|
---|
Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20210H2211999-07-22022 July 1999 Notice of Violation from Insp on 990314-0424.Violation Noted:Sss Was Not Inoperable for Thirteen Days Because Electrical Breakers Associated with SSS Motor Control Ctr Were Mispositioned ML20207A5881999-02-17017 February 1999 Notice of Violation from Insp on 981213-990123.Violation Noted:Licensee Made Change to Procedures as Described in Updated Final Safety Analysis Rept & Failed to Perform Written Safety Evaluation ML20154C4301998-09-14014 September 1998 Notice of Violation from Insp on 980705-0815.Violation Noted:Licensee Failed to Establish Adequate Surveillance Procedures ML20236V7351998-07-27027 July 1998 Notice of Violation from Insp on 980524-0704.Violation Noted:Licensee Failed to Identify & Take Prompt C/A Following Unit 1 Upper Surge Tank over-temp Events on 960120,980111 & 0507 ML20236J7471998-06-11011 June 1998 Notice of Violation from Insp on 980222-0411.Violation Noted:Adminstrative & Surveillance Procedures Not Implemented as Evidenced by Listed Examples ML20217G5551998-03-23023 March 1998 Notice of Violation from Insp on 980111-0221.Violation Noted:Licensee Failed to Perform Written Safety Evaluation for Closing Valves 1CA-6 & 2CA-6 ML20203L6251998-02-0909 February 1998 Notice of Violation from Insp on 971123-980110.Violation Noted:Changes to Radiological Conditions in 1B Residual Heat Removal Pump Room Not Logged to Reflect Changes in Dress Requirements ML20199L6301998-02-0202 February 1998 Notice of Violation from Insp & Exam on 971117-21 & 971201-19.Violation Noted:As of 971219,selected Officers from Site Security Force Had Not Been Retrained to Perform non-licensed Operator Emergency Tasks for Starting Ssf ML20197F2481997-12-19019 December 1997 Notice of Violation from Insp on 971012-1122.Violation Noted:Licensee Failed to Follow Radiation Protection Procedures in That,Current Radiation Dose Rates Were Not on Vacuum Cleaner Label as Required ML20199G0351997-11-10010 November 1997 Notice of Violation from Insp on 970831-1011.Violations Noted:Licensee Failed to Follow Procedures for Security Badge Access Control as Evidenced.On 970909,security Failed to Destroy & Unassign Access Badge of Terminated Individual ML20211L3051997-09-26026 September 1997 Notice of Violation from Insp on 970720-0830.Violation Noted:On 970727,technician Failed to Correctly Review Drawing Number CNEE-2792-01.02,connection Diagram,Main Steam Sys Terminal Cabinet 2SMTC1,rev 12 ML20210N7111997-08-18018 August 1997 Notice of Violation from Insp on 970608-0719.Violation Noted:On 970424,operations Test Group Technician Failed to Open Valve 2NV-873 as Required by Step 2.2.3 of PT/2/A/4200/01C,resulting in Closed Test Vent Flowpath ML20149F9061997-07-0707 July 1997 Notice of Violation from Insp on 970427-0607.Violation Noted:Control Room Annunciator Alarm Response for Main Feedwater Containment Isolation Valve Low Nitrogen Actuator Pressure Inadequate ML20148F9291997-05-23023 May 1997 Notice of Violation from Insp on 970323-0426.Violation Noted:Improper Sequencing of Valves to Isolate & Drain Containment Penetrations Resulted in Loss of Inventory from Component Cooling Water Sys ML20141K6611997-05-16016 May 1997 Errata to NOV from Insp on 960324-0504.Violation Noted: Licensee Failed to Accomplish Activities Affecting Quality IAW Procedures as Evidenced by Listed Info ML20137X3291997-04-16016 April 1997 Notice of Violation from Insp on 970210-14.Violation Noted:Licensee Failed to Include Number of Structures,Sys & Components within Scope of Maint Rule as Required ML20140B7581997-03-17017 March 1997 Notice of Violation from Insp on 970112-0215.Violation Noted:Activities Affecting Quality Were Not Accomplished, IAW Documented Prescribed Procedures & QA Condition Matls Were Not Stored in QA Controlled Hold Area ML20128R0861996-10-0707 October 1996 Notice of Violation from Insp on 960728-0907.Violation Noted:On 960804,residual Heat Removal Sys Was Inadequate Which Resulted in Failure of Valve 2ND-53 ML20059G1591993-12-30030 December 1993 Notice of Violation from Insp on 931117-19 & 1129-1203. Violation Noted:On 931130,licensee Written Plan & Schedule Did Not Provide for Code Required Surface Exams on safe-end to Pipe Weld Safety Injection Accumulator Tanks ML20059K6891993-10-29029 October 1993 Notice of Violation from Insp on 930905-1002.Violation Noted:Instrumentation & Electrical Technicians Failed to Adequatley Implement Catawba Nuclear Site Directive 4.2.2 & Procedure IP/O/A/3890/01 ML20127E8361993-01-0606 January 1993 Notice of Violation from Insp on 921108-1212.Violation Noted:Design Control Measures Associated W/Ca Sys Were Inadequate & Design Deficiencies Rendered Sys Inoperable ML20062A1011990-10-0303 October 1990 Notice of Violation from Insp on 900803-0905.Violation Noted:Shift Supervisor Failed to Follow Procedural Requirements ML20059H0161990-08-31031 August 1990 Notice of Violation from Insp on 900624-0802.Violation Noted:Failure to Follow Instrumentation Procedures During Conduct of Plant Mod & Failure to Perform Adequate 10CFR50.59 Safety Evaluation Prior to Securing Annulus Door ML20056A5751990-07-23023 July 1990 Notice of Violation from Insp on 900611-19.Violation Noted: Control Room Operator Failure to Verify That Manual Valve Closed Resulting in Inadvertent Diversion of Reactor Coolant to Refueling Water Storage Tank ML20056A5091990-07-20020 July 1990 Notice of Violation from Insp on 900527-0623.Violation Noted:Solenoids on 3 Pilot Valves Associated W/Unit 2 High Pressure Fire Protection Sys Installed Backwards During Const ML20247C7021989-08-31031 August 1989 Notice of Violation from Insp on 890616-28.Violation Noted: from 890602-16,both Channels of Reactor Vessel Water Level Instrumentation Inoperable in Modes 1,2 & 3 Due to Closure of Isolation Valves on upper-range Pressure Transmitters ML20247R7211989-07-25025 July 1989 Notice of Violation from Insp on 890528-0701.Violation noted:post-accident Liquid Sampling Sys Periodic Test Inadequate to Ensure Valve Locked Closed After Use on 890602 in That Valve Discovered Open & Unlocked ML20246P7051989-07-10010 July 1989 Notice of Violation from Insp on 890405-0510.Violation Noted:On 890413,valve 1-KC-9 Not Locked in Position While Unit 1 at 100% Power & on 890412 & 0502,operators Did Not Frisk Upon Leaving Contaminated Area ML20246C0761989-06-27027 June 1989 Notice of Violation from Insp on 890326-0429.Violations Noted:Selected Control Room Drawings Do Not Reflect as-built Conditions & Support Documents Necessary to Discern Scope of Mods Not Available in Control Room ML20246N4451989-05-0404 May 1989 Notice of Violation from Insp on 890403-07 & 13.Violation noted:1988 Semiannual Effluent Release Rept Listed Two Abnormal Releases,But Did Not Include Descriptions of Events ML20245G2981989-04-20020 April 1989 Notice of Violation from Insp on 890226-0325.Violation Noted:Licensee Failed to Implement Procedure in That While Attempting to Close 1SV-27A,operator Inadvertently Closed 1SM-7,Steam Generator 1A MSIV ML20244A8971989-03-29029 March 1989 Notice of Violation from Insp on 890204-25.Violation Noted:Procedure PT/1/A/4200/55, CA Check Valve Leak Rate Test Inadequate to Ensure Auxiliary Feedwater Suction Piping Vented After Filling ML20246L6591989-03-0303 March 1989 Notice of Violation from Insp on 890130-0203.Violations Noted:Two Licensee Employees Not Provided W/Info & Instructions Re Entering High Radiation Area & Area Not Posted ML20236A2161989-03-0202 March 1989 Notice of Violation from Insp on 881127-0204.Violation Noted:Failure to Declare Equipment Inoperable & Perform Written Safety Evaluation & 890126 Partial Obstruction of Unit 1 Pit Drain ML20206J5821988-11-16016 November 1988 Notice of Violation from Insp on 880926-1025.Violations Noted:Two Instrument & Electrical Technicians Working W/O Procedures & Procedures AP-0-A-5500-34 & Omp 2-29 Inadequate ML20195B7161988-10-24024 October 1988 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:Lack of Environ Qualification for Certain Components of Electrical Equipment in Isolated Sys ML20205K0891988-10-17017 October 1988 Notice of Violation from Insp on 880826-0925.Violation Noted:Air Regulator for Valve 1CF-89 Replaced & Returned to Svc on 880721,w/o Being Tested to Demonstrate That Parameter Affected,Within Acceptable Limits ML20207J8011988-09-16016 September 1988 Notice of Violation from Insp on 880719-22.Violation Noted: Licensee Failed to Adhere to Radiological Control Procedures in That on 880604,operations Personnel Stopped Leaking Valve W/O Waiting for Surveys,Evaluations or Job Coverages ML20154A6141988-09-0202 September 1988 Notice of Violation from Insp on 880801-05.Violation Noted:No Objective Evidence Exists That Catawba Safety Review Group Reviews NRC Issuances,Industry Advisories or Other Sources Which May Indicate Areas for Improving Safety ML20153C5261988-08-19019 August 1988 Notice of Violation from Insp on 880626-0725.Violation Noted:Failure to Maintain Two Operable Channels Per Valve for PORV Block Valve Position Indicators from Initial Licensing Until 880520 ML20151E5531988-07-0808 July 1988 Notice of Violation from Insp on 880526-0625.Violation Noted:Personnel Exceeded Overtime Guidelines on Numerous Occasions During Jan & Feb 1988 W/O Prior Approval ML20195K1191988-06-17017 June 1988 Notice of Violation from Insp on 880426-0527.Violation Noted:Failure to Establish Measures to Assure That Stopwatches Properly Controlled,Calibr & Adjusted & Valve Not Tested Before Returning to Svc ML20195E4261988-06-13013 June 1988 Notice of Violation from Insp on 880310-18.Violation Noted:W/Unit 2 in Mode 1 & Operating at 20% Power,Three Independent Steam Generator Auxiliary Feedwater Pumps Not Operable During Actual Turbine Trip ML20154D1081988-05-0606 May 1988 Notice of Violation from Insp on 880326-0425.Violation Noted:Diesel Generator 2B Inoperable for Period Exceeding Tech Spec Limits & Licensee Failed to Place Unit in Hot Standby & Subsequently in Hot Shutdown ML20151B3441988-03-31031 March 1988 Notice of Violation from Insp on 880225-0325.Violation Noted:Failure to Follow Tech Spec Administrative Requirements for Approval of Mods ML20148E6871988-03-18018 March 1988 Notice of Violation from Insp on 880202-04.Violation Noted: Failure to Establish Adequate Measures to Control Eddy Current Testing of Steam Generator Tubes ML20148E9431988-03-14014 March 1988 Notice of Violation from Insp on 880111-15.Violations Noted: Unit 2 Entered Mode 5 Exceeding by Approx 96 Hrs Time Required to Shutdown ML20148H7361988-03-10010 March 1988 Notice of Violation from Insp on 880126-0225.Violations Noted:On 880123,RCS Pressure Allowed to Exceed 1,955 Psig & on 880109,equipment Operator Designated to Remove Safety Tag 410 Removed Tag & Repositioned Switch W/O Approval ML20149H3571988-02-0404 February 1988 Notice of Violation from Insp on 871226-880125.Violation Noted:Failure to Maintain Automatic Valve in Flow Path in Open Position When Above 10% Rated Thermal Power IR 07100126/20120251988-01-11011 January 1988 Revised Notice of Violation from Insp on 871126-1225. Violation Noted:On 871113,licensee Failed to Properly Classify Start Attempt Number 548 on Diesel Generator 1A as Invalid Failure 1999-07-22
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000413/19993021999-10-12012 October 1999 NRC Operator Licensing Retake Exam Repts 50-413/99-302 & 50-414/99-302 (Including Completed & Graded Tests) for Tests Administered on 990921-23.Two Out of Three RO Candidates & One SRO Passed Retake Exam IR 05000413/19993011999-09-30030 September 1999 NRC Operator Licensing Exam Repts 50-413/99-301 & 50-414/99-301 (Including Completed & Graded Tests) for Tests Administered on 990524-27,0603,07-10 & 16.Eight of Fourteen Applicants Passed Exam IR 05000413/19990051999-09-24024 September 1999 Insp Repts 50-413/99-05 & 50-414/99-05 on 990718-0828. Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support IR 05000413/19990041999-08-13013 August 1999 Insp Repts 50-413/99-04 & 50-414/99-04 on 990606-0717. Non-cited Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20210H2211999-07-22022 July 1999 Notice of Violation from Insp on 990314-0424.Violation Noted:Sss Was Not Inoperable for Thirteen Days Because Electrical Breakers Associated with SSS Motor Control Ctr Were Mispositioned ML20209E2831999-07-0101 July 1999 Insp Repts 50-413/99-03 & 50-414/99-03 on 990425-0605. Non-cited Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000413/19990111999-06-0202 June 1999 Insp Repts 50-413/99-11 & 50-414/99-11 on 990422-23 & 0503. No Violations Noted.Major Areas Inspected:Licensee Identified Frost & Ice Buildup Which Affected Unit 1 Ice Condenser Lower Inlet Doors IR 05000413/19990021999-05-20020 May 1999 Insp Repts 50-413/99-02 & 50-414/99-02 on 990314-0424.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support PNO-II-99-017, on 990515,indication of Main Generator Ground Fault Was Received While Performing Turbine Startup in Preparation for Placing Unit on Line.Licensee Is Conducting Investigation to Determine Actual Cause of Ground1999-05-18018 May 1999 PNO-II-99-017:on 990515,indication of Main Generator Ground Fault Was Received While Performing Turbine Startup in Preparation for Placing Unit on Line.Licensee Is Conducting Investigation to Determine Actual Cause of Ground ML20206U4161999-05-10010 May 1999 Insp Repts 50-413/99-10 & 50-414/99-10 on 990314-0424. Violation Being Considered for Escalated Enforcement Action Noted.Major Areas Inspected:Operations PNO-II-99-015, on 990503,shutdown in Excess of 72 H Occurred. Licensee Is Still Conducting Investigation Into Cause of Main Generator Protection Lockout & Making Preparations to Inspect & Remove Any Excessive Fouling from Inside Afws1999-05-0505 May 1999 PNO-II-99-015:on 990503,shutdown in Excess of 72 H Occurred. Licensee Is Still Conducting Investigation Into Cause of Main Generator Protection Lockout & Making Preparations to Inspect & Remove Any Excessive Fouling from Inside Afws IR 05000413/19990011999-04-0606 April 1999 Insp Repts 50-413/99-01 & 50-414/99-01 on 990124-0313. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20207A5881999-02-17017 February 1999 Notice of Violation from Insp on 981213-990123.Violation Noted:Licensee Made Change to Procedures as Described in Updated Final Safety Analysis Rept & Failed to Perform Written Safety Evaluation IR 05000413/19980121999-02-17017 February 1999 Insp Repts 50-413/98-12 & 50-414/98-12 on 981213-990123. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000413/19980111999-01-11011 January 1999 Insp Repts 50-413/98-11 & 50-414/98-11 on 981101-1212.No Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support IR 05000413/19980151999-01-0404 January 1999 Insp Repts 50-413/98-15 & 50-414/98-15 on 981102-06 & 16-20. No Violations Noted.Major Areas Inspected:Licensee Corrective Action Program by Sampling Activities Defined in Nuclear Sys Directive 210,rev 1 IR 05000413/19980161998-12-0404 December 1998 Insp Repts 50-413/98-16 & 50-414/98-16 on 980915-1101.No Violations Rept Encl.Major Areas Inspected:Licensee Maint, Surveillance & Engineering Programs Involving Unit 2 Ice Condenser IR 05000413/19980101998-11-23023 November 1998 Insp Repts 50-413/98-10 & 50-414/98-10 on 980927-1031.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering & Plant Support ML20155B3821998-10-19019 October 1998 Insp Repts 50-413/98-13 & 50-414/98-13 on 980807-0915. Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Review Ice Condenser Related Problems,Which Led to Forced Shutdown ML20154C4301998-09-14014 September 1998 Notice of Violation from Insp on 980705-0815.Violation Noted:Licensee Failed to Establish Adequate Surveillance Procedures IR 05000413/19980081998-09-14014 September 1998 Insp Repts 50-413/98-08 & 50-414/98-08 on 980705-0815. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering PNO-II-98-037A, on 980807,update Shutdown in Excess of 72 H Made.Licensee Has Cleaned & Satisfactorily Inspected IC Flow Channels.Licensee Identified Discrepancies in Bolting of IC Intermediate Deck Door Frames & Hinges.Conditions Addressed1998-08-28028 August 1998 PNO-II-98-037A:on 980807,update Shutdown in Excess of 72 H Made.Licensee Has Cleaned & Satisfactorily Inspected IC Flow Channels.Licensee Identified Discrepancies in Bolting of IC Intermediate Deck Door Frames & Hinges.Conditions Addressed IR 05000413/19980091998-08-26026 August 1998 Insp Repts 50-413/98-09 & 50-414/98-09 on 980816-0826. Examples of Two Apparent Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support PNO-II-98-037, on 980808,shutdown in Excess of 72 H Occurred. Licensee Inspected Approximately Half of Unit 2 Ice Condenser Bay Flow Channels from Intermediate Deck W/No Ice Obstructions in Excess of TS Limit Identified1998-08-10010 August 1998 PNO-II-98-037:on 980808,shutdown in Excess of 72 H Occurred. Licensee Inspected Approximately Half of Unit 2 Ice Condenser Bay Flow Channels from Intermediate Deck W/No Ice Obstructions in Excess of TS Limit Identified ML20236V7351998-07-27027 July 1998 Notice of Violation from Insp on 980524-0704.Violation Noted:Licensee Failed to Identify & Take Prompt C/A Following Unit 1 Upper Surge Tank over-temp Events on 960120,980111 & 0507 IR 05000413/19980071998-07-27027 July 1998 Insp Repts 50-413/98-07 & 50-414/98-07 on 980524-0704. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support,Including Physical Security IR 05000413/19980051998-06-22022 June 1998 Insp Repts 50-413/98-05 & 50-414/98-05 on 980412-0523.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20236J7471998-06-11011 June 1998 Notice of Violation from Insp on 980222-0411.Violation Noted:Adminstrative & Surveillance Procedures Not Implemented as Evidenced by Listed Examples IR 05000413/19980061998-06-0505 June 1998 Insp Repts 50-413/98-06 & 50-414/98-06 on 980511-15. Violations Noted.Major Areas Inspected:Facts Surrounding Event Associated W/Degradation of CNS Unit Auxiliary Feedwater Sys During Rapid down-power on 980507 PNO-II-98-025, on 980507,AFW Sys Declared Inoperable.Licensee Isolated Valves 1CM-127 & 2CM-127 in Units 1 & 2, Respectively,To Prevent Recurrence Until Permanent Corrective Actions Can Be Developed1998-05-11011 May 1998 PNO-II-98-025:on 980507,AFW Sys Declared Inoperable.Licensee Isolated Valves 1CM-127 & 2CM-127 in Units 1 & 2, Respectively,To Prevent Recurrence Until Permanent Corrective Actions Can Be Developed IR 05000413/19980031998-04-30030 April 1998 Insp Repts 50-413/98-03 & 50-414/98-03 on 980222-0411. Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Aspects of Licensee Operations, Maint,Engineering & Plant Support IR 05000413/19980041998-04-20020 April 1998 Insp Repts 50-413/98-04 & 50-414/98-04 on 980302-06.No Violations Noted.Major Areas Inspected:Observation & Evaluation of Biennial Emergency Preparedness Exercise for Plant ML20217G5661998-03-23023 March 1998 Insp Repts 50-413/98-01 & 50-414/98-01 on 980111-0221. Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support ML20217G5551998-03-23023 March 1998 Notice of Violation from Insp on 980111-0221.Violation Noted:Licensee Failed to Perform Written Safety Evaluation for Closing Valves 1CA-6 & 2CA-6 IR 05000413/19980021998-02-17017 February 1998 Partially Withheld Insp Repts 50-413/98-02 & 50-414/98-02 on 980112-13 (Ref 10CFR2.790).No Violations Noted.Major Areas Inspected:Plant Support,Including Malevolent Use of Vehicles at Plant ML20203L6301998-02-0909 February 1998 Insp Repts 50-413/97-15 & 50-414/97-15 on 971123-980110. Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support ML20203L6251998-02-0909 February 1998 Notice of Violation from Insp on 971123-980110.Violation Noted:Changes to Radiological Conditions in 1B Residual Heat Removal Pump Room Not Logged to Reflect Changes in Dress Requirements ML20199L6301998-02-0202 February 1998 Notice of Violation from Insp & Exam on 971117-21 & 971201-19.Violation Noted:As of 971219,selected Officers from Site Security Force Had Not Been Retrained to Perform non-licensed Operator Emergency Tasks for Starting Ssf PNO-II-97-066, on 971230,RCS Leakage Requiring Forced Unit Cooldown Occurred.No Radioactive Release Outside of Reactor Containment Facilities Due to Leakage.Licensee Informed States on Nc & Sc1997-12-31031 December 1997 PNO-II-97-066:on 971230,RCS Leakage Requiring Forced Unit Cooldown Occurred.No Radioactive Release Outside of Reactor Containment Facilities Due to Leakage.Licensee Informed States on Nc & Sc PNO-II-97-064, on 971229,inadvertent Safety Injection Occurred Due to Operators Failing to Perform Step Which Resulted in Cold Leg Injection Valve Being Left Open. Licensee Engineers Performing Evaluation1997-12-29029 December 1997 PNO-II-97-064:on 971229,inadvertent Safety Injection Occurred Due to Operators Failing to Perform Step Which Resulted in Cold Leg Injection Valve Being Left Open. Licensee Engineers Performing Evaluation ML20197F2481997-12-19019 December 1997 Notice of Violation from Insp on 971012-1122.Violation Noted:Licensee Failed to Follow Radiation Protection Procedures in That,Current Radiation Dose Rates Were Not on Vacuum Cleaner Label as Required IR 05000414/19970081997-12-19019 December 1997 Notice of Deviation from Insp on 971012-1122.Deviation Noted:On 971020,licensee Had Not Performed Alarm Set Point Adjustment Evaluation Discussed in Violation 50-414/97-08-01 ML20197F2861997-12-19019 December 1997 Insp Repts 50-413/97-14 & 50-414/97-14 on 971012-1122. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20199G0351997-11-10010 November 1997 Notice of Violation from Insp on 970831-1011.Violations Noted:Licensee Failed to Follow Procedures for Security Badge Access Control as Evidenced.On 970909,security Failed to Destroy & Unassign Access Badge of Terminated Individual IR 05000413/19970121997-11-10010 November 1997 Insp Repts 50-413/97-12 & 50-414/97-12 on 970831-1011. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support as Well as Results of Announced Inspection by Regional Security Inspector ML20211L3051997-09-26026 September 1997 Notice of Violation from Insp on 970720-0830.Violation Noted:On 970727,technician Failed to Correctly Review Drawing Number CNEE-2792-01.02,connection Diagram,Main Steam Sys Terminal Cabinet 2SMTC1,rev 12 IR 05000413/19970111997-09-26026 September 1997 Insp Repts 50-413/97-11 & 50-414/97-11 on 970720-0830. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000413/19970101997-09-11011 September 1997 Insp Repts 50-413/97-10 & 50-414/97-10 on 970623-0731.No Violations Noted.Major Areas Inspected:Licensee Calculations,Analysis & Other Engineering Documents ML20210N7341997-08-18018 August 1997 Insp Repts 50-413/97-09 & 50-414/97-09 on 970608-0719. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support ML20210N7111997-08-18018 August 1997 Notice of Violation from Insp on 970608-0719.Violation Noted:On 970424,operations Test Group Technician Failed to Open Valve 2NV-873 as Required by Step 2.2.3 of PT/2/A/4200/01C,resulting in Closed Test Vent Flowpath 1999-09-30
[Table view] |
Text
., .' .t .
i e ENCLOSURE 1 NOTICE OF VIOLATION Duke Power Company Docket Nos. 50-413, 50-414 Catawba Units 1 and 2 License Nos. NPF-35, NPF-52 During the Nuclear Regulatory Commission (NRC) inspection conducted on January 11-15, 1988, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1986), the violation is listed below:
Technical Specification 3.7.4 requires at least two independent nuclear service water loops be operable in Modes 1, 2, 3 and 4. With only one nuclear service water loop operable, restore at least two loops to operable status withiri 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least hot standby within the next six hours in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Contrary to the above, on August 30, 1986, at 8:30 p.m. with Unit I shutdown for refueling and Unit 2 in Mode 1, Power Operation, Nuclear Service Water Train A was made inoperable with respect to Unit 2. On September 8, 1986 at 4:40 a.m., Unit 2 entered Mode 5, thus exceeding by approximately 92 hours0.00106 days <br />0.0256 hours <br />1.521164e-4 weeks <br />3.5006e-5 months <br /> the time required to shutdown to Mode 5.
This is a Severity Level IV violation (Supplement I).
Pursuant to the provisions of 10 CFR 2.201, Duke Power Company is hereby required to submit a written statement or explanation to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident Inspec-tor, Catawba, within 30 days of the date of the letter transmitting this Notice. This reply should be clearly marked as a "Reply to a Notice of ;
Violation" and should include [for each violation]: (1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time. If an adequate reply is not received within the time specified in this Notice, an order may be issued to show cause why the license should not be modified, suspended, or revoked or why such other ;
action as may be proper should not be taken.
FOR THE NUCLEAR REGULATORY COMMISSION ORIGINAL SIGNED BY
&$utd J. Nelson Grace Regional Administrator Dated at Atlanta, Georgia this/%dayofMarch1988
$. N Q
.,l'..
, MAR 141988 "
ENCLOSURE 2 ENFORCEMENT CONFERENCE
SUMMARY
On February 23, 1988, representatives of the Duke-Power Company (DPC) met with the NRC at the NRC's request in the Region II office in Atlanta, Georgia. The subjects of discussion were operability and reportability of several potential unanalyzed conditions in the Catawba Nuclear Service Water (RN) system. The list of conference attendees is contained in Attachment 1.
Following opening remarks given by M. L. Ernst, NRC Region II and H. Tucker, DPC, DPC gave a presentation which addressed the specific concerns of the NRC.
The presentation consisted of a review of RN system design features, a review of the various RN configurations of concern, safety significance, operability /
reportability decision points and corrective action.
The outline of the DPC presentation is contained in Attachment 2.
All NRC concerns on this issue were addressed in the meeting. ~It was evident that significant preparation time was expended. OPC also stated that as a result of this issue their sensitivity to reportability had been increased.
The NRC enforcement action concerning this issue is discussed in Enclosure 1.
- Attachments:
- 1. List of Attendees at the Catawba Enforcement Conference
- 2. Catawba Nuclear Station Nuclear Service Water System Region II Presentation 1
i l
., l',-.
s .
a .
MAR 141988 ATTACHMENT 1 ENFORCEMENT CONFERENCE DPC - CATAWBA ATTENDEES NRC M. L. Ernst, Deputy Regional Administrator L. A. Reyes, Director, Division of Reactor Projects (DRP)
V. L. Brownlee, Branch Chief, DRP T. A. Peebles, Section Chief, DRP P. K. Van Doorn, Senior Resident Inspector, DRP B. R. Bonser, Project Engineer, DRP C. A. Julian, Branch Chief, Division of Reactor Safety (DRS)
R. H. Bernhard, Reactor Inspector, DRS M. Thomas, Reactor Inspector, DRS G. A. Belisle, Section Chief, DRS A. F. Gibson, Director, DRS B. Uryc, Enforcement Coordinator G. R. Jenkins, Director, Enforcement and Investigation Coordination Staff G. Lainas, Assistant Director, NRR K. Jabbour, Project Manager, NRR J. D. Smith, Operations Inspector, NRR W. T. LeFave, Engineer Plant Systems, NRR H. Wong, Senior Enforcement Specialist, OE F. Hawkins, Section Chief, NRR Duke Power Company H. B. Tucker, Vice President, Nuclear Production N. Rutherford, Manager Licensing J. W. Hampton, Manager Catawba Nuclear Station (CNS) i T. B. Owen, Assistant Manager CNS i L. Hartzell, Compliance Engineer, CNS H. B. Barron, Operations Superintendent, CNS P. G. LeRoy, Licensing Engineer, CNS
- R. D. Sharpe, Nuclear Engineer, DPC
- E. W. Fritz, Design Engineer, DPC Design D. W. Eaves, Design Engineer, DPC Design t
e i
ii
- - - - - . _ . - - . . . - . , g.n ,
.u :
O O WAR 1 4 888 ATTACHMEf4T 2 l l-i CATAWBA NUCLEAR 8TATOON NUCLEAR SERVOCE WATER SYSTEM i
REGOOM 00 PRESENTATION FEBRUARY 28,1988 I<
ll t;
h m
J
.. . . t. .,
0 0 l -
. MAR 141988 CATAISA NUCLEAR STAT!0N NUCLEAR SERY!CE IdATER SYSTEM Sn5w.
t no a a l w 65 5A t.v.
v,u. m a v,n ,
4 8@ @@
h #2A #2 ett 2A ESS M ESS E55 28 0/G 6 " 4
- D/G 67A 488 47A 6M X X X M
~
47A #
67A 488 6M X X X M i,
1A o o < ,
0/G #I II Cosponent N ESS Essential CooHng Liquid Header Wasta Containment Spray gg, l Control Roon l Cooling l Assured Aux 528 28 l Feedwater E55 l 2A ESS n i r <r ,, <r 57A 8438 54A 538
- 2 63A 588 N ESS 2A 1A 18 28 0/G 0/G 0/G 0/G SNSW SNSW I
_ =w m = w w "m
.. .. - - - - - ~
CATAWBA NUCLEAR STATION NUCLEAR SERVICE WATER SYSTEM DE8IGN FEATURES EACH OF 2 LOOP 818 8 HARED BY BOTH UNIT 8.
EACH PUMP HA8 THE CAPACITY TO EITHER:
- 1. REMOVE COMBINED BLACK 0UT AND LOCA HEAT FROM ONE UNIT OR ,
- 2. REMOVE COMBINED BLACK 0UT AND C00LDOWN HEAT FOLLOWING TRIP FROM 100X FULL POWER. !
i LOOP ISOLATION OCCUR 8 ON COMBINED LOCA AND I LOSS OF LAKE WYLIE.
NON-ESSENTIAL EQUIP 9EENT 18180 LATED ON LOCA SIGNAL - Sp.
d AUTOMATIC TRANSFER FROM LAKE WYLIE TO SN8WP ON .
EITHER 8p OR LOS8 OF LAKE WYLIE.
l 1
4
l ,.
, , , ,' f r,w . . '* ' ' N&"
. MAR 141988 DECEMBER 1985 - SHARED ASPECTS OF RN RECOGN0 ZED
- SITE AND D0!81GN ENGINEERING EVALUAYLON CONDUCTED.
Unrestricted operating req'sirements were clear; issue addressed was proper handling of out-of-service equipment.
- SHORT AND EXTENDED (> 72 HR)
IN0PERABILITY ADDRESSED. I After 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, at least one unit is placed in cold shutdown with equipment isolated.
- LICENSE BASIS HEAT LOADS AND ACTUAL FLOW TEST DATA UTILIZED.
No special analysis involved.
- RE8IDENT INSPECTOR 8 BRIEFED.
l
- LER 414/88-31-1 ISSUED 8-29-88.
LER was a direct result of RN operating practices; otherwise event was not reportable.
O O uAR 141988 AUGUST 1988 - REQUOREMENTS FOR TWO TRAIN 8 0F RN WOTH DIESEL GENERATOR INOPERABLE CONFLOCT WOTH CPERATONG UNIT ,
REQUIREMENTS.
- FSAR DID NOT ADDRESS REQUIREMENT 8 WITH ONE UNIT ON COLD BHUTDOWN. i FSAR defined two pumps as necessary if both units are operating:
second pump needed to place non-LOCA unit cold shutdown.
- DESIGN ANALYSIS PERFORMED FOR CYCLE SPECIFIC FLOW REQUIREMENT.
l FSAR values used for LOCA (operating) unit requirements; refueling unit requirements took into account time since shutdown. Plant test confirmed system flow performance. l
- DESIGN STUDY s88 INITIATED TO !
DETERMINE GENERIC FLOW REQUIREMENT, Needed for future refueling outage work sequencing.
- RESIDENT INSPECTORS BROEFED.
- DESIGN ANALYSIS ADDRESSED EMERGENCY POWER SCURCE RATHER THAN FLC'.? PATH.
Closed valve IRN47A rather than IRN48B when IA D/G was out-of-service.
l
~ ~
l ., . , .
MAR 141988 JANUARY 1987 - lDENTIFIED UNNECES8ARY FAILURE SCENARIO WITH SNSWP TRANSFER.
- CNPR02350 INITIATED DESIGN STUDYe80 TO EVALUATE DELETION OF RN TRANSFER ON Sp CONSIDERING:
1- PROBLEM DEFINITION '
2- ADEQUACY OF RESOLUTION 3- ALTERNATE RESOLUTION 8 4- F8AR IMPACT FROM RESOLUTION
- DESIGN STUDY 880:
1- AGREED WITH PROBLEM DEFMTION 2- FOUND FAULT WITH RESOLUTION 3- lDENTIFIED PRE-ALIGNMENT AS ;
ALTERNATE RESOLUTION l 4- IDENTIFIED INCON818TANCY OF !
RESOLUTION WITH F8AR ;
- PRA INDEPENDENTLY REACHED CONCLUSION TO DELETE Sp INTERLOCK.
- NOT CURRENT OR FUTURE 8AFETY CONCERN. ;
- REEDENT IN8PECTORS BMEFED.
- REPORTABILITY EVALUATED BY DUKE 8% 3R COMPANY.
' i. . f. ,
O O ug u a JULY 1987 - NRC AUDOT . TEAM MEMBERS EXPRESSED CONCERN WITH RN SYSTEM D280GN.
- REPORTABILITY ONLY GPEclFIC CONCERN AT EXIT.
Material needed to be taken back to NRC for further analysis.
- 30.549 LETTER 8-7-87 REQUESTED INFORMA710N.
wi il n ra ou A '
lo k o e th r t n. ide Tech Spec bases.
- RESPONSE AND MEETING WITH NRC 8-27-87 DESCRIBED PROCEDURES.
INFORMA710N FROM LER 414/88-31-1.
ANALYSIS OF SCENARIO QU73lDE LICENSONG SA818.
Analysis performed in response to apparent concern, not to justify previous or future operation.
- NRC CONCURRED WITH PROCEDURE 4, REQUESTED INCLUSION IN TECH SPEC.
- COURTE8Y REPORT PREPARED,PREViCUS ALIGNMENT ERROR IDEN70FDED DURDNG FINAL REVIEW (10-12-87)- REPORT GUBMlTTED A8 TECH SPEC VOCLA7dSN.
1 ..
l MAR 141988 FEBRUARY 1988 - CURRENT STATUS OF 088UE8
. - REVISED LOCA DECAY HEAT LOADS. .
- DESIGN STUDY 888 RESOLVED:
- LOCA AND SHUTDOWN COOLING REQUIMSEENTS EQUAL (5200 GPM RN TO KC).
i
- DESIGN STUDY 880 RESOLVED:
l
- POST-LOCA SEISMIC REQUIREMENTS FOR 8N8WP CLARRED,8p RN TRANSFER DELETED.
- F8AR AND TECH 8PEC CHANGE 8 8UBMITTED. l 1
- PIT LEVEL INSTRUMENT MODIFICATION PLANNED.
l I
.i
~
- ~ s O O MAR 141988 ANALV808 0F TECM $PEC V00LA700% l 1
- ACCIDENT acENANO MOUOMO LOCA,LC28 CF 07F4072 POWER AND GPECIFiC FA0 LURE OF ONE VALVE. l
- EXISTING PLANT AENORMAL PROCEDURE TO ADDRECS SPECIFIC POSTULATED FA0 LURE DIRECTED CPERATOR TO PERFORM CORRECT AC700N FOR RECOVERY.
- APPROXIMATELY 40 MINUTES YiOULD BE AVA0LABLE TO PERFORM THE CORRECTIVE ACTION.
Only minimum cooltug is required until transfer to containment sump recirculation.
- NO PUMP DAMAGE WOULD MAVE CCCURRED PRIOR 70 PERFORMING THE CORRECTIVE ACTION.
Non-essential flow demand is equivalent to containment spray cooling which is not established until transfer to sump.
- UNIT 2 TfA8 SUBCRITICAL 72 NCURS P0"R 70 EXc.EEt0NIJ THE 70ME ALLOWED TO ENTER CCLD 2:NU700'XN.
l
- DECAY HEAT EXTREMELY LOW DUE 70 Lif GUM @.
1
.., s .. .
~
O MAR 14 888 CONCLUS00NS
- DUKE POWER COMPANY PERSONNEL WERE PROACTOWE IN EVALUATING RN SYSTEM OPERATION.
- THE RN SYSTEM WAS AT ALL TOME 8 OPERATED ON A MANNER CONSISTANT WITH THE FSAR.
l 3
- THE RN SYSTEM WA8 AT ALL TOMES ABLE 70 i' PERFORM 178 INTENDED FUNCTION, I
~ t..
O O MAR 141988 l
OPERABILITY /REPORTABILITY DECOSOON P00NTS TlHE FRAME TOPIC MAY 1988 RN EQUIPMENT / FLOW PATH 8 TO MEET T/8 (2 OPERABLE LOOP 8) FOR 2 UNIT MODE 1-4 OPERATION PUT IN T/8 INTERPRETATION FORMA 7.
ADDRESSE8 SINGLE FAILURE CRITERIA.
AUG 1988 LER IS8UED ON RN OPERABILITY, DESCRIBE 8 SHARED A8PECT OF SYSTEM AND REQUIRED ACTION 8 FOR OPERABILITY.
"lF A D/G 18 INOPERABLE,THE DEPENDENT RN TRAIN 18 CONSERVATIVELY DECLARED INOPERABLE ON BOTH UNIT 8 DUE TO THE 8 HARED NATURE OF THE RN SYSTEM"... .
" 0PERATION WITH LESS THAN 4 RN PUMP 8, REQUIRE 8- RN SYSTEM REALIGNMENT- TO EN8URE SUFFICIENT POST ACCIDENT FLOW IN THE EVENT ,
OF ANY 8 INGLE FAILURE."
OCT 1988 INITIAL DETERMINATION OF RN FLOW REQUIREMENT 8 WITH DIE 8EL OUT OF SERVICE.
..s.. .
O O MAR 141988 l
JAM 1987 POTENTIAL FOR PIT VALVE FAILURE I IDENTIFIED.TO DETERMINE IF BOUNDED BY ACCIDENT ANALYSIS. 4 MAR 1987 RN SNSWP SWAPOVER DESIGN STUDY,PART 1 DETERMINES PREVIOUSLY UNANALYZED CONDITION EXISTS.
APR 1987 PIR ISSUED TO DOCUMENT DETERMINATION OF SIGNIFICANCE OF UNANALYZED CONDITION.
MAY 1987 RN 8N8WP SWAPOVER LOGIC DESIGN STUDY, PART 2 CONCLUDE 8 Tl88 SPECFIC EQUIPMENT FAlLURE PREVIOUSLY UNANALYZED. DOE 8 NOT CONCLUDE RN FLOW REQUIREMENT 8 WOULD NOT HAVE BEEN MET. ADDITIONAL ANALYSIS REQUIRED.
AUG 1987 NRC REQUE8T8 ADDITIONAL INFORMATION ON RN QUESTION.DPC PROVIDE 8 RESPON8E.
LER SUBMITTED ON ERROR IN RN VALVE 1.BE-UP 30 AUG - 8 SEPT 1986. l SEP 1987 NRC CONFIRM 8 PREVIOU8 POSITION.RN '
MEET 8 GDC 5 AND 44 A8 OPERATED UNDER PROCEDURE 8.
_ . . ~
- q. . ..
O O mum CONCLUSIONS THE RN SYSTEM MAS ALWAY 8 BEEN OPERATED IN A MANNER WHICH 8ATISFIES THE F8AR ACCIDENT ANALYSIS AND THE 10 CFR 50 APPENDIX A GENERAL DESIGN CRITERIA.
THE TECHNICAL 8PECIFICATION INTERPRETATitN IMPLEMENTED QN MAY 1986 PROVIDED ONLY THE EQUDPMENT/All0NMENT DETAIL 8 NECESSARY TO MEET
. THE EXISTING RN T/8 REQUIRING 2 OPERABLE RN LOOPS.lT DOD NOT MODIFY THE EXISTING T/8 AND 17 DID NOT ADD ADDITIONAL REQUIREMENTS.
THE FSAR RN DESCRIPTION ONLY ADDRESSED RN REQUIREMENTS FOR 2 UNIT 8 IN MODE 1-4 OPERATION AND HA8 BREN CLARIFIED TO REFLECT THE RN ALIGNMENT FOR OTHER UNIT / EQUIPMENT COMBINATIONS.
(SUBMITTED WITH T/8 CHANGE REQUEST).
THE NRC WA8 COGNIZANT OF THE SHARED NATURE OF THE RN SY8 TEM AND DPC EFFORT 8 TO RESOLVE QUESTIONS OF REQUIRED EQUIPMENT AND SYSTEM ALIGNMENT.
DPC IDENTIFIED ALL OF THE IS8UES DEALING WITH RN OPERAT10N WITHOUT NRC PROMPTING AND RESOLVED THEM IN A TIMELY MANNER.(INCLUDING THE VIOLATION CITED FOR THIS ENFORCHENT '
CONFERENCE).
O O MAR 14 $88 OCT 1986 DESIGN ANALYZES RN FLOW REQUIREMENTS TO SUPPORT PLANT OPERATION WITH DIESEL OUT OF SERVICE GREATER THAN 72 HOURS.
. OPERABILITY - FLOW PARAMETERS FOR ONE UNIT OPERATING AND ONE UNIT SHUTDOWN (TWO LOOPS RHR) DETERMINED. ALIGNMENT ENSURES OPERABILITY UNDER TECHNICAL SPECIFICATION AND FSAR ACCIDENT ANALYSIS EDE IER OPERABLE ELDH LOOPS.
. REPORTABILITY - FSAR DOES NOT ADDRESS AB0VE FLOW CONFIGURATION OR PLANT OPERATION WITH ONE UNIT OPERATING AND ONE UNIT IN MODES 5/6. TVIS IS CONSISTENT WITH OTHER FSAR SYSTEM DESCRIPTIONS WHICH DO NOT' ADDRESS ALL POSSIBLE UNIT / EQUIPMENT COMBINATIONS OR MAINTENANCE CONDITIONS. TECHNICAL SPECIFICATIONS ARE STILL MET AND ACCIDENT ANALYSIS IS SATISFIED.
JAN 1987 STATION PROBLEM REPORT IDEN'TIFIES POTENTIAL FOR PIT VALVE FAILURE ON SWAPOVER AND RECOMMENDS MODIFICATION.
. OPERABILITY - CONDITION DESCRIBED (DIESEL INOPERABLE >72 HOURS) NOT PRESENT.
TECHNICAL SPECIFICATIONS WOULD CAUSE BOTH UNITS TO BE SHUTDOWN IF CONDITION OCCURRED WITH BOTH UNITS IN MODES 1-4.
. REPORTABILITY - SINCE FSAR DOES NOT ADDRESS THIS PLANT CONDITION (ONE UNIT UP, ONE UNIT DOWN) IT IS NOT APPARENT WITHOUT ADDITIONAL REVIEW IF THIS FAILURE IS B0UNDED BY PRESENT FSAR ACCIDENT ANALYSIS.
n 9
. MAR 141988 MAR 1987 RN STANDBY NUCLEAR SERVICE WATER POND SWAPOVER LOGIC DESIGN STUDY, PART 1 ISSUED.
. REPORTABILITY - STUDY CONCLUDES PROPOSED MODIFICATION MAY INVOLVE UNREVIEWED SAFETY QUESTION BY DELETING ONE OF TWO REDUNDANT SWAPOVER SIGNALS. POTENTIAL PIT VALVE FAILURE IS ALSO ADDRESSED AS "AN UNREVIEWED SAFETY QUESTION THAT NEEDS TO BE ADDRESSED." THIS STATEMENT WAS NOT INTENDED TO CONSTITUTE "AN UNREVIEWED SAFETY QUESTION" AS DEFINED IN 10 CFR 50.59, BUT AS A PREVIOUSLY UNANALYZED CONDITION WHICH REQUIRES ADDITIONAL ANALYSIS. THE ADDITIONAL ANALYSIS WOULD DETERMINE IF THIS FAILURE MECHANISM WAS REPORTABLE AS "AN UNANALYZED CONDITION WHICH SIGNIFICANTLY COMPROMISES PLANT SAFETY" AS DEFINED IN 10 CFR 50.72 AND 50.73.
APR 1987 PROBLEM INVESTIGATION REPORT (PIR) ISSUED (BASED ON FINDINGS IN THE AB0VE DESIGN STUDY)
TO DETERMINE IF THE PROBLEM DEFINED IN THE SPR IS "AN UNANALYZED CONDITION" THAT "SIGNIFICANTLY COMPROMISES PLANT SAFETY."
. OPERABILITY - POTENTIAL FAILURE MECHANISM DOES NOT CONSTITUTE NEAR TERM OPERABILITY PROBLEM. FOR DIESEL OUT OF SERVICE GREATER THAN 72 HOURS SYSTEM IS PARTIALLY ALIGNED TO POND REMOVING VALVE FAILURE AS PROBLEM.
LONGER TERM OPERABILITY QUESTION'WILL BE RESOLVED WHEN ADDITIONAL ANALYSIS IS COMPLETE.
1
2.
~
0, O rsAa141988
. REPORTABILITY - PRELIMINARY CORRESPONDENCE FOR PART 2 0F THE SNSWP SWAPOVER LOGIC DESIGN STUDY DEMONSTRATES LOW LIKELIHOOD OF EVENT IN QUESTION (I.E. SINGLE FAILURE, LOSS OF LAKE, BLACK 0UT, DIESEL IN0P). PRA ARGUMENT SEEN AS SUFFICIENT TO SHOW THIS IS NOT "AN UNANALYZED CONDITION THAT SIGNIFICANTLY COMPROMISES PLANT SAFETY" AT THIS TIME.
MAY 1987 RN STANDBY NUCLEAR SERVICE WATER POND SWAPOVER LOGIC DESIGN STUDY, PART 2 ISSUED.
. OPERABILITY - NO ADDITIONAL INFORMATION CHALLENGES THE EXISTING DETERMINATION OF CURRENT OPERABILITY.
. REPORTABILITY - THE STUDY CONCLUDES THAT THE PROBLEM IDENTIFIED IS A "PREVIOUSLY UNANALYZED SITUATION THAT NEEDS TO BE ADDRESSED." THE SINGLE ACTIVE FAILURE CAUSING LOSS OF TWO FN PdMPS IS RECOGNIZED AS WELL AS THE PROPOSED MODIFICATION, ALTERNATIVES, AND THE STATISTICAL PROBABILITY OF THE SEQUENCE OF EVENTS AFTER MODIFICATIONS. THE REPORT D0fS HDI CONCLUDE THAT THE PLANT WAS OPERATED OUTSIDE ITS DESIGN BASIS, OR THAT TECHNICAL SPECIFICATIONS WERE VIOLATED, OR THAT LOSS OF THE TWO PUMPS WOULD RESULT IN INSUFFICIENT RN FLOW FOR THE SCENERIO DESCRIBED. FOR REPORTABILITY UNDER 10 CFR 50.72 AND 50.73 THE "UNANALYZED CONDITION THAT SIGNIFICANTLY COMPROMISED PLANT SAFETY" IS CONSIDERED TO COVER THE
- REQUIREMENT FOR OPERABLE FLOW LOOPS RQI
- 1
r F
- .'- 7 O O WAR 141988 INDIVIDUAL EQUIPMENTS, NOTE THAT THE RULE ADDRESSES FAST TENSE CONDITIONS THAT EXISTED. THE PROCEDURES BY WHICH THE RN SYSTEM HAS BEEN OPERATED SINCE UNIT TWO CRITICALITY WERE DESIGNED TO ENSURE SUFFICIENT RN FLOW UNDER ALL ACCIDENT CONDITIONS. ABSENT A DISCOVERY OF THE POSSIBILITY OF PAST INSUFFICENT RN FLOW AS A RESULT OF THIS SCENERIO, IT WAS NOT DEEMED TO BE A REPORTABLE EVENT.
THE SRI ELEVATES THE ISSUE TO URI STATUS IN REPORT NUMBER 413/87-10. DPC ACTIONS TO JUSTIFY CONTINUED OPERATION AND THE ONGOING PRA/ DESIGN STUDY ARE SUMMARIZED.
JUL 1987 NRC QUALITY VERIFICATION INSPECTION (413/87-23) TEAM RAISES CONCERN THAT RN SYSTEM DESIGN IS NOT ANALYZED FOR THIS EVENT, THAT PRA IS NOT ACCEPTABLE TO DETERMINE SIGNIFICANCE, AND THAT DPC' FAILED TO REPORT UNDER REQUIREMENTS OF 10 CFR 50,72 OR 10 CFR 50,73 (THE NRC REPORT IS ISSUED IN NOVEMBER 1987),
AUG 1987 REVIEW 0F PAST INSTANCES OF PLANT IN THE CONDITION UNDER QUESTION CONCLUDE NO UNANALYZED CONDITION HAS EVER EXISTED. AN ACTUAL HEAT LOAD ANALYSIS WILL BE CONDUCTED TO RE-VERIFY THIS FOR 22 AUG - 1 SEPT 1986 TIME FRAME, NRC ISSUES REQUEST FOR ADDITIONAL INFORMATION ON RN,
l > . . '. + ~-
O n v MAR 14 $88 DPC PROVIDES RESPONSE TO 50.54(F) LETTER, CONCLUDES THE PLANT MEETS GDC 5 AND 44.
PROVIDES ADDITIONAL ANALYSIS THAT A SINGLE RN PUMP CAN REMOVE HEAT LOADS EXPECTED DURING POSTULATED CONDITIONS UNDER QUESTION (INCLUDING LOCA), AND PROVIDES JUSTIFICATION FOR CONTINUED OPERATION.
A REVIEW 0F VALVE LINE-UP DATA USED TO CONFIGURE RN FOR THE 30 AUG - 8 SEPT 1986 TIME FRAME IDENTIFIES ERROR. THIS ERROR IS DETERMINED REPORTABLE UNDER 10 CFR 50.73 AND LER 413/87-36 IS SUBMITTED.
SEP 1987 NRC ISSUES LETTER CONFIRMING RN SYSTEM MEETS GDC 5 AND 44 AS OPERATED UNDER PROCEDURES IN PLACE. REQUESTS TECHNICAL SPECIFICATIONS BE MODIFIED TO REFLECT SHARED ASPECTS OF RN SYSTEM.
l i
( . - *
' 6.' % ..
~ '
MAR 14 $88 CATAWBA NUCLEAR STATION TECHNICAL SPECIFICATION INTERPRETATION TECHNICAL SPECIFICATION (S) AFFECTED: 3.7.4, Nuclear Service Water System REVISION: 0 DETAILS:
The Nuclear Service Water System (RN) contains pumps which are unit designated, i.e., lA, 2A, 1B, 2B, yet supply both units through common discharge piping. All RN pumps receive auto-start signals from a safety signal on either unit. Accordingly, the following interpretations are made with respect to RN System OPERABILITY:
An RN pump designated to one unit may be assumed to supply post i accident RN requirements to equipment on the opposite unit 1
provided its associated emergency diesel generator is OPERABLE '
AND RN system valve alignments are such that the required RN equipment will receive the required flows. ,
Since three RN pumps can supply sufficient flow for four RN trains but cannot do so if a single failure occurs, this !
configuration does not represent two independent RN trains for l each unit. Therefore, with only three RN pumps OPERABLE, the l action stetament for one RN train out of service must be entered 1 for both units or sufficient RN supplied equipment isolated.
This assures that the required post-accident flows will be
)
I supplied to the remaining OPERABLE RN suppli'ed equipment in the l event of any single failure. Only isolated RN supplied equipment must be declared inoperable.
If less than three RN pumps are OPERABLE, both units must enter .
Tech Spec action statement 3.0.3 until sufficient RN supplied I equipment is isolated to assure that at least one RN train ~per unit or two trains on the same unit, will receive the required post-accident RN flows.
BASIS: Review of Technical Specification. Discussion with Design Engineering.
APPROVAL: = Ms J. W. Hampton,~ Manager Catawba Nuclear Station DATED: 5 - /r- rc