ML20151B380

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SALP 9 Board Rept 50-341/88-01 for Apr 1987 - Mar 1988
ML20151B380
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 07/11/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20151B378 List:
References
50-341-88-01, 50-341-88-1, NUDOCS 8807200347
Download: ML20151B380 (44)


See also: IR 05000341/1988001

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SALP.9-

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SALP BOARD REPORT.

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION III

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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

50-341/88001

Inspection Report No.

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Detroit Edison Company

Name of Licensee

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Fermi 2

Name of Fa:ility

April 1, 1987 through March 31, 1988

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Assessment Period

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8807200347 880711

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ADOCK 05000341

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TABLE OF CONTENTS

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I.

INTRODUCTION. . . . . . . .

1

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II. CRITERIA. . . . . . . . . . . . . . . . . . . . . . . . . . .

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III. SUMMARY OF RESULTS. . . . . . . . . . . . . . . . . . . . . .

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IV.

PERFORKANCE ANALYSIS. . . . . . . . . . . . . . . . . . . . .

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A.

Plant Operations . . . . . . . . . . . . . . . . . . . .

6

B.

Radiological Controls. . . . . . . . . . . . . . . ... .

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C.

Maintenance. . . . . . . . . . . . . . . . . . . . . . .

11

D.

Surveillance . . . . . . . . . . . . . . . . . . . . . .

14

E,

fire Protection.

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F.

Emergency Preparedness . . . . . . . . . . . . . . . . .

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G.

Security . .

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H.

Outages. . . . .

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1.

Quality Programs and Administrative

Controls Affecting Quality .

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J.

Licensing Activities

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K.

Training and Qualification Effectiveness . . . . . . . .

28

L.

Startup Testing

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H.

Engineerins/ Technical Support

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V.

SUPPORTING DATA AND SUMMARIES . . . . . . . . . . . . . . . .

36

A.

Licensee Activities. .

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B.

Inspection Activities. . . . . . . . . . . . . .

36

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C.

Investigation and Allegations Review.

38

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D.

Escalated Enforcement Actions. . . . . . . . . . . . . .

38

E.

Licensee Conferences Held During Assessment Period .

38

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F.

Confirmatory Action Letters . . . .. . .

40

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G.

Review of Licensee Event Raports,

and 10 CFR Part 21 Repor.s

Submitted by the Licensee. .

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H.

Licen si ng Acti vi ties . . . . . . . . . . . . . . . . . .

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INTRODUCTIDN

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data

on a periodic basis and to evaluate licensee performance based upon this

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information.

The SALP program is supplemental to normal regulatory

processes used to ensure compliance with NRC rules and regulations.

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SALP 1s intended to be sufficiently diagnostic to provide a rational

basis for allocating NRC resources and to provide meaningful guidance

to the licensee's management to promote quality and safety of plant

construction and operation.

An NRC SALP Board, composed of the staff members listed below, met on

June 14, 1988, to review the collection of performance observations and

data to assess licensee performance in accordance with the guidance in

NRC Manual Chapter 0516, "Systematic Assestment of Licensee Performance."

A summary of the guidance and evaluation criteria is provided in

Section II of this report.

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This report is the SALP Board's assessment of the licensee's safety

performance at Fermi 2 for the period April 1, 1987 through March 31,

1988.

SALP Board for Fermi 2 Station SALP 9 assessment:

NAME

TITLE

C. E. Norelius'

SALP Board Chairman, Direccor, Division

of Radiation Sefety and Safeguards

H. J. Miller *

Director, Division of Reactor Safety

E. G. Greenman*

Director, Division of Reactor Projects'

D. R. Muller *

Directo', , Project Directorate III-1,

NRR

T.

P..

Quay *

Project Hanager, NRR

R. C. Knop *

Chief, Projects Branch 3

W. G. Rogers'

Senior Resident Inspector

M. J. Virgilio

Acting Deputy Director, DRP

J. J. Stefano

Project Manager, NRR

L. Kelly

Project Manager, NRR

P. R. Pelke

Project Inspector

B. S. Mallett

Chief, Nuclear Materials and Safeguards

Brance

M. P. Phillips

Chief, Operational Programs Section

G. C. Wright

Chief, Opc ations Branch

R. L. Hague

Acting Chief, Technical Support Staf f

M. Scht.nacher

Chief, haaiological Effluents and

Chemistry Section

L. R. Greger

Chief, Facilities Radiation Protection

Section

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NAME-

TITLE

R. A.-Paul

Inspector, Facilities Radiation

Protection Section

G. L. Pirtle

Physical Security Inspector

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W. Snell

Chief, Emergency Preparedness Section

J. E. Focter

Inspector, Emergency Preparedness

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Section

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H. A. Walker

Reactor Inspector, Maintenance and

Outages Section

S. A. Reynolds-

Reactor Inspector, Maintenance and

Outages Section

J.-M. Ulie

Reactor Inspector, Plant Systems

Section

A. Dunlop

Reactor Engineer, Technical Support

Staff

' Voting Members

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II.

CRITERIA

The licensee performance is assessed in selected functional areas,

depending on whether the facility is in a construction, preoperational,

or operating phase.

Each functional area represents an area significant

to nuclear safety and the environment and corresponds to a normal

programmatic area.

Some functional areas may not be assessed because

of little or no licensee activities or lack of meaningful observations

in that area.

Special areas may be added to highlight significant

observations.

The following evaluation criteria were used in assessing each functional

area:

A.

Management involvement in ensuring quality.

B.

Approach to resolution of technical issues from a safety star.ipoint.

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C.

Responsiveness to NRC initiatives.

D.

Enforcement history.

E.

Operational and construction events (including response to, analysis

of, and corrective actions for).

F.

Staffing (including management).

However, the SALP Board is not limited to these criteria, and others may

have been used where appropriate.

Based upon the SALP Board assessment, each functional area evaluated is '

classified into one of three performance categories. The definitions

of these performance categories are:

_ Category 1:

Reduced NRC attention may be appropriate.

Licensee management

attention and involvement are aggressive and oriented toward nuclear safety;

licensee resources are ample and ef fectively used so that a high level of

performance with respect to operational safety and/or construction quality -

is being achieved.

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Category 2:

NRC attention should be maintained at normal levels.

Licensee

management 4ttention and involvement are evident and are concerned with

nuclear safety; licensee resources are adequate and are reasonably

effective so that satisfactory performance, with respect to operational

safety and/or construction quality, is being achieved.

Category 3:

Both NRC and licensee attention should be incrr r ^d.

Licensee

management attention er involvement is acceptable and cons

irs nuclear

safety, but weaknesse, are evident; licensee resources apt...

to be

strained or not effectively used, so that minimally satisfactory

performance, with respect to operational safety or construction, is being

achieved.

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Trend: The SALP Board may choose to include an assessment of the

performance trend of a functional area.

Normally, this performance trend

is only used where both a definite trend of performance is discernible to

the Board and the Board believes that continuation of the trend may result

in a change of performance level.

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The trend, if used, is defined as:

A.

Improving

Licensee performance was determined to be improving near the close

of the assessment period.

B.

Declining

Licensee performance was determined to be declining near the close

of the assessment period.

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III. SUMMARY OF RESULTS

Rating Last

Rating This

Functional Area

Period (SALP 8)

Period (SALP 9)

A.

Plant Operations

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B.

Radiological Controis

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C.

Maintenance

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D.

Surveillance

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E.

F're Protection

NR

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F.

Emergency Preparedness

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G.

Security-

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H.

Outages

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I.

Quality Programs and

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Administrative Controls

Affecting Quality

J.

Licensing Activities

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K.

Training and Qualification

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Effectiveness

L.

Startup Testing

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M.

Engineering / Technical Support

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NR = Not Rated

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IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

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Evaluation of this functional area was based on the resvits of

routine resident, region-based, NRC Restart Team, and Operational

Safety Team (OSTI) inspections.

Enforcement history consisted of nine violations. One Severity

Level III, four Severity Level IV and four Severity Level V

violations were associated with the operations area. A civil

penalty of $75,000 was issued for the Severity Level III

violation concerning a shift complement's inability to maintain

cognizance of plant parameters. This resulted in an unplanned

mode change.

The other violations were not as significant.

However, when viewed collectively they indicate a negative

trend showing a lack of attention to detail and poor

understanding of Technical Specification actions by operations

personnel. Almost all the violations were program implementa-

tion errors.

Most of the errors occurred during the performance

of Technical Specification mandated actions and activities

associated with valve lineups. The enforcement history

indicated a decrease in licensee performance from the previous

assessment period.

Four issues remained outstanding at the end of the assessment

period.

The first two issues are potential escalated

enforcement matters that involved a lack of organizational

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understanding of a Technical Specification support system, and

the adequacy of corrective actions associated with a previous

escalated enforcement violation.

The third issue arose late

in the assessment period and involves the scope of the valves

in the locked valve program. The final issue also occurred

late in the a ssessment period and involves instrument valve

lineup controls. The one outstanding issue from the previous

assessment period related to 50.59 was resolved by the issuance

of a notice of violation.

The reactor was critical for 4633.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of the assessment

period and the scram frequency was 1.29 scrams per 1000 critical

hours.

This is an improvement from the previous assessment

period.

Notwithstanding, nine unplanned shutdowns occurred;

six of which were reactor scrams. The majority of these

shutdowns occurred during the first half of the assessment

period, resulting in sporadic plant operations. Most of the

shutdowns were caused by design and personnel errors, and half

of the scrams were caused by rorsonnel errors. Approximately 23%

of the total LERs for this assessment period were associated

with this ;unctional area, with the majority of these involving

personnel errors.

The frequency of events increased during

plant outages.

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Three central areas were identified in the previous assessment

period as needing additional management attention.

The areas

were placing' equipment in service or out of service, taking the

appropriate actions mandated by the license for given equipment

conditions, and understanding the necessary Technical Specifica-

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tion support systems. To varying extents, all three of these

weaknesses were manifested again during this assessment period.

Management involvement to assure quality was ineffectiva in the

first half of the assessment period. Numerous instances of

personnel circumventing procedures and operator proficiency

deficiencies occurred.

Equipment was not placed or properly

maintained in service as evidenced by damage to the south

reactor feedpump turbine, steam binding of a heater feedwater

pump, and the High Pressure Coolant Injection (HPCI) test

return valve not being deenergized in the closed position

during system restoration activities.

Finally, an unplanned

mode change occurred through operator inattention.

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Short range improvement was noted following management changes

at the beginning of the second half of the assessment period.

Personnel circumventing procedures was significantly reduced

end an overall improvement in attention to detail was noted

due to management involvement.

However, an improper valve

lineup resulted in a draindown via RHR to the torus.

No major

equipment failures occurred while placing equipment in service

or out of service.

Extended plant operation was achieved for

the first time and permission was granted to ascend to 100% power.

However, similar problems to those in the previous assessment .

period appeared late in this assessment period.

Personnel did

not take the required Technical Specification actions as

reflected by HPCI not being placed in service at the correct

time during a plant startup and core spray header differential

pressure not being verified at the proper time interval. A

Technical Specification support system, Non-interruptible

Control Air Division I, became inoperable and a mix of

inadequate training and procedures did not alert operators

that a limiting condition of operation (LCO) was in effect.

Subsequently, the LCO was not met.

Licensee reviews have indicated a need for improvement in

the area of shift log keeping.

Reports to the NRC via the

Emergency Notification System (ENS) telephone were generally

appropriate and timely.

Shif t turnovers were consistently

thorough except for short term reliefs which we-e significantly

upgraded after the unplanned mode change.

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Technical resolution of issues from a safety standpoint varied.

Management exhibited a strong understanding of the issues but

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their response to those issues was not always adequate.

Long

term actions to improve operating procedures, procedural

compliance, and provide better insight and understanding of

Technical Specifications were slow in development and implemen-

tation. No actions were taken to ensure a more complete mix of

procedures / training of plant operators in the area of support

systems.

In contrast, corrective actions to the mode change

incident appeared thorough and timely.

Late in the assessment

period, management initiatives resulted in more thorough

evaluations of personnel errors to determine cause and

corrective action.

One of the most significant technical issues that arose during

the assessment period concerned deficiencies in the Technical

Specifications.

Present actions to review and assure proper

content of the Technical Specifications appear to be receiving

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appropriate management attention.

However, a final conclusion

can not be drawn until the Technical Specification Improvement

Program is concluded.

On-shift operations staffing was adequate with the licensee

continuing to staff six full shifts. All key positions were

filled. However, there was an identified weakness in the

experience level of the operations personnel with respect

to commercial Boiling Water Reactor (BWR) experience. This

weakness was counterbalanced somewhat by more experienced BWR

individuals being brought into senior operational management

positions.

Control room decorum and professionalism was

evident.

Shift personnel understanding of their duties and

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responsibilities was not always evident.

This was recognized

as a deficiency and operational standards were developed to

provide the necessary direction.

The development of the

operational standards is considered to be a positive licensee

initiative.

Li:ensee responsiveness to NRC initiatives was generally

adequate.

A letter midway through the assessment period from

the regional administrator requested the development of a

program to conduct training evolutions at power levels less

than 50's due to the minimal licensee performance observed by

the Operational Safety Team Inspection (OSTI).

The licensee

initiated a program that exceeded the NRC request. The operator

evolution evaluation program was established and provided a

baseline on which to judge operator performance.

Licensee

management worked closely with all operating shifts to develop

support for this program and to critique overall performance

on selected plant evolutions.

The program has been in effect

since November and will continue until at least completion of

the startup test program. Also, the operations engineer duty

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station was changed to be closer to the control room. Actions

taken dealing with operator rounds sheets and emergency

operator response to a loss of feedwater were other examples

of appropriate, timely action.

2.

Conclusion

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The licensee's performance is rated Category 3 in this area.

The licensee was rated Category 3 in the previous assessment

period.

3.

Board Recommendations

The SALP Board notes that while licensee performance has

generally improved during the assessment period, it appears

to be somewhat cyclical as highlighted by the standby liquid

control event which occurred subsequent to the assessment

period.

This indicates a need for improved team work,

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attention to detail, and procedural adherence.

B.

Radiological Controls

1.

Analysis

Evaluation of this functional area was based on the results of

six routine inspections performed during this assessment period

by regional inspectors and routine observations by resident

inspectors.

Enforcement history in this area was good; one Severity Level V

violation was identified during this period. Enforcement

history in the previous assessment period was similar with two

Severity Level V violations identified.

One LER was reported

in this area regarding personnel errors and inadequate

procedures which resulted in excess sodium pentaborate

concentrations in the Standby Liquid Control storage tank.

Staffing levels wa:e ample and qui.lifications appeared adequate

to implement the operational radiation protection and chemistry

programs. Operating radiation protection experience levels.are

understandably 109 due to plant newness.

Observation of

chemistry and radiation protection technicians and professional

staff performance during inspections indicated satisf actory

performance.

The radiological engineering staff continued to

provide assistance to the radiological control staff in identifi-

cation and resolution of technical issues. Only minimal staff

turnover was experienced; however, staff experience was weakened

by the losses of the Radiation Protection Manager (RPM) and the

chemistry supervisor.

NRC review determined that the licensee's

proposed replacement for the RPM did not meet the required

experience qualifications; subsequently, another staff health

physicist was appointed who met the qualifications.

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Management attention towards ensuring quality in this area was

evident and generally good.

Indications of corporate and

station management support for the radiological control program

included provisions for ample staff additions (contractors)

during the first major maintenance outage, acquisition of

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improved contamination monitoring equipment, and continued

support for the plant decontamination and tygon tubing removal

program.

In-line instrumentation appeared to be adequate for

monitoring the essential chemistry parameters, and improvements

were being considered; the laboratory was equipped with

state-of-the-art instrumentation. The licensee expended great

effort to improve reactor coolant water quality, which had been

degraded by demineralizer resin ingress.

These efforts greatly

reduced out-of-specification (005) time for conductivity, and

kept the cumulative 005 well within the limits allowed by the

technical specifications. While the licensee had not committed

to the BWR Owners Group Guidelines, the water chemistry control

program appears to be generally consistent with the guidelines

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as evidenced by licensee actions to reduce reactor power when

high sulfate levels were present during the last part of the

assessment period.

Licensee responsiveness to NRC initiatives was good. The hot

machine shop and tool crib contamination controls were upgraded,

including facility modifications.

The licensee continued to

improve the decontamination control program, the incident

report system, and egress controls. The chemistry group's

QA/QC program for the control of analytical measurements

appears to be adeqijate and has progressed satisfactorily

since the last assessment period. This program includes

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control charts of instrument performance checks,

interlaboratory comparisons, and technician testing programs.

However, improvement is needed to reduce the high biases

observed in interlaboratory comparisons of sodium, low level

boron, and copper.

The licensee's approach to resolution of technical _ issues has

generally been sound and timely with appropriate consideration

of radiological safety. The licensee is implementing a prograr,

for "hot particle" training, ioentification, and control, and

has strengthened the surveiliance/ calibration program for

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effluent monitoring. ALARA program initiatives were evident

during the two outages during this period.

Personnel

contaminations and cumulative doses (person-rems) were very

low during the assessment period due to a combination of good

licensee performance and limited operating history.

Radiological ef fluents were also very low, reflective of the

limi+.ed plant operating history. One minor transportation

problem was identified.

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Radiological confirmatory measurements showed weaknesses, with

only 76 agreements in 104 comparisons. The discrepancies

occurred mainly in the backup detectors and appeared to be

related to improper calibration, software problems, and lack

of intercomparison of the various detectors in the licensee's

interlaboratory comparison program. The results of the

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nonradiological confirmatory measurements program were generally

good, with only two disagreements with the NRC values in 27

comparisons.

However, some of the results had significant-

biases, and the analyst had difficulties in obtaining reliable

boron values.

These appeared to be due to deficiencies in the

use of performance check control charts, which are still under

development.

2.

Conclusion

The licensee's performance is rated Catepry 2 in this area.

The licensee was rated Category 2 in the previous assessment

period.

3.

Board Recommendations

None.

C.

Maintenance

1.

Analysis

Evaluation of this functional area was based on routine

inspections conducted by resident inspectors and two

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inspections conducted by region-based inspectors. Areas

examined included corrective and preventive maintenance.

Enforcement history consisted of four violations and a deviation

from Updated Final Safety Analysis Report (UFSAR) commitments.

The violations were categorized as three Severity Level IV and

one Severity Level V, which is an increase in violations from the

previous assessment period.

Two violations were programmatic

in nature and had potential safety implications. These

violations reflected a lack of implementation of a preventive

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maintenance program and numerous e u,tples where personnel

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failed to follow procedures.

The other violations were

isolated personnel errors of minimal safety significance.

The

destation was also programmatic and further emphasized the lack

of implementation of preventive maintenance in the area of

electrical circuit breakers and protective relays. Corrective

actions were initiated; however, the effectiveness of all these

actions has not yet been assessed.

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Management involvement and control in assuring quality in the

preventive maintenance area was lacking during the first part

of the assessment period. A preventive maintenance program

was established but there was insufficient management oversight

and direction in its implementation. inis resulted in a

significant percentage of preventive maintenance activities

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not being accomplished. Also a reactor shutdown was caused by

inadequate preventive maintenance scheduling for the reactor

recirculation M-G set brushes. Once identified as a problem

appropriate resources were applied resulting in considerable

improvement in this area by the end of the assessment period.

Management involvement in the corrective maintenance area was

mixed.

During the assessment period the material condition of

the facility improved primarily due to a maintenance outage

midway through the period which reduced the corrective

maintenance backlog from app-oximately 750 to 500. At the end

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of the assessment period, the licensee had a 6 to 7 week

backlog.

Nuisance annunciators continued to be reduced from

the previous assessment period.

However, one reactor scram was

caused by personnel not adbaring to procedures. Administrative

controls associated with lifted leads / jumpers were not always

adhered to.

There war little evidence of effective and efficient

pre planning of the Local Leak Rate Test (LLRT) outage from a

maintenance perspective.

For example, a number of electrical

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and mechanical maintenance procedures were poorly written and

often confused workers because of the numerous changes that

were required.

There was no evidence that the procedures were

validated prior to use. This contributed to the failure to

effectively accomplish maintenance activities.

No discernible

decrease in the number of lifted leads and jumpers was noted

during the assessment period.

This particular area was

identified in the previous assessment as needing additional

management attention. Although some improvement was noted in

the utilization of equipment history, management involvement

was lacking as evidenced by the lack of complete and accurate

equipment history information for deferrals of preventive

maintenance activities.

There was one major positive management decision during the

this time frame.

The work package closure process was changed

to mandate a maintenance staff and quality assurance review

prior to submittal to the shift supervisor.

This one action

has provided an incremental increase in assuring safety at

the facility. The backlog of work packages needing final

review after work completion, which had significantly increased

in size three fourths of the way through the assessment period,

should be virtually eliminated due to a change in the allocation

of resources for closing these packages.

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The licensee approach to resolution of technical issues in

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the area of preventive maintenance was weak. Technical

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justification for deferral or reschHuling of preventive

maintenance activities lacked thoroughness and depth, and

in some cases, was marginal if not unacceptable.

Effects

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on system operability, availability or reliability were

not evaluated by engineering; instead emphasis appeared to

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be on scheduling and availability of personnel.

The status and portrayal of backlogged preventive maintenance

activities was not clear and understandable making management

overview of preventive maintenance corrective actions

difficult.

Some improvement was noted in this area during the

end of tne assessment period; however, resolution of the

preventive maintenance issue is a continuing process, and

significant NRC management attention was required to affect

changes initially.

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Resolution of corrective maintenance issues was better. The

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licensee suspended all maintenance activities when an NRC

inspection identified that personnel were not following

procedures.

This stop work stayed in effect until all

personnel were briefed on the necessity to follow procedures.

Changes to the deficiency notice tag system were comprehensive

and positive. While the stop work order was commendable,

previous management involvement had not been effective in

instilling procedural adherence.

Responsiveness to NRC issues was considered ineffective during

the first part of the assessment period.

The preventive

maintenance issue was considered as an unresolved item

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during an inspection in 1985 but the same problems still existed

in mid-1987. At the end of the assessment period there was

considerable improvement in this area; however, in some cases,

action by the licensee was still slow.

For example, when

problems were noted in following maintenance procedures, work

was stopped and the problem addressed immediately; however,

response was slow to a question about possible overpressurization

of an emergency diesel engine water jacket.

All key positions were filled during the assessment period.

The one vacant position from the previous assessment period,

Instrumentation and Control (I&C) Supervisor, was filled three

fourths of the way through the assessment period.

2.

Conclusion

The licensee's performance was rated Category 3 with an improving

trend in this area.

The licensee was rated Category 2 in the

previous assessment period.

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3.

Board Recommendations,

The SALP Board notes that the Category 3 rating is not

reflective of a decline in performance from the previous

assessment period, but indicates that the increased NRC

inspection activity during this period identified significant

concerns which previously went undetected.

D.

Surveillance

1.

Analysis

Evaluation of this functional area was based on routine

inspections conducted by resident, NRC contract and

region-based inspectors and observations by the OSTI members.

Enforcement history consisted of eleven violations and a

portion of another violation. Only one of these violations

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was a Severity Level V and rest of the violations were Severity

Level IV.

Six of the violations reflected inadequate technical

procedure content of which three were programmatic in nature.

Two violations were programmatic deficiencies associated with

the control of surveillance activities. Three violations and

a portion of another were implementation breakdowns.

Five

violations were identified in the previous assessment period.

The previous assessment reflected the need for improvement

in management's involvement to assure quality. The same

occasional procedural quality inadequacies and proficiency

deficiencies were apparent in this assessment period.

Examples *

of inadequate procedure quality were improper Reactor Core

Isolation Cooling (RCIC) and HPCI logic circuitry overlap

testing, inaccurate sodium pentaborate concentration acceptance

testing criteria, improper switch verification for offsite

power sources, and incomplete testing of the remote shutdown

panel transfer logic.

Examples of proficiency deficiencies

were failure to perform shiftly instrument checks and failure

to document the periodic reactor coolant leakage.

Regarding the licensee's approach to resolution of technical,

issues, during the first part of the assessment period, the

licensee performed a line by line verification that each

Technical Specification surveillance requirement was

encompassed in a surveillance procedure, began rewriting all

the I&C surveillance procedures including the addition of loop

sketches, and revised the scheduling process for partially

completed surveillance procedures.

Retraining and consulting

was administered to reduce personnel errors.

All these actions were to address deficiencies from the

previous assessment period and were generally insufficient

to prevent reoccurrence. After completion of the Technical

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Specification line by line verification, similar deficiencies

in the surveillance program were identified reflecting

inadequate implementation of the Technical Specification

verification. The partial surveillance procedure scheduling

effort was not broad enough to prevent other scheduling errors.

Personnel errors did not appear to decrease even with the

-

corrective actions taken as reflected by the operational events

and the enforcement history.

Certain personnel errors had the

potential for safety significance involving ESF actuations and

reactor scrams.

Personnel errors often involved disregard of

procedural guidance, or occurred as a result of technicians

following deficient procedures.

The one positive area was

the I&C rewrite effort which appeared to be coordinated and

comprehensive.

Potential escalated enforcement was identified

regarding the inadequate corrective actions to the surveillance

problems.

In the second half of the assessment period the licensee

-

established the Technical Specification Improvement Program.

This program is comprehensive and adequate for the problems

identified in this area.

In conclusion, the licensee's

approach to resolution of technical issues was lacking in the

first part of the assessment period and showed improvement in

the second half with additional emphasis still needed on the

personnel error aspect.

The licensee was generally responsive to NRC initiatives with

the establishment of the Technical Specification Improvement

Program in response to the October 9, 1987, letter from the

regional administrator on numerous problems includino the

-

surveillance area. This program has all the necessary elements

to significantly upgrade the quality of this functional area.

Subsequent to the assessment period, the licensee enhanced the

program to include surveillances of essential support systems.

Completion of the Technical Specification verification and

the I&C procedure rewrite effort were not consistent with the

time frame committed to by the licensee. Additionally, the

schedular commitments made by the licensee regarding the

Technical Specification Improvement Program reflect

shortsightedness by licensee management and a lack of

understanding of the complexity and scope of tne effort.

This has necessitated a request by the licensee to extend

the completion date for the program by six months beyond

the originally scheduled completion date.

Staffing to support the surveillance effort was adequate

with no problems noted in the implementation of the in service

test pump and valve performance area which was a concern from

the last assessment period.

Previous assessment problems with

clearly defining duties and responsibilities appeared corrected

except in the scheduling and tracking areas which continued to

15

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exhibit occasional deficiencies.

Examples of this problem

were in improper test interval established for a Standby Gas

Treatment System fire protection test, an improper test

interval established for containment integrity valve position

verifications and not performing a Control Center HVAC chiller

-

pump performance test on schedule.

2.

Conclusion

The licensee's performance is rated Category 3 in this area.

The licensee was rated Category 3 in the previou' assessment

period.

3.

Board Recommendations

The SALP Board notes that senior licensee management involvement

is required to maintain adequate resources to keep the Technical

Specification Improvement Program on schedule.

.

E.

Fire protection

1.

Analysis

The licensee's performance in the functional area of fire

protection was evaluated based on the results of one fire

protection programmatic inspection (which included a review

of previous inspection findings, the fire protection

organization, administrative controls, fire protection system

inspection, maintenance and tes: programs, quality assurance,

technical specification review, deviation event report review,

and other fire protect'on requirements review) during this

assessment period.

Two violations regarding the fire protection area (one Severity

level IV and one Severity Level V) were identified during this

assessment period. One violation was for failure to conduct

quarterly firc

rigade classroom instruction meetings (the

licensee was conducting these meetings once every two

years).

The other violation was for f ailure to maintain

a critical diesel fire pump discnarge ,alve locked.

No

violations were identified in the prev 1cus assessment period.

Management involvement in assuring quality in the decision

making process was adequate as demon,trated by the prompt

resolution of inspector concerns as discussed below.

The licensee's approach to the reso'ation of technical issues

from a safety standpoint was technt, ally sound and thorough.

For example, the licensee took the initiative in a timely

ma n.;c t to re-emrhasize to control room operators the

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requirement to follow the "Plant Fires" procedure for

immediately activating (assembling) the fire brigade following

receipt of an unplanned fire alarm.

The licensee's responses to NRC initiatives were generally

i

completed in a timely mannt* and an effort was made during

.

this assessment period to reso be outstanding fire protection

issues.

Two minor issue; from 1984 regarding the installation

of gauges in the Reactor Building and a revision to an

emergency lighting surveillance procedure were not completed

as scheduled; however, both were planned to be completed withiri

30 days following startup from the local leak rate testing outage.

The licensee has submitted two event reports regarding fire

protection program deficiencies.

Both cf these event reports

l

were promptly reported although minor information was lacking

l

for one of the reports which required a revision.

'

The licensee's f,re protection program is staffed with a

qualified fire protection engineer and a qualified fire

protection specialist whose responsibilities are well defined

l

and include the engineering aspects as well as the day-to-day

'

implementation of the fire protection program.

The licensee's fire brigsde training and effectivenest. were

l

evaluated during the programmatic review. As previously

I

mentioned, a violation an( both event reports related to fire

l

brigade training inadequacies. H) wever, an unannounced fire

drill was witnessed that demo'strated that adequate fire

brigada response, mannint. and donning of the proper fire

,

protective clothing (including breathing apparatus) was

performed in a timely mainer.

Fire detection and suppression equipment was generally well

maintained with hose stations properly staged, fire

extinguishers routinely inspected, fire detectors in service

and fire doors closed.

In the area of control of combustibles,

NRC plant tours and licensee inspection records reviewed during

the assessment period generally showed adherence by the licensee

to the fire protection administrative procedures.

However,

small amounts of combustibles were observed in the Reactor

Building during the plant shutdown due to ot) going painting

activities. These were properly controlled.

General housekeeping was above average with only extraneous

items such as tools or portable equipment, occasionally found

in the Reactor Building.

~

17

_ _ _ _ _ _ _ _ _ _ - _ _ - ____- ______

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2.

Conclusion

The licensee's performance is rated Category 2 in this area.

The licensee was not rated in the previous assessment period.

3.

Board Recommendations

_

None.

F.

Emeroency Preparedness

1.

Analysis

Evaluation of this functional area was based on two routine

inspections and one annual exercise inspection conducted by

regional-based inspectors during this assessment period.

No violations were identified during this or the previous

assessment period.

Four exercise weaknesses and six open

items were identified during the August 1987 annual exercise

inspection, indicating that exercise performance needed

improvement.

De weaknesses related to information flow to

the Technical Stpport Center, an unacceptable demonstration of

Assembly and Accountability, unapproved changes to the Post

Accident Sampling System procedure, and an unacceptable medical

drill.

A manageme1t meeting with licensee personnel was held

in November 1987, to discuss the corrective actions intended

for the exercise weaknesses and other actions for ovt - all

program improvement. A subsequent inspection confirmed that

aggressive correction actions were being taken regarding

identified weaknesses, and other program improvements were

actively being pursued.

Management involvement in assuring quality in this area was

good.

Some initial weaknesses were evident as indicated

by the four exercise weaknesses which were identified in the

annual exercise inspection, but corrective actions were

promptly initiated for problem areas, and subsequent program

enhancements were made.

Overall, the program continues to

improve.

In all cases, the licensee had been responsive to NRC initiatives

and concerns by providing viable, sound and thorough responses

in a timely manner.

The licensee's approach to resolution of

technical issues from a safety standpoint has remained cons.stently

good.

There were no long-standing regulatory issues attributable

to the licensee.

Staffing at the management level was unchanged.

In addition,

staff training and qualification effectiveness was good as

demonstrated by the lack of violations or significant

issues during the assessment period, and performance during

routine inspection walkthroughs.

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Subsequent to the assessment period, a successful emergency

exercise was held, demonstrating the effectiveness of

corrective actions made during the assessment period.

2.

Conclusion

The licensee's performance is rated Category 1 in this area.

The licensee was rated Category 1 in the previous assessment

period.

3.

Board Recommendations

None.

G.

Security

1.

Analysis

Evaluation of this functional area was based on the results of

five inspections (three onsite, two in-office) conducted by

region-based physical security inspectors and inspections

conducted by the resident inspectors to routinely observe

security activities. One onsite inspection was conducted to

support plant startup evaluation, and the other two onsite

inspections were routine in nature.

The in-of fice inspections

pertained to a review of the licensee's investigation of

allegations, and support to the Senior Resident Inspector on

a security issue.

Enforcement history has significantly improved during this

-

assessment period.

Three violations (two Severity Level IV

and one Severity Level V) were identified compared to eleven

violations curing the previous assessment period.

Although,

',

two of the violations were identified by the licensee and did

not represent a major safety concern, an Enforcement Conference

conducted on April 13, 1988, emphasized the need for increased

evaluation and oversight of the personnel access control program,

to correct programmatic weaknesses.

Staffing for the security section has also improved.

Permanent

assignments for the five department heads within the section

have been made and department responsibilities have been

clearly defined.

Key supervisory assignments for security

shift operations have also been made.

The primtry staff is

'

one of the largest in the region, and sustained improved staff

'

functions have been noted in reference to responsiveness to NRC

concerns, timely review and submittal of security plan changes,

<

and response to allegations.

The security training department

has also upgraded facilities during this assessment period.

Management involvement in assuring quality has improved during

this assessment period.

Self-audits by the security compliance

department have improved; root cause analysis is performed for

audit findings and security events; the Performance Indicator

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d

Program continues to be upgraded; and followup action on

inspection and audit findings is well documented.

Equipment

available to the security section is well maintained. Senior

plant management personnel take aggressive corrective actions

for personnel who cause security violations and exit meetings

are routinely attended by senior managers, up to the Group

-

Vice President level.

Senior managers are aware of significant

security issues and trends.

Technical issues are resolved in a timely and technically

correct manner.

Security plan submittals are detailed in

nature and complete.

Effective communication pertaining to

security issues exist between the licensee and NRC Region III

staff.

The security department is very responsive to NRC concerns.

Twelve of 13 inspection findings noted during the Regulatory

Effectiveness Review (RER) inspection, conducted in June 1987,

have been closed by the NRC, and licensee actions for the

remaining issue are adequate.

Some of the findings were

corrected during the RER inspection period.

Licensee

investigations pertaining to allegations have been thorough,

well documented, and timely.

Inspection concerns receive the

same leve' of management attention and action as violations.

Security ~.anagement is responsive to noted observations even

if they do not involve enforcement issues.

Procedural guidance for Security Event Reports (SERs) is detailed

and generally conforms to the guidance in the appropriate

regulatory cuide.

Thirteen SERs have been reported during this

assessment period, compared to nine in the previous assessment

period.

SER criteria changed in October 1987 and the licensee

has established a conservative approach to security event

reporting.

Eight of the thirteen SERs were caused by personnel

error, three were equipment-related, and the remaining two SERs

were beyond the licensee's control (bomb threat and contraband

found during vehicle search). The total

.7 umber of reported SERs

is not considered excessive. Two of the SERs resulted in

violations being cited.

Some security computer-related problems identified in inspection

reports still need to be fully resolved.

personnel security

screening and procedural deficiencies were noted during an

inspection conducted in March 1985 and require further action

action to resolve.

In summary, the improved trend in security performance can be

attributed to greater operational experience, an aggressive

self-audit program, effective root cause analysis for identified

problems, and a more stabilized management cadre within the

section.

20

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2.

Conclusion

The licensee's performance is rated Category 1 in this area.

The licensee was rated Category 2 in the previous assessment

period.

,

3.

Board Recommendations

None.

H.

Outaces

1.

Analysis

Evaluation of this functional area was based on routine

inspections conducted by resident inspectors. Areas examined

included steam line instrument tap repairs, Raychem heat

shrink inspections and repairs, block wall repairs, and

moisture separator reheater repairs.

Enforcement history in this area continued to represent

regulatory conformance.

No violations or deviations were

identified during this assessment period.

.

During the assessment period three outages in. excess of two

weeks occurred.

The first outage, early in the assessment

period, was to repair numerous steam line instrument taps that

were failing from vibration.

The second outage, midway through

the assessment period, was to improve overall material

condition of the plant.

However, problems were identified in a-

number of areas requiring modification / repair prior to plant

restart.

These areas included modification of the 72Cf swing

bus, examination and repair of heat shrink installations, repair

of emergency drain lines to the condenser, and installation of

additional bracing to select block walls.

The third outage,

in progress at the end of the assessment period, was to perform

local leak rate testing, eliminate backlogged preventative

maintenance activities, perform 18 month surveillances, and

complete select plant modifications.

Equipment damage was

identified af ter the shutdown involving major repair of the'

moisture separator reheater and a condensate pump.

No refueling

activities occurred during the assessment period.

Management involvement in assuring quality was generally

adequate.

All repair / modification activities were accomplished

satisfactorily.

Instructions for performing the modifications

were satisf actory for work performance. Documentation was

occasionally lacking.

Some modification work packages required

significant resources to assure the work was satisfactorily

accomplished after the equipment was in service. The 72CF

package was an example of this weakness.

Planning and

scheduling of testing was generally adequate as evidenced by

coordination for local leak rate tests.

In the last outage of

the assessment period, appropriate management planning was not

exhibited with regards to operating shif t work dynamics.

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Approach to resolution of technical issues from a safety

standpoint was evident.

Comprehensive actions were established

and implemented to resolve the Raychem splice, masonry block

wall, moisture separator reheater, and instrument tap problems.

Good corrective actions to work package documentation problems

_

were implemented with the establishment of quality "eviews

prior to submittal to the shift supervisor.

Eleven of the thirty five unplanned engineering safety features

(ESF) actuations occurred during outages.

Four of the ESF

actuations were personnel error related. This is an improvement

from the previous assessment period in terms of personnel

caused ESFs during outages. However, the licensee continues

to demonstrate a laxness in attention to detail that manifests

itself in an increase in events during plant outages. Continued

effort in this area is warranted.

2.

Conclusion

.

The licensee's performance is rated Category 2 in this area.

The licensee was-rated Category 2 in the previous assessment

period.

3.

Board Recommendations

None.

I,

Quality Programs and Administrative Controls Affecting Quality

1.

Analysis

,

The evaluation of this functional area addresses two related

but separate functions.

First, this assessment addresses the

licensee's internal independent oversight activities performed

by the quality control / quality assurance (0C/0A) organizations.

Secondly, this assessment addresses the effectiveness of

management's activities to achieve a high levei of performance

with respect to nuclear safety.

With respect to the evaluation of the licensee's internal and

independent quality oversight activities, results of routine

inspections conducted by resident, operational safety team

and region-based inspectors were considered. Areas examined

included quality verification methods, audit content,

documentation and frequency. Also cursory reviews of committee

activities and safety evaluations were performed by the

operational safety team.

Enforcement history consisted of one Severity level IV and one

Severity Level V violation.

Due to the inclusion of the new

Technical Support functional area a meaningful parallel between

the previous assessment period can not be drawn. The Severity

Level IV violation was for failure to verify compliance with

and determine the effectiveness of implementing the quality

22

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program, including failure to identify a significant condition

adverse to quality in an audited area. The Level V violation

included multiple examples of a failure to perform audits

within the periods specified by the Technical Specifications

and a procedural deficiency that allowed some of the noted

-

conditions to occur.

Corrective actions to all violations were

verified as acceptable.

One outstanding issue associated with

this area occurred late in the assessment period.

The matter

dealt with the onsite review committee approval of draf t

procedures. Due to this process, modifications were made to

some procedures changing their intent.

Regarding the licensee's internal and independent quality

oversight activities, management involvement and controls in

assuring quality appeared to be minimal during the first part of

the assessment period.

There was little evidence of management

reviews or efforts to ensure that audits were complete and

adequate, nor that noted problems were resolved in a timely

manner.

In some cases, audits appeared to be conducted merely

to fulfill audit requirements rather than to verify adequate

performance in functional areas.

In many cases, substantial

numbers of audit checklist items were not audited and no

evaluation was performed to determine the impact on the audited

area. With little or no justification, there were multiple

extensions granted to dates established for implementation of

corrective action.

Safety evaluations appeared weak and not

properly supportive of their conclusions.

During the second half of the assessment period, substantial

improvements were noted; for example, a new QA manager had been-

assigned and QA personnel were relocated inside the controlled

area, which provides improved access for verification of plant

activities. Management appeared to be concerned and actively

involved with the improvement of quality verification methods

and results.

Stricter controls were established on who could

review safety evaluations and additional training was given on

performing safety evaluations. One area where a weakness was

noted was QC inspectors.

The inspectors were not always aware

of procedural and acceptance criteria for maintenance activities

in progress; however, no problems were noted for inspection of

specific "hold" and "witness" points.

The approach to the resolution of technical issues was weak

during the first half of the assessment period. Audits were

concerned with compliance to procedures rather than with

technical aspects of the activities.

In several instances,

problems documented as observations, which required nt

corrective action, were actually valid audit findings.

23

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.

.

Considerable improvement was noted in this area during the

second half of the assessment period. However, in some cases,

conclusions were reached by the licensee in the evaluation of

audited conditions that did not appear to be substantiated by

the details included in the audit records. Methods of

_

preparing audit checklists had changed which appeared to make

the audits more performance-oriented. Additional management

reviews were evident, both before and after the audit.

Responsiveness to NRC initiatives was generally good.

Corrective actions to the problems in the audit area were

started imt.,ediately upon identification.

The proposed

resolutions were acceptable and accomplished in a timely

manner.

Staffing to perform required verification activities appeared

to be adequate.

Based upon a region-based inspection early in

,the assessment period there was a sufficient number of auditors

and certified lead auditors.

During an inspection late in the

assessment period, the licensee stated that 15 QC inspectors,

including some contract inspectors, were available to provide

QC coverage during the LLRT outage. This appeared to be

adequate based on a cursory review of the work to be performed.

With respect to the effectiveness of management's activities

to achieve a high level of performance, certain areas assessed

during this period, specifically emergency preparedners,

security and startup testing, the licensee achieved and

sustained a high level of performance with respect to nuclear

safety.

Management response was prompt and effective when

problems occurred or deficiencies were identified.

In certain other program areas such as plant operations,

maintenance, surveillance and engineering / technical support,

the licensee demonstrated minimally satisfactory performance

with respect to nuclear safety.

Management was ineffective in

its attempts to recognize and/or achieve sustained resolution

of deficiencies, many of which can be traced back through

several years of poor performance. At the onset of this

evaluation period, NRC and the licensee identified and

discussed weaknesses in each of these critical areas,

Operations and surveillance received a Category 3 rating

in SALP 8.

Maintenance and engineering / technical support

wet e the subject of NRC/ licensee management meetings following

inspections early in the assessment period, that identified

significant deficiencies.

From July 26, 1987 through August 7, 1987, NRC conducted a

special team inspection at Fermi, an Operational Safety Team

Inspection (OSTI).

The OSTI findings were discussed with the

licensee at the exit meeting. The team found no single root

cause.

Problems encompassed a broad range of activities

including operating practices, administrative controls,

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surveillances, training and the corrective action process.

In

general these findings supported previous assessments performed

by INPO, the Independent Overview Committee, NRC's restart team,

and the licensee.

A majority of these problems and deficiencies were evident

throughout the remainder of the assessment period.

Due to a

lack of attention to detail, personnel errors continued to

occur including the failure to comply with procedures.

Improvemente, in administrative controls, specifically the

Technical Specification Verification program and the I&C

procedure rewrite effort, suffered schedule slippages.

Deficiencies in the implementation of the surveillance program

continued throughout the assessment period. Design changes to

correct deficiencies that have caused repeated ESF actuations

during testing remain to be accomplished.

Closecut of LER

actions and assurance that actions taken in response to

Information Notices were not always perfo,med in a timely

.

manner. The deficiencies that resulted in the issuance of

$375,000 in civil penalties in July 1986 and a $100,000 civil

penalty in May 1987 were present throughout most of this

assessment period.

Early in the assessment period the licensee relied heavily on

improvement programs that were an outgrowth of lessons-learned

from events that occurred in 1985, at the time the full power

license was issued.

The Nuclear Operations Improvement Program,

Reactor Operations Improvement Prograv and Business Plans were

the licensee's road map to improved performanc.e.

However,

during this portion of the assessment period, while a general

improvement was noted, problems continued to occur intermittently

in areas specifically addressed by tnese programs which showed

demonstrated difficulty in achieving sustained improving

performance.

A number of changes occurred part way through the assessment

period that are beginning to have an everall positive impact

on performance.

Changes were made ir the plant manager, QA

manager and licensing supervisor positions to increase the

quality and experience leveis.

Additionally, the Vice

President of Engineering assumed an a:tive operational role,

and the I&C Supervisor position was filled.. Using new

techniques, the licensee performed m:re rigorous assessments

of events and identified problems to determine causes and

appropriate corrective actions.

The threshold to situations

requiring corrective action was lowe.ed and management

visibility of the probicm and corrective actions status has

been enhanced.

In addition, with regard to personnel performance

problems, accountability meetings anc disciplinary actions were

tools utilized to underscore management expectations.

In

parallel with these activities, in response to NRC initiatives,

25

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the licensee developed methods to better monitor performance of

operating crews, maintenance status, technical specification

improvement program progress and the status of implementation

of commitments to the NRC.

_

In summary, management has not been effective in its ability

to sustain improved performance above that considered minimally

acceptable to the NRC.

Extensive NRC oversight and involvement

was required to overcome licensee shortcomings and reactive

response to problems. Although less significant and frequent,

deficiencies were evident in personnel performance, administra-

tive controls and plant hardware at the end of the evaluation

period.

2.

Conclusion

The licensee's performance is rated Category 3 with an improving

trend in this area. The licensee was rated Category 2 in the

.

previous assessment period.

3.

Board Recommendations

The SALP Board recognizes a positive improving trend in

performance due in part to the new management team's efforts

and the acquisition of new management talent in key areas.

J.

Licensing Activities

1.

Analysis

Evaluation of this functional area was based on the licensee's'

performance in support of licensing actions. The items

evaluated were 10 Technical Specifications changes, two relief

requests, one exemption request and followup activities

associated with a Detailed Control Room Design Review / Safety

Parameter Display System (DCRDR/SPDS) audit from the last

,

'

assessment period.

The project managers and applicable NRR

technical reviewers performed the evaluation.

One Severity Level V violation was identified for failure to

l

submit a Technical Specification change request to reflect

l

changes in offsite and unit organizations.

No violations

!

were identified in the previous assessment period.

f

The licensee management's role in assuring quality in licensing

related activities continued to improve during the period.

Licensee submittal quality during the initial portion of the

period was less than desired until the hiring of a new licensing

supervisor.

This supervisor worked closely with NRR to promote

a better working relationship and improvements continued.

Recent submittals have been generally clear and of higher

quality.

Licensee submittals however, have generally been

26

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untimely, resulting in the need for the staff to expedite

several reviews. This is due in part to some lack of planning

by the licensee as well as some problems identified during

operation.

However, toward the end of the period, the licensee

has demonstrated a willingness to meet with NRR on short notice

to better coordinate the scheduling of licensing activities.

Many of the licensing activities during this period have been

related to startup issues and the Technical Specification

improvement program.

Because of this program, the volume

of Technical Specification change requests during this

period has been unusually high and is expected to remain high

until the end of the program which is scheduled for completion

in December 1988.

Management appears to be taking a more direct role in licensing

activities; however, there is still a need for improvement in

the planning and timeliness of licensing submittals.

,

The licensee's approach to resolution of technical issues has

shown some improvement in that the licensee has usually

demonstrated an understanding of the technical issues involved

in licensing activities and proposed acceptable resolutions.

During the period, significant progress was made on the DCRDR

and SPDS and the licensee's submittals on these subjects tre

currently under staff review.

The quality of licensee submittals has also improved during the

period as has the licensee's approach toward resolution of

technical issues. The licensee is demonstrating far greater ,

interest in resolving technical issues and has taken the initiative

in contacting NRC.

Licensee submittal quality can still be

improved.

The licensee's responsiveness to NRC initiatives improved

during the period.

In response to concerns identified by the

NRC, the licensee made submittals to correct deficiencies in the

SPDS and DCRDR that were identified during an audit at the very

end of the previous period.

Licensee efforts during this

period have these issues on the path tc,<ard resolution. During

the latter portion of the period, the licensee has responded

promptly and accurately to information requested by the staff.

The licensee has provided appropriate members of their

organization at meetings with the staff.

In addition, the

licensee has hired a new plant manager and licensing supervisor.

The licensing supervisor has extensive background and

experience in licensing. These individuals have improved the

licensee's performance in licensing activities. The licensing

staff is located in the Nuclear Operations Center (NOC). The

NOC is located on the Fermi-2 site a nd consequently, the

proximity of the licensing staff to the plant appears to be

a significant advantage.

27

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2.

Conclusions

'

The licensee's performance is rated Category 2 in this

area. The licensee was rated Category 2 during the previous

assessment period.

~

3.

Board Recommendations

None.

K.

Training and Qualification Effectiveness

1.

Analysis

Evaluation of this functional area was based on the results of

licensed operator examinations administered to six candidatos,

one special inspection to evaluate the adequacy of the

impleaientation of the licensed operator requalification program,

and observations by resident, Operational Safety Teans and

region-based inspectors while inspecting other functional areas.

Three apparent violations were identified during the assessment

period associated with the operator requalification program.

The severity level of these violations was under consideration

at the end of the assessment period. The licensee took

comprehensive corrective actions addressing each of the

potential violations.

Further, the licensee presented their

corrective actions and implementation schedule to the NRC in a

meeting held on June 9,1987.

NRC review determined that the

corrective actions were adequate; however, followup inspection

in the area was not conducted in that the violations have not

yet been issued and as such, a formal response from the

licensee has not been required. A violation related to

training is discussed in the Fire Protection functional area.

No violations were identified in the previous assessment period.

As discussed in the previous assessment period an inadequate level

of management attention to the operator requalification training-

aspect of this functional area was evident. Management

involvement in this area was subsequently increased and tighter

administrative controls were established.

The inadequacies in the operator requalification program

resulted in the issuance of a Confirmatory Action Letter (CAL).

The CAL required the licensee to perform a number of analyses

and reviews and submit the results to the NRC. By May 15,

1987, all the required information had been received. Based

on NRC acceptance of the licensee's response and actions taken,

the NRC resumed processing of license renewal applications

which had been held in abeyance pending completion of the CAL

items.

28

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.

.

.

Also, management efforts were focused on improving operator

instructor skills during the assessment period.

Personnel

exchanges ber. ween the operations department and the training

organization helped to increase the credibility and awareness

of the training organization. As evidenced by some of the

,

operator responses to plant cond'tions, additional refinements

in the site simulator were necessary. These changes were

accomplished. These actions are viewed as positive.

Stronger feedback mechanisms were established from management

to the shifts regarding their performance.

Efforts to assure

consistent performance from the operating shifts were not

totally successful.

Training initiatives to correct original

weaknesses in understanding the Technical Specifications were

slow in developing.

Operator licensing examinations were administered in December

1987.

Four of the six candidates passed their examination.

The sample size was too small to draw any meaningful

quantitative conclusion.

However, the success rate of the

operator licensing program showed no improvement.

The training and qualification effectiveness of other

organizations appeared adequate in most areas such as security,

radiation / chemistry, and emergency planning.

Mechanical

and electrical engineering personnel were trained to the

appropriate level of expertise with the exception of how to

provide proper justification for preventive maintenance

deferrals.

Key personnel received environmental qualification

([Q) training with the only exception being maintenance personnel.

The maintenance individuals responsible for EQ activities were

not formally trained regarding specific EQ requirements. Also

in the maintenance area, based on several procedural violations,

training of first line supervisors and craft personnel needed

improvement in the areas of quality consciousness and awareness

of administrative controls that affect safety and quality.

Training and qualification of auditors and lead auditors

appeared to be adequate.

INPO completed accreditation of all

the training programs in May, 1987.

2.

Conclusions

The licensee's performance is rated Category 2 in this area.

The licensee was rated Category 3 during the pre'ious

assessment period.

3.

Board Recommendations

None.

29

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L.

Startup Testing

1.

Analysis

Evaluation of this functional area was based on routine

inspections of Test Condition 3 and 5 test results conducted by

region-based inspectors and resident inspector observations of

Test Condition 3 and 5 testing.

Enforcement history in this area continued to indicate

regulatory conformance.

No violations or deviations were

identified during this assessment period.

Management involvement to assure quality in this functional

continued to be apparent. Testing evolutions were properly

controlled and scheduled to minimize impact on normal plant

activities.

Proper planning was always evident with extra

preparation taken on the more difficult and complex evolutions.

Reflective of this was the execution of HPCI testing at lower

than normal power levels without causing major operational

transients. A specific shift team was assigned to complete

shutdown from outside the control room testing.

This dedicated

shift team received additional training and familiarization

prior to test performance and is considered to be a positive

licensee initiative.

Proper procedural adherence was always

noted and good documentation of test deficiencies was always

performed.

As a result of these actions a significant design

deficiency in the HPCI system and degraded equipment

performance in the feedwater control system were identified.

The licensee's approach to resolution of technical issues

was appropriate as evidenced by reperformance of the major

HPCI startup tests following major modifications to that

system.

No reportable events were attributed to startup

testing personnel errors.

There were few NRC initiatives in

this functional area.

In those few instances management was

responsive and appropriately addressed the cencerns.

Staffing was adequate.

Personnel were experienced and

knowledgeable.

Authorities and responsibilities were well

defined even during the transition period when the Startup

Manager changed half way through the assessment period.

2.

Conclusion

The licensee's performance is rated Category 1 in this area.

The licensee was rated Category 1 in the previous assessment

period.

30

.

1

.

.

.

.

3.

Board Recommendations

None.

M.

Engineering / Technical Suorort

.

1.

Analysis

This is a new functional area and consequently was not rated in

the previous assessment period.

Evaluation of this functional

area was based on the results of several inspections performed

by region based inspectors, resident inspectors, and one

Operational Safety Team inspectiv... Areas examined included

equipment environmental qualification, licensee actions in

response to certain NRC documents (IEB 85-03, Generic Letter 84-11, Unresolved Safety Issue A-7), licensee activities

with regard to selected mechanical, electrical and structural

deficiencies and enginaaring support to the maintenance / operations

.

departments.

Enforcement history during the assessment period was poor and

consisted of ten violations. One Severity Level III, six

Severity Level IV, and three Severity Level V, were identified

during the assessment period. The Severity Level III violation

highlighted inappropriate engineering decisions during final

construction / initial licensing.

These decisions resulted in

the Low Pressure Coolant Injection (LPCI) loop select bus being

vulnerable to a single failure.

The violation incurred a

civil penalty of $25,000.

Three of the violations reflected inadequate technical decisions

by engineering personnel during the assessment period that

affected equipment / structures performance capability. Three of

the violations reflected a failure to correctly translate the

design basis into drawings, one of which was safety signifi: ant

and resulted in modifications to some of the masonry block

walls.

One violation dealt with a breakdown in the spare parts

dedication process, and another involved failure of engineering

personnel to properly classify a minor electrical modifications.

The last violation dealt with isolated environmental qualification

documentation deficiencies and was of minimal safety significance.

Another issue similar to the LpCI swing bus and of the same

timeframe remained outstanding at the end of the assessment

period. This issue dealt with the containment isolation

,

portion of the primary containment monitoring piping

configuration net being in conformance with Ger.aral Design

Criteria 56.

The matter is under consideration for escalated

enforcement.

31

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t

Manag nent involvement in assuring quality by addressing

identi'ied engineering problems was mixed.

Proper involvement

was i.oted in resolving main steam line instrument tap failures,

vibration testing, resolving swing bus electrical circuit

deficiencies, and resolution to moisture separator reheater

damage.

Management involvement was lacking in issues dealing

_

with the Jamesbury butterfly valves, MSIV spring failures, use

of Furmanite, analysis of masonry block walls and concrete

expansion anchors, and engineering support provided to the

Maintenance Department.

It appears that several of the

problems encountered by the Maintenance Depar. ment could have

been prevented by accurate and effective support from the

Engineering Department.

Though some initiatives were made to

increase engineering presence in the freility, this was not the

norm.

The engineering effort applied to the issue of flow induced

vibration cracks of instrument lines on the main steam system

.

significantly improved the piping configuration with respect to

fatigue design.

This effort demonstrated excellent management

involvement and attention. Similarly, during startup vibration

testing, the er.gineering records were found to be generally

complete, well maintained, and available.

In contrast, the engineering effort with respect to analysis of

black walls and concrete expansion anchors resultec in three

violations with multiple examples.

Engineering records were in

some cases not complete and contained numerous errors. With

respect to the Jamesbury butterfly valves, repeated valve

failures occurred due to common causes because the design

weakness of the materials used was not well evaluated after the'

first failure.

In addition, gradual degradation in the valve's

performance was allowed to continue until valve failure without

taking any corrective action. With respect to the failure of

several MSIV springs, corrective action was taken, but was not

effective because the lessons learned on one component were

not extrapolated to similar components.

For example, the

licensee's investigation of the broken MSIV springs was limited

to inner springs until a broken outer spring was found.

The heat

treatment, which was eventually established as the cause of,the

problem, was performed for both sets of springs and for the

"proposed" replacement springs by the same vendor at about the

same time.

Site engineering had concluded that based on spring

compression tests of 105% the r placement springs could be used

despite corporate engineering'., analysis that a 105%

compression test was unacceptable.

The site had failed to

assume embrittled material when the fracture analysis was

conducted, even though testing had identified that the material

32

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was embNttled.

These inconsistencies in the quality of

engineering ~ performance appear to be function of the individual

assigned a specific tast rather than engineering discipline or

level of management review.

An NRR audit conducted at the end of the previous period

~

(March 1987) on the Detailed Control Room Design Review (DCRDR)

and the Safety Parameter 91 splay System (SPDS) identified

significant deficiencies Un management ovessight.

In particular,

one of the findings with respect to the DCRDR was that there

was an apparent lack of licensee mr.nagement support to perform

a meaningful and effective DCRDR. Meetings on these two items

were held during the current period in August and November

1987. As a result of these meetings, the licensee submitted

an updated summary DCRDR report and SpDS report.

This is

further evidence that the licensee's management is demonstrating

greater involvement. With respect to the DCRDR/SPDS and MSIV

spring issues, significant NRC management involvement was

,

required to achieve appropriate resolution.

The OSTI identified that overall technical support to operations

appeared to be weak.

Actions on operational improvement

documents were slow as evidenced in the establishment of

ambient room temperature criteria and electrical load lists.

Operations administrative support appeared strained.

Some

improvements were noted in the last part of the period as

evidenced by modifications to the emergency equipment cooling

water system in an effort to reduce unplanned ESF actuations.

However, this type of performance needed to be exhibited on a

broader, more consistent basis.

The licensee's approach to resolution to technical issues from

a safety standpoint was mixed.

In the area of environmental

qualification, the licensee demonstrated viable and generally

sound approaches in resolving techni;al issues.

In several

other cases, such as validation of feedwater suction piping

pressure qualification, replacement of unqualified check valve

soft seats and HPCI overpressurization, resolution of

engineering issues was generally sound, conservative, and

thorough.

owever, poor resolution of technical issues from a safety

standpoint was identified in a number of areas:

the lack of

a program to address testing or long-term operability of MOVs

identified in Bulletin 85-03, the lack of depth and timely

correction of multiple failures of the Jamesbury butterfly.

valves, and MSIV spring failures.

In addition, the Engineering

Department in a number of instances did not provide effective

support of the preventive maintenance (PM) program. The most

significant case was the justification to defer or reschedule

137 PM activities on Class IE circuit breakers.

The engineering

justification lacked thoroughness, depth, technical completeness,

33

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and accuracy; and failed to evaluate the effects on system

operability, availability, or reliability.

Scheduling and

availability of personnel were the predominant reasons listed

for deferrals of PM items.

The licensee indicated that steps

would be taken to re-evaluate the justification to ensure

_

operability and reliability of the breakers; however, the

deferral of PMs without adequate justification appeared to be

a pervasive and chronic problem.

Responsiveness to NRC initiatives was mixed. Generally the

licensee provided sound, timely, acceptable responses.

The

licensee's analysis and documentation to support proposed

resolution to EQ issues was adequate.

In response to the NRC

identified deficiencies relative to the ECCS motor adapters

and termination box mountings, the licensee performed a

comprehensive review and identified additional deficiencies.

All deficiencies had been scheduled to be corrected in a timely

manner and the program has prevented further deficiencies in

,

this area.

Response to Bulletin 85-03, on the other hand, was poor in

that requirements of the bulletin were not implemented by the

requested completion date.

Similarly, initial responses to

two of tha violations were inadequate in that they failed to

adequately eddress the concerns identified by the original

violations. Acceptable responses were subsequently received

after the NRC provided a written description of how the original

responses were inadequate.

A number of operational events assoc 4 ted with this functional

area occurred during the assessment period.

Twelve of thirty-

five unplanned ESFs were due to either design or design control

deficiencies.

Approximately 25% of the LERs were due to the

Three of the nine unplanned reactor protection

same ceuse.

system actuations were the result of design / design control

p rot,l ems . A number of these events were due to original design

deficiencies.

Staffing was adequate.

Key positions were identified and

responsibilities were well-defined.

EQ personnel were

knowledgeable of technical and regulatory requirements. Only

one key position, Te:hnical Engineer, was not permanent 1'

filled.

2.

Conclusion

The 1 censee's per.s wance is rated Category 3 in this area.

This area was not rated in the previous assessment period.

34

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3.

Board Recommendations

-

The SALP Board notes that licensee ranagement attention is

required to further integrate the engineering function into

the support of plant operations, to provide consistency in

the resolution of technical issues within engineering, and to

~

encourage engineering to become more proactive in anticipating

plant problems.

.

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, _ _ _ _ . . . . _ _ _ _ _ . _ _ - . . _ _

.

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as

.

.

V.

SUPPORTING DATA AND SUMMARIES

-

A.

Licensee Activities

During the SALP 9 assessment period, the licensee continued to

implement the startup testing program.

Significant outages and

~

major events which occurred during the period are summarized below:

1.

On April 11, 1987, the plant was shut down to re, air several

steam leaks.

2.

On May 13, 1987, the plant scrammed due to failure of the south

reactor feed pump.

3.

On May 21, 1987, the plant was shut down to repair a valve

packing which had been leaking in the reactor water cleanup

system.

4.

On June 25, 1987, the plant was manua'lly scrammed because of

excessive arcing from the "B" recirculation M-G set due to

excessive wear of the generator brushes.

5.

On June 26, 1987, an unplanned mode change occurred.

6.

On July 31, 1987, the reactor scrammed while shutting down to

repair feedwater check valve leakage. The plant entered an

extensive maintenance outage until October 10, 1987.

7.

On December 5, 1987, the plant was authorized to operate up to

75 percent power.

8.

On January 15, 1988, the plant was authorized to exceed 75

percent power, the final NRC restart effort holdpoint.

9.

On February 27, 1988, the olant entered a planned local leak

rate testing outage following a shutdown when all four diesel

generators were declared inoperable.

Fermi 2 experienced 35 ESF actuations, and 9 reactor scrams.

B.

Inspectisn Activities

Forty-six inspection reports were issued during April 1, 1987

through March 31, 1988, however, four of these inspection reports

(87006, 87008, 87012, and 87013) were addressed in the previous

SALP 8 report.

Forty-eight inspection reports are discussed in

this SALP report and are listed below, some of which have not yet

been issued to the licensee.

Significant inspection activities are

listed in Paragraph 2 (Special Inspection Summary) of this section.

36

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1.

Inspection Data

Facility Name: Fermi

Unit: 2

Docket No. 50-341

_

Inspection Reports Nos. 87000, 87001, 87007,

87014 through 87016, 87018 through 87050, 88002

through 88007, and 88009 through 88011.

Table I

Number of Violations in Each Severity level

Functional Areas

I

II

III

IV

V

A.

Plant Operations

1

4

4

B.

Radiological Controls

1

C.

Maintenance

3

1

'

D.

Surveillance

10

1

E.

Fire Protection

1

1

F.

Emergency Preparedness

G.

Security

2

1

H.

Outages

I.

Quality Programs

1

1

and Administrative

Controls Affecting

Quality

J.

Licensing Activities

1

K.

Training & Qualification

Effectiveness

L.

Startup Testing

'

M.

Engineering / Technical

1

6

3

Support

TOTALS

I

II

III

IV

V

2

27

14

2.

Special Inspection Summary

a.

During July 1-10, 1987, a special inspection was conducted

as a result of the unplanned mode change incident of

June 26, 1987 (Inspection Report No. 341/87027).

b.

During July 13-30, 1987, members of Region III's Quality

Assurance Program Section, and NRR conducted an inspection

of the licensee's QA program, this included a followup on

corrective actions taken in response to the NRR maintenance

survey.

37

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.

.

c.

During July 27-August 7,1987, an Operational Safety Team

.

Inspection was conducted which focus <d on the effectiveness

of management oversight of plant operational performance.

This was part of RIII's overall regulatory assessment to

determine the licensee's readiness to operate at power

levels greater than 50'4 (Inspection Report No. 341/870030).

_

d.

During August 27-20, 1987, the annual emergency preparedness

exercise was conducted (Inspection Report No. 341/87029).

C.

Investigation and Allegations Review

'

Sixteen allegations relating to Fermi 2 were received in Region III

during this assessment period.

Ten allegations were closed during

the assessment period.

Overall, seventeen allegations remained

open at the conclusion of the assessment period.

D.

Escalated Enforcement Actions

1.

A severity level III violation and proposed imposition of civil

penalty in the amount of 575,000 was issued to the licensee on

September 24, 1987. This action was based on the June 26, 1987,

Technical Specification violation, involving the uncontrolled

hea+.-up of the reactor which resulted in a change from Mode 4

te 'dode 3.

The escalated and mitigation factors in the

Enforcement Policy were consider and the civil penalty was

increased by 100'4 because of the licensee's past poor

performance in this area.

However, unusually prompt and

extensive corrective actions by the licensee, including

disciplinary actions of the individual (s) involved warranted a

50 percent reduction in the civil penalty (Enforcement Case

-

No. EA-87-133, Enforcement Notice No. EN-87-081, Preliminary

Information No. PN-III-87-091, Inspection Report No. 341/87027).

2.

A severity level III violation and proposed imposition of civil

penalty in the amount of $25,000 was issued on February 11,

1987.

This action was based on a design error discovered on

September 8,1987, in the circuitry of the swing electrical

bus, which would have resulted in the loss of both divisions

of low pressure coolant injection, during an accident condition.

The civil penalty was mitigated by 50 percent because of the

licensee's prompt and extensive corrective action (Enforcement

Case No. EA-87-232, Enforcement Notice No. EN-88-011,

Inspection Report No. 341/87049).

E.

Licensee Conferences Held During Assessmer.t period

1.

On May 11, 1987, a management meeting was conducted at the

site with RIII management, NRR, and licensee representatives

to discuss the status of the maintenance program including

preventative maintenance, staffing, material control,

training and planned corrective actions in response to the

NRR Maintenance Survey.

38

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2.

On June 4,1987, a management meeting was conducted at

Region III with licensee representatives to discuss actions

being taken by the licensee to ensure that all activities

required by the operator licensing requalification program are

implemented and to resolve the processing of pending reactor

operator renewal applications.

.

3.

On July 7, 1987, a management meeting was conducted at

Region III with licensee representatives to discuss the

licensee's investigation and corrective actions associated

with the unplanned mode change on June 26, 1987.

4.

On July 31, 1987, an Enforcement Conference was conducted in

the Region III office with licensee representatives to discuss

the inspection findings concerning the June 26, 1987, incident

in which an unplanned mode change occurred.

5.

On August 7, 1987, a management exit meeting was conducted at

the site with ifcensee representatives, at which time the NRC

Operational Safety Team Inspection (OSTI) findings were presented

to the licensee.

6.

On August 24, 1987, a management meeting was conducted at Monroe

County Community College to discuss SALP 8, the status of

ongoing licensee programt, addressing issues discussed in the

December 1985,10 CFR 50.54(f) letter, the Reactor Operations

Improvement Plan, and the Nuclear Operations Imr-ovement Plan.

7.

On October 5,1987, a management meeting was conducted at the

site to review outstanding issues which must be resolved prior

to exceeding 50'. power.

~

8.

On October 29, 1987, a management meeting was conducted at

Region III to discuss Fermi 2 plant status and plans.

9.

On November 2,1987, a management meeting was conducted at

Region III to discuss the Control Room Evolution Evaluation

Program.

10.

On November 16, 1987, a management meeting was conducted at

Region III to discuss corrective actions taken as a result of

deficiencies identified during the emergency preparedness

annual exercise.

11.

On November 18, 1987, a management meeting was conducted at

Region III to review the results of the Control Room Evolution

Evaluation Program.

12.

On December 22, 1987, an Enforcement Conference was held at

Region III to discuss the violation of 10 CFR 50.59 on two

separate occasions.

39

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13. On February 1,1988, a monthly meeting to discuss plant ' status,

schedules, improvement programs, and NRC commitments was held

at the site,

,

14.

On March 29. 1988, a monthly meeting to discuss plant status,

schedules., improvement programs, and NRC commitments was held

.

at Ren'.sn III.

15.

On April 13, 1988, an Enforcement Conference was conducted to

discuss access control programmatic weaknesses and a violation

pertaining to use of force by a security officer.

F.

Confirmatory Action Letters

1.

On April 3,1987, a Confirmatory Action Letter (CAL-RIII-87-003)

was issued to the licensee addressing corrective actions to be

taken regarding licensed operator requalification training

deficiencies.

G.

Review of Licensee Events Reports and 10 CFR Part 21 Reports

Submitted by the Licensee

1.

Licensee Event Reports (LER's)

Fermi 2

Docket No.: 50-341

LER Nos.: 87007, 87009, 87010 through 87056, and

88001 through 88008.

Fifty-seven LER's were issued during this assessment period.

-

A table of cause code comparisons it shown below:

(12 mo)

(12 mo)

CAUSE AREAS

SALP 8

SALP 9

Personnel Errors

40.7% (22) 28.1% (16)

Design Problems

12.9% ( 7) 24.5% (14)

Ft.ternal Causes

0% ( 0)

0% ( 0)

Procedure Inadecuacies

22.2% (12) 28.1% (16)

Component / Equipment

9.2t ( 5)

10.5% ( 6)

Other

9.2% ( 5)

3.5% ( 2)

Unknown

5.8% ( 3)

5.3% ( 3)

TOTALS

1004 (54)

1004 (57)

. REQUENCY (LERs/M3)

4.5

4.8

"

NOTE:

The above information was derived from review of LER's

performed by NRC Staff and may not completely coincide

with the licensee's cause assignments.

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2.

10 CFR Part 21 Reports

a.

A Part 21 was reported by the licensee on June 30, 1987,

regarding premature failures of hydrogen and oxygen

sensors manufactured by Exosensor, Inc.

The sensors are

.

used in the post accident h/drogen/ oxygen analyzers.

b.

On December 3, 1987, the licensee notified the NRC of a

potential 10 CFR 21 regarding unqualified Kalrez soft

seats used in feedwater check valves supplied by Atwood

and Morrill.

H.

Licensing Activities

1.

NRR/ Licensee Meetings

August 1987

SPDS and DCRDR

Oetober 30, 1987

Compensatory measures in

support of GDC-56 exemption

request.

November 17, 1987

Progress on SPDS

February 17, 1988

To discuss interpretations

of certain Technical

Specifications.

2.

Commission Meetings - None

3.

Schedular Extensions Granted - None

-

4.

Reliefs Granted

September 28, 1987

Inservice Testing

October 6, 1987

ASME Code,Section XI

5.

Exemptions Granted

November 13, 1988

Exemption to GDC-56 for

Primary Containment

Radiation Monitor

6.

Orders Issued - Not.<

7.

Emergency Technical Specifications '.ssued

October 9, 1987

TS table changes for leakage

testing

January 6,1988

Setpoints for reactor coolant

system interface

i

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O

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8.

License Amendments Issued

=

Amendment No.

Description

Date

8

Editorial correction to

July 17,1987

T.S.

-

9

APRM setpoint action

July 21,1987

statement and control

rod block information

20

Leakage test requirements

October 9, 1987

for containment isolation

valves

11

Administrative controls

October 22, 1987

12

Emergency diesel generator

December Ic, 1987

lube oil surveillance

program

13

Battery surveillance

January 11, 1988

requirements

14

Reactor coolant leakage

Janua ry 12, 1988

15

LPCI cross-tie valve

March 14, 1988

16

Primary containment

March 21, 1988

isolation valves

17

Addition of isolation

March 29, 1988

valves for the primary

containment radiation

monitor

42