactor operator (SRO) to
coordinate the work associated with different jobs.
Prior to the
outage, equipment to support major tasks w'as prepositioned to aid in
the work starting smoothly.
Pre-briefing and discussions between
major departments were performed to assist in keeping all responsible
departments abreast of the work. However, as the pace of activity
increased, such as the transition from operations to outage work, or
during plant startup, these communication links between departments
weakened. This contributed to the RB iodine buildup event and 0TSG
worker contamination event during initial set up of OTSG ECT condi-
tions.
Overall, the licensee adequately controls modification work in the
plant. Major startup activities were well supported at the site and
e
corporate level. The modification control program is well defined,
but implementation needs improvement.
Corrective actions for these
problems have been weak and a significant increase in management
attention to this area is warranted.
Conclusion
Category 3, Consistent
Recommendations
Licensee:
In light of recurring problems in the environmental qualification
(EQ) area, assess the adequacy of or the need for better accountabiliti
on specific engineering projects, such as EQ.
Conduct a critical evaluation of tne design review process with
emphasis on the role of peer review adequacy and first line
supervisory oversight.
NRC:
Conduct team inspections of the off-site engineering efforts with
particular emphasis on preparations / modifications planned for the
forthcoming refueling outage.
-
--
-
c
-
--
- . -
,
.
,
-
-
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=
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.
-
-
.-
. _ . - . . _ . .
.
. .
--
-.
-.
-
i
-
.
>
,
J
28
I.
Trainino and Qualification Effectiveness
.
Analysis
During this assessment period, training and qualification effective-
ness has been considered as a separate functional area. However, the
various aspects have been considered and discussed as an integral-
'
part of other functional areas and the respective inspection hours
i
have been included in each one. Consequently, this discussion is a
,
synopsis of the assessments related to training conducted in other
l
areas. Training effectiveness has been measured primarily by the
!
observed performance of licensee. personnel and, to a lesser degree,
as a review of program adequacy. The discussion below addresses
'
three principal areas:
licensed operator training, non-licensed
staff training, and status of INPO training accreditation.
i
i
The interim SALP noted licensee performance as a Category 1 and noted
j
a strong licensee commitment to licensed operator and certain non-
i
-
licensed operator training areas that resulted in an effective train-
!
ing program for startup. These program areas were oriented toward
j
improving on-the-job performance.
In general, personnel were know-
i
ledgeable of plant design features and status and they conducted
1
activities with care during special testing and major evolutions.
There was a problem of workers in various plant areas having the
.
potential to cause a safety-system challenge in that the workers were
i
not sufficiently careful when working around plant equipment.
Inex-
i
perience was noted, especially among non-licensed personnel, but it
t
was compensated for by enhanced supervisory attention.
l
During the remainder of the SALP I period, personnel enhanced their
'
experience level during continuous power operations and during tran-
j
sition periods at the beginning and end of outage.
Reportable events
!
attributed to personnel errors remained relatively few; and, for
j
those that did occur, no significant safety concerns were raised.
-
'
No additional examples were noted of workers not having respect for
equipment in safety-related areas which could cause a challenge to a
j
safety system (i.e., the " worker in the spaces" issue)'
This indi-
.
cated that the licensee's corrective actions of personnel counselling
(plant wide) were apparently effective in enhancing performance.
There were two plant trips partly related to personnel error, however
i
they were due to the way secondary plant equipment was operated and
unrelated to the " worker in the spaces" issue.
i
The PAT I inspection confirmed the positive elements of the
l
licensee's training program noted in the interim SALP. The team
4
found a high level of management commitment and involvement in
licensed operator and certain nonlicensed operator training programs
l
at TMI-1.
For example, senior plant management regularly
!
-
participated in Babcock and Wilcox simulator training in order to
monitor and evaluate shift, performance in non-routine evolutions and
.
-
.
.
!
!
_ _ _ - - . , .
_ . _ , -
. . . . . _ . . . . , ,
_ _ . ~ _ _ _ . , _
. . - - _ _ . , , _
_ , .
-
. . . , _ _
. , _ , , - . . . _ , . _ . , _ . _ , _ _
-
.
_ _ - .
w
.
-
29
emergency situations.
Training in this area was given the highest
priority by plant and corporate managers and supervisors. Generally,
policies and procedures were clearly written, broadly disseminated
and well understood by all.
Maintenance training was considered especially strong, well con-
ceived, and well implemented. Maintenance personnel typically
attended one week of classroom training during each six-w;ek rotation
cycle. The training covers industry experience, administrative
procedures, and craft-specific areas.
Some problems with regard to procedure implementation for routine
activities continued to persist.
This was originally attributed to'
individual procedure step inadequacies. However, the PAT I and other
inspection findings identified a number of examples of licensee
'
personnel not properly implementing procedures, most notably in the
modification control area, both at the corporate and site levels.
'
The PAT also found that some design packages did not meet safety-
_
grade criteria and that some corporate engineering personnel were not
knowledgeable in records retrieval system use.
The effectiveness of
]
training in this area warrants further review by the licensee.
Fire brigade training meets minimum requirements; but lacks realism
due to the large number of brigade members.
In. contrast to the
licensed /nonlicensed training area, licensee management's attitude
appears to be more oriented toward minimum regulatory requirements
than toward committing to excellence.
However, licensee initiatives
outside of regulatory commitments; e.g. , burn building training, help
to compensate for thi's shortcoming.
t
The licensee has received training program accreditation from INP0 in
the following five areas: control room operators; senior reactor
operators; shift technical advisors; auxiliary operators; and radio-
logical control technicians.
-
All five SRO and five RO candidates for operator licenses passed
the NRC license examinations. No licensed operator training program-
matic weaknesses were identified.
Some practical weaknesses were
uncovered however, such as, the candidate familiarity with the use of
the plant computers and various data plots.
In summary, the licensed operator training program for startup and
subsequent operation was effective and performance oriented.
Experi-
ence is being gained with continued full power operations and person-
nel errors remain-relatively few. The licensee was responsive to
certain training needs; such as, for the " workers in the spaces"
,
issue. The licensee demonstrates a poor attitude with respect to
_
fire brigade training. Site and corporate engineering training may
-
__ need enhancement.
Lic~ensee management should direct its attention to
-
-
training effectiveness ~on the procedure adherence 1::"c.
-
.__
__
_
.
e
_ _~
-
.
.--
_, _-
.
.
.
30
Conclusion
Category 1, Consistent
Recommendations
None
r
.
_
,
d*
ew
"
W
O
9
. ~=- .
-
--.-
-
-
_
- -_-
.
. - .
- --
.--
'
.
-
.
i
31
i
i
i
J.
Assurance of Quality
Management involvement and control in assuring quality is being con-
sidered as a separate functional area for this assessment period.
4
However, the various aspects of the programs to assure quality have
been considered and discussed as an integral part of each functional
area and the respective inspection hours are included in each one.
'
Consequently, this discussion is a synopsi's of the assessments
relating to the quality of work conducted in other areas. It should
be emphasized that this function area evaluates management assurance
of quality; and, as such, is much broader than merely an assessment of
QA/QC department performance.
,
!
The interim SALP rated licensee performance as a Category 1.
It
I
noted an aggressive management and quality assurance department
i
(QAD) presence and involvement in site activities.
However, manage-
"
ment attention to the QAD sffectiveness reviews was questioned in
light of the procedure adequacy and implementation problems that
persisted,
{
r
i
The procedure implementation problem appears now to involve more than
4
j
individual procedure step inadequacies challenging people toward
,
proper implementation. Considering the interim SALP results, recent
j
inspection findings, and PAT I findings in the modification control
1
area, this problem is symptomatic of an apparent corporate and site
1
level problem in fully adhering to procedures for routine activities.
I
It appears that personnel rely on memory or rush to meet schedules to
j
complete action items without referral to the appropriate licensee
i
procedures.
Indirectly middle management appears to be adversely
j
affecting performance on properly implementing procedures by their
.
aggressive attitude toward schedule adherence.
In this regard,
!
indications are that management has not followed through.to assure
that their procedure adherence goals are being achieved.
\\
~
l
Overall general plant operation procedures and safety system opera-
tional procedures are adequate. However, many other important to
i
safety procedures have individual step inadequacies, a persistent
j
problem identified throughout the SALP I period. These instances of
procedure inadequacy are too numerous to be considered an isolated
problem and they indicate a lack of attention to detail on the part
,
1
of individual reviewers along with poor supervisory oversight of the
!
procedure review process. Compounding this problem is the lack of
}
diagnosis in the analysis reports on the review process which are
submitted to the cognizant vice presidents.
Licensee initiatives are
i
needed to improve required review process.
!
The quality assurance (QA) department is well staffed and is focused
on enhancing operational experience. The QA program employs many
j
~~
- - - initiatives to uncover problems in programs or program implementation.
j
]
Other oversight groups employ substantially experienced personnel who
+-
.-
-
.
-
I
- _
-.
.
}
1
' . , _ , _ ,
-___ _ . - .
, - - , . _ - - - _ , _ _ _ _ . _ . _ , - ~ _ _ . , _ _ . .
_ , _ _ - , _ . _ _ . .- _ . - - - - -
i
. - _ _ _ _ - _
.
-
,
.
32
appear to be effective in their problem identification reviews. How-
ever, for problems not directly affecting plant operations, licensee
management is not effectively using these assets.
For example, pro-
cedure adherence and drawing control problems are long-standing
issues at TMI.
Licensee corrective actions were ineffective in this
area.
Furthermore, QAD apparently has been unable to assure appro-
priate corrective action.
In addition to examples noted above, EQ
problems and the lack of a component level quality classification
list were issues that QAD did not escalate within the licensee
organization in a timely and effective matter to assure licensee
management took appropriate corrective action before they became
issues with NRC staff.
Also in some instances, personnel and management lacked initiative
toward effective corrective action without oversight pressure.
Examples include slow action to resolve instrument anomaly problems.
In regard to a violation for failure to establish procedures the
licensee exhibited poor understanding of related management assurance
"
requirements.
In summary, strong quality assurance and oversight review pro-
grams employing unique techniques are in place. Nonetheless, line
organizational management needs to more effectively use these assets.
Improved personnel and management attitude toward proper procedure
implementation is warranted.
Conclusion
Category 2, Consistent
Recommendations
Licensee:
,
Establish and enforce a policy that can be understood by mid-level
managers and workers to ensure procedural adherence and resolve the
perception that schedules are of a higher priority.
Reassess the process used for assuring individual procedures are
technically adequate and complete.
In particular, assess the
relative roles of peer review and management oversight in procedure
reviews and changes.
Assess the need for better indoctrination and/or training for
individuals associated with engineering design work and design
change control.
-
-
-
- --
..
_ _ _
_
--
,
_
.-
.
4
6
eW
"=
m
-
w
.
.
33
K.
Licensing
Analysis
This area was not addressed in the interim SALP.
In the previous
SALP evaluation for this area (February 1,1984, to January 31,
1985), the licensee received a Category 2 rating.
In that SALP
report, we noted that management involvement was above average for
significant matters which could affect plant restart. But there were
other areas where management involvement and control appeared to be
lacking, particularly in areas of less significance to restart.
The licensee has been very aggressive in meeting with NRR on a
monthly basis to discuss all active licensing issues.
Priorities of
review are discussed. As expected, the higher priority reviews are
proceeding in an efficient manner.
But another result of these
meetings is that the lower priority reviews are proceeding more
smoothly than before and are being completed. Another aspect of
these meetings is that future licensee submittals are discussed along
r
with their priority.
There was one notable breakdown in communication.
Specifically, a
10 CFR 50 Appendix H time extension request on analyzing reactor
vessel surveillance capsules was not submitted in a timely fashion.
Although the specific issue involved had a low safety significance
from a regulatory viewpoint, the request should have been submitted
earlier.
Since this is the only notable exception found to date,
this incident was "ot considered to be representative of the
licensee's performa nce.
The licensee's understanding of the technical issues has generally
been good and the proposed resolutions have been generally con-
servative and sound. There are occasional differences between the
NRC and licensee on how to proceed on a technical issue, but, in
-
general, when these differences occur, the licensee has a reasonable
technical basis for their decision. However, in view of the finc'ings
under the Technical Support / Outage Management section of this SALP,
questions are raised on the underlying basis of licensee submittals.
Resolving the concerns in the Technical Support section will resolve
these questions.
In the last SALP appraisal on licensing activities (prior to
1
'
restart), the licensee was requested to improve their No Significant
Hazards Determination (NSHD) submitted with each technical specifica-
tion change request (TSCR). The licensee has shown considerable
improvement in this area. The best examples are contained in TSCR
148 and TSCR 153, involving extensive reviews of steam generator
repair criteria. Even on less extensive TSCRs, the licensee is
-
providing a more meaningful technical analysis for the NSHD.
_
_
.
,
_
_
. . _--
-
, - -
-
.
'
,
l
1
34
The licensee has an effective system for tracking and respondir.g to
NRC requests.
It is evident in the monthly meetings between NRR and
the licensee that management attention is focused on meeting sched-
ules.
Rescheduling of lower priority work is done in a conscious,
controlled manner.
Licensee staff was sufficient to support startup
and operation and to adequately support completion of a number of
older licensing actions.
Additionally, the licensee has been very responsive to requests for
information on a short notice for such items as congressional inquiry
and internal NRC surveys of plant status.
,
In summary, the licensee's performance has improved in the licensing
area.' Older licensing issues are being resolved and the licensee is
trying to minimize the backlog of licensing actions. The licensee's
significant hazards determination evaluations have improved. This
functional area will require continuous diligence on the licensee's
part to maintain the observed level of improvement,
e
Conclusion
Category 1, Consistent
Recommendations
None
.
"
~m
,,
em
,
-
-
mp
g
e
m e.*
- =
+
@
.-
-
_
_
- - . - -
- , - _ _ - - _ - -_
.
.
.
.
35
a
V.
SUPPORTING DATA AND SUMMARIES
A.
Investigations and Allegations Review
l
There are no open investigations for TMI-1. The investigation on the
environmental equipment qualification apparent material false state-
ment was completed during this period and it is being reviewed by IE
and Region I staff.
Two allegations were received outside the interim SALP period. One
dealt with concerns on the design adequacy of certain restart and
past-restart modifications. The allegation was reviewed in NRC
Inspection 50-289/86-06 and it was not substantiated. An unresolved
i
item was identified for the licensee to define a thermal transient on
nozzles for cold water injections to high temperature systems. The
other allegation dealt with a concern on the potential for recriti-
cality during post-engineered safety feature actuation situations.
This is currently under review by Region I.
3
-
B.
Escalation Enforcement Actions
None
C.
Management Conferences
There were three management conferences during this period. On
December 17, 1985, NRC management (Region l'and NRR) met with the
!
licensee at the site to discuss the status of the power escalation
program and various related technical problems identified during the
startup process. On March 31, 1986, NRC management (Region I and
<
NRR) met with licensee management in the Region I, King or Prussia,
i
{
Pennsylvania, to discuss the interim SALP issued on March 13, 1986.
i
On April 18, 1986, NRC management (Region I, IE and NRR) met with
licensee management at the site to discuss technical issues on the
-
licensee's environmental qualification program, specifically for
TMI-1 but also applicable to Oyster Creek.
D.
Licensee Event Reports
In reference to Table 5, six Licensee Event Reports (LERs) were due
]
to personnel error, three were dua to component failure / malfunction,
and one was due to a system design error on the two-hour backup air
supply for the EFW system (which has as a root cause, personnel
error).
i
l
!
No causal link can be inferred among the ten LERs. Although the
population of 10 LERs is small, there was a relatively large number
of these attributable to personnel error.
-
7
_ _ _
_
._
- -
,
.
-
~
i
. .
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re
-
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.
-
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- --
-
,7
-
_.
'
.
36
E.
Reactor Trips / Forced Outages
Table 6 represents the unplanned reactor trips and unplanned outages
along with root causes. Also, the main turbine was taken off line
with the reactor critical at low power during October 13-18, 1985,
and April 24-25, 1986, for turbine steam inlet drain line repairs.
The following reactor trips and outages, which occurred during this
period, were planned in accordance with the licensee's test program
or regulatory requirements.
--
October 15, 1985, Manual
PLANNED trip in accordance with
startup test procedures
October 21, 1986, Loss of
PLANNED trip in accordance with
--
power escalation procedures
January 2, 1986, Turbine
PLANNED trip in accordance with
--
Trip
power escalation procedures
7
--
March 21-April 21, 1986,
PLANNED outage in accordance with
Outage
license conditions issued as a
result of steam generator tube
repair hearing
'
.
--
- . __
_
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9
6
mee
M
e
O
- - - - - -,
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,
- - - -
.
.
-
T1-1
TABLE 1
INSPECTION REPORT ACTIVITIES
TMI-1 NUCLEAR GENERATING STATION
REPORT / DATES
INSPECTION TYPE
HOURS
ACTIVITY
85-22
SHIFT
683
Power Operations
9/16/85-10/11/85
RESIDENT / PROJECT
Startup Testing
STARTUP TESTING
ENGINEERING SPECIALIST
85-23
EMERGENCY PREPARE 0 NESS
242
Annual Emergency
11/19/85-11/21/85
SPECIALIST
Exercise
_
-
RESIDENT / PROJECT
85-24
SHIFT
369
Power Operations
10/11-18/85
RESIDENT / PROJECT
Startup Testing
STARTUP TEST
Licensed Operator
.
RADIATION SPECIALIST
Training
Radiological
Effluent Control
85-25
SHIFT
352
Plant Operations
10/18-25/85
RESIDENT / PROJECT
Startup Testing
STARTUP TEST
85-26
SHIFT
501
Plant Operations
10/25-11/12/85
RESIDENT / PROJECT
Startup Testing
.
RADIATION SPECIALIST
Radiological
Effluent Control
85-27
SHIFT
603
Plant Operations
-
11/12-27/85
RESIDENT / PROJECT
Startup Testing
STARTUP TESTING
Radwaste Manage-
ment
85-28
SHIFT
540
Plant Operations
11/27-12/13/85
RESIDENT / PROJECT
Startup Testing
STARTUP TEST
Radiological
RADIATION SPECIALIST
Effluent Control
85-30
SHIFT
888
Plant Operations
12/13/85-1/10/86
RESIDENT / PROJECT
..
__
Startup Testing
STARTUP TEST-
_ ~_
Radration Protec -
-RADIATION SPECIALIST
tion
ENGINEERING SPECIALIST
-
--
-
. . _
_.
_
O
.
.
TI-2
TABLE 1 (Continued)
,
86-01
SHIFT
388
Plant Operations
i
1/10/86-2/7/86
RESIDENT / PROJECT
Shutdown /Startup
RADIATION SPECIALIST
Activities
SECURITY SPECIALIST
Radiological
!
FIRE PROTECTION SPECIALIST
Effluent Control
i
Security Program
I
Fire Protection
86-02
RESIDENT / PROJECT
273
Plant Operations
2/7/86-3/7/86
RADIATION SPECIALIST
New Fuel Receipt
Radiation Protec-
tion
e
86-03
SAFETY SYSTEM
770
EFW Operational
1'
3/3/86-3/27/86
FUNCTIONAL INSPECTION
Readiness and
BY THE PERFORMANCE
Functional
APPRAISAL TEAM (PAT)
Assessment
'
86-04
SAFETY SPECIALIST
38
Performance of
4/23/86
GPU Employee
86-05
RESIDENT
440
Plant Operations
i
3/7/86-4/11/86
FIRE PROTECTION
Fire Protection
SPECIALIST
i
RADIATION SPECIALIST
Radiation Protec-
ENGINEERING SPECIALIST
tion
!
86-06
RESIDENT / PROJECT
374
Plant Operations
4/11/86-5/16/86
RADIATION SPECIALIST
and Startup
J
ENGINEERING SPECIALIST
Transportation
!
86-07
OPERATOR LICENSING
Operator Licensing
EXAMINER
Examinations
'
l
- Not Tabulated
l
i
-
i
-
f
, ,,_ _. -
.
.r.._
. _ . . .
-
, _ . _
,
..
.
.
.
.
_
'
I
'
l
T2-1
TABLE 2
INSPECTION HOURS SUMMARY (9/16/85 - 4/30/86)+
TMI-1 NUCLEAR GENERATOR STATION
INTERIM
TOTAL
% OF TIME
HOURS
TOTAL HOURS
- Plant Operations
974
3528
54
(shift inspection hours)
(1617)
Radiological Controls
244
389
6
,
!
- Maintenance
288
426
7
- Surveillance Testing
252
339
5
Stavtup Testing
561
561
9
'
NA
242
4
Security and Safeguards
NA
79
1
l
- Technical Support
NA
127
2
.
- Training and Qualification
(included in above)
l
Effectiveness
!
- Assurance of Quality
(included in above)
,
.
'
Licensing
NA
NA
NA
.
- PAT Hours
NA
770
12
Total
3936
6461
.
i
NA - Not Applicable
- PAT - Performance Appraisal Team hours are included in the total but have not
been broken down into individual functional areas.
,
!
+ Include, IR 86-06 Inspection to 5/16/86
-
-
-
____
__
_ , __
_
-
,
_
-
-
@
_W
M
-!
-
__
- _
-
,
e
w.e-
,
.~,, -
. - - - . . - -
mem
-4--
9.-----
-4
- - - - - - - - -
_
.
--,y
-
. - - - , - - - - . - . - -
. - - - --- -
.
-
_
..
_ _ _ _ - -
_
.
-
I
~
l
>
.
T3-1
i
TABLE 3
!
ENFORCEMENT SUMMARY (9/16/85 - 4/30/86)
l
TMI-I NUCLEAR GENERATINJ STATICN
,
i
'
A.
Number and Severity Level of Violations
-
!
-
-
10
1
'
i
j
_
Total
11
B.
Deviation:
1 in Radiological Control (Transportation) Area
C.
Violations vs. Functional Area
I
Functional Area
_ Severity Levels _
.!
I
II
III
IV
V
Total
i
j
Plant Operations
5
5
Radiological Controls
2
2
Maintenance
1
1
2
i
Surveillance Testing
1
1
Startup Testing
I
Security and Safeguards
1
1
.
Technical Support
j
Training and Qualification
Effectiveness
'
Assurance of Quality
!
]
Totals
10
1
11
!
i
}
\\
~
-
. _. l
-
-
)
-
'-
-
'
.
l
. .
)
i
.-
_ _,
__
__
_ - . -
._-
. _ .
-, . _ , ,
-
-
.
_ . - _ .
,
,
.
1
T4-1
i
1
TABLE 4
ENFORCEMENT DATA
TMI-I NUCLEAR GENERATING STATION
Inspection
Inspection
Severity
Functional
Report No.
Date
Level
Area
Violation
A.
Violations
85-22
9/16-10/11/85
IV
Maintenance
Failure to
properly control
scaffolding in
safety-related
areas
85-25
10/18-25/85
V
Maintenance
Failure to
properly control
drawings inside
control room elec-
trical cabinets
4
85-27
11/12-27/85
IV
Plant
Failure to
Operations
establish or
properly change
procedures for
safety-related
activities
85-27
11/12-27/85
IV
Plant
Failure to
.
Operations
completely review
for adequacy pro-
cedures for inde-
pendent verifica-
tion of
safety-related
activities
85-27
11/12-27/85
IV
Plant
Failure to
Operations
properly implement
i
technical specifi-
i
cations and relat-
1
ed adainistrative
i
control for inde-
! __ _
,_
_
--
-
safety review
pendent on-site
, _
_
group (IOSRG)
.
-
-
-
activities
._
__
_
.
.
-
.-
-
.
_.
.
- - -
. . . . -
-
.
.
.
_
i
,
T4-2
TABLE 4 (Continued)
!
Inspection
Inspection
Severity
Functional
1
Report No.
Date
Level
Area
Violation
j
85-27
11/12-27/85
IV
Security
Failure to
properly implement
security personnel
'
badge identifica-
tion control
measures
85-30
12/13/85
IV
Surveillance
Failure to
properly inspect
a fire door on
'
_
'
the specified
frequency
86-01
1/10/85-2/7/86
IV
Plant
Failure of fire
Operations
brigade members to
respond to a drill
j,
wearing respira-
tory protection
'
apparatus
!
86-05
3/7/86-4/11/86
IV
Radiological
Failure to perform
l
Controls
timely evaluation
of airborne radio-
'
iodine in the
i
reactor building
.
I
86-05
3/7/86-4/11/86
IV
Radiological
Failure to con-
j
Controls
spicuously post
radiation caution
j
signs at a radia-
tion area acces-
,
{
sible to personnel
86-06
4/11/86-5/16/86
IV
Plant
Failure to imple-
i
Operations
ment, in part,
important to
'
safety procedures
during startup
^
=-
r
---.
__
.
__
-
,
_
- - -
-
.
M
!
-
_
_ _
-
. .
-_.,-*--_--,--,,,,vm
-m,,.r-
--- - , + -,
y,,
y-
-
r--.
. , _
---.y--_
_ -,_
.y.,
__. . .
.-
s
-- -.--
- _ -
-
.
r
.
S
.
M
i
T4-3
TABLE 4 (Continued)
!
Inspection
Inspection
Severity
Functional
Report No.
Date
Level
Area
Violation
a
B.
Deviation
1'
86-06
4/11/86-5/16/86
NA
Radiological
Failure to meet a
commitment to re-
train a radwaste
'
supervisor bienni-
ally
i
C.
Other Violations
"
.By letter dated January 25, 1986, the NRC staff 1ssued a Notice of
Violation as a result of NRC investigations into management issues related
to TMI-1 restart.
Specifically, the violation dealt with only the TMI-1
reactor coolant system (RCS) leak rate for which the licensee had taken
sufficient corrective and preventive action (see below). No response was
required for the Notice of Violation. Other violations may be issued when
the staff completes its review of those investigations and management issues.
The below-listed violations do not relate to licensee performance during
the SALP I period, since they involve plant activities between April 1978
and September 1979.
,
Failure to adequately control the RCS leakrate by having a deficient
--
surveillance procedure and by not properly implementing that
procedure.
'
.
)
Failure to maintain records of the RCS leakrate for invalid tests.
--
Failure to properly identify and correct malfunctions and
--
j
deficiencies in a makeup tank equipment configuration.
These violations relate to the Plant Operation and/or Surveillance area.
Collectively, they were classified as a Severity Level III Violation.
i
1
'
!
-
.
.
.
i
4 _
-_ . - _ , _ - - * . _
.-
,y
77
c_%_ _ ,_,
_,-s.,
-.-
, , ,
,
%
,
,g
_
m.
9_,
__,,%,_,m_
%
.,,,,, , _
m
_,p-
.7
y
y__,
w
m__
.
.
.
-
T5-1
TABLE 5
LER SYN 0PSIS - 9/16/86 - 4/30/86
THREE MILE ISLAND - UNIT 1-
LER Number
Summary Description
85-02
Manual reactor trip due to response to a fire in the rod
control system. Root cause:
Equipment / component mal-
function
85-03
Reactor trip due to a malfunction of a main generator relay
that caused a main turbine rejection which caused a RCS tran-
sient. Root cause:
Equipment / component malfunction
,
85-04
Inoperable fire barrier to a make-up pump cubicle without a
fire watch during modification work.
Root cause:
Personnel
error
86-01
Inoperable pressurizer spray line snubber was found while plant
was in hot standby condition. The snubber was found unpinned
at one end.
Root cause:
Personnel error
86-02
Reactor trip following a main turbine trip due to high moisture
separator level. A faulty valve controller in the heater
drains flow path caused the high separator level.
Root cause:
Equipment / component malfunction
86-03
Incorrect position of a jumper internal to an undervoltage
-
relay associated with the shunt trip feature for a control rod
drive trip breaker rendering one-of-four RPS channels out of
service.
Root cause: Personnel error
86-04
Isolation of condenser offgas radiation monitor RM-A-5L in
violation of technical specification.
Improper valve alignment
caused the isolation.
Root cause:
Personnel error
86-05
Fire door C310 was found inoperable due to excess door-to-floor
clearance and a continuous fire watch was not posted within an
hour of occurrence as required by technical specification.
Root cause:
Personnel error
86-06
Reactor trip following a main turbine trip due to a low
-
pr_ essure. spike _in the turbine lube oil system caused by valving
_
in a standby lube oil codier that was not fully pressurized.
-
~
Root cause:
Personnel error and procedure inadequacy
.
_
..
,_
m
. *
.
. .
.
.
.
.
.
.
.
.
.
.
-
.
.
. _ -
. - _ _ .
.
_
.
_
_ _ _ _ _
-
-
/
,
..
I
T5-2
86-07
The Performance Appraisal Team (PAT) found that the installed
two-hour backup air supply does not meet single failure crite-
ria. The original system design verification did not identify
this discrepancy in the final design.
Root cause: Engineering
design
,
,
I
i
.i
--
1
I
I
r
!
-
i
i,
.
A
i
I
!
I
j
-
.
_
_
-
4
_
_
e.
.i
=
!
.
. .
.
t
.
T6-1
1
TABLE 6
UNPLANNED REACTOR TRIPS
AND
SHUTDOWNS
(9/16/86 - 4/30/86)
DATE
DESCRIPTION
CAUSE
Unplanned Reactor
Trip Signals / Power Level
-
December 1, 1985,
The high RCS pressure resulted
Load dispatcher
_
High RCS Pressure / due to a load rejection with
allowed grid voltage to
,
j
from 75% power
the tripping of the main
drift up coupled with a
generator breaker due to an
relay setpoint drift
overexcitation protective relay
malfunction coupled with relay
setpoint drift during a regional
grid voltage transient
January 4, 1986,
The turbine trip resulted from
Equipment malfunction
an abnormal high level in one
in the secondary
.
from 22% power
of six moisture separators due
plant - level controller
'
to a level controller malfunction
in the feedwater heater drain
l
collection tank
.
March 15, 1986
The turbine trip resulted
Personnel error coupled
from an abnormal low turbine
with weak operating
from 100% power
lube oil pressure caused by
procedure
valving in a standby lube oil
cooler that was not fully
a
]
pressurized
i
April 21, 1986
The reactor tripped after all
Equipment malfunction
'
Failure of "0"
four reactor coolant pumps
in the electrical
(vital) bus
tripped following loss of or e
supply system coupled
supply breaker /
(of two) 4160 volt vital buses
with weak operating
reactor sub-
and all three 4160 volt non-
procedures
critical
vital buses
---
._
_ _ __
_
-m
.
t'
-
.
I
yp
dp=
- --
_
- - , .
, _ .
,
.,
-
- - - - , , , -
-
-
. _ - _ -
- .
_ .
._ . . - .
. - .- -.-. . .
.
-
.
. _ . .__- ._ - . . - _.
_ . .
-
,,
i
-
-
4
I
.
'
T6-2
i
i
TABLE 6 (Continued)
Dat_e
Description
Root Cause
a
,
April 23, 1986
High RCS pressure resulted
High RCS Pressure / from a main feedwater (FW)
to operations personnel
i
.
from 9% power
transient in which the
error
'
turbine-driven FW pump
decreased speed during the
transfer of steam supply
i
from the auxiliary system
!
to the main steam system
i
Unplanned Shutdowns / Duration
,
January 27, 1986
Due to a 20 MW reduction in
Secondary plant fabri-
.
Steam Line
electrical output first
cation defect which
- !
!
Bellows Leak /
observed on January 17, the
occurred during initial
.
]
One week
licensee shut down and in-
construction welding
i
spected the main condenser
j
for extraction steam expansion
bellows leakage
,
i
i
.
I
i
f
,
i
I
i
i
^
-
_ _ _
,_
_ ~ ~~
4
,
.
m
4
e emn*
- *
a
-
m.-.
.
.
-
.
m.
.
-
.
- .
.
.
.
- .
- .
. - -
. - -
,.
,
T7-1
TABLE 7
LICENSING ACTIONS
ACTIONS
NUMBERS
NRR/ Licensee Meetings
6
NRR Site Visits
4
Commission Briefings - One by the
1
Licensee
Schedule Extensions Granted -
_
Appendix J (LLRT)
1
Appendix H (Surveillance Capsule)
1
Reliefs Granted
0
Exemptions Granted
Appendix J (LLRT)
1
Appendix H (Surveillance Capsule)
1
Licensee Amendments Issues
6
.
Emergency Technical Specification
0
Changes Issues
Orders Issued
None
_
+
e
.
-
-
-
.
-
. .
,
,
.
T8-1
,
TABLE 8
RADIOLOGICAL EFFLUENT RELEASES
i
Non-Routine Events Resulting in Off-Site Releases of Noble Gases (Licensee
Reported)
i
i
% of Technical
Specifications
Component
Release
Activity
Quarterly
Date
Involved
Point
Released (C1)
_ Limit, Gamma _
10/21/85 Reactor Trip
1.07 E-6
3.8 E-8
at 40%
Relief Valves
(MSRV)
e
10/28/85 Makeup Pump
Station Vent
0.7
0.0015
(SV)
11/2/85
Reactor
1.05
0.025
Coolant
.
Evaporator
i
l
11/19-
1.6 E-7
3.48 E-9
!
20/85
Valve Testing
I
12/1/85
7.32 E-6
1.5 E-7
at 75%
4
12/17/85 Waste Gas
1.4
0.001
-
Compressor
12/30/85 Makeup Pump
46.3
0.07
1
1/2/86
1.22 E-5
2.3 E-7
'
at 88%
v
1
1/4/86
2.14 E-5
3.06 E-7
1
at 22%
,
'
1/9/86
RCLD Gas
1.6E-1
8.34 E-5
4
Sample
1/9/86
Flush of
2.76
2.22 E-3
MU-V-129A
-
-
,
-
. .-
_
m
M
g
1
-
-
.
.
.
-
-
.
_ . -
_
.
f
. -
--.--m-y.--,c-,----+
~%
_7
y--,
. - . . - - -
--
g.,
- - _ .,,
-...7-----------g-
, . - . . _ , , , - - _
-
,
y.
-. - -
-,,,
- .-- - - --,
,
.-
.
..
-
_
-..
.
, . . . -
.
.
TABLE 8 (Continued)
,
RADIOLOGICAL EFFLUENT RELEASES
<
1/28/86
DH-V-57B
3.96
2.0 E-3
i
2/13/86
AHC-14C
6.5 E-1
3.3 E-4
l
Fan Shutdown
2/13/86
Drain Trap
1.5
1.16 E-9
<
Chem Lab
1
]
Sample Sink
2/24/86
CA-V-2
11.6
6.44 E-9
]
Leakage
2/24/86
CA-V-2
2.79
1.91 E-3
-
Repair
_
3/4/86
Waste Gas
1.47
7.7 E-4
Comoressor
3/15/86
3.7 E-5
7.86 E-7
from 100%
5
3/22/86
CA-V-5
14.8
8.54 E-3
Relief Lift
T
Normal (Routine / Continuous) Operating Re?>Jses - Predominantly Noble Gas
!
% of Technical
.
!
Specification
i
Activity Released (C1)
Quarterly Limit, Gamma
-
'
!
j
October
0.15
1.32 E-3
November
18.8
2.0 E-2
'
December
5.29
7.6 E-3
January
262
2.78 E-1
.,
4
February
1150
1.23 E-0
i
.
March
830
8.8 E-1
l
-
-
..
._
r
__
,
<
_
..
.
.
I
.
-
,
,
h
-
._
_
_ .
.-,g.
. - ,r.,
-..,
,
- ,
-
-
-c.
.m
,, ,
.-_m+.-
-~ . . ,
, , .
.__y-
_
.rw
- . . .-
r.
rv,
-
-,-
_ . _ _ _ -_
. _ _ . _ _ _ _ _ _ _ _
_ _ _
_ _ . _ . . _ .
. _ . _ _ . - _
_ - _ _ . _ - _ __ _ -.
_ _ _ _
_
.. *
a
!
]
i
!
4
T8-3
..
TABLE 8 (Continued)
,
i
]
RADIOLOGICAL EFFLUENT RELEASES ~
,
1
Normal (Routine) Operating Releases - Liquid - Predominantly Tritium
'i
Activity
Date
Released (C1)
i
~
October
1.0
1
1
November
1.19
i
r
December
5.99
January
24.1
February
26.3
Mr.rch'
17.6
i
i
!
1
1
!
r
'
.
l
4
l
l.
i
1
1
!
3
-
-
_
-
.
-
- ._
_
.
!
, . .
- - . .
,
- . . . .
_ _ .
-
. ..
. - - .
.. -
..
>
-. -
.
-
.-
_
.
-
..
-
-
.
_
,
f '
,
9
U. S. NUCLEAR REGULATORY COMMISSION
REGION I
,
SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
INSPECTION REPORT 50-289/85-98
GENERAL PUBLIC UTILITIES NUCLEAR CORPORATION
THREE MILE ISLAND NUCLEAR GENERATING STATION UNIT ONE
ASSESSMENT. PERIOD:
SEPTEMBER 16, 1985 - JANUARY 10, 1986
BOARD MEETING DATE: JANUARY 24,198b
.
1
I
d
s
..
-
-
-
c.
.
_
__
___
_
.
m
-
.
.
_
.
.
TABLE _DF'C NTENTS
__ _ -.
--
_ _ - -
.
_
_
Page
I.
INTRODUCTION
1
A.
Purpose and Overview. . . . . . . . . . . . . . . .
2
B.
SALP Board Members
................
3
-
C.
Background. . . . . . . . . . . . . . . . . . . . .
6
II.
CRITERIA . . . . . . . . . . . . . . . . . . . . . . . .
III.
SUMMARY OF RESULTS
8
A.
Facility Performance. . . . . . . . . . . . . . . .
9
B.
Overview. . . . . . . . ..............
IV.
PERFORMANCE ANALYSIS
Il
A.
Plant Operations. . . . . . . . . . . . . . . . . .
14
B.
Radiological Centrols . . . . . . . . . . . . . . .
16
C.
Maintenanc
. . . . . . . . . . . . . . . . . . . .
.
19
D.
Surveillance Testing. . . . . . . . . . . . . . . .
21
E.
Startup Testing . . . . . . . . . . . . . . . . . .
24
F.
Training and Qualification Effectiveness
.....
26
G.
Assurance of Quality. . .
.............
V.
SUPPORTING DATA AND SUMMARIES
28
A.
Investigations and Allegations Review . . . . . . .
B.
Escalated Enforcement Actions . . . . . . . . . . .
28
28
C.
Management Conferences. . . . . . . . . . . . . . .
28
D.
Licensee Event Reports. . . . . . . . . . . . . . .
29
E.
Reactor Trips / Forced Outages
...........
29
F.
Planned / Unplanned Releases. . . . . . . . . . . . .
TABLES
T1-1
Table 1 - Inspection Report Activities . . . . . . . . . . . . .
T2-1
Table 2 - Inspection Hours Summary . .
.............
T3-1
Table 3 - Enforcement Summary. .
................
T4-1
-
Table 4 - Enforcement Data . . . . . . . . . . . . . . . . . . .
T5-1
,
Table 5 - Unplanned Reactor Trips and Snutdowns
........
T6-1
Table 6 - Radiological Effluent Releases . . . . . . . . . . . .
.
_
I.
,-
- -
, , .
_
1
.
-
.
.
.
-
-- I.
'INIEODUCTION
-
-
=
-
.
_
A.
purpose and Overview
The Systematic Assessment of Licensee Performance (SALP) is an inte-
.
grated NRC staff effort to collect available observations and data on
a periodic basis to evaluate licensee performance. The SALP process
'
is supplemental to the normal inspection ~ processes used to ensure
compliance with NRC rules and regulations.
It is intended to be suf-
ficiently diagnostic to provide a rational basis for allocating NRC
resources and to provide meaningful guidance to the licensee's man-
agement in order to improve the quality and safety of plant opera-
tions and modifications.
This SALP is termed an interim SALP in that it covers the period from
a few weeks prior to criticality to several days after the completion
of the power escalation program. The purposes of this interim SALP
are (1) to assist in the preparation for the first of two Commission-
directed performance appraisal team (PAT) inspections, (2) to verify
performance during the transition from a long-term shutdown condition
to commercial power operation, and (3) to determine the allocation of
NRC resources for future inspections.
An NRC SALP Board, comprised of the staff members listed in Section B,
met on January 24, 1986, to review the collection of performance
observations and data to assess the licensee's performance in accor-
dance with the guidance in NRC Manual Chapter 0516, " Systematic
Assessment of Licensee Performance." A summary of the guidance and
~
evaluation criteria is provided in Section II of this report.
This report is the SALP Board's assessment of the licensee's
performance at THI-1 Nuclear Generating Station for the period
September 16, 1985, through January 10, 1986. The summary findings
and totals reflect a relatively short period compared to the normal
assessment period which is at least 12 months.
,
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B.
SALP Board Members
-.
Chai rman
R. Starostecki, Director, Division of Reactor Projects
Members
.
R. Bellamy, Chief, Radiation Protection Branch, DRSS (Part Time)
i
L. Bettenhausen, Chief, Operations Branch, DRS
R. Blough, Chief, Reactor Projects Section No. lA, DRP
R. Conte, TMI-1 Senior Resident Inspector
S. Ebneter, Director, DRS (Part Time)
W. Kane, Deputy Director, DRP
H. Kister, Chief, Projects Branch No.1, DRP (Part Time)
P. McKee, Chief, Operating Reactor Programs Branch, Division of
Inspection Programs, IE
J. Thoma, THI-I Operating Reactors Project Manager, Project
Directorate No. 6
Other Attendees
N. Bluccerg, Lead Reactor Engineer, DRS (Part Time)
R. Urban, Reactor Engineer, RPS 1A, DRP (Part Time)
R. Weller, Section Leader, Project Directorate No. 6
F. Young, TMI-l Resident Inspector
1
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BacEiro~und
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1.
Licensee Activities
The major milestones of the licensee's power escalation program
along with completion dates are listed in Figure 1.
This sched-
ule was proposed by the licensee and agreed to by the NRC staff.
The licer.see completed its program within a few days of the plan-
,'
ned schedule. The program included six NRC Region I hold points.
The
The assessment period began with the plant in hot shutdown.
reactor was taken critical on October 3,1985, for natural cir-
culation testing and other low power tests. On October 9, 1985,
the main generator was placed on-line.
Between October 13 and 18, 1985, the turbine was taken off-line
several times with the reactor at low power to repair weld fail-
ures on drain lines from steam inlet piping to the main turbine.
On October 19, 1985, a test of the reactor trip on loss of main
feedwater was initiated from 40 percent power and a subsequent
natural circulation test was completed. The reactor was re-
started and the main turbine generator placed on-line on
October 23, 1985, then taken to 48 percent power.
The reactor was then op2 rated at 48 percent power for operator
training and steam generator leakage monitoring. Between
November 24, 1935. and December 27, 1985, the licensee completed
additional plannen steady-state power operation at 75 percent
power. On December 27, 1985, the NRC released the licensee to
take the plant to full power. However, the maximum achievable
power was limited due to secondary side fouling of the steam
generator, which caused higher than expected steam generator
water levels. Even after raising the steam generator water
level limit, as has been done at other B&W plants which experi-
enced the same problem, the licensee was able to achieve only
88 percent of full power.
On January 2, 1986, the licensee satisfactorily completed the
final power ascension tests -- reactor trip on turbine trip and
EFW initiation on loss of reactor coolant pumps. After the
planned January 2 trip and an unplanned trip during start-up on
January 4, the steam generator fouling was apparently alleviated
and the plant reached full power.
During the above period, two unp'anned reactor trips occurred:
l
on December 1, 1985, from 75 percent power, as discussed above,
and on January 4, 1986, from 22 percent power. The first
l
occurred because of a main generator breaker trip due to a mal-
function in a main electrical generator protection relay.
The
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other occurred because of another secondary plant malfunction
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that caused a high level in a moisture separator which resulted
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in a turbine-to-reactor trip.
'
The annual emergency preparedness exercise was comple'ted satis-
l
factorily on November 20, 1985. Also, the licensee completed
'
construction of a new annex to the training building which,
among other support functions, will house the plant-specific
!
simulator scheddled for delivery in June 1986.
l
2.
Inspection Activities
,
l
In May 1985, Region I established the TMI-1 Restart Staff organ-
ization to provide an intensive review of licensee activities
1
using an augmented shift coverage plan. This organization
"
continued to function from that time through delays in restart
i
authorization and through the licensee's power escalation
testing (PET) program. There was a high level of Region I
management involvement including the Deputy Director, Division
of Reactor Projects, who served as THI-I Restart Director on
i
I
site.
Because of his knowledge of the TMI-1 plant and experience with
the TMI-1 restart process, the senior resident inspector was
designated TMI-1 Restart Manager and assigned the responsibility
to manage inspection activities. Shift inspectors, experienced
in B&W plant operations, included resident / project engineers
,
from Region I, other regions, the NRt. training center, and NRC
contractors. Shift inspector activities ranged from 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
per day to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> per day, depending on the pace of licensee
'
activities. The resident inspector and Region I inspectors
conducted follow up reviews of a programmatic nature in response
to shift inspector concerns. As time permitted, they conducted
reviews of equipment operability and of the technical adequacy
l
of selected procedures. Region-based specialist reviews also
occurred in the areas of radiation protection, training,
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j
engineering support, security, and emergency preparedness.
To provide additional technical expert,ise and experience 'sith
the TMI-1 restart, the former senior resident inspector 'or
i
TMI-1 was assigned as a technical assistant to the THI ' Restart
l
Director.
!
A total of 3936 inspection hours were expended during the period
!
(shift inspector coverage was approximately 40% of that total)
with a distribution in the appraisal functional areas as shown
in Table 2.
The inspection hours occurred during a 17-week
period which converts to 232 hours0.00269 days <br />0.0644 hours <br />3.835979e-4 weeks <br />8.8276e-5 months <br /> / week or approximately 12,000
,
l
hours annually.
Summaries of inspection activities and identi-
fied violations a-e tabulated in Tables 1 and 4 respe:tively.
f
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This report also discusses " Training and Qualification Effec?
_ '
tiveness" and " Assurance of Quality" as separate functional
Although these topics, in themselves, are assessed in
areas.
the other functional areas through their use as criteria, the
i
.
two areas provide a synopsis.
For example, quality assurance
i
'
effectiveness has been. assessed on a day-to-day basis by resi-
dent inspectors and as an integral a.spect of specialist inspec-
tions. Although quality work is the responsibility of every
employee, one of the management tools to measure this effec-
tiveness is reliance on quality assurance inspections and audits.
Other major factors that influence quality, such as involvement
of first-line supervision, safety committees, and worker attitudes,
are discussed in each area.
.
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~~ II. CRtTERIA 3
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Licensee performance was assessed in selected functional areas significant
to, nuclear safety and the environment. Assessment areas were selected
based on facility status (i.e., restart testing phase) and, for this in-
terim SALP, NRC inspection program focus. Consequently, this interim SALP
does not include certain typical SALP functional areas, such as emergency
preparedness, security and safeguards, fire protection, technical support,
and licensing. These will be addressed in the next SALP.
,
One or more of the following evaluation criteria were used to assess each
functional area:
1.
Management involvement and control in assuring quality
2.
Approach to resolution of technical issues from a safety standpoint
3.
Responsiveness to NRC initiatives
4.
Enforcement history
5.
Report and analysis of reportable events
6.
Staffing (including management)
,
7.
Training effectiveness and qualification
Based upon the SALP Board assessment, each functional area evaluated is
classified into one of three performance categories. The definitions of
these performance categories are:
Category 1.
Reduced NRC attention may be appropriate. Licensee manage-
ment attention and involvement are aggressive and oriented toward nuclear
safety; licensee resources are ample and effectively used so that a high
level of performanc,e with respect to operational safety or construction is
being achieved.
The NRC attention recommendation may not be consistent with the above
categories for a given SALP rating in a specific functional area.
This is because of unique aspects of TMI-1 and because of public sen-
sitivity to operational activities at the facility to which the NRC
-
"
staff must be prepared to respond.
Category 2.
NRC attention should be maintained at normal levels. Licensee
management attention and involvement are evident and are concerned with
nuclear safety; licensee resources are adequate and reasonably effective
so that satisfactory performance with respect to operational safety or
construction is being achieved.
,
Category 3.
Both NRC and licensee attention should be increased. Licensee
management attention or involvement is acceptable and considers nuclear
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safety, but weaknesses are evident; licensee resources appear to bi~
--
strained or not effectively used so that minimally satisfactory perfor-
mance with respect to operational safety or construction is being
achieved.
Normally, the SALP Board assesses each functional area to compare the
licensee's performance during the last quarter. of the assessment period
to that during the entire period in order to determine the recent trend
for each functional area. Because of the short period covered by this
SALP, the trend categ6 ries are not addressed, however, perceptible changes
in performance in the last month of the period are addressed in the
functional areas.
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III. SURMARY OF RESULT F - -
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A.
Facility Performance (September 16, 1985 - January 10,1986)
Category
This Period
Functional Area
2
1.
Plant Operations
1
2.
Radiological Controls
2
3.
Maintenance
1
4.
Surveillance Testing
1
5.
Startup Testing
1
6.
Training and Qualification
Effectiveness
7.
Assurance of Quality
1
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1
-B.
Overview
Overall, licensee management prepared their operators and the plant
well for restart in light of the long shutdown.
Licensed operators
conducted themselves competently and exhibited a detailed knowledge
of the facility design and plant status. They demonstrated their
skills especially well in operating the integrated control system in
the manual mode. Despite signs of inexperience, non-licensed person-
nel also performed well. No plant trips occurred due to personnel
error, but workers in safety-related spaces were not always careful
in working around the equipment; this had the potential to cause
safety system challenges. A strong training program contributed to
the overall good results in operator performance.
Plant equipment was in good material condition and it reflected a
strong preventive and corrective maintenance program applied during
The startup group assured that the numerous re-
the long shutdown.
start modifications were adequately tested to minimize operational
problems during power ascension.
Plant maintenance adequately
maintained equipment-subsequent to plant turnover. Very little
safety-related equipment needed repairs during the startup test
program.
In general, procedures were adequate but, in certain instances, prob-
lems with individual procedure steps challenged personnel in the prop-
er implementation of the procedures. Even though a strong precedure
control policy exists, apparently not all workers understand their
responsibilities when procedures cannot be followed.
To varying degrees, the oversight review groups performed adequately.
However, it appears that certain important findings by review groups
were not effectively acted on by licensee management.
The radiological controls program continued to be implemented effec-
-
tively during power operation. The unplanned radiological releases
that occurred were due to poor work planning, not radiological plan-
ning.
The surveillance and starttp test programs were strong, involved com-
petent and dedicated personnel, and complemented each other in the
The power escalation program was slow and deliberate, and
restart.
was effective in providing familiarization training for operators. "
-
It was also effective in identifying and correcting overall system
integration problems.
The assessment covered a period of intense NRC staff review during
transition from a long shutdown to commercial power operation.
Licensee personnel attentiveness to the plant was probably heightened
Although many of the licensee's programs are
by these circumstances.
strong, continued gooc ruclear safety performance will result only
with ef fective program implementation and sustained personnel
attentiveness and involve ent.
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Technical Support
!
Technical support staffing was ample with definite signs of both cor-
4
porate and site engineering presence and involvement in plant activi-
In general, management exhibited conservatism when faced with
ties.
technical problems and, overall, technical support by licensee per-
sonnel was adequate but not aggressive. When technical problems
could not be resolved immediately, appropriate interim measures ware
provided to assure nuclear safety, such as with the relief / safety
valve problems associated with both-the steam generators and the
In
turbine-driven emergency feedwater pump steam inlet piping.
certain instances, however, appropriate measures or investigations
were established only after prodding by NRC staff.
Further, licensee
review of certain problems or events could have been more thorough
and complete'. Apparently, engineering personnel and management were
not always sufficiently inquisitive to assure a complete understand-
ing of problems.
In certain instances, especially during meetings
on the sixth and final NRC hold point, there was an apparent attitude -
of shortsighted analysis of events. Upon final resolution, no
unreviewed safety questions were identified, and ultimately, the
licensee competently resolved the technical problems.
,
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IV. -PERFORMANCE ANAt% SIS
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Plant Operations (974 hours0.0113 days <br />0.271 hours <br />0.00161 weeks <br />3.70607e-4 months <br />, 25';)
!
Analysis
The licensee displayed excellent overall control of the plant. Li-
censed shift personnel were professional and competent in handling
routine evolutions and tests and were especially skillful in operat-
ing the integrated control system.
Further, operators performed well
and demonstrated a safety conscious attitude during unexpected
events, such as the two unplanned reactor trips. The operators
l
showed a high level of knowledge and the ability to use that knowledge
in operating the plant safely.
Shift turnovers were thorough and
The shift technical advisor was integrated into plant
professional.
-
operations, especially in the evaluation of individual parameter
trends and of plant transients. Licensee management instilled a team
concept in the shift organization. Operations management insisted on
a quiet, professional control room atmosphere. Resources were well
managed to avoid excessive operator overtime while optimizing perfor-
The licensee made
mance and training benefits of the test program.
effective use of pre-briefings for special evolutions and tests and
Licensee
was responsive to NRC comments for improving the briefings.
management asserted their presence and involvement during the dayshift
as well as backshifts. In summary, noteworthy performance by licensed
i
operators, supervisors, and operations management resulted in excel-
lent overall plant control.
1
Administrative controls, procedures, and procedural adherence are
generally strong, but exceptions have been noted that require
liceasee management attention. Administrative controls for TMI-1 are
well established and they reflect a strong commitment to meeting re-
quirements to assure nuclear safety. These procedures also include
licensee initiatives beyond regulatory requirements. However, cer-
tain equipment control administrative procedures are inconsistent
with each other and with sub-tier documents with respect to indepen-
dent verification of equipment control measures as described in
NUREG-0737, TMI Task Action Plan item I.C.6.
Some of these proce-
4
dures impose independent verification for less than the full
safety grade scope of equipment to which it is intended to apply.
1
l
Although most licensee personnel exhibited respect for administrative
controls and attention to detail in implementing procedures, a sig-
nificant numbe'r of exceptions were noted. These included three cases
(two of which involved safety-related equipment) of conducting activ-
ities without a procedure, several minor examples of failure to ad-
here to procedures, and several other examples where personnel worked
around obvious procedure errors rather than stopping implementation
to obtain procedure change approval. There were also cases where a
more conservative approach was needed in implementing equipment con-
trol (tagout) measures.
In two cases, reliance on minimal isolation
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barriers for maintenance work resulted in small releases of
-
f.
radioactivity when single isolation points leaked. Management'atten-
!
tion is needed to ensure that all personnel properly and conserva-
tively implerent administrative and procedural controls. Aleo, some
upgrading of the quality of reviews of routine system operating and
-
test procedures may be warranted to fos,ter worker respect for proce-
This is highlighted by the fact that where procedures have
dures.
received extra attention, they are genera'11y of good quality and are
strictly followed. Examples include safety system valve lineups and
major tests.
There was a definite presence and attentiveness on the part of vart-
ous oversight groups. The Nuclear Safety and Compliance Committee
(NSCC) performed well. They scheduled their reviews and were able to
implement their plans well. Their reviews were thorough. The NSCC
staff has a high level of experience and good channels of communica-
tions to the board of directors. The Quality Assurance (QA) depart-
ment's presence on site was strong. This was exemplified by their
use of shift monitors, a unique and important licensee initiative.
The presence of experienced (formerly licensed) operations personnel
in the QA department enhances performance and credibility. Some
<
problems were noted with the Independent On-Site Safety Review Group
(IOSRG), including (1) f ailure to follow its own procedures and (2)
lack of a systematic approach and sufficient, depth in procedure re-
l
Overall, the oversight groups provide potentially beneficial
view.
insights, but the degree to which the licensee uses the information
is unclear.
For example:
Board dispositions for some NSCC recommendations were not clear;
--
Management did not respond effectively to QA assessments regard-
--
ing procedure implementation problems; and,
IOSRG discovery of a part of the independent verification prob-
--
lems did not lead to comprehensive resolution of
inconsistencies.
In general, management exhibited conservatism when faced with techni-
cal problems and, overall, licensee technical support was adequate
but not aggressive. When technical problems could not be resolved
immediately, appropriate interim measures were provided to assure
nuclear safety, such as with the relief / safety valves problem fof
steam generators and the emergency feedwater pump steam inlet piping.
In certain instances, however, these measures were established only
after predding by NRC staff.
Further, licensee review of certain
Exam-
problems or events could have been more thorough and complete.
pies included review of an RpS breaker malfunction, evaluation of
letdown cooler leakage, and evaluation of decay heat system pressure
,
,
indicator discrepancies.
In general, corrective action was timely,
but there were exceptions.
For example, had a more aggressive ap-
proach been taken towa-d ver.tilation system balancing, noble gas
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contamination incidents might-have-been precluded or_minimiz_ed.
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er functional areas describe related instances of poor technical sup-
port, most notably reflected in "Furmanite" repair jobs. Apparently,
6
engineering personnel and management were not sufficiently inquist- ~
!
tive to assure a complete understanding of certain problems, espe-
cially when a short-term, multi-disciplined review was needed. Upon
final resolution, no unreviewed safety questions were identified and,
ultimately, the licensee competently resolved the technical problems.
-
In summary, licensee management prepared the plant and their opera-
For the most part, procedures were techni-
tors well for restart.
cally adequate but individual procedure step inadequacies challenged
personnel in strictly adhering to those procedures. In general,
there is respect for procedure adherence, but there were too many
instances where personnel either did not follow or sidestepped a
It appears that in certain instances, personnel
procedure step.
understanding of the licensee's strong procedural control policies
are not well understood. To varying degrees, the oversight review
groups are performing adequately; however, some important findings
Overall
were not acted on effectively by licensee management.
licensee performance in this area was effective and well oriented
toward nuclear safety.
Conclusion
Category 2
Recommendation
Discuss at the SALP meeting (1) licensee actions to im-
~
Licensee:
prove the technical support area, (2) measures to instill in all
workers appropriate attention to operations phase administrative con-
trols, and (3) licensee measures to ensure optimal benefits from
oversight group findings.
PAT I should review extensively the licensee's independent
NRC:
technical and safety review process; by PAT II, an assessment
should be made of the licensee's plant safety review processes; in
particular, the reliance on individual. reviews as contrasted with
interdisciplinary committee reviews.
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E.
Radiological- Control s (244 hours0.00282 days <br />0.0678 hours <br />4.034392e-4 weeks <br />9.2842e-5 months <br />, 6%)
-
Analysis
The licensee's radiation protection program continued to be well de-
fined by clear policies and directives. Startup inspections indicat-
,
ed that the licensee satisfactorily implemented the radiation
An
protection program in accordance with reg 01atory requirements.
'
adequate staff.was available to carry out the program, and the per-
sonnel involved were well qualified and capable of performing satis-
A formalized-
factorily in their assigned areas of responsibility.
training program for the radiation protection staff continued to be
implemented and provided sufficient technical and practical instruc-
tions to assure competence in the organization.
Adequate management review and oversight are consistently evident as
demonstrated by their awareness of daily activities, the establish-
ment of effective inter-departmental communications and cooperation.
The quality assurance department has a lead monitor in this area
The radiation
for oversight of radiological control activities.
protection management staff takes the initiative in improving and
For example,
enhancing radiological control practices and procedures.
(1) the licensee's radiological staff initiated the investigation of
noble gas migration pathways in the auxiliary and fuel handling build-
ings, and consequently effected corrective measures to better control
airborne activity in the facility; (2) both health physics-field
operations and radiological engineering groups perform frequent
planned inspections and audits of radiologically controlled areas,
work activities, policies and procedures to assure quality perform-
ance; and (3).all anomalous occurrences that have the potential to
affect exposures to workers or the general public are aggressively
reviewed and evaluated to ascertain causal factors, corrective
measures, and dose effects. Additionally, radiological controls
awareness meetings are held monthly by the radiation protection,
maintenance, and operation departments to exchange information and
resolve concerns pertaining to radiological work, practices, and pol-
These meetings are also attended by representatives from the
icies.
bargaining unit, the Vice. President and Director of TMI-1, and con-
cerned workers.
The licensee generally exhibits good radiological-control practices
and they implement a very thorough radiation worker training program
in'an effort to ensure that radiation workers are aware of radiolog-
ical safety procedures and are' able to implement them competently.
The TMI-I Restart Staff noted that the licensee consistently demon-
strated a strong commitment to ALARA. During radiological work
performed in this assessment period, the licensee used ALARA
engineering practices, job planning, and worker training to reduce
j
personnel exposure.
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Effective programs relative to radioactive waste management, effluent
__
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monitoring, and control and transportation of radioactive materials
{
were implemented and maintained.
Effective quality control measures
are embodied in laboratory procedures and practices. The licensee's
performance in this area was consistent with regulatory requirements.
In general the licensee's performance during various operations and
maintenance activities involving high levels of radioactivity demon-
strated reasonable planning and preparation, good procedure develop-
ment and/or use, and the establishment of. appropriate radiological
controls. However, there were examples where better planning could
have prevented releases of radioactivity and the contamination of
workers.
For example, the work on the waste gas compressor resulted
in a release because a check valve was relied upon to isolate the
waste gas header (see Functional Area A, Plant Operations). Other
similar instances were noted which related to poor work planning,
although not specifically poor radiological planning. Licensee re-
view of the above events was thorough with extensive use of the radi-
ological awareness report and investigative reports.
In summary, the licensee was able to demonstrate that program ele-
ments continued to be effectively implemented during power operations,
and the licensee acequately trained and qualified personnel responsi-
ble for implementation of the radiological control program. Implemen-
tation problems were not due to programmatic weaknesses but were
related to poor individual worker performance or inadequate support
from other departments such as operations or engineering. The
licensee's program in this area is technically sound.
Conclusion
Category 1
Recommendations
None
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_ _ _ -
-
- -_
'l*
. .
..
.
. .e
16
'
-
.
.
.
..
t
.
'
f
~
C.
Maintinance ~(288 hours0.00333 days <br />0.08 hours <br />4.761905e-4 weeks <br />1.09584e-4 months <br />, 75) 1" ~
-
.
_.
_
.
_
Analysis
The maintenance organization was staffed with knowledgeable and
skilled personnel to support the required maintenance activities to
maintain safety-related equipment in a proper condition. When
,
maintenance-related work was identified by operations, the mainte-
,
nance department was aggressive in. scheduling and completing the work
based on the priority assigned by management. Managerial involvement
on a daily basis in supervising, tracking, identifying and resolving
problems resulted in a high level of plant operational readiness.
A. continued positive management initiative was that of permanently
assigning maintenance personnel to one of the six rotating shifts.
This reduced the typical power plant peaks of high maintenance
activity during the dayshift.
It also allowed the maintenance
department to schedule and perform corrective maintenance on vital
equipment as problems developed. Placing a portion of maintenance
personnel on shift work did, however, dilute the experience level in
the I&C area. This dilution of experience in the I&C area caused
minor operational problems which resulted in delays in retests until
'
supervision arrived on site.
The electrical and mechanical main-
tenance experience remained at a high level. The collective know-
ledge of the maintenance department was sufficient to resolve equip-
ment problems.
In addition, maintenance personnel appeared to be
highly motivated and supportive of management.
Administrative controls in the area are adequate and properly imple-
mented along with maintenance procedures. The staff identified a
^
minor drawing control violation with respect to posted drawings in-
side control room cabinets.
This was uncharacteristic of the
licensee's drawing control program. Another instance was noted where
individuals failed to follow a maintenance procedure and this result-
ed in the loss of a safety-related electrical bus. The individuals
,
'
involved were disciplined for failing to cooperate in the licensee's
i
review of this event.
I&C personnel were involved to a limited ex-
tent in the procedure implementation problems addressed in other
sections.
.
,
j
During this assessment period, several major safety-related systems
were reviewed closely by inspectors to determine overall reliability
l
'
and operability of the equipment.
Emphasis was placed on preventive,
as well as~ corrective maintenance by management in response to plant
restart.
Preventive maintenance procedures appropriately reflected
,
vendor technical manual recommendations. Safety-related eauf pment was
<
found to be in good material condition. Machinery history and mainte-
nance records reflected proper documentation (consistent with restart
hearing board requirements) and this resulted in development of a
useful historical data base on plant equipme.nt.
Records and field
observations reflected the involvement of the QA department in as-
suring operability of safety-related equipment.
.
. - - .
-
- - .
v.
-
-
- . -
- - - . - - . - - - _ . - - - - , .
, - -
_ _ _
_ _ _ ,
.
.
.
17
"
.; .'
-
-
h
-
No instances were noted of inoperability or poor testing because of
,!-
-
_
maintenance procedures. However, certain maintenance procedures
-
'I
lacked specificity and clarity associated with the recording and/or
'
evaluation of as-found conditions. This lack of clarity has forced
maintenance personnel, independent of plant engineering, to evaluate
!
and determine the operability of equipment in the field with limited
~
guidance. This has pointed out a need for enhanced procedure review
and approval and better technical support on the evaluation of
~
as-found conditions.
p w .e
Maintenance personnel, in particular, and other groups of personnel
doing work in safety-related spaces, were somewhat insensitive to the
change to an operating mode.
In certain instances, personnel contin-
ued their working habits as though the plant was in a shutdown condi-
-
tion. As a result, a violation occurred on unsecured scaffolding
'
that in a seismic event may have jeopardized the ability of the die-
sel generator to function. Other potentially adverse conditions oc-
curred, the most significant of which was the inadvertent tripping of
the emergency feed pump during scaffold construction, causing the
pump to De inoperable for several hours. The day-to-day approach and
attitudes of non-operations personnel was changing but not completely
corrected by the end of the period.
Housekeeping and fire protection measures remained consistent with
the previous high standards implemented during the long shutdown.
Extensive use of absorbent material to collect oil drippings was used
and contaminated drainage was directed to floor drains using tygon
tubing. However, certain areas of the turbine building were not re-
flective of those cleanliness standards that were applied to safety-
related areas. No fire hazards were created in the turbine building;
by the si.J of the period, conditions improved substantially in that
}
building.
Sufficient technical support was provided to maintenance and good
j
communication existed between this department and plant engineering.
There was consistent evidence of engineering evaluations in mainte-
i
nance packages. There was, however, incomplete support for " Fur-
,
.
manite" repair to leaking flanges and valves. The licensee. started
work during the 40% trip outage without considering the stress
induced by this process on the flange bolts. Another example was the
,
poor control of the amount of Furmanite for repeat injections evi-
denced during the full power trip outage. As a result, an OTSG level
1
instrument root valve clogged during the injection process and the
material was later blown into the OTSG. Further, no consideration ~
was given to the effects of the material in the OTSG until questioning
j
by the NRC staff occurred. Upon complete review of these problems,
no unreviewed safety questions were identified by the licensee.
These examples reflect a need for licensee management to assure a
more inquisitive evaluation of plant problems.
.
..
_
. . _ . _ _
__
, . , . . . _
_
,
_ . _ .
.
I[ ,
. -
.
.
_
_ _ .
._
_
~
18
s' ;
-
.
.
-
.
-
.
Overall, the maintenance program is properly established, imp.1[ement _
__
~
.
ed, and adequately staffed. Management involvement at all levels is'
~'
evident. Equipment and plant material condition are wel1 maintained
and in a condition that supported unit startup. The QA department is
5
Personnel attitude toward work in the
very active in this area.
spaces still reflects attitudes associated with a plant in cold shut-
down; however, it has not as yet had an adverse effect on plant
safety.
Conclusion
Category 2
Recommendations
None
.
!
i
-
m
-
. _ _ .
.
._ . _ . .
-
-
-
- -
.
. _
-
. - . _ _ _
l'
,
i
.
- -
i
.
,
- -.
-
.
_ -
19
)
i
..
-
-
[
,
.
'
-
-
D'.__3ufveillance . Testing'. (252 hours0.00292 days <br />0.07 hours <br />4.166667e-4 weeks <br />9.5886e-5 months <br />, M)
I
>
- l
-
Analysis
,r
During this inspection there was a high level of NRC inspection cov-
erage in this area as evidenced by inspection report documentation of
all or portions of over sixty surveillance tests. This included all
types of surveillances, including maintenance, operations, radiolog-
,
i
ical controls, and instrument and control surveillance.
In addition,
i
the data and calculations of numerous other surveillance tests were
i
reviewed.
,
The licensee has a strong administrative program which assures that
tests are conducted at the specified frequency. The overall adminis-
trative program was properly implemented except for minor problems.
,
A computerized scheduling system was used for the surveillance test
Accordingly, surveillance tests were effectively integrated
program.
.
with routine plant operations and well coordinated with operations
department activities. Surveillance procedures, with a few minor
exceptions, were properly implemented. Surveillance tests required
i
l
by the technical specifications were conducted at the specified fre-
'
l
quency with one exception. A fire surveillance was missed for sever-
al days due to the improper issuance of a procedure change. This-
violation of requirements was considered minor.
During this inspection period, NRC staff performed an extensive re-
view of safety-related equipment operability regarding the following
)
,
components: the makeup pumps, decay heat pumps, and the diesel gen-
The review included operating procedures, technical speci-
)
fication compliance, inservice testing, preventive maintenance,
erators.
i
!
1
maintenance history, and surveillance testing. Applicable surveil-
lance tests were found to be technically adequate in that they met
!
l
all applicable NRC requirements. Surveillance test procedures, along
with. maintenance procedures and post-maintenance testing, provided
adequate assurance that the selected safety-related components were
i
1
operable when called upon.
Surveillance procedures were properly followed. Tests were performed
in a deliberate manner ensuring that each step was completed prior to
proceeding to the next step.
Records were well kept. For a surveillance test of frequency of
ninety days or longer, a hard copy record of the last completed test
was maintained in the control ~ room. Once a test was completed, the
2
'
newer test was placed in the file and the older test was sent to
plant records for microfilming. This system enabled technicians or
operators good access to the most recently completed tests, .if neces-
In addition, extensive test records were reviewed by NRC and
'
sary.
l
found to be complete with one exception, discussed below.
.
-
-
,_..,_--y
-
-
. _ - , . ~ , - . . , , . . - - _ _ , _ _ _ - -
. - . .
-
.r..
r
.
.
-
20
1
_
.
.
h
Of particular concern during this period were the circumstances that
--
developed during and after'a routine surveillance test of the
pressurizer power operated relief valve (PORV). The issues of con-
r
{
cern included:
(1) a routine test that could not be completed be-
cause a portion of the test was not conducted correctly, (2) the
unnecessary creation of both a deficiency sheet and an exception
sheet as a result of that test and, subsequently, throwing these
sheets away and (3) the confusing documen tion used to substantiate
the shift supervisor's determination
ability of the PORV.
There was prompt involvement by senior management in the retest when
operability questions arose. However, the NRC staff's early involve-
ment in this process led to discovery of the exception and deficiency
sheets that had been thrown away and the identification of the poor
instructions for handling exceptions and deficiencies. This records
handling problem was considered uncharacteristic of the licensee's
records management program.
It did point out a need for additional
attention to detail on the part of licensee personnel in handling
these particular records.
Further, the licensee's review and approv-
al process could have developed better instructions for the handling
of test problems.
Although other mistakes were made by personnel, in general, licensee
supervision caught them before any adverse condition resulted. A
number of examples were noted in which supervision or senior person-
nel corrected errors made by junior personnel. Tnis was especially
evident in the I&C area. Because of supervisory presence, corrective
actions were appropriate to satisfactorily complete tests and avoid
challenges to safety systems.
Staffing was ample in this area along with good interdepartment in-
terfacing. A specially assigned staff representing the maintenance
and operations department assured overall good coordination of sur-
veillance test implementation and records. Personnel, in general,
were qualified to perform surveillances but as noted above, some in-
experience was evidenced by a few individuals.
None of the unplanned
reactor trips during this period were caused by surveillance tests.
Overall, the licensee has a strong surveillance program. Management
and 0A department involvement in this area is evident. The problems
observed were few in number and did not adversely affect plant safe-
ty.
The licensee safely conducts surveillance tests during plant
operations.
Conclusion
Category 1
Recommendations
None
-
.
_ _ _ .
l
- -
..
.-
_
21
.,.
- -
..
.
.
.
.
'
l
E.
Startup Testing (-56F hours,14%)
~_ ~~~
_
_ . -
_
.
-
.
_
5
4
During this SALP period, the licensee performed an extensive power
escalation test program over a three-month period. This program was
successfully completed with only minor performance problems noted.
Testing was performed at predetermined power levels from 0 to 100
,
!
percent power for both transient and steady-state conditions and in-
cluded tests of reactor physics performance, natural circulation,
integrated control system, feedwater system, emergency feedwater sys-
tem, plant performance during reactor trips, and measurements of re-
actor coolant system and steam generator leakage. NRC inspectors
witnessed all scheduled plant transients and portions of selected
steady-state tests, and reviewed all licensee test data and resolu-
tions to all test exceptions and deficiencies.
Overall test performance by licensee personnel, including plant oper-
ators, reactor ergineers, test engineers, and supporting personnel
.
from the headquarters safety analysis group, was very good. Opera-
I
tors always remained in control of the plant during special and in-
tensive test periods. The reactor engineering group, which performed
the physic testing, was well prepared in this aspect of the startup
The licensee assured that ample supporting specialists
test program.
i
from the fuel vendor and corporate fuel groups were present.
In
addition, innovative software programs were employed to monitor and
predict core status on a real time basis. With proper intorfacing
with the licansed operators, this resulted in tests being completed
<
in an effective and well-controlled manner. Although reactor engi-
1
neers initially were aggressive in their requests to operators to
establish plant test conditions, plant operators were always in
control of plant operations.
l
The startup test engineers had the largest portion of the program;
directing test evolutions from natural circulation testing through
the final reactor trip at 88 percent power, to subsequent steady-
state testing at 100 percent power. Except for the first.part of the
natural circulation test, plant testing was well-coordinated with
good interface with the plant operators. Data were properly taken,
data stations were adequately manned, and data reduction was per-
formed properly. Test exceptions and deficiencies (E&Ds) were pro-
perly resolved and all data along with test problems were reviewed by
the Test Acceptance Group in formal meetings conducted periodically
during each test phase.
In spite of some minor delays during the
program, all testing was completed within the scheduled time frame of
the test program.
The extensive pre-test training of reactor engineering and test engi-
neering personnel was evident in the overall lack of personnel prob-
lems during test performance. Test briefings for major evolutions
i
were thorough and extensive.
Problems noted during earlier tests,
where applicable, were factored into briefings for later tests.
Quality assurance involvement in startup testing was extensive in
.
v-mw-
'--v'
-
7'
7--
_
_______
l'
-
1
l
,.
-.
22
r,
-
~
-
'
.;
--
-
. that QA monitors were on shift for all testing.
In addition, QA had
I
-
!
prepared a detailed test monitoring plan and documentation of QA mon-
-
?
itoring activities was comprehensive.
Licensee management attention
and involvement were very evident in that top management was present
and witnessed major test evolutions and power escalations.
Generally, in handling technical problems, licensee management did
exhibit conservatism. During the initial startup, licensee manage-
ment ordered the reactor to be stabilized high in .the source range
until one of the two instrument channels for the intermediate range
neutron power was fixed. While performing an all-rods-out boron mea-
surement test during zero power physics testing, too much boron was
added to the reactor causing suberiticality. This " boron overshoot"
condition was promptly noted and the reactor engineers and operators
displayed a cautious approach in the boron dilution needed to correct
the problem. The licensee was responsive to staff concerns on the
emergency feedwater system turbine relief valve inadvertent actuation
problem and to the interaction problem between the steam generator
safety valves and the turbine bypass valves. Adequate interim
corrective action in terms of procedural guidance was provided to the
operators for both of these technical problems. Overall, licensee
management competently resolved their technical problems.
Based on staff review, the startup test procedures were comprehensive
and accomplished the desired test objectives with some minor problems
as discussed below.
Procedures were followed completely during the
All test data reviewed by the NRC staff were correct, and E&Ds
test.
were properly resolved.
Notwithstanding the positive aspects of the test program, some
problems with procedures and personnel were observed. During the
first part of natural circulation testing, test engineers did not
appear to be fully organized. This problem was recognized by manage-
ment and was quickly corrected. The test could have been better
planned to instruct the operators how to recover from the unique plant
conditions. As a result, at initial restoration of forced circulation
flow, a steam generator safety valve lifted. Other procedure defi-
ciencies were noted with respect to clarity of instructions. Test
management took corrective actions to improve these situations. At
the conclusion of the test program followin'g the reactor trip at 88
percent power, one further test deficiency was noted in that the
reactor trip test failed to document the reset function of the let-
down isolation valve MU-V3 following the reactor trip. The adequacy
of MU-V3 to open af ter a trip was subsequently demonstrated through a
separate retest after NRC staff prodding on the issue.
In summary, the licensee performed very well during the TMI-1 restart
startup testing program. Aggressive management attention and involve-
ment at the upper and middle management levels contributed to the
i-
l
_
.
.
.
.
_
__
__
23
k-
_
-
.
'
.
I
_
_..
effective program. The startup program was effective-in identifying ---
equipmer.t problems, especially from the viewpoint of integrated
.
system operations. The test program was thoroughly planned, accom-
i
t
plished on a realistic schedule, and provided ample time for operator
j
training and familiarization.
Licensee initiatives having generic
B&W applicability in this area were noteworthy. Although they
,
constituted unique tests, more comprehensive reviews should have
been considered by the licensee before implementation.
<
Conclusion
Category 1
Reccmmendations
None
,,
I.
a
.
M
__
.- _
'
<
.
.
.
24
,:1.
.
.
l
.
-
k
- - F.
Training ar.ddual'ification _Ef fectiveness (NA)
,S
Analysis
.
The various aspects of this functional area have been considered and
discussed as an integral part of the other functional areas and the
respective inspection hours have been incorporated into the respec-
tive functional areas. Consequently, this discussion is a synopsis
of the assessments conducted in other areas. Training effectiveness
is measured primarily by the obser'ved performance of licensee per-
sonnel and, to a lesser degree, as a review of program adequacy.
This discussion addresses three principal areas:
licensed operator
training, non-licensed staff training, and the status of INPO
training accreditation.
The training department was staffed with knowledgeable and experi-
enced personnel. The lesson plans, specialized manuals and courses,
hands-on experience, and/or extensive use of simulator and basic
principles simulator training provided meaningful and practical
training not only to licensed operators but also to other operator
I
technical personnel. This was evident in the performance of new
1
candidates for operator licenses. All candidates for licenses or
instructor certifications passed. They included four SR0 candidates,
,
'
one RO candidate (on retake), and one instruction certification can-
didate.
As noted in the plant operations section, observations of licensed
operator personnel by shift-inspectors produced a good deal of infor-
mation relative to their level of knowledge and performance skills.
The results of that review were favorable. The special interviews and
discussions on shift confirmed a high level of knowledge of facility
design with only minor weaknesses observed. Operators were well pre-
pared for restart and demonstrated especially strong skills in manip-
ulating the integrated control system in the manual mode. The
training for the non-licensed staff consisted of both formal and
!
1
on-the-job training. Based on NRC observations, this program was
also effective in producing performance-oriented personnel.similar to
the licensed operator program. During the implementation of work
activities, in general, non-licensed personnel were appropriately
,
knowledgeable in the ~ requirements of the' procedures and plant design.
Experienced personnel provided adequate guidance to less experienced
personnel.
4
No plant trips occurred due to personnel error. However, inspectors
saw a persistent problem with workers in various plant areas having
,
I
the potential to cause a trip or a challenge to a safety-related
system.
Personnel (licensed operators included) were also involved
in the problem with the proper implementation of administrative
controls for procedure implementation. There seemed to be a dis-
connect between the wel'-stated management policies in these areas
and the understanding of tho,e policies by certain individuals.
8
.
.
.
25
.
h-
I_-
Even with the corrective action initiated before the end of the power
-
!
escalation program, licensee management had not completely reached
!
all plant workers and corrective action is not yet complete.
The licensee received training program accreditation from INPO in the
following five areas: control room operators; senior reactor opera-
tors; shift technical advisors; auxiliary operators; and radiological
control technicians.
In summary, the licensee's training program is effective and is ori-
ented toward improving on-the-job performance. The program has the
'
support and commitment of management. The QA department is actively
involved in training.
In general, personnel are knowledgeable of
work and procedural requirements, and conduct activities with care.
When faced with problems, personnel take conservative measures and
seek help.
Conclusion
Category I (based on functional areas addressed)
Recommendations
None
l
.
.
___
__
__
.
-
_ _
3., . . -
1
'
-
26
l
.,
'
-
G.
Assurance of Quility (NA)
-
--
-
---
.:
..
-
The various aspects of quality assurance program requirements have
been considered and discussed as an integral part of each functional
-
area and the respective inspection hours are included in each one.
,
Consequently, this discussion is a synopsis of the assessments
conducted in those areas.
The quality assurance department continued their aggressive involve-
ment in oversight activities. -This was reflected in their unique
three levels of review along with a substantial resource initiative
--24-hour QA shift monitors.
Licensee management continued their
J
orientation in staffing the department with experienced personnel
along with providing career enhancement positions for licensed (or
formerly licensed) THI-1 operators. This had the added benefit for
licensee management of enhancing the operational expertise of the QA
department to fulfill its responsibilities in the oversight of
operations.
r
There was a definite QA presence and involvement in the various fac-
ett of field activities.
The monitoring level of review was effective
in identifying the procecure implementation problems later noted by
the NRC staff. As a result of successful monitoring, the audit group
more effectively used their time in reviewing programs and program
iraplementation. However, licensee management apparently did not
effectively respond to the QA department for the procedure implemen-
tation problem, which was highlighted in the QA department's annual
effectiveness review.
In summary, there was management and quality assurance (QA) depart-
ment presence and involvement in all facets of activities at the site.
Licensee management may need to provide additional attention to the
QA department's effectiveness reviews.
Conclusion
Category 1 (based on the functional areas addressed)
l
~
_
_ _ _
!
-
. -
.,
--
-
.
27
+
.
-
.
~
i
_
l
--
__
Recommendatiorm
.
-
I
Licensee: Non'e
NRC: PAT look at the effectiveness of the QA review process.
m
W
9
_ - -
_
.
?
I"
.
.
_
28
'
E-
-
.
-
'
V.
Supoorting Data and Summaries
~~
--
-
A.
Investigations and Allegations Review
There are no open investigations for THI-1. The investigation on the
environmental equipment qualification apparent material false state-
ments was completed during this period and it is being reviewed by
Region I staff.
There were no allegations received during this assessment period.
B.
Escalated Enforcement Actions
None
C.
Management Conferences
9
None
D.
Licensee Event Reports
Only three licensee event reports were submitted during this period.
They are listed below instead of being tabulated in a separate table.
LER 85-002, dated October 3, 1985, for the manual reactor trip
--
(from hot shutdown condition) that occurred on September 7,
1985, due to operator action in response to a fire in the rod
control system. The root cause was an equipment / component mal-
function (re: PLANT OPERATIONS AREA).
LER 85-003, dated December 31, 1985, for the reactor trip from
--
75 percent power that occurred on December 1,1985, due to a
proximate cause'of high pressure in the RCS. The root cause was
an equipment / component malfurction with a main generator relay
that caused a main turbine rejection which caused the transient
in the RCS (re:
PLANT OPERATIONS AREA).
--
LER 85-004, dated December 26, 1985, for inoperable fire barri-
ers found on November 26, 1985, to a m.akeup pump cubicle without
a fire watch during modification work. This was due to person-
nel error (re:
PLANT OPERATION! AREA).
In summary, all LERs were listed in the plant operations area; two
with component failure causes and one with-a personnel error cause.
No casual link can be inferred among the three LERs. However, LER
85-003 and an LER to be submitted outside this assessment period re-
flects a possible need for improvement in the design of secondary
trip function logic in which a one-out-of-one malfunction caused a tran-
sient on the RCS.
i-i
- -
.
- . . . -
-
29
-
)
__i* .-
-_
.
.
V.
-
-
r
-
LER 85-004_was indicative nf the worker in the spaces.probl_em identi-
~
!
fied in the maintenance area.
-
~
-
'
I*
E.
Reactor Trips / Forced Outages
Table 5 reflects the unplanned reactor trips and reactor shutdowns
along with root causes. Also, the main turbine was taken off-line
with the reactor critical at low power during October 13-18, 1985,
for turbine steam inlet drain line repairs, as discussed in paragraph
I.C.1.
The following reactor trips that occurred during this period were
planned per the licensee' test program:
--
October 15, 1985, Manual
PLANNED in accordance with
startup test procedures
--
October 21, 1985, Loss of
PLANNED in accordance with
power escalation procedures
Jar.uary 2,1986, Turbine Trip
PLANNED in accordance with
--
p'ower escalation procedures
F.
planned / Unplanned Releases
Table 6 is a summary c the more significant unplanned releases for
the period, along with a summary of the routine releases from the
plant on a montniy basis.
No regula*.ory limits were violated.
.
-
,
-
'
T1-1
-
-
j.
-
,
!
f_
__
-
TABLE 1
i
INSPECTION REPORT ACTIVITIES
TMI-1 NUCLEAR GENERATING STATION
AREAS
REPORT NO./ PERIOD
AREA INSPECTED
INSPECTOR TYPE
HOURS
INSPECTED
85-22
SHIFT
683
Power Operations
9/16/85-10/11/85
RESIDENT / PROJECT
Startup Testing
STARTUP TESTING
ENGINEERING SPECIALIST
85-24
SHIFT
369
Power Operations
10/11-18/85
RESIDENT / PROJECT
S.tartup Testing
STARTUP TEST
Licensed Operator
RADIATION SPECIALIST
Training
Radiological
Effluent Control
85-25
SHIFT
352
Plant Operations
10/18-25/85
RESIDENT / PROJECT
Startup Testing
STARTUP TEST
,
f
85-26
SHIFT
501
Plant Operations
10/25-11/12/85
RESIDENT / PROJECT
Startup Testing
RADIATION SPECIALIST
Radiological
Effluent Control
!
85-27
SHIFT
603
Plant Operations
11/12-27/85
RESIDENT / PROJECT
Startup Testing
STARTUP TESTING
Radwaste Management
85-28
SHIFT
540
Plant Operations
11/27-12/13/85
RESIDENT / PROJECT
Startup Testing
STARTUP TEST
Radiological
RADIATION SPECIALIST
Effluent Control
85-30
SHIFT
888
Plant Operations
12/13/85-1/10/86
RESIDENT / PROJECT
Startup Testing
STARTUP TEST
Radiation Protec-
RADIATION SPECIALIST
tion
ENGINEERING SPECIALIST
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INSPECTION HOURS SUMMARY (9/16/85 - 1/10/86)
4
TMI-1 NUCLEAR GENERATOR STATION
HOURS
% OF TIME
i
974
25
Plant Operations
(Shift Inspection Hours)
1617
41
Radiological Controls
244
6
Maintenance
288
7
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Surveillance Testing
252
7
Startup Testing
561
14
Training and Qualification Effectiveness
(included in above)
i
Assurance of Quality
(included in above)
Total
3936
100
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TABLE 3
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ENFORCEMENT SUMMARY (9/16/85 - 1/10/86)
TMI-1 NUCLEAR GENERATING STATION
A.
Number and Severity Level of Violations
-
-
-
6
1
Deviations
-
Total
7
B.
Violations vs. Functional Area
Functional Area
Severity Levels
I
II
III
IV
V
Dev Total
Plant Operations
4
4
Radiological Controls
Ma'ntenance
1
1
2
Surveillance Testing
1
1
Startup Testing
Training and Qualification
Effectiveness
Assurance of Quality
Totals
6
1.
7
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TABLE 4
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ENFORCEMENT DATA
TMI-1 NUCLEAR GENERATING STATION
Inspection
Inspection
!everity
Functional
Report No.
Date
Level
Area
Violation
85-22
9/16-10/11/85
IV
Maintenance
Failure to
properly control
scaffolding in
safety-related
areas
85-25
10/18-25/85
V
Maintenance
Failure to
properly control
drawings inside
control room elec-
trical cabinets
85-27
11/12-27/85
IV
Plant
Failure to
Operations
establish or
properly change
procedures for
safety-related
activities
85-27
11/12-27/85
IV
Plant
Failure to
Operations
completely review
for adequacy proce-
dures for indepen-
dent verification
of safety-related
+
activities
85-27
11/12-27/85
IV
Plant
Failure to
Operations
properly implement
technical specifi-
cations and related
administrative con-
trol for~1ndepen-
dent onsite safety
review group
(IOSRG) activities
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TABLE 4 (Continued)
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Inspection
Inspection
Sevarity
Functional
Report No.
Date
Level
Area
Violation
85-27
11/12-27/85
IV
Security
Failure to
(Plant
properly implement
l
Operations)
security personnel
badge identifica-
tion control
'
measures
,
85-30
12/13/85
IV
Fire
Failure to
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Protection
properly inspect
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(Surveillance) a fire door on
the specified
frequency
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TABLE-5
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_ _ _
UNPLANNED REACTOR TRIPS
AND
SHUTOOWNS
-
4
Unolanned Reactor Trips
Date
Description
Root Cause
December 1, 1985,
The high RCS pressure resulted
Secondary plant trans-
High RCS Pressure
due to a load rejection with
ient due to electrical
!
the tripping of the main
grid transient
generator breaker. An over-
excitation protective relay
malfunctioned when a regional
grid voltage transient coupled
with a relay setpoint drift
l
occurred
January 4,1986,
The turbine trip resulted
Random equipment mal-
because of an abnormal high
function in the second-
level in one of six moisture
ary plant
separators due to a level
controller malfunction in
the feedwater heater drain
collection tank
Unplanned Shutdowns
None
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TABLE 6
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RADIOLOGICAL EFFLUENT RELEASES
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Anomalous Occurrences Resulting in Off-Site Releases of Noble Gases
% of Technical
Specifications
Component
Release
Activity
Quarterly
Date
Involved
Point.
Released (C1) Ouration
Limit, Gamma
10/21/85
1.07E-6
10 sec
3.8 E-8
at 40%
Relief Valves
(MSRV)
10/28/85
Makeup Pump
..ation Vent
0.7
42 min
0.0015
(SV)
11/2/86
Reactor
1.05
75 min
0.027
Coolant
Evaporator
11/19-
1.6 E-7
5 sec
3.48 E-0
20/85
Valve Testing
.
12/1/85
7.32 E-6
7 min
1.5 E-7
at 75%
12/17/85
Waste Gas
1.4
54 min
0.001
Compressor
12/30/85
Makeup Pump
46.3
274 min
0.07
Normal Operating Releases - Predominantly Noble Gases
October
0.15 (0.02%
0.00132-
particulates)
November
18.8 (0.0003% tritium)
0.02
December
5.29
0.0076
Normal Operatine Releases - Liquid - Predominantly Tritium
October
1.0 (0.03% non-tritium)
.
November
1.19 (0.01% non-tritium)
5.99 (4.4 E-3% non-tritium)
December
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