ML20206C957

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Insp Repts 50-413/86-15 & 50-414/86-16 on 860226-0325. Violations Noted:Tech Spec 3.2.1 Not Followed & Details for Safety Evaluation Not Documented Per 10CFR50.59
ML20206C957
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 06/05/1986
From: Brownlee V, Skinner P, Van Doorn P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20206C894 List:
References
50-413-86-15, 50-414-86-16, NUDOCS 8606190609
Download: ML20206C957 (11)


See also: IR 05000413/1986015

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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Report Nos.:

50-413/86-15 and 50-414/86-16

Licensee: Duke Power Company

422 South Church Street

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Charlotte, NC 28242

Docket Nos.:

50-413 and 50-414

License Nos.:

NPF-35 and NPF-48

Facility Name: Catawba 1 and 2

Inspection Conducted:

F bruary 26 - March 25, 1986

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Approved by:

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V.~L. Bdownlee, Section Chtef

D~ ate Signed

Projects Branch 3

Division of Reactor Projects

SUMMARY

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Scope: This routine, unannounced inspection was conducted at the site in the

areas of review of licensee event reports (Units 1 and 2); review of inspector

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identified items (Units 1 and 2); plant operations licensee identified items-

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(Unit' 2); preparation for refueling (Unit 1); surveillance observation (Units 1

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and 2); maintenance observation (Units 1 and 2); preoperational test ' program

implementation (Unit 2); and observation of initial fuel loading (Unit 2),

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Results: Of the ten areas inspected, two apparent violations were identified in

two areas (Failure to follow Technical Specification 3.2.1.,

paragraph-5.g;

Failure to document required details for . safety evaluation per 10 CFR 50.59

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requirements, paragraph 7e).

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8606190609 860606

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REPORT DETAILS

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1.

Persons Contacted

Licensee Employees

  • J. W. Hampton, Station Manager

E. M. Couch, Construction Maintenance Central Manager

  • H. B. Barron, Operations Superintendent

W. F. Beaver, Performance Engineer

W. H. Bradley, QA Surveillance

  • A. S. Bhatnager, Performance Engineer

T. B. Bright, Construction Engineering Manager

  • S. Brown, Reactor Engineer

B. F. Caldwell, Station Services Superintendent

J. W. Cox, Superintendent, Technical Services

T. E. Crawford, Operations Engineer

  • B. East, I&E Engineer

J. R. Ferguson, Assistant Operating Engineer

  • C. L. Hartzell, Licensing and Projects Engineer

R. A. Jones, Test Engineer

J. Knuti, Operating Engineer

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  • P. G. LeRoy, Licensing Engineer

W. W. McCollough, Mechnical Maintenance Supervisor

W. R. McCullum, Superintendent, Integrated Scheduling

C. E. Muse, Operating Engineer

  • K. W. Reynolds, Construction Maintenance

F. P. Schiffley, II, Licensing Engineer

  • G. T. Smith, Maintenance Superintendent

D. Tower, Operating Engineer

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J. W. Willis, Senior QA Engineer, Operations

Other licensee employees contacted included technicians, operators,

mechanics, segurity force members, and office personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on March 25, 1986, with

those persons indicated in paragraph 1 above. The inspector described the

areas inspected and discussed in detail the inspection findings.

No

dissenting comments were received from the licensee. The licensee did not

identify as proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

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3.

Licensee Action

on

Previous Enforcement Matters

(Units 1 & 2)

(92701 and 92702)

a.

(0 pen) Unresolved Item 414/85-56-02: Evaluation of Cold Spring in

Safety Related Piping.

This item involves allegations of cold

springing made to licensee personnel.

The technical aspects of this

issue had been previously reviewed.

The inspector reviewed the

licensee's final report of the investigation which included affidavits

of feedback interviews.

No additional concerns were expressed by the

employees which had expressed concerns relative to cold soring. This

item remains open pending the licensee's personnel action.

b.

(Closed) Unresolved Item 413/85-43-03: Correction and Investigation of

problems Associated with Locking Methods for Plant Valves. Guidance

and training has now been provided to operators on proper methods for

locking valves. This is covered by Operations Management Procedures

2-33, Valve and Breaker Position Verification and Valve Operation and

had been incorporated into the training curriculum for nuclear

equipment operators.

c.

(Closed) Violation 413/85-43-01:

Failure to Follow QA Procedure for

Control of Nonconforming Items.

The response for this item was

submitted on December 6,1985.

The inspector verified completion of

corrective actions described in the response and considers licensee

actions to be acceptable.

d.

(Closed) Violation 414/85-56-01:

Failure to Follow Procedure for

Nonconforming Items - Water Hammer in Containment Spray System. The

responses for this item were submitted on January 10, 1986 and

February 24, 1986.

The Inspector verified completion of corrective

actions identified in the responses and considers licensee actions to

be acceptable.

e.

(Closed) Violation 413/85-48-01:

Entry Into an Operational Mode with

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Outstanding Work Open. The licensee's response to this violation was

contained in Duke Power Company letter to Region II dated January 10,

1986. The inspector reviewed the corrective actions identified in this

letter and considers the actions to be acceptable.

4.

Unresolved Items *

New unresolved items are identified in paragraph 5.e, 5.f, 7.c, and 7.d.

5.

Plant Operations Review (Units 1 & 2) (71707 and 71710)

a.

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirew its. Technical

Specifications (TS), and administrative controls.

Cci.. ol room logs,

danger tag logs, Technical Specification Action Item Log, and the

  • An Unresolved Item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation or deviation.

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remov'al and restoration log were routinely reviewed.

Shift turnovers

were observed to verify that they were conducted in accordance with

approved procedures.

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The inspectors verified by observation and interviews, that the

measures taken to assure physical protection of the facility met

current requirements.

Areas

inspected

included the

security

organization, the establishment and maintenance of gates, doors, and

isolation zones that access control and badging were proper and

procedures were followed.

In addition to the areas discussed above, the areas toured were

observed for fire prevention and protection activities. These included

such things as combustible material control, fire protection systems

and materials,

and fire protection associated with maintenance

activities.

b.

On March 10, 1986, the licensee requested a 96 hour0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> extension to the

time allowed under the Action statement of TS 3/4.7.7 for the Auxiliary

Building Filtered Exhaust System.

This request was made due to

required replacement of the carbon bed.

The 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> allowed by the

Action statement was not sufficient to replace the carbon and also

perform the required testing. Relief of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> was granted based on

discussions between NRR, Region II, the Resident Inspectors and the

licensee.

The licensee has addressed this issue in a letter to

Region II dated March 10, 1986.

c.

The inspector observed cable pulling of a Unit 2 electrical cable for

conformance to procedural requirements.

The cable specifically

observed was No. 2KC804 for the Component Cooling System to the

Auxiliary Shutdown Panel.

The inspector observed a craftsman

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carelessly stepping on small diameter piping and insulation during this

operation. Although no damage occurred, the inspector cautioned the

leading man for this activity and mentioned this problem to licensee

management.

d.

During a review of the operation of Diesel Generator IB conducted in

January 1986 (See inspection report 50-413/85-55, 50-414/85-68), the

inspector identified to the licensee a diesel start attempt that

appeared to be a valid failure but was identified as an invalid test.

Subsequent investigation by the licensee confirmed that this was a

valid failure and in addition the diesel had been left in an inoperable

status without taking compensatory actions required by TS.

This had

been documented with corrective actions in Licensee Event Report 86-10.

Since this finding occurred as part of the investigation begun in

January, the inspector has requested the licensee address this valid

failure and the failure to take compensatory action for the out of

service condition as part of the response to violation 50-413/85-55-04.

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e.

On March 10, 1986, the licensee identified that one channel of

Automatic Turbine Trip on Reactor Trip had been inoperable since

December 20, 1985. This was identified by a reactor engineer as a

result of re-reviews of past reactor trip reports.

The inspector

discussed the process of the initial reviews required by station

directives and the guidance provided therein with licensee management.

Although the present procedures appear to be adequate for an experi-

enced individual, the procedure may not adequately cover required

details for an individual that is less experienced.

The licensee is

committed to reviewing this procedure and the training provided to

personnel that conduct these reviews to determine if additional

training and guidance should be provided.

Pending completion of this

determination and review of the results by the inspector, this is

identified as a Unresolved Item 413/86-15-04:

Review of Training and

Guidance for Performing Reactcr Trip Reviews.

f.

During general plant observations in Unit 2 on March 14, 1986, the

inspector noted two (2) electrays which appear to be overfilled with

electrical cables.

These electrays are above the Ventilation

Condensate Drain Tank in the Auxiliary Feedwater pump room.

The

licensee was asked to evaluate this problem. Nonconforming Item Report

CN-399 was written to track this item.

This item remains unresolved

pending further licensee and NRC review.

This is Unresolved Item

414/85-16-03:

Evaluation of Apparent Electrical Cable Overfill in

Electray in the Unit 2 Auxiliary Feedwater Pump Room.

g.

On March 17, 1986, the licensee identified that ten (10) bellows type

penetrations had not been tested within twenty-four (24) months as

required by TS 4.6.1.2h.

As a result of this, at 3:10 p.m.,

the unit

commenced reducing power at a rate of 10*4 per hour.

Axial Flux

Difference (AFD) went outside the TS operating limits at 3:25 p.m. but,

this was not recognized due to a malfunction of the Operator Aid

Computer (OAC).

Although other instrumentation existed to identify

that AFD was not within prescribed requirements, the operators,

including performance engineering personnel, continued to monitor the

OAC.

At 6:19

p.m.,

the reactor operator noticed that the AFD

instrumentation, which is on the panel' adjacent to the OAC, were pegged

low. Power was reduced to less than 50*4 as required by TS at 6:25 p.m.

At 6:40 p.m.,

the bellows testing was completed and the unit exited the

TS action that initiated the reduction in power.

A<., a result of this

AFD problem, the licensee violated the Action requirements of TS 3.2.1.

as follows:

(1) Action item a. requires that with the indicated AFD outside of the

target band and thermal power greater than or equal to 90*4 of

rated thermal power, within fifteen (15) minutes either restore

the indicated AFD to within the target band limits or reduce

thermal power to less than 90%. Since it was not recognized that

AFD was outside the target band power was not reduced to less than

90% until about 4:15 p.m.

This exceeded the TS requirement by

approximately forty-five (45) minutes.

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(2) Action item b. requires that with the indicated AFD outside the

acceptable operation limit of Figure 3.2-1 and with thermal power

less than 90% but equal to or greater than 50% of rated thermal

power, reduce power to less than 50% of rated thermal power within

thirty (30) minutes and set the Power Range Neutron Flux-High

Setpoints to less than or equal to 55% of rated thermal power

within the next four (4) hours. Since the AFD indication was not

identified, power was not reduced to less than 50% within thirty

(30) minutes. In addition, the power range instruments were not

reset to less than or equal to 55% as specified within the

required four (4) hours.

The above event is identified as a Violation 413/85-15-02:

Failure to

follow required actions of TS 3.2.1.

No violations or deviations were identified except as noted above.

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6.

Surveillance Observation (Units 1 and 2) (61726)

a.

During the inspection period, the inspector verified plant operations

were in compliance with various TS requirements.

Typical of these

requirements were confirmation of compliance with the TS for reactor

coolant chemistry, refueling water tank, emergency power systems,

safety

injection,

emergency

safeguards

systems,

control

room

ventilation, and direct current electrical

power sources.

The

inspector verified that surveillance testing was performed in

accordance with the approved written procedures, test instrumentation

was calibrated, limiting conditions for operation were met, appropriate

removal and restoration of the affected equipment was accomplished test

results met requirements and were reviewed by personnel other than the

individual directing the test, and that any deficiencies identified

during the testing were properly reviewed and resolved by appropriate

management personnel.

Typical of the surveillance items that were witnessed in part or in

full were various calibrations of the nuclear instrumentation,

auxiliary feedwater system testing, turbine stop valve testing, and

residual heat removal system testing.

b.

The inspector received a copy of a memorandum to R. W. Starostecki,

Region I from W. T.

Russell, ONRR, dated March 7,

1986, subject:

Technical Specification Interpretation Concerning Surveillance Testing

Methods for Diesel Generator Lockout Features. The conclusions reached

in this memo as to the proper method to conduct surveillance testing of

these features were reviewed against the methods provided in

PT/1/A/4350/15A and ISB, Diesel Generator 1A (18) Periodic Test. This

review indicated that the method used by these procedures do perform

this testing as detailed in the above memo.

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c.

During a routine review of TS the inspector noted a typographical error

in Table 3.6-2.a and 3.6-2.b.

In these tables under column 3 valve

SA-1# is. identified as SM-1#. This was discussed with the licensee and

with the Catawba licensing project manager in NRR. The licensee has

included a correction for this error in a letter to NRR dated March 7,

1986, containing amendments to Unit 1 and 2 Technical Specifications.

No violations or deviations were identified

7.

Maintenance Observations (Units 1 and 2) (62703)

a.

Station maintenance activities of selected systems and components were

observed / reviewed to ascertain that they were conducted in accordance

with requirements. The inspector verified licensee conformance to the

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requirements in the following areas of inspection: the activities were

accomplished using approved procedures, and functional testing and/or

calibrations were performed prior to returning components or systems to

service; quality control records were maintained; activities performed

were accomplished by qualified personnel; and materials used were

properly certified. Work requests were reviewed to determine status

of outstanding jobs and to assure that priority is assigned to

safety-related equipment maintenance which may effect system perfor-

mance,

b.

The inspector requested the licensee to determine whether updated

information relative to Woodward Governors has been specifically

requested from appropriate vendors. This request is based on recent

NRC information indicating that the manufacturer only supplies this

information if specifically requested. The licensee is reviewing this

matter.

This is Inspector Followup Item 413/85-15-01, 414/85-16-01:

Verification that Licensee is Obtaining Updated Information Relative to

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Woodward Governors.

c.

On January 3, 1986, the licensee identified four pipe supports that

were pulled loose from their structural attachments on the steam line

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(SA) to the Auxiliary Feedwater Pump Turbine (CAPT).

A regional

specialist inspector investigated this occurrence (see Inspection

Report 50-413/86-06 and 50-414/86-08).

Several Duke Power Company

memoranda were written in regard to the investigation of this

occurrence.

The inspector reviewed these memos and has requested the

licensee address several areas that do not appear to have been

included. The areas that are questioned are as follows:

(1) One memo states that the steam lines are heat traced to prevent

steam from condensing.

It also says that the system will be

declared inoperable if the temperature drops below 220 F.

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10.3.2-2 of the Final Safety Analysis Report (FSAR) Note 15 states

that the heat tracing is to maintain the temperature of the line -

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at 2550 F.

There appears to be an inconsistency between these two

doce ents.

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(2) All the memoranda that were reviewed by the inspector addressed

damage due to water hammer or steam hammer.

If this line is

allowed to cool to approximately 220 F and the steam valves

suddenly opened, it appears that there could be damage due to

thermal shock in addition to water / steam hammer.

(3) One of the memo's address actions to be taken if the temperature

in the pipe decreases to less than 220 F.

Discussions with

operations personnel on shift indicate a lack of guidance or

awareness that design has specified actions to be taken for this

problem.

The above items are identified as Unresolved 413/86-15-03; Questions

Concerning Engineering Analysis of SA Support / Restraint Failures,

pending additional review and discussion by the inspector with licensee

personnel,

d.

The FSAR, Sections 15.1.4.1 and 15.1.5.1 state that part of the

protection provided for the accidents, associated with these sections,

is a feedwater isolation signal that will rapidly close all feedwater

control valves and backup feedwater isolation valves, trip the main

feedwater pumps, and close the feedwater pump discharge valves. The

inspector reviewed various documentation to determine the method used

to perform these functions.

The licensee identified that during the

construction period, the feedwater pump discharge valves had been

removed.

This was accomplished by Variation Notice (VN) #50047. This

finding is being identified as an Unresolved Item 414/86-16-04: Review

of design change VN50047, Removal of Automatic Closure of 2 CF-10 and 2

CF-17, pending additional review by the inspector.

e.

In addition to the removal of the Automatic Closure of the feedwater

pump discharge valves as discussed in 7d above, the feedwater pump

turbine trip feature was also removed on Unit 2.

This change was

performed in accordance with Nuclear Station Modification (NSM)

CN20084. The inspector reviewed the safety evaluation associated with

the NSM which is required by 10 CFR 50.59. This safety evaluation

stated no unreviewed safety question was judged to be involved or

created by this modification.

In addition, it referenced only

Chapter 7.0 of the FSAR as being reviewed.

10 CFR 50.59 (b) requires

that the records of changes to the facility include a written safety

evaluation which provides the bases for the determination that the

change does not involve an unreviewed safety question. There was no

bases provided in this NSM safety evaluation and no reference to the

accidents described in Section 15.1.4.1 and 15.1.5.1 for which these

features were identified to provide protection. This is identified as

a Violation 414/86-16-02: Failure to provide the bases for determining

that a change to the facility does not involve an unreviewed safety

question.

No violations or deviations were identified except as noted above.

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8.

Review of Licensee Nonroutine Event Reports (Units 1 and 2) (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine if

the information provided met NRC requirements. The determination included:

adequacy of description, verification of compliance with Technical Specifi-

cations and regulatory requirements, corrective action taken, existence of

potential generic problems, reporting requirements satisfied, and the

relative safety significance of each event. Additional implant reviews and

discussion with plant personnel, as appropriate, were conducted for those

reports indicated by an (*).

The following LERs are closed:

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LER 413/84-03 and

Control Rod Drive Assemblies Removed

413/84-03 Rev 1

Improperly

LER 413/85-57

Comparison of Digital Rod Position to

Demand Position Not Performed

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LER 413/85-65

Auto-Start of Auxiliary Feedwater

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During Testing of Reactor Trip Breakers

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LER 413/85-66

Mode Changes Made With Inoperable

Equipment Due to Mishandling Work

Requests

LER 413/85-67

Reactor Trip on Loss of Main Feedwater

Pump Due to Design Deficiency

No violations of deviations were identified.

9.

Information Meetings with Local Officials (Units 1 and 2) (94600)

A meeting was held with local Rock Hill city government officials on

March 4,

1986.

This meeting was conducted to familiarize the local

officials with the mission of the NRC, to introduce key NRC personnel

associated with Catawba, to discuss lines of communications available

between local officials and the NRC, and to discuss the status of the

facility and related community concerns with these local officials. A copy

of general information was provided to the mayor and council members.

The

following local officials were present:

Betty J. Rhea, Mayor

Bidwell Ivey, Councilman

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Henry T. Wood, Councilman

10.

Preparation for Refueling (Unit 1) (60705)

The inspector reviewed preparations for refueling of Unit 1 presently

scheduled to commence in August 1986.

This review was concerned only with

the receipt, inspection and storage of new fuel in the fuel storage area.

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This process was performed in accordance with approved procedures and used

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instrumentation that had been recently calibrated in accordance with

calibration requirements.

In addition, the inspector reviewed training

records of various personnel handling the new fuel and crane operations.

Four fuel assemblies were observed (D-04, 0-19, D-26 and D-34).

No violations or deviations were identified.

11.

Inspector Witnessing of Initial Fuel Loading (Unit 2) (72524)

The inspectors witnessed fuel loading operations to verify that a well

coordinated effort was conducted in accordance with procedure and - TS

Requirements. The inspectors witnessed the installation of the first five

bundles, the last 13 bundles and additional bundles on an intermittent

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basis.

No violations or deviations were identified.

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Preoperational Test Program Implementation Verification (Unit 2) (71302)

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The inspector witnessed operational aspects of portions of selected tests

associated with the preoperation program to verify that activities were well

controlled, coordinated and performed in accordance with applicable

procedures. Included in this review were thermocouple calibrations and

running of Diesel Generator 2A for governor trouble shooting.

No violations or deviations were identified.

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13.

Licensee Identified Items 50.55(e) (Unit 2) (W3)

(Closed) CDR 414/86-02: Diesel Generawor Valve Spring Failures. The report

for this item was submitted on January 16, 1986.

The inspector verified

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that the licensee has performed appropriate inspections of the affected

springs and has a long term plan to provide replacement springs. Licensee

actions are acceptable.

No violations or deviations were identified.

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14.

Previously Identified Inspector Findings (Units 1 and 2) (92701)

a.

(Closed) Inspector Followup Item 413/85-52-01, 414/85-62-01: Revision

of OMP 3-1 for Senior Operator License Applications. The licensee has

implemented a procedure change correcting the subject procedure. This

action is acceptable.

b.

(Closed) Inspector Followup Item 414/84-42-02: Downgrading Operator

Candidate Exam Results.

This item is closed based on previous

inspections described in NRC Report No. 50-413/85-12.

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c.

(Closed) Inspector Followup Item 414/84-42-04: Need to Improve NED Qual

Checklist Record Keeping.

This item is closed based on previous

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inspections described in NRC Report No. 50-413/85-12.

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d.

(Closed) Inspector Followup Item 413/84-93-05, 414/84-42-05: Review

Catawba Requalification Program to Ensure it Meets Requirements of

10 CFR 55.

The

inspector

reviewed

the

licensees

operator

requalification program entitled Requalification Program for NRC

Licensed Personnel Revision 1, dated November 27, 1984.

This review

indicates that the requalification program meets the requirements of 10 CFR 55. This item.is closed.

e.

(Closed) Inspector Followup Item 413/84-93-03, 414/84-42-03: Develop

Program to Ensure Licensed Personnel Periodically Perform Licensed

Duties. Operations Manaaement Procedure 3-5, Revision 3, Maintenance

of Operating Experience for NRC License (R0/SRO) Renewal contains

guidance and documentation requirements for maintenance of licensed

personnel . This identifies the frequency at which a person must stand

a prescribed duty in order to maintain his licensed position. Based on

the inspectors review of this procedure this item is closed.

No violations or deviations were identified.

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