|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License ML20196J7651999-06-29029 June 1999 Provides Updated Info Re Loss of Feedwater & Loss of Electric Power Accident Analyses to Support TS Change Request 279 Re Core Protection Safety Limit,As Discussed at 990616 Meeting ML20196J7701999-06-29029 June 1999 Forwards LAR 285 for License DPR-50,clarifying Authority to Possess Radioactive Matls Without Unit Distinction,So That After Transfer of TMI-1 License to Amergen,Radioactive Matls May Continue to Be Moved Between TMI-1 & TMI-2 Units ML20209C0391999-06-29029 June 1999 Forwards LAR 77 to License DPR-73,clarifying Authority to Possess Radioactive Matls Without Unit Distinction,So That After Transfer of TMI-2 License to Amergen,Radioactive Matl May Continue to Be Moved Between TMI-1 & TMI-2 Units ML20196G2061999-06-23023 June 1999 Requests That NRC Update Current Service Lists to Reflect Listed Personnel Changes That Occurred at TMI 05000289/LER-1999-006, Forwards LER 99-006-00,providing Complete Description,Extent of Condition & Actions Taken in Association with Determination of Inability of Pressurizer Support Bolts to Meet FSAR Requirements1999-06-23023 June 1999 Forwards LER 99-006-00,providing Complete Description,Extent of Condition & Actions Taken in Association with Determination of Inability of Pressurizer Support Bolts to Meet FSAR Requirements ML20196D2171999-06-17017 June 1999 Forwards Pmpr 99-9, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990508- 0604.New Summary Personnel Table Was Added to Rept Period.Matl Scientist Joined Staff Period ML20196A0431999-06-15015 June 1999 Providess Notification That Design Verification Activities Related to Calculations Supporting Analytical Values Identified in Gpu Nuclear Ltr to NRC Has Been Completed 05000289/LER-1999-004, Forwards LER 99-004-00,re Discovery of Emergency FW Pump Bearing Failure During Performance of Oil Change on 990510. Event Was Determined Reportable IAW 10CFR50.73,since Pump Was Determined to Be Inoperable Longer than TS AOT1999-06-0909 June 1999 Forwards LER 99-004-00,re Discovery of Emergency FW Pump Bearing Failure During Performance of Oil Change on 990510. Event Was Determined Reportable IAW 10CFR50.73,since Pump Was Determined to Be Inoperable Longer than TS AOT ML20212K2541999-06-0808 June 1999 Submits Concerns Re Millstone NPP & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Requests That NRC Provide Adequate Emergency Planning in Case of Radiological Accident ML20212K2671999-06-0808 June 1999 Submits Concerns Re Millstone NPP & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Requests That NRC Provide Adequate Emergency Planning in Case of Radiological Accident ML20195E2751999-06-0404 June 1999 Informs That PCTs & LOCA Lhr Limits Submitted in Util Ltr for LOCA Reanalysis Performed in Support of TMI-1 20% Tube Plugging Amend Request Have Been Revised.Revised PCT & LOCA Lhr Limit Values Are Provided on Encl Table 1 ML20195E3281999-06-0404 June 1999 Forwards Application for Amend to License DPR-50,modifying Conditions Which Allow Reduction in Number of Means for Maintaining Decay Heat Removal Capability During Shutdown Conditions ML20195C5721999-06-0202 June 1999 Forwards Description of Gpu Nuclear Plans for Corrective Actions for 1 H Fire Barriers in Fire Zones AB-FZ-3,AB-FZ-5, AB-FZ-7,FH-FZ-2 & Previous Commitments for Fire Zones CB-FA-1 & FH-FZ-6 ML20207E2561999-05-25025 May 1999 Submits 30-day Written Rept on Significant PCT Change in ECCS Analyses at TMI-1 ML20195B2461999-05-21021 May 1999 Forwards Itemized Response to NRC 990506 RAI for TS Change Request 279 Re Core Protection Safety Limit ML20206R6461999-05-13013 May 1999 Forwards Rev 39 of Modified Amended Physical Security Plan for TMI 05000289/LER-1999-003, Forwards LER 99-003-00, Discovery of Condition Outside UFSAR Design Basis for CR Habitability, Which Was Determined Reportable on 990310.Rept Is Being Submitted Four Weeks Later than Required,Per Discussion with NRC1999-05-0707 May 1999 Forwards LER 99-003-00, Discovery of Condition Outside UFSAR Design Basis for CR Habitability, Which Was Determined Reportable on 990310.Rept Is Being Submitted Four Weeks Later than Required,Per Discussion with NRC ML20206K6301999-05-0707 May 1999 Provides Addl Info Re TMI-1 LOFW Accident re-analysis Assumptions for 20% Average SG Tube Plugging as Discussed on 990421 ML20206H0781999-04-30030 April 1999 Forwards Rev 0 to 1092, TMI Emergency Plan. Summary of Changes Encl ML20206J4811999-04-30030 April 1999 Provides Summary of Activities at TMI-2 During First Quarter of 1999.TMI-2 RB Was Not Inspected During Quarter.Routine Radiological Surveys of Auxiliary & Fuel Handling Bldgs Did Not Identify Any Significant Adverse Trends ML20206E4121999-04-27027 April 1999 Requests That TS Change Request 257 Be Withdrawn ML20206C5211999-04-23023 April 1999 Requests Mod to Encl Indemnity Agreement Number B-64,on Behalf of Gpu & Affiliates,Meed,Jcpl,Penelec & Amergen Energy Co,Llc.Ltr Supersedes & Withdraws 990405 Request Submitted to NRC ML20206C8261999-04-22022 April 1999 Submits Financial Info IAW Requirements of 10CFR50.71(b) & 10CFR140.21 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059H5351990-09-10010 September 1990 Forwards Encls 1-3 of Generic Ltr 90-07 Re Operator Licensing Exam Schedule ML20059G0641990-08-31031 August 1990 Advises That Util Agreed to Revised Frequency of Once Every 12 Months for Corrective Actions Audits Per Tech Spec Change Request 65 Based on 900718 & 19 Discussions ML20059F1691990-08-30030 August 1990 Requests Exemption from Requirements of 10CFR50,App J, Section III.D.1(a) for Facility Re Schedule Requirements for Connecting Type a Testing w/10-yr Inservice Insp Interval, Per 10CFR50.12(a)(2) ML20064A4661990-08-30030 August 1990 Responds to 900803 SALP Rept 50-289/89-99.TMI Does Not Expect to Be Lead Plant for Installation of Advanced Control Sys.Maint Backlog Goals Established.Info on Emergency Preparedness & Engineering/Technical Support Encl ML20059C8791990-08-29029 August 1990 Forwards TMI-1 Semiannual Effluent & Release Rept for Jan - June 1990, Including Executive Summary of Effluent Release Rept,Disposal & Effluent Release Data & Assessment of Radiation Doses.No Changes to ODCM for Reporting Period ML20059D5491990-08-29029 August 1990 Responds to NRC Re Notice of Violation & Proposed Imposition of Civil Penalty Re Personnel Inattentiveness & Failure of Site Managers to Correct Condition.Shift & Immediate Supervisor Discharged ML20059C7851990-08-27027 August 1990 Forwards Rev 5 to Sys Description 3184-007, Solid Waste Staging Facility, Updating Minor Changes to Pages 6,8,9 & 13 ML20059C1091990-08-24024 August 1990 Forwards Rev 6 to Physical Security Contingency Plan.Rev Withheld ML20059B8251990-08-24024 August 1990 Forwards Payment of Civil Penalty in Amount of $50,000,per NRC ML20056B4651990-08-20020 August 1990 Corrects Statement Made in 900716 Response to NRC Bulletin 90-001, Loss of Fill-Oil in Rosemount Transmitters. Identified That Only Half of Operating Crews Provided W/ Briefing on Bulletin ML20058Q1851990-08-17017 August 1990 Requests That Distribution List for TMI-2 Correspondence Be Updated to Be Consistent W/Recently Implemented Organizational Changes.Ee Kintner,Mb Roche & Wj Marshall Should Be Deleted ML20058Q1721990-08-13013 August 1990 Forwards TMI-2 Effluent & Offsite Dose Rept,First Quarter 1990, Update ML20058Q1821990-08-13013 August 1990 Advises That Util Will No Longer Provide Annual Update to Dewatering Sys for Defueling Canisters Sys Description,Per NRC .W/Completion of Defueling & Shipment of All Defueling Canisters Offsite,Sys Has Been Deactivated ML20058M7201990-08-0303 August 1990 Forwards Rev 2 to TER 3232-019, Div Technical Evaluation Rept for Processed Water Disposal Sys. Mods Include Elimination of Pelletizer & Relocation of Druming Station to Discharge of Blender/Dryer ML20055J4581990-07-27027 July 1990 Responds to Violations Noted in Insp Rept 50-289/90-10. Corrective Actions:Missing Support Brace on Cable Tray Support Found & Corrected ML20055J4561990-07-27027 July 1990 Advises That Info Contained in Generic Ltr 90-06,not Applicable to Current Nonoperating & Defueled Condition of Facility.Generic Ltr Will Be Reevaluated,If Decision Made to Restart Facility ML20055H6901990-07-20020 July 1990 Forwards Rev 25 to TMI-2 Organization Plan for NRC Review & Approval.Rev Proposes Consolidation of Plant Operations & Maint Sections Into Plant Operation & Maint Section ML20055G4431990-07-19019 July 1990 Forwards Rev 12 to 990-1745, TMI-1 Fire Hazards Analysis Rept & Update 9 to FSAR for TMI-1 ML20055G8781990-07-19019 July 1990 Discusses Compliance W/Reg Guide 1.97 Re Containment High Range Radiation Monitors,Per 900507-11 Insp.Physical Separation of Power Cables & Required Isolation Will Be Provided to Satisfy Reg Guide Category 1 Requirements ML20055F9601990-07-11011 July 1990 Forwards, 1990 TMI Nuclear Station Annual Emergency Exercise Scenario to Be Conducted on 900912.W/o Encl ML20044A9531990-07-0909 July 1990 Forwards Util Response to Weaknesses Identified in Maint Team Insp Rept 50-289/89-82.Corrective Actions:Engineering Personnel Reminded to Assure Documented Approval Obtained Prior to Proceeding W/Work ML20055E0481990-07-0505 July 1990 Documents Action Taken by Util to Improve Heat Sink Protection Sys & Current Status of Sys.Main Feedwater Logic Circuits Modified Prior to Startup from 8R Outage to Eliminate Potential for Inadvertent Isolation ML20055E0011990-07-0202 July 1990 Forwards Revs 1 & 2 to Topical Rept 067, TMI-1 Cycle 8 Core Operating Limits Rept, Per Tech Spec 6.9.5.4 ML20055C9971990-06-28028 June 1990 Forwards Rev 27 to Physical Security Plan.Rev Withheld ML20055D2071990-06-28028 June 1990 Forwards Certification of TMI-1 Simulation Facility,Per 10CFR55.45.b.5.Resumes of Personnel Involved Encl. Resumes Withheld (Ref 10CFR2.790(a)(6)) ML20055D0861990-06-25025 June 1990 Documents Deviation from Requirements of Reg Guide 1.97,per Insp on 900507-11.Based on Most Limiting Analysis,Existing Range of 0-1,200 Psi Sufficient.Deviation Consistent W/B&W Owners Group Task Force Evaluation of Reg Guide ML20043H4851990-06-18018 June 1990 Forwards Application for Amend to License DPR-50,consisting of Tech Spec Change Request 179 ML20043H4031990-06-18018 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issue Resolved W/Imposition of Requirements or Corrective Actions. ML20043F9921990-06-11011 June 1990 Forwards Listing of Exam Ref Matl Sent on 900601 in Response to 900505 Ltr ML20043F0661990-06-0404 June 1990 Forwards Inservice Insp Data Rept for Period 880816-900304. Owner Rept for Repairs or Replacements Performed on ASME Section XI Class 1 & 2 Components,Also Encl ML20055C9041990-05-23023 May 1990 Advises That App a to Rept Is Set of Recommendations from Safety Advisory Board on Possible Research Opportunities ML20043B2391990-05-18018 May 1990 Revises Commitments in Encl Met Ed 800430 Ltr Re QA of Diesel Generator Fuel Oil.Requirement for QC Review for Acceptability Prior to Filling Diesel Generator Fuel Oil Storage Tanks Deleted from Procedure ML20043A5441990-05-16016 May 1990 Discusses Status of Safety & Performance Improvement Program Portion of B&W Owners Group EOP Review Project ML20043A5311990-05-15015 May 1990 Responds to Violations Noted in Insp Rept 50-289/89-82. Corrective Actions:Periodic Insp Program Established Utilizing Checklist for Stored Equipment & Existing Tool Rooms Will Be Purged of Controlled or Unneeded Matls ML20043A2321990-05-11011 May 1990 Forwards TMI-1 Reactor Bldg 15-Yr Tendon Surveillance (Insp Period 5) Technical Rept 069.Evaluations Conclude That Test & Insp Results Demonstrate TMI-1 Reactor Bldg post- Tensioning Sys in Good Condition ML20042G2741990-05-0404 May 1990 Forwards Semiannual Update of Projects Listed in Categories A,B & C of long-range Planning Program Integrated Schedule ML20012F2621990-04-0202 April 1990 Responds to Violation Noted in Insp Rept 50-289/89-26. Corrective Actions:Util Policy of Shift Supervisor Involvement in Bypassing & Resetting Safety Sys Expanded to Include Shutdown Conditions & Technicians Briefed ML20012F2611990-04-0202 April 1990 Provides Supplemental Response to Station Blackout Rule. Target Reliability of 0.975 Chosen for Emergency Diesel Generators.Diesel Generator Reliability Program May Change Based on Final Resolution of Generic Issue B-56 ML20012F2731990-03-30030 March 1990 Confirms 900328 Conversations & Provides Technical Basis for Planned Actions to Correct Present Power Limitation Due to High Steam Generator Secondary Side Differential Pressure. Main Turbine Will Be Tripped from 80% Power ML20042D8281990-03-23023 March 1990 Fulfills Requirements of Tech Spec Section 4.19.5.a Re once-through Steam Generator Tubes post-inservice Insp Rept for Unscheduled Outage 8U-1 ML20012D7001990-03-22022 March 1990 Forwards Util Response to Generic Ltr 90-01 Re NRC Regulatory Impact Survey.Site Mgt & Staff Hour Categories Added to Response ML20012D7121990-03-21021 March 1990 Forwards Rev 0 to TMI-1 Cycle 8 Core Operating Limits Rept. ML20012C4771990-03-12012 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' Per 10CFR50.54(f). Current Design Adequate W/O Addl Tech Specs ML20012B8241990-03-12012 March 1990 Forwards Application for Tech Spec Change Request 199 to License DPR-50,revising Tech Specs Re Steam Generator Tube Insp Requirements ML20055C3931990-02-23023 February 1990 Documents Interpretation of Tech Spec 4.19.5.a Re once- Through Steam Generator Tube post-inservice Insp Rept for Refueling Interval 8R.Total of Eight Tubes Removed from Svc by Plugging ML20011F5251990-02-23023 February 1990 Documents Interpretation of Tech Spec 5.3.1.1 Re Design Features of Fuel Assemblies in Light of Issuance of Generic Ltr 90-02.Tech Spec Change Request Re Utilization of Dummy Fuel Rods or Open Water Channels Will Be Filed by 900420 ML20011F6651990-02-22022 February 1990 Forwards Updated Status Summary of Consideration of TMI-1 PRA Recommendations as of 891231.Changes to Torque Switch Settings for DH-V-4A & B Will Be Implemented in Refueling Outage 8 Re Closing Against High Differential Pressure ML20006C2901990-01-26026 January 1990 Provides Addl Info Supporting Deferral of Seismic Qualification Util Group Walkdowns to 10R Outage.Performance of Walkdowns Provide Proper Scheduling & Priority for Resolution of USI A-46 for TMI-1 ML20011E1221990-01-26026 January 1990 Forwards Response to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Audit Rept Determined That Operation of Decay Heat Closed Cooling Water Sys Consistent W/Design Basis Documents ML19354E8601990-01-25025 January 1990 Requests Approval for Use of B&W Steam Generator Plugs Mfg W/Alternate Matl (nickel-base Alloy/Alloy 600).Alloy 600 Has Superior Corrosion Resistance to Primary Water Stress Corrosion Cracking 1990-09-10
[Table view] |
Text
.
GPU Nuclear Corporation Nuclear :::,ome::rteo s
Middletown, Pennsylvania 17057-0191 717 944 7621 TELEX 84 2386 Writer's Direct Dial Number:
April 17,1986 5211-86-2055
(
Dr. Thomas E. Murley Region I, Regional Administrator U.S. Nuclear Regulatory Commission 631 Park Averue King of Prussia, PA 19406
Dear Dr. Murley:
Three Mile Island Nuclear Station Unit 1 (TMI-1)
Operating License Ho. DPR-50 Docket No. 50-289 10 CFR 50.59 Report for 1985 In accordance with the requirements of 10 CFR 50.59, enclosed are two copies l of changes to TMI-l Systems and Procedures as described in the FSAR.
l Sincerely, I
l . D. H ll Director, TMI-1 HDH/SM0/spb cc: Director, Office of Inspection & Enforcement Document Control Desk (40 copies)
J . F. Stol z 0541 A l
nrosenM8Tr P
i I g
'O GPU Nuclear Corporation is a subsidiary of the General Public Utilities Corporation ,
r 1
Modification: B/A 412471 - Qualified Transmitters for Containment Spray Flow Description of Modification:
This modification consisted of replacing the Containment Spray Flow Transmitters with environmentally qualified transmitters. The modification was minor in nature and resulted in the same configuration for measuring flow as existed with the original transmitter.
Safety Evaluation Summary:
The replacement transmitters are fully compatible with those that were originally installed. Therefore, the functions and basic configurations remain the same. Thus, this modification does not reduce the margin of safety of the TMI-l plant as described in the FSAR.
4
Modification - B/A 412483 BWST/SHST D/P Transmitter Mod Description of Modification:
This modification replaced LI-819 with a Rosemount D/P transmitter DPT-819.
The output of DPT 819 was connected to the computer using existing wires previously utilized for the sodium thiosulfate level. In addition, a new power supply for the Rosemount transmitter was added to the NNI cabinets. A local pressure gauge was added to the sodium thiosulfate tank for determining level if required in the future.
Safety Evaluation Summary:
The containment building spray system at TMI-1 takes a suction on both the Borated Water Storage Tank (BWST) and Sodium Hydroxide Storage Tank (SHST) during an accident. In order to ensure that pH and boron concentration values are within the proper range during spray injection, it is required that the two tanks drain down properly. Draw down analysis has shown that proper draindown under all single failures requires the tank levels to be precisely maintai ned. Technical Specification limiting condition for operating (LCO 3.3.1.3.b) requires that SHST be 8' + 6" lower than the BWST. The reactor shall not be made critical unless this LCO is satisfied and is to be shutdown to cold shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> if the LCO is not satisfied for a continuous period of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
Replacing LI-819 provides a D/P transmitter which is less susceptible to transient and reverse pressure breakdown. This mod provides computer pt.
readout as opposed to requiring an operator to go to the BWST tunnel to take a reading. Providing accurate control room readout of differential level and appropriate operating procedures to periodically check to see that LCO is met provide the lowest risk that TMI-1 will not inadvertently violate the LCO. It also provides the best assurance that violating the LCO will be detected promptly. Thus, this modification does not reduce the safety of the plant as described in the FSAR.
Modification: High Range Containment Area Monitor, EQ Upgrade Description of Modification:
This modification installed new environmentally qualified triaxial cables and connectors in an existing conduit between the RB penetrations and the High Range Containnent Radiation Detectors (RMG-22 & RMG-23). A qualified environmental seal between the connectors and the penetration was provided.
Safety Evaluation:
This modification enhances the safety of the plant by installing triaxial cables inside containnent which are qualified to 10 CFR 50.49 for the High Range Rad Monitors RMG-22 and RMG-23, and sealing off the detectors from the LOCA steam environnent thereby assuring their operation during and af ter accident conditions. There are no unreviewed safety questions as a result of this modification.
~
- Modification: B/A 412468 - Qualified Decay Heat and HPI Flow Indication Description of Modification:
This modification consisted of replacing the Decay Heat Removal, the HPI and the RC Pump Seal Return Flow transmitters with environmentally qualified transmitters. The Makeup Tank Level transmitter was also replaced with an environmentally qualified transmitter. The modification was minor in nature and resulted in the same configuration for measuring flow and level es existed with the original transmitters.
This modification also included replacement of the Decay Heat Coolers Outlet temperature and the Incore Thermocouple Cold Junction Compensation Temperature RTDs with environmentally qualified RTDs. There was no other change to the system and, therefore, the temperature measurement configuration remained the sa me.
In addition to the above, the Makeup Pump Auxiliary lube oil pressure switches were replaced with environmentally qualified pressure switches. There was no other change to the system and, therefore, the system operates the same as with the original switches.
Safety Evaluation Summary:
The equipment that was replaced is fully compatible with those in the existing systems. Therefore, the functions and basic configurations remain as originally designed. Thus, this modification does not reduce the margin of safety of the TMI-1 plant as described in the FSAR.
Modification - Fire Detection System Modification in the Auxiliary Building (B/A 412388 Phase III)
Description of Modification:
Seventeen ionization (smoke) detectors were added in the Auxiliary Building to comply with the requirements of 10 CFR 50 Appendix R. The smoke detectors are monitored by the existing / iliary Building ionization detector control panel on the Auxiliary Building ? elevation (fire zone AB-FZ-6). This existing control panel provides a loco, alarm and relay contacts for remote alarms in the TMI-l Control Room. Ten of the ionization detectors are installed in the heat exchanger vault (fire zone AB-FZ-1) over cable trays containing circuits required for safe shutdown. Seven ionization detectors are installed in the north end of the Auxiliary Building elevation 281' (fire zone AB-FZ-5) in the area adjacent to fire zone AB-FZ-4 and in the corridor leading to the heat exchanger vault. The existing control panel is equipped with a four-hour self-contained emergency power supply.
Safety Evaluation Summary:
Installation of the seventeen ionization smoke detectors neets a commitment made to the NRC in GPUN Report "TMI-l Fire Hazards Analysis Report and Appendix R Section III G Safe Shutdown Evaluation." The ionization detectors installed are commercial grade equipnent. The engineering and installation was performed as Inportant to Safety (ITS). All equipment is seismically mounted so as not to create a missle hazard. The probability of occurrence, or the consequence of an accident or malfunction of equipment previously evaluated in the Safety Analysis Report has not been increased. It is, therefore, concluded that the subject modification does not involve an unreviewed safety operation ~ per the criteria of 10 CFR 50.59.
=
- - - - - _- , - m .--- .v..
Modification - 480V ESV Control Center Firewall (8/A 412387)
Description of Modification:
A one hour rated firewall was installed between switchgear 480 VAC ESV CC 1 A and 480 VAC CC 1B. This equipment is located at floor elevation 305' in the Auxiliary Building.
This firewall was installed in order to comply with NRC requirement 10 CFR 50, Appendix R, Sections III G, J, and O. It separates redundant Nuclear Safety Related motor control centers which are located in the same fire zone and which are needed to bring the plant to safe shutdown.
Safety Evaluation Summary:
The engineering and installation of this firewall were performed as Important to Safety. It is seismically qualified. The probability of occurrence, or the e cuences of an accident or malfunction of equipment previously eval- :n the Safety Analysis Report has not been increased. This mot on does not involve any unreviewed safety questions per the criteria of lb 50 "" .
E T
- , _ - - ~_ _ _ _ . . _ _ . . _ _ _ . , . - _ _ __
Modification - Removal of THI-l Fluid Block Tanks and Foundations Description of Modification:
The Fluid Block tanks, foundations and local piping and instrumentation have been renoved from the Intermediate Building. The piping and instrument lines were cut and capped with threaded caps. The electrical connections for the two Fluid Block tank main control room alarms were cut and labeled as spares and annunciator windows left blank. The control instrumentation for the tank and valves was also removed. The renoval of the Fluid Block tanks and foundations provided much needed extra space at the entrance to the Reactor Buil ding.
Safety Evaluation Summary:
Amendment No. 93 to the TMI-1 Technical Specifications removed all discussions of the Fluid Block System from the Technical Specifications. The system's original design basis had been to ensure that certain lines penetrating the containnent are pressurized with fluid to provide a seal against leakage of the containment atmosphere to the environment during any condition requiring containnent isolation. Since then, the penetration isolation valves served by the Fluid Block System have been tested to the requirements of 10 CFR 50 Appendix J. This means the Fluid Block System is no longer necessary for containment isolation. The removal of the tanks, foundations and accessories was performed to the required TMI procedures.
As a result, the probability of occurrence or the consequence of an accident or malfunction of equipment previously evaluated in the Safety Analysis Report has not been increased. This modification does not involve an unreviewed safety question per the criteria of 10 CFR 50.59.
Modificatio_n - Small Tool Decontamination Trailer Ventilation System (B/A 412261)
Description of Modification:
This modification converted the temporary ventilation system for the Small Tool Decontamination Trailer into a permanent installation. The permanent system utilized new ductwork from the roof openings of the Decon Trailer, through the opening in the west wall of the Auxiliary Building, to the connection with the Auxiliary / Fuel Handling exhaust duct.
Safety Evaluation Summary:
The Small Tool Decon Trailer ventilation system collects air from the Decon Trailer laboratory hoods and directs it into th.e Auxiliary Building returr air ductwork. It then mixes with other plant exhaust air and flows through the Auxiliary / Fuel Handling Building charcoal filter before being discharged to the atmosphere through the main plant vent. This modificatf or, ties the Decon Trailer ventilation system to the Auxiliary / Fuel Handling Building ventilation system, such that the approximately 2500 cfm design flow is provided by the main plant exhaust fans AH-E-14A-D. The ventilation requirements for the Decon Trailer are within the design basis for the Auxiliary / Fuel Building ventilation system and thus will not impact the existing system. The modification's design and installation criteria meet the applicable TMI-l requirements.
As a result, the probability of occurrence or the congquence of an accident or malfunction 6f equipment previously evaluated in the Safety Analysis Report has not been increased. This subject modification does not involve an unreviewed safety question per the criteria of 10 CFR 50.59.
Modification - B/A 412325 - Chemical Addition Modification for the Waste Evaporator Condensate Storage Tank Description of Modification:
This modification provided chemical feed piping and equipnent for pH control of the liquid radwaste in the waste evaporator condensate storage tanks WDL-T-11 A/B. Prior to implementing this modification, chemical addition was accomplished by manual feed. A portable pumping unit and associated feed line were installed.
Safety Evaluation Summary:
This modification provided a permanent system for adding the required chemicals to control pH in the waste evaporator condensate storage tanks WDL-T-11 A/B. The modification complies with all applicable regulatory and system design requirements for TMI-1. Proper pH control is essential for the liquid radwaste system operation. This modification allows the pH to be controlled within the prescribed limits.
As a result, the probability of occurrence or the consequence of an accident or nelfunction of equipment previously evaluated in the Safety Analysis Report, has not been increased. It is, therefore, concluded that the . subject modification does not involve an unreviewed safety operation per the criteria of 10 CFR 50.59.
4 Modification - B/A 412172 - Liquid Radwaste Pungs WDL-P-14A/B Upgrade Description of Modification:
The existing liquid radwaste pumps WDL-P-14A/B were replaced with new larger capacity pumps (60 gpm vs. 30 gpm). The larger capacity pumps increase the capability to mix the waste evaporator condensate tanks WDL-T-ll A/B.
Thorough mixing is required to provide an accurate sample of the tank contents prior to transfer of the mixture and/or release to the environment.
Safety Evaluation Summary:
Replacement of the existing radwaste pumps WDL-P-14A/B improves the reliability and operability of the liquid radwaste punps. Insufficient mixing in Tanks WDL-T-ll A/B due to the undersized pumps has been eliminated by the higher capacity replacenent pumps. This ensures an accurate sample of the tank contents. The design and installation of the new pumps is consistent ifith the design basis for the liquid radwaste pumps.
As a result, the probability of occurrence or the consequences of an accident or nelfunction of equipment previously evaluated in the Safety Analysis Report, has not been increased. It is, therefore, concluded that the subject modification does not involve an unreviewed safety operation per the criteria of 10 CFR 50.59.
.m .
Modification - B/A 412291 - Chemical Addition Modification for Concentrated Waste Storage Tank Description of Modification:
This modification provided chemical feed piping and equipnent for pH control of the liquid radwaste in the concentrated waste storage tanks WDL-T-6A/8.
Prior to implementing this modification, chemical addition was accomplished by manual feed. A portable pumping unit and associated feed line were installed to introduce the required chemicals for pH control.
Safety Evaluation Summary:
This modification provided a permanent system for adding the required chemicals to control pH in the concentrated waste storage tanks WDL-T-6A/8.
The modification complies with all applicable regulatory and system design requirements for TMI-1. Proper pH control is essential for the liquid radwaste system operation. This modification allows the pH to be controlled within the prescribed limits.
As a result, the probability of occurrence or the consequence of an accident or malfunction of equipment previously evaluated in the Safety Analysis Report, has not been increased. It is, therefore, concluded that the subject modification does not involve an unreviewed safety operation per the criteria of 10 CFR 50.59.
Modification - B/A 412021 - Reactor Coolant System High Point Vents Description of Modification:
This modification f r. stalled 1/2" vent piping and valves at the following points in the Reactor Coolant System:
- The top of each Hot Leg (2 total)
- The top of the Pressurizer
- The top of the Reactor Vessel
- The top of the Reactor Coolant Drain Tank Piping for these vents is routed to various points outside the "D" ring where they discharge to containment atmosphere. The instrumentation and controls for these vents required installation of switches and position indication lights on panel "PC" in the control room. Each vent line is equipped with a differential pressure flow orifice and differential pressure transmitter which also provides indication to lights installed on panel "PC."
Safety Evaluation Summary:
The requirements for Reactor Coolant System Venting is documented in 10 CFR 50.44, NUREG 737 (Section II.B.1), and the TMI Restart Report (Section 2.1.2.2). All vents are located in the Reactor Building and are operable from the control room. This modification enhances plant safety by providing the capability of venting non-condensible gases from the Reactor Coolant System, thereby promoting natural circulation cooling and by increasing the plants ability to deal with large quantities of non-condensible gas.
All piping, valves, conduit and associated supports have been designed and installed in accordance with Seismic Category I criteria. Electrical and instrumentation installation is Class IE. The engineering and installation of this modification was performed as Important to Safety / Nuclear Safety Related. The probability of occurrence or consequence of an accident or malfunction of equipment previously evaluated in the Safety Analysis Report has not been increased. This modification does not involve an unreviewed safety question per the criteria of 10 CFR 50.59. '
- . . - - . - - -- - -- -_. _. - -~
- p. - . .
Modification - B/A 123100 - Diesel Generator Differential Relay Replacement Description of Modification:
INP0 SER 18-84 advised that General Electric Model CFD relays used for differential protection of the diesel generators are not seismically qualified. TMI-l used these relays in both diesel generators. As corrective action for LER 84-005-00 submitted August 15, 1984, the CFD relays have been re-placed with seismically qualified BBC 87M relays.
Safety Evaluation Summary:
This modification provides the resolution of LER 84-005 00. The replacement of the CFD relays does not degrade the 4KV engineered safeguards system. This modification does not constitute an unresolved safe question as defined by 10 CFR 50.59.
i l
i i
m Modification - B/A 412023 - Installation of Reactor Coolant Inventory Trending System (RCITS)
Description of Modification:
The water level trending portion of the RCITS reasures the water level from the bottom to the top of the reactor coolant loop A and B hot leg pipes and measures the water level from the bottom of the hot leg pipes to the reactor vessel head vent nozzle. This is accomplished by two differential pressure transmitters installed between an upper connection at the top of the steam generator hot legs and a lower connection upstream of the decay heat line isolation valve (DH-V-1), and by two differential pressure transmitters installed between an upper connection at the reactor vessel head vent valves and a lower connection upstream of valve DH-V-1. The upper connection for the r transmitters is equipped with a condensate pot and provides a water column reference leg for the transmitter. Resistance temperature detectors measure the temperature of the water in the reference leg. A thermocouple measures the temperature of the reactor coolant to compensate for density changes. The density compensated level output is displayed via the plant computer.
The void fraction trending portion of the RCITS transmits RC purp power signals to the plant computer where these are converted to void fractions via dn empirical algorithm utilizing RCP power, pump status and RCS cold leg temperature data. This is acconplished by four isolated signal transmitters mounted in the RCP Power Monitor Rack A which receive input from an existing
{ watt-transducer and provides a non-lE pump power signal to the plant computer.
_ Safety Evaluation Summary:
The RCITS provides a reans for the Control Room operator to monitor the water
. inventory of the Reactor Coolant System (RCS). The RCITS is operational when the reactor coolant pumps are on or off. Displayed water inventory data with the pumps off is useful as confirmatory information to other instrumentation
_ of conditions which ney interrupt natural circulation leading to a potential umdequate Core Cooling (ICC) event. The RCITS also provides a neans for the control room operator to monitor the void content of the RCS when the pumps
- a re ru nni ng. Displayed void fraction data provided by the RCITS will be
, useful as anticipatory information of conditions which may interrupt nornal E circulation.
r Note that this system is installed but is not operational pending NRC approval of operating requirements.
E E
P
=
Procedure M-155, Main Steam Relief Support System Clearance Readings Description of Procedure Change,:
Changed feeler. gauge length and thickness; provided allowance to perform measurements at 6 month intervals, instead of one month; specified area over which clearance readings must be within limits. -
Safety Evaluation Summary:
Results of testing during the Restart Test Program supported by engineering analysis provide assurance that these procedure changes achieve additional personnel safety without compromising the capability of the Main Steam Relief Support System to perform its safety function.
Procedure 1101-4, Balance of Plant Setpoints Description of Procedure Change:
Revise Setpoint cf MS-V6 (EF-P1 Steam Supply Pressure Regulating Valve) from 175 psig to 150-160 psig to prevent the periodic lif ting of MS-V228 (relief valve) when EF-P1 is operated on Main Steam.
Safety Evaluation Summary:
Analysis indicates EF-P1 will perform its design function at an inlet steam pressure as low as 140 psig. The 150-160 psig inlet steam pressure setpoint can produce the required 835 horsepower which is sufficient to deliver in excess of 400 gpm to the Once-Through Steam Generators.
1 i
i
m .
Procedure 1101-1, Plant Limits and Precautions Description of Procedure Change:
Change maximum OTSG allowable operating range level limit from 82.5% to 92%
during power operations, to provide for apparent OTSG fouling.
Safety Evaluation Summary:
Analysis of Babcock & Wilcox and GPU Nuclear show that no unreviewed safety question is involved. An assuned inventory of 55,000 lbs was used for the Main Steam Line Break analysis in the FSAR, and is greater than the total inventory in the steam generator as calculated for a steam generator with 1,217 tubes removed from service and operated at 92% operating range level. A small percentage increase in true inventory in the steam generator due to tube plugging and operating level increase will not make the previous MSLB analysis invalid.