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MONTHYEARML20198A0081985-09-0909 September 1985 Forwards SER Input Re Nonconformance W/Requirements of App R as Defined by Region V Task Interface Agreement 85-37. Licensee Corrective Actions & Interim Compensatory Measures Acceptable,W/Exception of High/Low Pressure Valves Project stage: Approval ML20140B8251985-12-0404 December 1985 Safety Evaluation Accepting Util Re Conformance to App R Requirements Project stage: Approval ML20140B8191985-12-0404 December 1985 Forwards SER Re App R Nonconformance Issue,Per 850619 Memo. Util 850617 Resolutions to Acceptable W/Listed Provision.Task Initiation Action 85-37 Complete Project stage: Approval ML20140B8111986-03-14014 March 1986 Forwards SER Re App R Nonconformance Issue Identified in Kirsch 850607 & Sorensen s.Implementation of Item 7 on RHR Values Requested.Corrective Actions Will Be Verified in Future Insp Project stage: Approval 1985-09-09
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20213F1841986-11-0606 November 1986 Safety Evaluation Re Util 850614 Request for Approval to Use ASME Boiler & Pressure Vessel Code,Section XI,1983 Edition, Winter 1984 Addenda,Subsection IWA 2213.NRC Evaluation of Winter Addenda Incomplete.Request Denied ML20140B8251985-12-0404 December 1985 Safety Evaluation Accepting Util Re Conformance to App R Requirements ML20198F4041985-10-30030 October 1985 Safety Evaluation Supporting Licensee 830624 & 1110 Ltrs Addressing License Condition 22, Control Sys Failures & IE Bulletin 79-27 ML20198F5871984-03-20020 March 1984 SER Recommending Acceptance of Applicant Action Re Magnetic Particle Linear Indications on Containment Weld Pads ML20198E9781984-01-27027 January 1984 SER Concluding Applicant Demonstrated That Structural Integrity of Sacrificial Shield Wall Will Meet Design Requirements W/Known & Postulated Flaws ML20198E9311984-01-23023 January 1984 SER Recommending Applicant Actions Re Magnetic Particle Linear Indications on Containment Weld Pads ML20213D6771981-04-13013 April 1981 Safety Evaluation Concluding That Proposed Spent Fuel Storage Racks Meet General Design Criteria 62 Criticality Requirements 1986-11-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
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.i. r SAFETY EVALUATION REPORT WASHINGTON NUCLEAR PROJECT NO. 2 APPENDIX R REQUIREMENTS - NONCOMPLIANCE AUXILIARY SYSTEMS BRANCH We have reviewed the licensee's'. submittal dated June 17, 1985 per Region V's request for NRR's assistance dated June 19, 1985, concerning the conformance
-of WNP-2 to the requirements of Appendix R. The region's letter stated that certain equipment required to safely shutdown the plant "may become inoperable in the event of a design basis control room fire." - This same letter implies that the requirements of Appendix R apply to WNP-2 by stating in the subject of the letter: "Nonconformance of Safety Equipment to' Appendix R Require-ments." Appendix R does not apply to'WNP-2. Only the guidelines of Section 9.5.1 of NUREG-0800 (Standsrd Review Plan) apply to WNP-2.
The li onsee's submittal dated June 17, 1985, referenced WNP-2 Licens'e
-Condition No. 12. This license condition refers to having an operable second panel for remote shutdown by the first refueling. A discussion of this
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licensee condition can be found in Section 7.4 of the SER and is associated with meeting General Design Criterion 19, " Control Room," not the require-ments of Appendix R or the guidelines of Section 9.5.1 of NUREG-0800.
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The attachment to the licensee's submittal identified sesen items which, if they failed during a control room fire, would impair the ability to' safely ,
_ shutdown the plant. .The licensee stated that these' items and the associated design modification packages will "be reported in LER 84-031-04." Thus the licensee has been and continues to be conscientiously informing the staff of problems as they are di. overed, of interim measures, and of planned resolution. Of the seven ftems, five of the items deal with loss of power from diesel generator Number 2 by tripping various output breakers. For each of the five f.tems the licensee has proposed interim procedures in the event of a control room fire in order to maintain the capability to safely shutdown
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the plant. The proposed long term corrective actions, which will be completed by the second refueling outage, are reasonable.
Noh ! 7
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p >
2 The sixth item concerns the . loss of a 24 VD_C instrument ~ power supply. The loss of this ~ power supply would result-in no standby service water pump dis-charge header pressure indication in the remote shutdown room. The loss of this instrumentation is acceptable because indication of proper operation of the standby service water pump can be inferred by local observation of the operating punp and of the ultimate heat sink, performance of.the serviced equipment, and diesel generator loadings. The licensee will install a trans-fer switch, by the second. refueling, to isolate tne power supply from the.
control room. The. proposed corrective actions are acceptable.
Item seven-deals with the potential opening of the high/ low RHR pressure 3 interface 'due to a control room fire generating an open signal to both valves )
RHR-V-53A and RHR-V-123A which are in series. As an interim measure, the \
licensee must remove power from one of these valves, such as by opening the
-3 breake'r to the valve.~ Although this is an acceptable means to resolve the high/ ,
low pressure interface problem the licensee has proposed installing a' transfer switch outside of the control room in order to isolate one valve from the control room in the event of a fire in the control room. This is acceptable provided that the transfer. switch is maintained normally in the " isolate from the control: room" position. Pending acceptance of this interim measure, the interim measures and corrective actions are acceptable.
Based on the low probability of a control room fire, the interim compensatory measures, the ability to safely shutdown, and the acceptability of ~the corrective actions, we conclude that with the power removed from an RHR isolation _ valve and the RHR isolation switch maintained in the isolate position that the approach taken by the licensee is reasonable and acceptable. Therefore we conclude that continued operation of the facility will not adversely effect the health and safety of the public and is, therefore, acceptable.
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