ML20135F571
| ML20135F571 | |
| Person / Time | |
|---|---|
| Site: | Maine Yankee |
| Issue date: | 12/09/1996 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20135F544 | List: |
| References | |
| 50-309-96-12, NUDOCS 9612130130 | |
| Download: ML20135F571 (87) | |
See also: IR 05000309/1996012
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U. S. NUCLEAR REGULATORY COMMISSION
REGION i
Docket No:
50-309
License No:
Report No:
50-309/96-12
Licensee:
Maine Yankee Atomic Power Company (MYAPC)
Facility:
Maine Yankee Atomic Power Station
Location:
Bailey Point
Wiscasset, Maine
Dates:
September 15 through October 26,1996
Inspectors:
Jimi Yerokun, Senior Resident inspector
Division of Reactor Projects
William Olsen, Resident inspector
Division of Reactor Projects
{
John Lusher, Emergency Prepardness Specialist
Division of Reactor Safety
Lonny Eckert, Radiological Controls Specialist
Division of Reactor Safety
Jason Jang, Radiological Controls Specialist
Division of Reactor Safety
Approved by:
Richard Conte, Chief, Reactor Projects Branch No. 5
Division of Reactor Projects
9612130130 961209
ADOCK 05000309
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EXECUTIVE SUMMARY
Maine Yankee Atomic Power Company
NRC Inspection Report 50-309/96-12
This integrated inspection included aspects of licensee operations, engineering,
maintenance, and plant support. The report covers a 6-week period of resident inspection;
in addition, it includes the results of announced inspections by regional inspectors in the
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areas of Radiological Controls and Emergency Prepardness.
Ooerations
The operators performed all observed tasks in accordance with station procedures with a
very good safety perspective in evidence. The decision to reduce station power to
investigate the bearing cooling water problem with the circulating water pump was well
controlled. Operators responded well to the unplanned reactor trip and properly completed
the steps of emergency operating procedure E-0, Reactor Trip or Safety injection; along
with other challenges due to the material condition problems. The Shift Operating
Supervisor displayed excellent command and control of the operating crew during the
period of observation. The Post Trip Review Team provided a very detailed report with an
excellent basis for the conclusions that were drawn and the recommended corrective
actions (short and long term). Station management provided good oversight and direction
to ensure that all the necessary corrective actions were completed prior to plant restart.
A violation of the station Off-Site Dose Calculation Manual and T.S. 5.8.a.3 was identified
when the Primary Vent Stack Air Particulate and Gas Monitoring System filters were not
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installed during maintenance and apparently due to procedure inadequacy and/or personnel
error (VIO 50-309/96-12-01, Section O2.1). Prompt immediate corrective action was
)
taken, however, root cause and long term corrective actions are yet to be determined.
Instances of operator performance weakness were noted, such as the unplanned power
excursion during a RCS delithiation. While operators performed well to restore the reactor
to a steady power level of 2440 MWt, performance weaknesses contributed to the power
excursion occurring in the first case. The licensee's root cause analysis was still on-going
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and the appropriateness of implemented corrective actions still needs to be verified
(URI 50-309/96-12-02, Section 04.1).
PORC meetings were conducted well and safety focused. PORC continued to demonstrate
good technical and safety perspective in addressing plam~ issues.
Maintenance
l&C personnel provided good support to the plant and conducted troubleshooting activities
in a safe and controlled manner. In the case of the RPS trip breakers the decision to
replace all the circuit components was very conservative and displayed an excellent safety
perspective. Station maintenance management properly provided guidance to ensure that
all possible avenues of repair were exercised prior to completion of repairs.
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Maine Yankee promptly accessed the operability of the containment high range radiation
monitor and conservatively declared the channel inoperable until troubleshooting and
calibration activities were complete.
Electrical maintenance personnel demonstrated excellent support to operations by timely
identifying and resolving the problem with control rod (malfunctions), thereby preventing
an unnecessary transient to the plant. However, based on problems experienced in the
past, it appeared that this was indicative of a weakness in the licensee's process. What
appeared to be appropriate actions were planned and are being taken to control the
problem. During and following troubleshooting activities, plant personnel showed good
safety perspective and ensured that the plant was always maintained safely. However, the
problems with the Control Element Assemblies (CEAs) were similar to those that occurred
during reactor startup the previous month and it appears that the right solution of the
previously identified problems had not been made. While the problems concern a non-
safety related system, they produced unnecessary burden on control room operators during
their operation of the plant.
l&C personnel responded timely and performed well by safely and quickly diagnosing the
problem (failed RPS channel C trips) and correcting it. Plant personnel showed good safety
focus and ensured that the plant continued to be operated safely while the troubleshooting
and repair efforts were on-going.
Enaineerina
Engineering personnel demonstrated good efforts at addressing the turbine building design
issues affecting cold weather operations. The activities of the corporate engineering and
licensing department personnel appeared technically sound and detailed. There was good
management attention and involvement in addressing these issues.
Plant Sucoort
Maine Yankee radiation protection department properly responded to unplanned exposure
events. The analysis of the data was thorough with proper review by independent
expertise. Most of the conclusions were appropriate. However, the inspector noted that
one of the conclusions for the Duratek event did not properly take into consideration the
experience and training of the two individuals that were involved in the event. While no
personnel exposures exceeded regulatory limits, the contamination and exposure controls
at Maine Yankee were weak.
The licensee established, implemented, and maintained effective radioactive liquid and
gaseous effluent control programs. The Radiation Monitoring Systems (RMSs) for effluent
processes were well maintained. Licensee completion of several RMS upgrades and the
RMS manual demonstrated the licensee's commitment to a strong Radiological
Environmental Monitoring Program (REMP).
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Overall, maintenance and surveillance of the ventilation systems was adequate. The
licensee had not documented the plant air balance surveillance results to demonstrate
consistency with Chapter 9.13 of the UFSAR assumptions. Section 9.13.2.4 of the
USFAR had not been updated. These items will be reviewed during a subsequent
inspection (IFl 50-309/96-12-03, Section R2.3).
The licensee's Off-Site Dose Calculation Manual (ODCM) contained sufficient specification,
information, and instruction to implement and maintain the radioactive liquid and gaseous
effluent control programs. The content of the Annual Report was very good and met the
TS reporting requirements. Oversight of the REMP was improved. No degradation was
noted as a result of the reorganization.
In the area of Emergency Preparedness both the CATS and the self-assessment program
appeared to be an effective licensee control. Facility inventories were complete, radiation
survey instrumentation was within the calibration requirements and the emergency
response facilities were found to be in a state of operational readiness. However, an
instance was identified where maintenance activity might have negatively affected the
Emergency Response Facility (ERF) ventilation system (URI 50-309/96-12-04, Section
P8.2).
The training program was being effectively implemented and the Emergency Response
Organization (ERO) is adequately staffed. The licensee maintained on-shift dose
assessment and adequate back-up capabilities to ensure that on-shift dose assessments
could be performed.
A violation for failure to properly control Safeguards Information SI was identified
(VIO 50-309/96-12-05, Section S1.1). This violation is notable in that there have been
severalinstances of failure to properly control safeguards information in the last three
years. It appears that previous corrective actions have been too narrow in scope to
prevent recurrence.
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Maine Yankee, with assistance from off site security specialists, properly performed the
required annual audit of the security program. The audit was comprehensive with the
proper involvement of the station quality programs department. Corrective actions were
appropriate to resolve the observations. However, the observation concerning the control
of Si material appears to require more extensive corrective actions to resolve the problem
of continued failures in this area.
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TABLE OF CONTENTS
TA B LE O F C O NTE NTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v
l . O p e ra t io n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
01
Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
01.1 General Comments (71707) . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
01.2 Plant Trip During Surveillance Testing . . . . . . . . . . . . . . . . . . . . . 1
02
Operational Status of Facilities and Equipment
3
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02.1 Primary Vent Stack Sampling Filters Not Installed
(VIO 50-309/96-12-01V)
3
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02.2 Loss of Plant Computer . . . . . . .
4
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02.3 Spurious Trip of Reactor Protection System, Channel C . . . . . . . . 5
04
Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 6
04.1 Unplanned Reactor Power increase During Delithiation
(URI 50-309/9 6- 12-0 2) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
08
Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8
08.1 Plant Operations Review Committee . . . . . . . . . . . . . . . . . . . . . . 8
11. Maintenance . . . . . . . . . . .
9
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M1
Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
M 1.1 G eneral Activitie s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
M1.2 Troubleshooting of Reactor Protection System Matrix
Trip Circ uit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
M1.3 Troubleshooting and Repair of Containment Radiation Monitor . . 10
M2
Maintenance and Material Condition of Facilities and Equipment . . . . . . 11
M2.1 Broken Handwheel on Valve LSI-M-11
11
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M2.2 Operability of Containment High Radiation Monitor
12
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M2.3 Inoperable Pressurizer Proportional Heater Trains . . . . . . . . . . . . 13
M2.4 Control Element Assernbly Problems During Reactor Startup . . . . 14
111. Engineering
16
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E2
Engineering Support of Facilities and Equipment
16
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E2.1 Design issues Affecting Cold Weather Operations
in the Turbine Building (update URI 50-309/96-08-02 and
50-309/96-08-04)
16
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I V. Pl a nt S u p p o rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
R1
Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 17
R 1.1 Multiple Contamination Events and Unplanned Exposures
17
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R1.2 Implementation of Radioactive Liquid and Gaseous Effluent
Co ntrol Prog ra m . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
R2
Status of RP&C Facilities and Equipment
20
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R2.1 Effluent / Process Radiation Monitoring Systems . . . . . . . . . . . . . 20
R2.2 Air Clea ning Systems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
R2.3 Ventilation Systems Air Balance (IFl 50-309/96-12-03)
23
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R3
RP&C Procedures and Documentation
23
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R3.1 Off Site Dose Calculation Manual Review . . . . . . . . . . . . . . . . . 23
R6
RP&C Organization and Administration . . . . . . . . . . . . . . . . . . . . . . . . 24
R6.1 Radioactive Liquid and Gaseous Effluent Program Review
24
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R7
Quality Assurance in RP&C Activities . . . . . . . . . . . . . .
25
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R7.1 Quality Assurance Audit Report Review . . . . . . . . . . . . . . . . . . 25
R8
Miscellaneous RP& C issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
R8.1 Review of Updated Final Safety Analysis Report (UFSAR)
Com mitm e nts . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
P1
Conduct of Emergency Preparedness (EP) Activities
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P1.1 Emergency Planning Self-Assessment Program and Corrective
Action Tracking System
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P2
Status of EP Facilities, Equipment, and Resources . . . . . . . . . . . . . . . . 27
P2.1 Emergency Planning Equipment Inventories and Surveillance
27
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P3
EP Procedures and Documentation
28
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P3.1 Review of Emergency Response Plan Changes (Closed, URI 50-
309/9 6-007-01 ) . . . . . . . . . . . . . . . . . . . . . . . . . .
28
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P5
Staff Training and Qualification in EP . . . . . . . . . . . . . . . . . . . . . . . . . 29
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PS.1 Emergency Planning Training Program Evaluation
29
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P6
EP Organization and Administration . . . . . . . . . . . . . . . . . . . . . . . . . . 30
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P6.1 Emergency Planning Staffing and Management Changes . . . . . . 30
P7
Quality Assurance (QA) in EP Activities
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P7.1 Review of Annual Emergency Planning Program Audit Reports . . 30
P8
Miscellaneous EP Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
P8.1 Updated Final Safety Analysis Report (UFSAR) Inconsistencies . . . 31
P8.2 Emergency Response Facilities Ventilation System
(U RI 50-3 0 9/9 6-12-04) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
S1
Conduct of Security and Safeguards Activities . . . . . . . . . . . . . . . . . . 33
S1.1 Control of Safeguards Information (VIO 50-309/96-12-05)
33
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S7
Quality Assurance in Security and Safeguards Activities . . . . . . . . . . . 34
S7.1 Review of Annual Security Program Audit . . . . . . . . . . . . . . . . . 34
V. M a n a g e m e n t M e e ting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 35
X1
Exit Meeting Summ a ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 35
X 1.1 Routine Resident inspection Exit Meeting . . . . . . . . . . . . . . . . . 35
X1.2 Radiological Control Inspection Exit Meeting . . . . . . . . . . . . . . . 35
X1.3 Emergency Preparedness inspection Exit Meeting
35
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X3
Management Meeting Summary
35
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X3.1 Independent Safety Assessment Team Exit Meeting
35
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PARTIAL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
INSPECTION PRO CED URES USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 37
LIST OF ACRONYMS USED
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Report Details
Summary of Plant Status
Maine Yankee began this inspection period at 82% power. This was due to a power
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reduction on September 10,1996, when a problem with main circulating water pump,
P-6D, bearing cooling water flow was identified. The plant returned to 90.3% power on
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September 17, after completion of repairs to the pump. On October 9,1996, the plant
tripped from 90.3% power during reactor trip breaker surveillance testing. The reactor was
re-started on October 12,1996, and the plant returned to 90.3% power on October 14,
1996, and remained there for the remainder of the inspection period.
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I. Operations
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Conduct of Operations
01.1 General Comments (71707)
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Using Inspection procedure 71707, the inspectors conducted reviews of ongoing
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plant operations. The operators performed all observed tasks in accordance with
station procedures with a very good safety perspective in evidence. The reduction in
station power to investigate the bearing cooling water problem with the circulating
water pump was well controlled. In addition, station operators responded very well
to the unplanned reactor trip during reactor trip breaker surveillance testing.
Operator performame, when challenged by material condition problems, was good.
In particular, Plant Shift Superintendent (PSS) questioning attitude led to the
identification of a material condition problem (Section M2.3).
01.2 Plant Trio Durina Surveillance Testina
a.
Inspection Scope (92901)
The inspector observed the on-shift operations crew during the recovery phase of a
plant trip in the control room. In addition, the inspector reviewed the Post Trip
Review Team report which documented the event and attended the station plant
operations review committee (PORC) meeting when the report was reviewed. The
inspector also observed the instrument and controls (l&C) technicians during the
retest of the reactor trip breakers after troubleshooting and repairs were completed.
b.
Observations and Findinas
On October 9,1996, The reactor automatically tripped off line from 90% power. At
the time of the trip, station l&C personnel were conducting routine monthly
surveillance testing of the reactor trip breakers in accordance with station procedure
3-6.2.2.11, " Logic Relays Trip Test". The trip was uncomplicated and all control
rods fully inserted into the reactor core. Both emergency feedwater pumps
automatically started on low steam generator level and one of the two non-safety
electric motor driven feedwater pumps automatically started on low feedwater
header pressure (the other feedwater pump was isolated from service as expected).
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When steam generator water level stabilized, both emergency feedwater pumps were
stopped. The inspector observed operator performance and equipment response
from the control room. Operator performed well and maintained the plant safely. All
safety related systems responded as expected. There was no need for a safety
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injection actuation and none occurred.
The computer sequence of events log was printed out for the event and is listed
below:
- Reactor Trip Breakers Open
- Reactor Trip Computer Alarm (PTID 3809)
- Relay Actuation for Turbine Trip (20 ET)
- Relay Actuation for Backup Turbine Trip (20 AST)
- Turbine Valves Shut
- Reactor Trip (loss of load, Thermal Margin / Low Pressure,
- Low Steam Generator Level)
The normal sequence of events for a reactor trip is listed below:
- Reactor Trip (Due to a normal initiating signal)
- Reactor Trip Breakers Open
- Reactor Trip Computer Alarm (PTID 3809)
- Relay Actuation for Turbine Trip (20 ET)
- Relay Actuation for Backup Turbine Trip (20 AST)
- Turbine Valves Shut
The above information indicated that the reactor trip initiating event was an
inadvertent opening of the reactor trip breake"s without a reactor trip signal.
In response to the reactor trip, Maine Yankee station management directed that a
Post Trip Review Team be assembled to evaluate the event and provide
recommendations for corrective actions. The inspector noted that the team
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demonstrated a good questioning attitude and a good safety focus. The team
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determined that the most probable cause for the trip was a loss of test power voltage
during performance of reactor protection system (RPS) logic trip relay testing.
The inspector also observed maintenance activities being conducted to determine the
cause of the trip. Troubleshooting by I&C personnel did not identify any failed or
degraded components. Simulation of a failed test power supply gave the identical
indications that were observed during the reactor trip. As a precautionary measure
l&C technicians replaced the RPS trip matrix test power supply and the test hold
push button which were part of the circuit undergoing testing at the time of the
event. Also, prior to performance of the next routine monthly surveillance test,
Maine Yankee plans to replace the matrix relay trip select switch. During the next
monthly surveillance test, the test power supply voltage will be constantly monitored
to ensure that the voltage remains stable during testing or the testing will be
terminated.
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On October 12,1996, the plant was restarted after plant management reviewed and
approved the findings and conclusions of the Post Trip Review Team report. This
included a review of the completed maintenance and surveillance testing on the
equipment that was undergoing testing at the time of the plant trip.
c.
Conclusions
Operators responded well to the unplanned reactor trip and properly completed the
steps of emergency operating procedure E-0, Reactor Trip or Safety injection. The
Shift Operating Supervisor displayed excellent command and control of the operating
crew during the period of observation. The Post Trip Review Team provided a very
detailed report with an excellent basis for the conclusions that were drawn and the
recommended corrective actions (short and long term). Station management
provided good oversight and direction to ensure that all the necessary corrective
actions were completed prior to plant restart.
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Operational Status of Facilities and Equipment
02.1 Primarv Vent Stack Samolina Filters Not Installed (VIO 50-309/96-12-01 V)
a.
Inspection Scope (71707)
The inspector reviewed the event involving the primary vent stack filters, the short
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term corrective actions and discussed the chronology of the event with operations
department personnel. This inspection was to assess the licensee's actions to
determine the appropriateness and regulatory compliance.
b.
Observations and findinas
On October 1,1996, the primary vent stack (PVS) high range particulate, gas,
halogen, and particulate filters were taken out of service to allow station instrument
and controls technicians to repair the PVS air particulate detector (APD). Alternate
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sampling was invoked to compensate for the loss of halogen and particulate filters.
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This consisted of removing the normal halogen and particulate filters and operating
an alternate filter cartridge. The normal station practice is to remove the filters from
the normal cartridge and reinstall them in the alternate cartridge,
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The normal sampling system was returned to service on October 4,1996. The
station radiochemist, upon being informed that the normal sampling system was back
in service, performed an independent verification of the filter arrangement and found
that the iodine and particulate filter cartridges were not installed. The filters were
immediately installed in the normal PVS sampling system and the system was
returned to normal operation.
The plant operations department investigated the problem and determined that
station procedure 1-12-8, " Primary Vent Stack Air Particulate and Gas Monitor"
section 6.3, Auxiliary PVS Sampling System, did not specifically direct operators to
ensure that the halogen sampler cartridge and a particulate filter paper disk were
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installed in the normal sampling system prior to operation. A temporary procedure
change (TPC 96-328) was initiated to revise procedure 1-12-8 to resolve this
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problem prior to the system configuration being changed again.
Maine Yankee personnel disabled the Primary Vent Stack Air Particulate and Gas
Monitoring System by not installing the filter cartridge for a period of approximately
one hour due to a deficient procedure and personnel error. The f ailure to install the
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Primary Vent Filter is a violation Station T.S. 5.8.a.3. Technical Specification 5.8.a.3
requires in part that monitoring, sampling and analysis of radioactive gaseous effluent
is in accordance with 10 CFR 20.106 and with the methodology and parameters in
the ODCM (VIO 50-309/96-12-01).
At the completion of the inspection the licensee revised the station procedure
1-12-8, " Primary Vent Stack Air Particulate and Gas Monitor" and trained all
operations personnel as to the requirements of the procedure change.
c.
Conclusion
The inspector identified a violation of the station Off-Site Dose Calculation Manual
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and T.S. 5.8.a.3 when the Primary Vent Stack Air Particulate an Gas Monitoring
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System filters were not installed as required during conduct of maintenance activity.
02.2 Loss of Plant Computer
a.
Insoection Scope (71707)
The inspector reviewad the licensee's actions and processes to deal with the loss of
the plant computer on October 22,1996.
b.
Observations and Findinas
During the daily control room observation on October 22,1996, the inspector
observed operators following a problem with the computer not being available.
Inquiries revealed that the computer had failed and that the loss of the computer also
involved a loss of the Safety Parameter Display System (SPDS) in the Control Room
and the Emergency Centers. Also, the loss involved a loss of the on-line incore
analysis (INCA) program.
The computer system consists of two parallel front end systems (FES) for data
collection which input into two parallel operational support system (POSS) which
then input into two parallel emergency supply systems (ESS). The inputs into the
SPDS and the Emergency Response Data System (ERDS) is provided by the ESS.
The on-line INCA program is provided by the OSS. Three data gathering channels
(CH20, CH22 and CH24) provide data into each of two FES.
The loss of SPDS for over a period of 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> was reported to the NRC in accordance
with 10 CFR 50.72(B)(1)(V) for a major loss of emergency assessment capability.
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The Emergency Notification System (ENS) phone to the NRC was available as backup
to the ERDS. Plant personnel continued to perform incore analysis as required by
TS 3.10.C, Power Distribution Limits, without the plant computer. Operators also
began performing Precedure 1-4-1, Plant Operations Without the Plant Computer.
The inspector verified that plant information and parameters continued to be available
to operators who maintained safe operation of the plant. The loss of the computer
had no effect on the safe operation of the plant. The loss would have been a
challenge to operators during emergency response because the data on the computer
would not have been readily available. However, all the necessary information would
still be available on the various indicators and recorders.
The licensee's computer department personnel identified several failed data
acquisition controlled cards and a failed power supply during troubleshooting
activities. These failed components were replaced and subsequently tested
satisfactory.
Also, there appeared to be some inadequacies in the control of parts especially
during the change of vendors in early 1992. Two versions (Revision 5 and 6) of
power supplies for the file in the FES had been used when the update (Revision 5
and 6) had been inadequately communicated to the new vendor. The wrong version
of power supply reflects a communication problem, but it is not clear it led to the
failure of the power supply (UOR No.96-101).
c.
Conclusion
Troubleshooting efforts by computer department personnel were good. Operators
responded well to the problem and completed the required actions to ensure that loss
of the support functions provided by the computer did not affect the safe operation
of the plant. However, the inspector noted some weaknesses in the control of the
plant computer system.
The computer was repaired and restored to service on October 23,1996, and has
remained operational since.
02.3 Sourious Trio of Reactor Protection System, Channel C
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a.
Insoection Scone (71707. 62707)
On September 27,1996, a spurious trip of the reactor protection system (RPS)
Channel C; High Power, Symmetric Offset, and Thermal Margin Low Pressure trips
occurred. The inspector observed control room and troubleshooting and repair
activities following the channel trip.
b.
Observations and Findinas
During a control room tour on September 27, the inspector observed that three
channel C trip bins on the RPS panel were lit. The trips were as stated above. The
inspector verified that the corresponding annunciator panel alarms for these trips
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were illuminated. The annunciators were R3-4, Power Dependant insertion Lo-Lo
Limit Any Group and R3-11, Hi Power Level Channel C. The inspector reviewed the
actions discussed in Alarm Response Procedure (ARP) 2-37.R to be taken in response
to the alarms. The inspector also reviewed the current plant conditions and
parameters; and ascertained, that despite the channel C trips, an actual plant trip
was not required. The plant was operating steadily at 90% power with all plant
parameters normal. Allindications on RPS channels A, B and D remained normal.
Operators responded well and promptly to the failed channel C trips. They entered
the remedial action of TS 3.9.A.1 which required that an inoperable trip channel be
restored to operable within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Instrument and Controls (l&C) department was
notified of the problem and personnel from that department began troubleshooting.
At the time, the failed channel trips were declared inoperable for troubleshooting
maintenance and operators entered the exception staternent number 1 for TS 3.9.A
and exited the remedial action. The exception allowed a channel to be inoperative
for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> for troubleshooting maintenance.
Later on, l&C personnel were able to identify a failed 18 volt power supply in
Channel C Symmetric Offset Trip Calculator. The power supply was replaced, the
trips cleared, and I&C surveillance procedures for Power Range Safety Channels,
Thermal Margin / Low Pressurizer Pressure, and Symmetric Offset were successfully
completed. With the RPS restored to normal, operators exited the exception for
TS 3.9.A on the same day.
The inspector observed and reviewed operators and l&C personnel actions during this
event and determined that they were appropriate. The inspector also per.'ormed a
walkdown of the control room panels including the RPS after the event and verified
that the RPS was in operational condition and that plant parameters were normal. No
discrepancy was identified.
c.
Conclusions
Operators performed well and took safe and appropriate actions in response to the
failed RPS channel C trips. l&C personnel responded timely and performed well by
safely and quickly diagnosing the problem and correcting it. Plant personnel showed
good safety focus and ensured that the plant continued to be operated safely while
the troubleshooting and repair efforts were on-going.
04
Operator Knowledge and Performance
04.1 Unolanned Reactor Power increase Durina Delithiation (URI 50-309/96-12-02)
a.
Inspection Scope (71707)
The inspector reviewed the circumstances leading to an unplanned power increase to
2457 MWth from 2440 MWth during a delithiation of the RCS, using purification
demineralizer,1-28.
.
.
7
b.
Observations and findinas
During a control room observation on September 23,1996, the inspector observed
operators taking actions to maintain the plant in a steady condition. Earlier, they had
been conducting a delithiation of the RCS when a power excursion had occurred.
The delithiation process involves taking the inservice demineralizer ott of service
while placing another fresh demineralizer in service. The demineralizer placed in
service could be previously borated to RCS boron concentration or not. A
predetermined quantity of RCS would then be flushed through the fresh demineralizer
to the primary drain tank (PDT) while a pre-calculated blended makeup to the volume
control tank (VCT) would be provided for making up the inventory in the RCS.
Operators had determined that the delithiation would be 8,000 gallons on this day.
Procedure 1-11-3, CVCS Filter and Demineralizer Operation, contains the instructions
for accomplishing the evolution. On this day, operators had removed 1-2C from
service and placed I-2B in service. Since 1-2B was considered ti
a unborated,
operators were performing section 5.2 (placing an unborated det. .seralizer in service)
of procedure 1-11-3. A power decrease was observed and attempts to restore
power to 2440 MWth resulted in a power increase to greater than 2450 MWth. The
approximate sequence of events was as follows:
initiation of delithiation by placing 1-2B in service and isolating 1-2C.1-2B was
e
being flushed with RCS to the PDT. Blended makeup was being added to the
VCT.
!
Power decrease (to about 2415 MWth) observed.
l
Operators attempted to restore power by adding primary water to the VCT.
Power increase observed and operator attempted to compensate by borating
and later by inserting rods (a total of 8 steps). But a peak power level of
about 2457 MWth was reached before power decrease was attained.
A power oscillation to another low of about 2423 and a high of about 2445
MWth occurred before the steady state 2440 MWth could be attained.
Delithiation was completed successfully.
The inspector observed most of the activities during this event from the control
room. Operators performed wellin trying to recover from the power oscillation. Shift
supervision maintained excellent command and control of activities. The plant shift
superintendent (PSS) and the shift operating supervisor (SOS) discussed and
analyzed the information being provided by the operator calmly and methodically
before the SOS provided directions to the operator. The crew performed very well
during the event.
The inspector's review of recent RCS delithiations showed that such a magnituda of
power increase was unusual and not expected. It appeared to be due to weak
performance by the operators. The inspector independently calculated the ratio of
..
.- . _-
-_
- -
-
- - - . - . _ - . - -
- - -
_ - .
.
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.
i
8
!
primary water to boric acid that, based on RCS boron concentration, would have
'
been required for blended makeup per procedure 1-11-3. The calculated ratio
corresponded to that which operators had determined earlier, and so would have
been using the correct blended makeup to the VCT. The licensee is conducting a
!
>
i
root cause of the event.
The inspector reviewed procedure 1-11-3, that was being used for the delithiation,
and portions of Procedure 1-4, Operations at Power, Section 6.3.2 of Procedure 1-4
requires that a power reduction to less than 2440 MWt shall be initiated if the
,
instantaneous power exceeds 2450 MWt. Operators complied with this requirement.
The hourly average power over a period of four hours covering the event were less
than or equal to 2440 MWt.
,
c.
Conclusions
While operators performed well to restore the reactor to a steady power level of
>'
2440 MWt, it appeared that performance weaknesses contributed to the power
excursion occurring in the first case. The licensee's root cause analysis was still
'
on-going and the appropriateness of implemented corrective actions still needs to be
verified. Therefore, this item remains open pending completion of licensee's root
cause analysis and the NRC's review of the results and the appropriateness of
instituted corrective actions (URI 50-309/96-12-02).
,
08
Miscellaneous Operations issues
08.1 Plant Operations Review Committee
a.
Inspection Scope (71707)
On September 20,1996, the inspector attended a Plant Operations Review
Committee (PORC) meeting,
b.
Observations, Findinas and Conclusions
I
The meeting was conducted in accordance with the requirements of TS 5.5.A, Plant
Operations Review Committee. The proper quorum was present. The issues were
well discussed with good safety focus evident, and personnel were available to
provide detaile on the issues and to answer questions raised by the PORC members.
l
Some of the issues discussed were: Design Basis Screen (DBS) No.96-060,
j
Containment Spray Pump NPSH; Event Review Board Report (ERB-013), HPSI Pump
P-14A Auto Start Severed Wire and Design Basis Screen No.96-059, DG-1 A(B)
Integral and Day Tank Capacity. A member of the Event Review Board for the HPSI
l
Pump Severed Wire presented the board's findings at the PORC meeting. The
I
presentation was clear, logical and concise. The inadequacies identified by the board
l
were discussed such that if any immediate corrective actions were needed, they
,
could be implemented.
1
.
.
9
The inspector concluded that the PORC meeting was conducted well and safety
focused. PORC continued to demonstrate good technical and safety perspective in
'
addressing plant issues.
11. Maintenance
M1
Conduct of Maintenance
M 1.1 General Activities
a.
Insoection Scope (62707)
The inspector observed maintenance troubleshooting and repair activities for the RPS
trip breakers channel failure, containment radiation monitors and LS-M-11 valve
repair and selected portions of the following activities.
WO 96-02769-00, Perform PM-26-M-E, Startup Check an J
Lube Oil Sample
WO-96-02761-00, Perform PM-26-SA-B, Check Oil in
Starting Air Lines and Check Lubrication Performance
WO 96-02760-00, Perform PM M-26-O-B, Drain Condensate
From Oil Cleaner and Fill Tank
WO 96-0344-00, Perform EM-26-2A-E DG-2 Panel Meter Testing
WO 96-03605-00, Troubleshooting of RPS System Matrix
Trip Circuit
b.
Observations, Findinas, Conclusions
The performance of these activities was observed to be very professional with
excellent diagnostic skills in evidence. Repairs were timely with excellent interaction
and cooperation between operations, radiation protection, and engineering
departments. The maintenance activities were conducted with good supervisory and
quality controls involvement. Workers followed procedures, had the workorders at
the work site and displayed excellent knowledge of the activities they were
conducting. Specifics of the observed work activities are described below:
M1.2 Troub!echootina of Reactor Protection System Matrix Trio Circuit
a.
Inspection # 70e (62707)
The inssee' r observed portions of the troubleshooting activities to identify the cause
of the
uvertent reactor trip that occurred during routine monthly surveillance
testing of the reactor protection system trip breakers,
b.
Observations and Findinas
The l&C technicians were very thorough and systematically tested all circuit
components to identify the source of the problem. However, they did not identify
l
.
l
.
10
any failed components during this activity. After discussions were held with
maintenance management, it was decided to replace all components of the test
l
circuit that was undergoing testing at the time of the plant trip. After replacement of
l
the components, l&C personnel performed surveillance test 3-6.2.2.11, " Logic
Relays Trip Test". The results were satisfactory with no problems identified.
l
c.
Conclusions
'
The inspector noted that I&C personnel conducted the troubleshooting activities in a
safe and controlled manner and properly tested all components in an attempt to
identify the cause of the failure. The decision to replace all the circuit components
showed a good safety perspective. Station maintenance management provided good
guidance to ensure that all possible avenues of repair were exercised prior to
completion of the repairs.
M1.3 Troubleshootina and Repair of Containment Radiation Monitor
a.
Insoection Scoce (62707)
The inspector reviewed the activities to troubleshoot and repair radiation monitor
]
RI-6113A, Containment High Range Radiation Monitor. (Se also section M2.2).
b.
Observations and Findinas
i
On September 26,1996, operators determined that the containment high range
radiation monitor, RI-6113A, was operating erratically. After comparing the observed
readings to those of the redundant channel (RI-6113B), which was operating
,
normally, the instrument was declared inoperable. A workorder was written for I&C
technicians to investigate and repair the radiation monitor. The l&C technicians
inspected and tested several components in the instrument and performed a
calibration check which was satisfactory. The instrument was returned to service for
trending only. On October 25,1996, the radiation monitor was returned to full
service after no further spiking was observed. In addition, a spare instrument channel
was ordered as a backup to reduce the unavailability time if a problem develops with
the instrument in the future.
c.
Conclusions
The inspector concluded that Maine Yankee promptly accessed the operability of the
radiation monitor and conservatively declared the channel inoperable. The l&C
technicians pro;;erly performed troubleshooting activities in accordance with the
station work control program. Although no particular problem was identified, the
decision to operate the radiation monitor for trending purposes only was appropriate
and after several weeks of operation with no further spiking, the equipment was
demonstrated to be stable. Also the decision to purchase a spare instrument to
reduce radiation monitor down time appeared to be sound.
i
.
l
.
11
M2
Maintenance and Material Condition of Facilities and Equipment
M2.1 Broken Handwheel on Valve LSI-M-11
a.
Inspection Scope (62707)
The inspector inspectud valve LSI-M-11, in the containment spray building while in
the as-found damaged condition, observed the handwheel removal, reviewed the
work package, and plant engineering department Technical Evaluation (TE). The
inspection was to determine if the maintenance department personnel properly
adhered to plant procedures and to verify the quality of the plant engineering
department assessment to resolve the problem.
b.
Observation and Findinas
On September 26,1996, a Maine Yankee Plant Shift Superintendent (PSS), during a
plant inspection tour of the containment spray building, observed that the handwheel
spokes for a motor operated valve LSI-M-11 were broken. This valve is a normally
open containment isolation valve and is in the low pressure safety injection line to
reactor coolant loop one. The PSS and the Shift Technical Advisor (STA) assessed
the problem and determined that the valve was operable because there was no
apparent damage to the valve itself, but only the handwheel. The valve was also
verified to be open which is the required safety function position. Maintenance
personnel were called in to verify the material condition of the valve (internal and
external). After completion of the evaluation, a decision was made to partially stroke
the valve. A partial stroke test manually (from the control room) was performed and
no malfunctions were observed and the valve was then re-opened.
Plant engineering department personnel generated a technical evaluation (TE) to
address the status (operability) of the valve. The inspector reviewed the TE and
determined that it included the proper design reviews, including a 10 CFR 50.59
screening which concluded that no full safety evaluation was needed. The failure of
the valve handwheel was evaluated to determine if there was risk to other
components on or nearby the valve. It was determined that only minor damage
could occur due to valve operation with a broken handwheel and that there were no
seismic concerns. The TE also included a determination that the handwheels on
valves LSI-M-11,21 and 31 were constructed of the same material and susceptible
to the same failure mechanism and should be removed. The failed welds were sent
to an outside testing facility to determine the failurc mechanism and at the close of
the inspection period the data was not available for review and the problems is being
tracked by a licensee Unusual Occurrence Report (UOR No. 96-87).
c.
Coriciusic ns
The inspector determined that the PSS displayed an excellent questioning attitude by
identifying the valve handwheel problem. The location of the valve handwheel was
not conducive to easy problem identification. The work package to perform the work
was properly performed by the maintenance mechanics and radiation protection
-.- .-
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_ - . - - . - - . . - - - . - .--- ... . - .
.
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12
1
personnel provided proper support to the field activities. The TE that was written to
l
provide engineering analysis and guidance was well written and comprehensive with
!
j
excellent supporting data.
J
f
M2.2 Operability of Containment High Radiation Monitor
!
a.
Inspection Scope (62707)
l
The operability of the containment high radiation monitor was questioned due to
^
erratic operation. The inspector reviewed Maine Yankee's troubleshooting and repair
l
activities to resolve the problem.-
j
b.
Observations and findinas
4
On September 26,1996, Maine Yankee operations personnel responded to main
I
control board panalarm RH-2-8 (Containment Radiation High). The operators noted
'
that control room indicator, RI-6113A, was reading approximately 10 r/hr but the
instrument needle was fluctuating and dropped to below zero r/hr as well. The
redundant channel (RI-6113B) was steady and reading normal (less than 2 r/hr).
After checking other containment instrumentation which were reading normal, the
operators concluded that Rl-6113A was inoperable and logged into the remedial
action of station technical specification 3.9C. This remedial action required that the
instrument be returned to service within seven days or a letter written to the NRC
j
delineating Maine Yankee's plans to effect repairs and return the instrument to
i
service.
)
A station workorder (WO 96-3456) was written to troubleshoot and repair the
)
instrument. However, the troubleshooting did not identify any failed component in
j
the instrument. Operations department management made a decision to operate the
1
instrument for trending purposes only to determine its reliability. This was performed
until October 25,1996, at which time the instrument was declared operable after no
I
further instances of spiking occurred. As a backup, another spare instrument was
i
ordered from the vendor to minimize the equipment downtime in the event of another
j
equipment problem.
I
Maine Yankee sent the technical specification required letter to the NRC within the
,
required time period. The letter, dated October 3,1996, discussed the plans for
'
resolving the problem. The letter stated in part, that the monitor was removed from
!-
'
service, inspected, cleaned and place back in service for trending purposes only.
j
Plant operations and I&C personnel continued to monitor the instrument closely for
signs of erratic operation to ensure the equipment is reliable for operation.
'
c.
Conclusion
Maine Yankee l&C technicians properly performed the troubleshooting as required by
<
j
the station work controls program. Maine Yankee personnel properly tested and
restored the instrument to service after the period of observations. The procurement
of another instrument as a spare was appropriate to prevent excessive periods of
'
downtime.
-
4
a
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_ , .
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.
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-,
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.
.
13
M2.3 Inocerable Pressurizer Proportional Heater Trains
a.
Inspection Scope (71707)
The inspector reviewed the circumstances that caused both trains of the Pressunzer
i
Proportional Heaters to be inoperable on October 18,1996. The inspection also
'
included a review of operator actions during the event.
b.
Observations and Findinas
On October 18,1996, with the reactor at 90% power, operators observed a
decreasing trend in reactor coolant system (RCS) pressure. A drop from 2230 to
2220 psig was noted. At that time, pressurizer proportional heaters E-2P-A and
E-2P-B were ir service as well as back-up heaters E-2-A and E-2-F.
There are 120 pressurizer heaters divided into eight groups with a total heating
,
capacity of 1500 Kw. Six of the eight groups (E-2A, E-2B, E-2C, E-2D, E-2E, and
E-2F) are backup heaters with fixed outputs, while the other two groups E-2P-A and
E-2P-B are proportional heaters whose output varies with the demand of the pressure
control program. Technical Specification Section 3.3.C.1 requires that at least one
j
bank of proportional heaters be operable during normal system operation whenever
i
the reactor coolant system Tavg is greater than 500 F.
During the event, once operators noted the pressure drop, they placed standby
backup heater, E-2-C, in service and the pressurizer pressure recovered to 2228 psig
i
and later to 2232 psig.
Electrical maintenance personnel conducted an investigation of the heaters electrical
j
circuit and discovered that there were blown fuses in phase A and phase C of
proportional heater E-2P-A. Operators then declared E-2P-A inoperable. Further
investigation by the electrical maintenance personnel revealed that both fuses on the
A phase of proportional heater E-2P-B were also blown. Operators then declared
E-2P-B inoperable. With both banks of proportional heaters inoperable, the Technical
'
Specification (TS) Limiting Condition for Operation (LCO) of section 3.3.C.1 was not
met and operators entered TS 3.0.A at 12:16 pm. Specification number 2 of
TS 3.0.A required a reactor shutdown within one hour. Meanwhile, maintenance
personnel were able to replace the blown fuse in E-2P-B. After a successful testing
of the heater, E-2P-B was declared operable and a reactor shutdown was averted.
Later, E-2P-A was also repaired, tested and declared operable.
Testing of the proportional heaters is normally accomplished per Attachment E,
Testing Pressurizer Proportional Heaters, of Procedure 1-1, Plant Heatup. The test
verifies power output from each bank of proportional heaters to ensure their
functionality. Electrical Maintenance also conducts a semi-annual Preventive
Maintenance (PM) for these heaters and had just completed one within the past
month and a half. The PM, E-11-SA-G(H), Check Heater Amperage, checks the
output of the proportional heaters under full load condition to verify functionality.
. . ~. .
.
. __
-.
- -
. - . . _ -
-
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. . _ ._
.-
. . - -
-
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I
14
i
in addition, under the Supplemental Engineering Reliability Program, plant Engineering
Department personnel conduct a quarterly infrared surveillance of the heater circuitry.
j
Those tests failed to detect the fuse problem.
l
j
The inspector reviewed all applicable documents and noted that the licensee had
observed instances of blown fuses in the past in the proportional heater circuits.
However, no significant actions had been taken to thoroughly understand and correct
the problem. The licensee indicated that reviews were ongoing to develop a design
enhancement for the system. Meanwhile, the licensee stated that the electrical PM
'
would now be conducted at monthly intervals, and that the PED infrared checks
would be done on a weekly basis.
.
l
However, based on problems experienced in the past, the frequency of monitoring
j
the heaters was increased in response to this problem. In addition, extensive actions
to identify the root cause of the failed fuses to eliminate the problem was not
pursued.
c.
Conclusion
.
!
l
Operators responded well to the failure of both banks of proportional heaters.
Electrical maintenance personnel demonstrated excellent support to operations by
,'
timely identifying and resolving the problem, thereby preventing an unnecessary
transient to the plant. The licensee recognized a weakness in the process and what
appeared to be appropriate actions were planned and are being taken to control the
j
problem (UOR No. 96-99).
'
M2.4 Control Element Assembly Problems Durina Reactor Startuo
i
a.
Inspection Scope (62707)
The inspector observed plant restart activities in the control room and reviewed the
i
licensee's efforts to correct the problems encountered while withdrawing certain
control element assemblies (CEA) during reactor startup.
t
4
b.
Observations and Findings
I
During the reactor startup on October 10 - 11,1996, the inspector noticed some
discrepancies with the operation of the CEAs. There were instances of dropped
,
rods (similar to these experienced during the September 1,1996, reactor startup)
i
and instances of the reed switch CEA position indication not keeping up with the
pulses for CEA movement.
3
i
The significant problems were as follows:
I
I
Partial drop of Rod 4 (in Group 4)
Partial drop of Rod 4 (in Group 4)
3
Rod 2 reed switch indication not keeping up with the pulses
j
Partial drop of Rod 3 (in Group 4)
i
.-
.
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..
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. - - _ - . - .
.
. . .
.- .
_
-
-
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.
15
Following each rod drop, the affected group (Group 4) was re-inserted and realigned
in accordance with Abnormal Operating Procedure (AOP) 2-21, Misaligned (Dropped)
CEA, however, the situation presented a challenge'to the operators during their
attempt to restart the reactor. The restart was aborted and all previously withdrawn
regulating rods (groups 1,2, and 3) were re-inserted, so that extensive trouble
shooting efforts could be conducted to resolve the problems.
The inspector observed some of the troubleshooting activities and noted that they
were conducted properly. At the end of these activities, a modification to procedure
l
3-6.2.1.19, Rod Drop Time and Functional Check, was required so that it could be
-
used for exercising the group 4 rods, one at a time for functional testing purposes.
The modification was made under the temporary procedure change process
(TPC # 96-331). The inspector reviewed the approved copy of the change and
verified that it had been properly processed, and did not create a situation for
operating the reactor outside previously analyzed conditions. Operators had
l
conservatively assigned the previously calculated and approved boron concentration
l
required to maintain the reactor subcritical with group 4 withdrawn as that to be
!
maintained with a single CEA withdrawn. The inspector reviewed the calculations
l
with the shift technical advisor and verified that they were accurate and in
accordance with the numbers and charts provided in the Technical Data Book (TDB).
i
The repair activities included the following:
!
for Rod #2, replacement of the timer module, the upper gripper power switch
and the pull down power switch.
for Rod #3, replacement of the upper gripper power switch and the pull down
coil.
for Rod #4, replacement of the timer module, the upper gripper power switch,
and the pull down switch.
The CEAs functioned well following the repair and the reactor was successfully
restarted.
c.
Conclusions
Operators performed wellin response to the CEA problems. They followed the
appropriate procedures and maintained the plant in a safe condition. During and
following troubleshooting activities, plant personnel showed good safety perspective
and ensured that the plant was always maintained safely. However, the problems
with the CEAs were similar to those that occurred during reactor startup the previous
l
month and it appeared that the right solution of the previously identified problems
l
had not been made. These equipment malfunctions posed an unnecessary challenge
to the control room operators during their startup of the plant.
l
,
.
.
16
til. Enaineerina
E2
Engineering Support of Facilities and Equipment
E2.1 Desian Issues Affectina Cold Weather Operations in the Turbine Buildina (uodate
URI 50-309/96-08-02 and 50-309/96-08-04)
a.
Inspection scope (37551)
The inspectors reviewed and discussed the status of Maine Yankee's engineering
efforts to address the design issues affecting cold weather operations.
I
On October 21,1996, the inspector met with representatives frorn the corporate
engineering department (CED) to discuss the status of ongoing licensee activities to
address the concerns with the High Energy Line Break (HELB) and Flooding
Conditions in the turbine building. Specifically, the review was to understand and
assess Maine Yankee's turbine building modifications to ensure that safety related
components would continue to function during a design bases HELB or flood in the
turbine building. The review was also to determine if the modifications are suitable
j
for cold weather operation.
j
b.
Observations and Findinas
A HELB Condition could occur in the turbine building if a postulated rupture of high
energy lines in the building occurred. Originally, the limiting or worst case scenario
was postulated to be a break of a 30 inch main stream wire. However, recent
reviews have determined that a postulated slot break of the main feed wire could
present the worst case scenario because a higher energy at a lower pressure could
<
be released without the Turbine Building panels blowing open.
A flooding in the Turbine Building could occur if a postulated failure of non-safety
related water pipes in the Building occurred. Previous analyses performed to mitigate
the effect of the postulated flood had considered a guillotine break of the circulating
water system pipe as the worst case scenario. This break would result in a spill of
about 110,000 gpm. However, the flood protection saving panels installed were not
capable of mitigating a flood of 3,500 gpm resulting from a crack in the circulating
water would not provide enough static head to open the swing panels.
In NRC Inspection Reports 50-309/96-03 (Section 3.0) and 50-309/96-08
(Section E2.2 and E2.4, respectively), the issues involving flooding and HELB
concerns in the turbine building were discussed. As compensatory measures, Maine
Yankee had secured the roll-up doors open at least 5 inches to ensure flood relief
would be available. As for the HELB concern, the licensee had left some banks of
roof louvers open, removed some of the plywood covering from the walllouvers and
secured the building unit heaters which were to be used only as needed. These
compensatory measures were suitable for temporarily addressing the concerns and at
.
.
17
that time, they did not create any habitability or environmental concerns in the
turbine building. However, with the onset of cold weather conditions, the potential
habitability or environmental concerns needed to be resolved.
In a letter to the NRC, dated August 14,1996, Maine Yankee committed to
j
conducting an analysis of the postulated HELB condition with a " winter condition"
ventilation lineup. The analysis was to be submitted to the NRC by October 1,1996,
along with a description of any plant modifications which appear to be warranted. In
another letter to the NRC dated October 1,1996, Maine Yankee indicated the need
for an extension of the submittal date of the analysis.
j
The inspectors reviewed the licensee's close out plans which included the actions to
be taken to address each of tha issues. Engineering analysis were still ongoing to
determine the turbine building environment based on the worst case scenario for a
HELB in the turbine building. The licensee was considering a feedwater line slot
break as the worst case. A design discrepancy evaluation (DDE No. 96-63) was
generated to address this issue.
i
To address the flooding concerns, a design change was being generated to raise the
berm at the entrance to the corstrol room from 4 to 6 inches (present flooding in the
control room) and to install a gravity flap in the north wall of the turbine building
allowing water build-up to leave the turbine building. The inspectors will review the
i
details of each issue resolution when they become available. At this time, the
inspectors identified no safety concerns, with the licensee's activities and will
continuo to follow-up on these issues.
c.
Conclusions
Maine Yanken was making good efforts to address the turbine building design issues
affecting cot Neather operations. The activities of the corporate engineering and
licensing depa anent personnel appeared technically sound and detailed. There was
good management attention and involvement in addressing these issues.
IV Plant Suocort
R1
Radiological Protection and Chemistry (RP&C) Controls
R1.1 Multiple Contamination Events and Unolanned Exoosures
a.
Insoection Scope (71750)
The inspector reviewed the licensee's corrective actions concerning several
unplanned exposures during this and the previous inspection periods.
b.
Observations and Findinas
The first unplanned exposure was to an operations department radiation waste
handling operator. This event occurred during a routine filter changout of the
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Duratek System. The Duratek System is used by Maine Yankee to remove
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radioactive waste from waste liquid prior to disposal. The second unplanned
!
exposure occurred to a contractor during repair activities on the auxiliary steam
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system in the primary auxiliary building. The loss of contamination control occurred
when a radioactively contaminated sheet of metal was taken outside the restricted
area, and returned to the station warehouse.
4
On April 16,1996, the pre and post filters of the Duratek liquid waste ion exchange
demineralizer processing unit were changed out. A Maine Yankee operator and a
radiation protection technician were assigned to the task and no abnormal conditions
,
were identified during the change out process.
!
On July 11,1996, Maine Yankee radiation controls supervisory personnel reported
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that during a review of the second quarter TLD data it was identified that the station
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radiation waste handling operator had received an unplanned skin dose of 6.94 rem.
This is approximately 14% of the extremity annual limit. On July 12,1996, station
I
management suspended the operator's access to the restricted area pending a dose
evaluation and investigation of the event.
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On July 16,1996, the preliminary results of the investigation were presented to
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station management and corrective actions were implemented to allow filter
changout to recommence on July 19,1996. The corrective actions included
i
mandatory issuance of extremity dosimetry for filter changeouts, increased frequency
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of extremity dosimeter processing and increased personnel and area survey
requirements in potentially discrete (HOT) particle and highly contaminated areas.
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The inspector reviewed the completed corrective actions, held discussions with
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radiation protection technicians and supervisors and discussed the event with the
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radiation control manager. The corrective actions were very comprehensive in scope
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with excellent use of independent analysis to determine the source of the exposure.
The investigation was unable to pinpoint the exact cause of the exposure, but the
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most plausible scenario appeared to be that a discrete (Hot) particle was deposited
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on the workers rubber glove during the filter changeout process and caused the
)
exposure. The inspector did note that one of the conclusions in the radiological
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incident report (RIR) was that "since the operator is not expected to recognize that a
failed gasket seal might change radiological conditions, he would have no reason to
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alert the technician to this fact." This statement does not appear to coincide with
stated Maine Yankee policy that operators and all radiation workers are expected to
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use a questioning attitude during all plant evolutions. With the bag filter being used
for the first time, extreme caution should have been required for the evolution. Also
with the seal being identified as being disturbed there appears to have been good
'
reason to alert the technician to the potential of an abnormal condition in the filter
,
housing. This problem was discussed at a management meeting in Region I on
August 9,1996 as documented in NRC Inspection Report No. 50-309/96-09.
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in another situation on October 1,1996, a Maine Yankee maintenance mechanic
brushed against a lead shield blanket and received an unplanned exposure of
,
approximately 88 mrem from a discrete (hot) particle which lodged on the seat of
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the worker's coveralls. The particle swipe sample was analyzed by the radiation
protection department and determined to primarily consist of magnesium 54 and
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cobalt 60.
And yet in another situation on August 22,1996, Maine Yankee Radiation Protection
personnel reported to the NRC that several steel plates had been identified with
internal contamination. Upon further review the licensee determined that the
contamination was in fact external and milling activities would remove the
contamination. The steel plate was determined to have been used during the last
refueling outage, on the reactor coolant system decontamination project and
subsequently returned to the warehouse. On October 7,1996, Maine Yankee
notified the NRC to provide an update to the previous notification.
Maine Yankee is currently reviewing the station program that surveys material prior
to release from the station restricted area. The inspector will review the licensee's
finding in a subsequent inspection.
c.
Conclusions
The inspector determined that Maine Yankee radiation protection department properly
responded to the unplanned exposure events. The analysis of the data was thorough
with proper review by independent expertise. Most of the conclusions were
appropriate. However, the inspector noted that one of the conclusions for the
Duratek event did not properly take into consideration the experience and training of
the two individuals that were involved in the event. The inspector determined that
while no personnel exposures exceeded regulatory limits, the contamination exposure
controls were weak.
R1.2 Imolementation of Radioactive Liauid and Gaseous Effluent Control Proaram
a.
Inspection Scope (84750)
Inspection of this area consisted of:
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physical walkdown of facilities and equipment, including air cleaning
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systems;
review of selected licensee's procedures, and
review of selected radioactive liquid and gaseous discharge permits with
respect to TS ODCM requirements.
b.
Observations and Findinas
The inspector toured all effluent RMSs, several process RMSs, and the air cleaning
systems and noted the below findings:
All RMSs were operable at the time of this inspection.
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The background readings of effluent RMSs were reasonably low to allow
monitoring of any unusual releases
The differential pressure between the high efficiency particulate air (HEPA)
charcoal filters were within the licensee's acceptance criteria
The effluent control procedures were detailed, easy to follow, and ODCM
requirements were incorporated into the appropriate procedures.
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The discharge permits were complete and met the TS/ODCM requirements for
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sampling and analysis at the frequencies and lower limits of detection
established in the TS.
c.
Conclusion
)
The licensee established, implemented, and maintained effective radioactive liquid
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and gaseous effluent control programs.
R2
Status of RP&C Facilities and Equipment
R2.1 Effluent / Process Radiation Monitorina Systems
a.
Insoection Scoce (84750)
The inspectors reviewed the most recent calibrated results, upgrades, and
workorders for the following effluent and process RMSs to determine the
implementation of the TS/ODCM requirements and the Updated Final Safety Analysis
Review (UFSAR) commitment for:
Liquid Radwaste Effluent Monitor
Service Water Effluent Line Monitor
Condenser Air Ejector Monitor
Steam Generator Blowdown Line Monitor
Plant Vent Stack Noble Gas Monitors (Normal and High Range)
Waste Gas Holdup System Monitor
Containment Noble Gas Monitor, and
Main Steam Line Monitors
b.
Observations and Findinas
The Instrumentation and Controls (l&C) Department had the responsibility of
performing electronic and radiological calibrations for the above effluent process
RMSs. The I&C system engineer had the responsibility to maintain the operability for
the above RMSs and upgrade the system, as necessary. All calibration results
reviewed were within the licensee's acceptance criteria.
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During the review of the above RMSs radiological calibration data, the inspector
independently verified several calibrated results, including linearity tests and
conversion factors. The comparison results between the licensee's values and
inspectors' calculation values were in agreement.
The licensee issued an RMS Manual, " Radiation Monitoring System (Design Basis
Summary Document)", in June,1996. The purpose of this manual was to document
the design basis of the effluent process RMSs installed at the site. The manual also
provided a means to verify and validate system reliability and functionality. The
inspectors reviewed this manual and noted that it contained the following useful
information for users (e.g., control room operators, chemistry staff, and l&C staff):
Functional Requirements and Capabilities
External Events Considered in the Design Basis for the System
Historical Narrative of Modifications and Analysis
Synopsis of System and Component Testing
Piping System Analysis of Record
Setpoint Sumw y and
Component Summary of Design Conditions
Several important RMS upgrades were completed since the last inspection of the
REMP. These upgrades included: addition of a polished sleeve for the liquid radwaste
effluent monitor, which helped to minimize radionuclide plateout; refurbishment of
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the three air particulate detector (APD) paper drives; and replacement of several self-
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rolling ribbon cables.
The inspectors' review of open and closed licensee workorders pertaining to the
RMSs indicated no recurring equipment problems other than recurring problems with
the self-rolling ribbon cables (which, as a consequence, were recently replaced as
need).
c.
Conclusion
Notwithstanding the RMSs calibration discrepancy noted in Section R7.1 of this
report, the RMSs were well maintained. Licensee completion of several RMS
upgrades and the RMS manual demonstrated the licensee's commitment to a strong
REMP.
R2.2 Air Cleanina Systems
a.
Insoection Scope (84750)
The inspector reviewed the licensee's most recent surveillance test results to
determine the implementation nf TS requirements and UFSAR commitments, and
walked down the following ventilation systems:
Spent Fuel Pool
Containment Ventilation / Purge
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Control Room (CR) Recirculation and CR Breathing Air, and
Primary Auxiliary Building
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The inspectors reviewed the following surveillance test results:
Visual Inspection
In-Place HEPA Leak Tests
In-Place Charcoal Leak Tests
Air Capacity Tests
Pressure Drop Tests, and
Laboratory Tests for the lodine Collection Efficiencies
b.
Observations and Findinas
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All test results of the above systems were within the licensee's acceptance criteria
with the exception of: 1) the laboratory test methodology for the iodine collection
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efficiency for the containment ventilation / purge system, and 2) tLe failure of the in-
place leak test for control room recirculation system.
Section 4.11.D,2.b of the TS, Containment Ventilation / Purge System, requires that
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radioactive elemental iodins be used as a challenging agent to determine the iodine
collection efficiency. In past surveillance, methyl iodide was used as the challenging
agent, rather than elemental radioiodine. All other air-cleaning systems require the
methyl iodide be used as a challenging agent to determine the iodine collection
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efficiencies. Although the use of elemental radiciodine as a challenging agent to
determine iodine collection efficiency is available (described is ASTM D-3803-79),
use of methyl iodide is the general industrial practice because it is readily available,
cost effective, and is considered to provide better test results. Isee Regulatory
Guides 1.58 (for post accident condition) and 1.140 (for normal ventilation), and
ANSI N510-1975 for details.] During an October 22,1996, telephone call with
licensee representatives, the inspectors were informed that the licensee had decided
to change TX 4.11.d,2.b to denote methyl iodide as the challenge agent. The
licensee committed that this TS change would be approved by PORC and Nuclear
Safety Audit and Review Committee (NSARC) and submitted to the NRC by
March 1997. The inspectors assessed the safety significance of this matter to be
negligible because elementaliodine can be used as a charcoal challenge agent. This
failure constitutes a violation of minor significance and is being treated as a Non-
Cited Violation, consistent with Section IV of the NRC Enforcement Poliev.
The in-place halogenated hydrocarbon leak test for the control room recirculation
,
system failed on October 31,1995. After replacing the charcoal filter gaskets ad
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repairing the filter frarne, the licensee retested on December 5,1995, and the result
was within the TS acceptance criteria.
c.
Conclusion
The licensee adequately implemented TS requirements except for one minor violation.
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R2.3 Ventilation Systems Air Balance (IFl 50-309/96-12-03)
a.
Inspection Scope (84750)
Section 9.13 of the final safety analysis report (FSAR) describes the general
ventilation systems and each building ventilation system throughout the plant. Air
balance for the Primary Auxiliary Building, Fuel Building, Containment Spray Pump
Area, and Service Building were reviewed.
b.
Observation and Findinas
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The inspectors discussed with the heating, ventilation, and air conditioning (HVAC)
'
engineer, the maintenance and testing of the ventilation systems committed in
Chapter 9.13 of the FSAR. Section 9.13.2.5 of the FSAR, Turbine Building, details
'
turbine building ventilation system supply and exhaust air flow rates.
Section 9.13.2.7 of the FSAR, Office Building, details office building ventilation
system supply and exhaust air flow rates. No surveillance requirements are detailed
in Sections 9.13.2.5 or 9.13.2.7 of the UFSAR. The inspectors noted that there
were no routine surveillance tests documented for the Turbine and the Office
Buildings. Such tests are not specifically required by the technical specifications.
The independent safety assessment team identified a number of examples of weak
and inadequate testing indicating a broad and programmatic concern and this area is
pending further review (See also, NRC Inspection Report No. 50-309/96-09,
Section E2.1).
The inspector noted that the Service Building was divided into two areas, a
contaminated area and a clean area. The licensee maintained a positive pressure for
the clean area and a negative pressure for the contaminated area. Section 9.13.2.4
of the FSAR, Service Building, denotes that HV-8 removed 6,200 cfm from the
Service Building contaminated area in order to maintain a negative pressure. The
inspectors determined that this fan should have been denoted as FN-8 (an exhaust
fan) in the UFSAR. The fan HV-8 (5,000 cfm) was an air supply fan. The licensee
acknowledged the error and stated that the UFSAR would be revised accordingly.
c.
Conclusion
Overall, maintenance and surveillance of the ventilation systems was adequate. The
licensee had not documented the plant air balance surveillance results to demonstrate
consistency with Chapter 9.13 of the FSAR assumptions. Section 9.13.2.4 of the
FSAR had not been updated. These items will be reviewed during a subsequent
inspection (IFl 50-309/96-12-03).
R3
RP&C Procedures and Documentation
R3.1 Off Site Dose Calculation Manual Review
a.
Inspection Scooe (84750)
The inspection reviewed the ODCM implemented at the Maine Yankee site, including:
1) dose factors,2) setpoint calculation methodology, and 3) bioaccumulation factors
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for aquatic sample media. The inspectors also reviewed the 1995 Annual
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Radioactive Effluent Report.
b.
Observations and Findinas
The ODCM provided descriptions of the sampling and analysis programs, which are
established for quantifying radioactive liquid and gaseous effluent concentrations,
and for calculating projected doses to the public. All necessary parameters, such as
effluent radiation monitor setpoint calculation methodologies, site-specific dilution
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factors, and dose factors, were listed in the ODCM. The licensee adopted other
'
necessary parameters from Regulatory Guide 1.109.
The inspectors reviewed the 1995 annual radioactive effluent release report. This
report provided data indicating total released radioactivity for liquid and gaseous
effluent. This annual report also summarized the assessment of the projected
maximum individual and population doses resulting from routine radioactive airborne
and liquid effluent. Projected doses to the public were well below the TS limits. The
inspectors determined that there were no anomalous measurements, omissions or
adverse trends in the report.
c.
Conclusion
Based on the above review, the inspectors determined that the licensee's ODCM
contained sufficient specification, information, and instruction to implement and
maintain the radioactive liquid and gaseous effluent control programs. The
inspectors also determined that the content of the Annual Report was very good and
met the TS reporting requirements.
R6
RP&C Organization and Administration
R6.1 Radioactive Liauid and Gaseous Effluent Proaram Review
a.
Insoection Scope (84750)
The inspectors reviewed changes to the organization and administration of the
radioactive liquid and gaseous effluent control programs and the REMP.
b.
Observations and Findinas
The inspectors determined that there had been no changes since the last inspection
conducted from May 1-5,1995. The Chemistry staff had primary responsibility for
conducting the radioactive liquid and gaseous effluent control programs. The
departments of Operations, System Engineering, Radwaste Operations and l&C
support the radiological effluent control programs relative to air cleaning systems,
radioactive liquid discharge, and radiation monitoring system calibrations.
The licensee reorganized the REMP in September 1996. The REMP moved from the
Radiation Protection Section (Dosimetry) to the cognizance of the Environment Health
and Safety and Emergency Preparedness (EMS & EP) section. The inspectors
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25
interviewed the EMS & EP section head regarding the implementation of the REMP.
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The inspectors assessed that this change was an improvement in oversight because
many technical aspects of EP and the REMP are similar in nature. The former Maine
Yankee chemistry section head, who had very good knowledge in the areas of
effluent controls and the REMP, was assigned to oversee the environmental specialist
who was assigned the REMP. An individual from another nuclear power plant was
recently assigned as the acting chemistry section head for one year.
c.
Conclusion
Oversight of the REMP was improved. No degradation was noted as a result of the
reorganization.
R7
Quality Assurance in RP&C Activities
R7.1 Quality Assurance Audit Report Reviga
a.
Inspection Scoce (84750)
The inspection consisted of a review of Quality Assurance (QA) Audit Reports
required by the TS and a review of corrective actions implemented to address audit
findings. The inspector reviewed the 1995 QA Audit Report No., MY-95-02,
" Chemistry / Radiological Effluent Technical Specifications (RETS)/Off-Site Dose
Calculation Manual (ODCM)", and the 1996 Audit Report No., MY-96-02, " Chemistry
Audit". These audits were conducted by the Quality Programs Department,
b.
Observation and Findinas
The inspectors noted that individuals with appropriate technical expertise were used
to assist the audit team leader, which was considered to be a strength.
The 1996 audit findings, focused mainly on administrative aspects of the Chemistry
program. No " technical" issues of regulatory significance were identified.
The 1995 audit identified that the primary vent gas monitor RM-3902Y had not been
calibrated at the frequency required by TS 4.1. No calibration records were found for
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the time period 9/92 to 3/95. TS required this instrument to be calibrated once every
18 months. The tracking system for surveillance had been established to key on
individual procedures rather than on an individual RMS. RMS calibration procedures
were established so that a single procedure would provide calibration guidance for
several RMSs of the same manufacturer and model. l&C supervisory review also
failed to initiate a timely calibration of RM-3902Y. Licensee corrective actions
included (1) calibrating RM-3902y and (2) improving the administrative controls for
tracking of RMS calibration / surveillance due dates by tracking by RMS channel
numbers rather than by RMS calibration procedure numbers. The inspectors
considered the corrective actions to be appropriate. The inspectors' assessment of
the safety significance of the failure to calibrate RM-3902Y at the frequency required
by TS 4.1 was minimal due to the fact that (1) daily grab samples were taken (due to
a pre-existing agreement with the State of Maine) and (2) the March,1995,
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26
calibration of RM-3902Y demonstrated no significant change in the calibration factor.
This licensee-identified and corrected violation is being treated as a Non-Cited
Violation, consistent with Section Vll.B.1 of the NRC Enforcement Poliev.
The inspectors noted that the failure to calibrate RM-3902Y was not formally
communicated to be NRC by either submittal of an LER or annotating the Annual
Radioactive Effluent Release Report. The inspectors questioned licensee personnel as
to the basis of the reportability determination that no LER was required for this
matter and found the determination adequate. The inspectors also discussed with
the licensee a means of notifying the NRC of future cases of RMS inoperability such
as by writing as LER or by noting such cases in the Annual Radioactive Effluent
Release Report. Licensee representatives noted to the inspectors that a
February 1996 revision to section 2.3.3 of the ODCM dictated that if an RMS could
not be returned to an operable status within 30 days, an explanation of the delay
was to be provided in the next Annual Radioactive Effluent Release Report. The
inspectors had no further questions regarding how the licensee would notify the NRC
of future cases of an inoperable RMS.
c.
Conclusion
Based on the above reviews, the inspectors determined that the licensee met the QA
audit requirements. Licensee corrective actions to audit findings were considered
appropriate.
R8
Miscellaneous RP&C lssues
R8.1 Review of Updated Final Safety Analysis Reoort (UFSAR) Commitments
i
A recent discovery of a licensee operating their facility in a manner contrary to the
UFSAR description highlighted the need for a special focused review that compares
plant practices, procedures and/or parameters to the UFSAR description.
l
While performing the inspection discussed in this report, the inspectors reviewed the
applicable portions of the FSAR that related to the areas inspected. The following
inconsistency was noted between the wording of the FSAR and the plant practices,
procedures and/or parameters observed by the inspectors.
Section 9.13.2.4 of the FSAR noted that HV-8 was an exhaust fan and was designed
to maintain a negative pressure in portions of the Service Building. The inspectors
determined that this fan should have been denoted as FN-8 (exhaust fan) in the
FSAR. The f an HV-8 was an air supply fan. This FSAR discrepancy was considered
to be minor in nature and is discussed in more detail in Section R2.3 of this report.
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P1
Conduct of Emergency Preparedness (EP) Activities
P1.1 Emeraency Plannina Self Assessment Proaram and Corrective Action Trackina
System
i
a.
Insoection Scope (82701)
The inspector reviewed the licensee's action item tracking system and the
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Emergency Planning self-assessment program to determine the effectiveness
of licensee controls.
b.
Observations and Findinas
The inspector reviewed the corrective action tracking system (CATS) for EP items.
There were 14 open items on CATS. Most of the open items pertained to exercise
and drillissues. One long range item being tracked was the possible addition of
another fiber-optic telephone line into the site from another area. This line is being
contemplated to preclude the loss of long distance capabilities and the NRC systems,
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which occurred in June of 1995 when the AT&T fiber-optics line in Freeport, ME was
i
damaged.
Additionally, the inspector reviewed five self-assessments of different areas of the
emergency preparedness program. These self-assessments were performed on
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emergency preparedness equipment inventories, exercise development review,
training in the use of portal monitors, offsite scenario interface, and monthly
communication drills. The self-assessment of monthly communication drills identified
that the February drill was missed (see Section P2). The inspector noted that the
other self-assessments adequately identified additional areas where improvements
could be made in the emergency preparedness program, and that they were being
actively pursued.
The EP items were being properly tracked. The closure of EP items required the
approval of the Environmental Health and Safety / Emergency Preparedness Section
Head.
c.
Conclusions
Both the CATS and the self assessment program appeared to be an effective licensee
control.
P2
Status of EP Facilities, Equipment, and Resources
P2.1 Emeraency Plannina Eauipment inventories and Surveillance
a.
Insoection Scone (82701)
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The inspector reviewed facility equipment inventories and surveillance conducted
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from January 1996, through September 1996, for completeness and accuracy. The
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inspector also conducted an audit of emergency equipment in the Control Room,
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Operations Support Center (OSC), Technical Support Center (TSC), Emergency
Operations Facility (EOF) to determine if any changes had been made and whether
the facilities were operationally ready.
b.
Observations and Findinas
The inspector noted that the inventories were thorough and that items found
depleted were immediately replaced and equipment found inoperable was replaced
with back up equipment, and it was noted on the inventory the equipment was out
for repair. All dosimetry had been exchanged in the time frame required by the
emergency plan. All survey instruments were calibrated on the same date instead of
on various dates throughout the six month calibration period as had been the
previous practice.
While reviewing the communication drill surveillance, the inspector noted that the
February 1996 notification drill was not conducted. This missed notification drill had
been identified by the licensee during a July self-assessment. The licensee found
that the request to conduct the drill was apparently lost and the follow up to ensure
its conduct had not occurred. The NRC Resident inspectors had been informed of
the missed notification drill on July 3,1996. The inspector determined that all other
surveillance were completed in accordance with the emergency plan with the
exception of the TSC, OSC and EOF ventilation discussed in Section P8.2.
During an inspection tour of the control room, TSC, OSC, and EOF, the inspector
conducted a selected inventory of the equipment lockers. The equipment was found
to be operationally ready and within calibration, as required by the emergency plan.
The inspector also noted that the licensee's potassium iodide supply had an
expiration date of 2000. The inspector tested the emergency notification system
telephone line from the EOF to the NRC Operations Center and found it in working
order.
c.
Conclusions
Facility inventories were complete, radiation survey instrumentation was within the
calibration requirements and the emergency response facilities were found to be in a
state of operational readiness.
P3
EP Procedures and Documentation
P3.1 Review of Emeraency Response Plan Chanaes (Closed. URI 50-309/96-007-01)
a.
Inspection Scope (82701)
The inspector reviewed recent emergency response plan changes to assess the
impact on the effectiveness of the EP program. The inspectors also assessed the
process that the licensee uses to review emergency plan changes.
a
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29
b.
Observations and Findinas
The inspector reviewed emergency plan change 96-01 and 96-02 and the process
used to evaluate the changes to determine if they met the requirements of
10 CFR 50.54(q) and did not decrease the effectiveness of the emergency plan.
Change 96-01 revised Table 6-1 giving the functional responsibility for rescue
operations and first aid to the Security Supervisor instead of the Plant Shift
Supervisor (PSS). Change 96-02 added the 60 minute goal of staffing the
emergency response facilities to Section 6.1 of the emergency plan. This change
addressed the NRC discrepancy that was identified during the licensee's graded
exercise June 1996. URI 50-309/96-007-01 is closed.
c.
Conclusions
Based on the licensee's determination that the changes did not decrease the overall
effectiveness of the emergency plan and after limited review of the changes by the
inspector, in accordance with 10 CFR 50.54(q), no NRC approval is required to
implement the changes. However, implementation of these changes may be subject
i
to further inspection at a later time to confirm that the changes have not decreased
I
the overall effectiveness of your emergency plan.
P5
Staff Training and Qualification in EP
PS.1
-meraency Plannina Trainina Proaram Evaluation
a.
inspection Scone (82701)
The inspector reviewed EP training records, training procedures, lesson plans,
emergency plan, and EPIPs associated with on-shift dose assessment to evaluate the
licensee's EP training program and obtain information for NRC's Temporary
Instruction 2515/134 " LICENSEE ON-SHIFT DOSE ASSESSMENT CAPABILITIES."
b.
Observations and Findinas
The inspector reviewed thirty percent of the emergency response organization
training records. Additionally, the inspector reviewed the dose assessment training
for operations personnel, emergency directors, and radiation protection. The
inspector found that all training was current.
The inspector was given a demonstration of the offsite dose projection system
(ODPS)in the control room by the PSS and the shift technical advisor (STA). The
demonstration included obtaining the meteorological and radiological monitoring data,
entering it, in the correct format, into the ODPS system, obtaining the results, and
printing it out. In addition, emergency response organization (ERO) management, and
the radiation protection staff are trained in the use of ODPS, the Meteorological Post
Accident Computer Model (METPAC) computer dose projection system, and the
backup nomogram.
The ERO is staffed three deep in all major positions.
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c.
Conclusion
The training program was being effectively implemented and the ERO is adequately
staffed. The inspector concluded that the licensee maintained on-shift dose
assessment and adequate back-up capabilities to ensure that on-shift dose
assessments could be performed.
P6
EP Organization and Administration
P6.1 Emeraency Plannina Staffino and Manaaement Chanaes
a.
Insoection Scope (82701)
l
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The inspector reviewed the licensee's EP group staffing and its management to
'
determine what changes have occurred since the last program inspection
(July 1995), whether changes if any had an adverse effect on the EP program.
b.
Observations and Findinas
i
Responsibility for EP program is assigned to the Manager, Licensing and
'
Engineering Support. Reporting to this Manager is the Environmental Health
and Safety / Emergency Planning Section Head. There is one onsite and one
!
offsite Emergency Planning Coordinator who report to the Section Head.
Additional resources from the Yankee Atomic Electric Company are available
to assist in the administration and implementation of the program.
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The inspector interviewed the President of Maine Yankee Atomic Company,
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Vice President Operations, the Plant Manager, Environmental Health and
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Safety / Emergency Planning Section Head, Senior Emergency Preparedness
Coordinator, Principal Emergency Preparedness Coordinator, and Emergency
Preparedness Specialist, Yankee Atomic Services Division. All personnel interviewed
were members of the ERO and were very familiar with and supportive of the
emergency preparedness program, its issues and requirements.
c.
Conclusions
There were no changes in the emergency planning staff since the last inspection.
The staff is knowledgeable and appears adequate to administer and implement the
program properly.
P7
Quality Assurance (QA)in EP Activities
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P7.1 Review of Annual Emeraency Plannina Proaram Audit Reoorts
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a.
Inspection Scope (82701J
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The inspector reviewed the QA audit reports of the EP program, conducted in 1995
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and 1996, to determine compliance of NRC requirements and licensee commitments.
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31
b.
Observations and Findinas
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The reports reviewed were MY-95-14 and MY-96-14, as well as the corresponding
audit plans and checklists. Tnere were no adverse findings in either report. Audit
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report 95-14 had four observations, three which indicated areas for improvement in
the facility and equipment inventories and one on training' course descriptions and
lesson plan content. The 96-14 audit report had three observations which consisted
of emergency plan clarifications, minor facility maintenance items and administrative
inconsistencies. The inspector also noted that there were no recurring items in either
of the audit reports.
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The inspector interviewed the QA Supervisor. The QA Supervisor stated that he
uses the " Risk-Based Quality Verification Process," a portion of Procedure 21-205,
Revision 6, Attachment C, to assess appropriate areas of the program. By applying
the associated factors designated in the procedure, he establishes which areas of the
program may need more resources applied during the audits. Additionally, the
inspector noted, and the QA supervisor indicated, that emergency preparedness
expertise from organizations outside of Maine Yankee assisted with both of the
audits.
The audit reports were distributed to the appropriate levels of management. The
results of all audits on emergency plan offsite group interface were made available to
]
the outside agencies. Timely and appropriate corrective actions were taken on the
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observations.
c.
Conclusion
The licensee conducted audits that were thorough and met the requirements of
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P8
Miscellaneous EP issues
P8.1 Updated Final Safety Analvsis Reoort (UFSAR) Inconsistencies
A recent discovery of a licensee operating its facility in a manner contrary to the
UFSAR description highlighted the need for a special focused review that compares
plant practices, procedures, and/or parameters to the UFSAR description.
Section 12.5 of the UFSAR refers to the emergency plan. Since the UFSAR does not
specifically include emergency plan requirements, the inspector specifically addressed
Section 6.3.3 Offsite Radiation Levels Assessment and Section 6.6.4 Medical
Treatment in the emergency plan. The inspector also reviewed on shift dose
assessment capabilities and training as discussed in Section P5.
The inspector visited the Midcoast Hospital in Bath, ME, which is the primary facility
for care of contaminated injured patients frorn Maine Yankee. The inspector toured
the facihties used for handling of contaminated injured personnel, interviewed two
emergency room doctors and the head nurse regarding their radiation training and
reviewed a video tape of the 1994 medical drill held at the facility. All had received
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training from the licensee and one doctor had received training at the Radiation
Emergency Assistance Center / Training Center (REACTS), Oak Ridge, Tennessee.
The telephone number for REACTS assistance was listed in the procedure for the
emergency room.
No inconsistencies with the emergency plan requirements were noted.
P8.2 Emeraency Resoonse Facilities Ventilation System (URI 50-309/96-12-04)
During the review of the emergency facility surveillance and information provided by
{
the Resident inspectors, the inspector found that the 3rd quarter emergency
ventilation system surveillance, performed in accordance with Plant Engineering
Department (PED) Procedure 3.17.5.1, Attachment 8, "Special Operating
Instruction," identified that damper MVD#2, which is normally open, failed to close.
The damper is solenoid-operated to open and spring return to close. When this by-
pass damper fails to close, unfiltered air is admitted into the TSC, OSC and EOF.
The damper is located in Room 116 of the Maine Yankee staff building. The
ventilation system failure had been documented on September 26,1996, in Unusual
Occurrence Report Number 90-090.
While touring the TSC, OSC, and EOF, the inspector observed maintenance in
progress to repair the ventilation system. The inspector observed that the solenoid
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operator for MVD#2 had been replaced with a new, larger model, and that the
!
maintenance technician was installing a new position indicator and repairing the
wiring for the position indicator light in Room 118.
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The inspector reviewed the plant alteration specifications, and EPIP 2-50-8,
ATTACHMENT B, " EMERGENCY VENTILATION SYSTEM," and noted that the Plant
Alteration Specification, Section 3.e, stated, in the fifth paragraph, that the air is
brought in through an air tight duct and that MVD#2 is normally closed, but opens
during an emergency condition to allow air through the filtration system. In actuality,
MVD#2 is normally open and is closed under emergency conditions to prevent
unfiltered air from entering the TSC, OSC and EOF. Because of the inconsistencies
between the plant alteration specifications and the EPIP 2-50-8, Attachment B,
the inspector asked the Onsite Emergency Preparedness Coordinator to pursue the
following questions:
1.
Had the plant alteration specifications, drawings, and EPIP 2-50-8,
Attachment B, been compared for accuracy and correctness of damper
labeling and description?
2.
Had the damper actuator component substitution been evaluated to see if it
complies with the original design specifications?
3.
Since the actuators for both MVD#1 and MVD#2 were being replaced and
were notably larger than the original design and were inside the duct, would
there be an effect on air flow characteristics and capacity?
4.
Were the rubberized gaskets and transition boots between the duct wcrk and
fans were covered under a preventive maintenance program?
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5.
Because of the discrepancies noted in question 1, are the position indication
lights for the actuators in Room 118 correct?
Section 7.1.2 of the emergency plan states: "The first floor ventilation system for the
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EOF and TSC is equipped with HEPA and charcoal filtration which is placed in
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operation when the TSC is activated. The system is designed to provide
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approximately 1000 cfm of filtered air to all ERF's collectively, and to also provide
2000 cfm of recirculated / filtered air to the TSC."
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During the inspection, the Onsite EPC transmitted a memorandum to PED requesting
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responses to the inspectors questions. This is considered to be an Unresolved item
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(URI 50-309/96-012-04).
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Conduct of Security and Safeguards Activities
S1.1 Control of Safeauards Information (VIO 50-309/96-12-05)
a.
Insoection Scope (71750)
The inspector reviewed the licensee's response and corrective actions upon
identification of a failure to properly control Safeguards information.
This review was initiated due to several past problems with the control of Safeguards
information. Security event reports were issued in May 1996, and June 1993
documenting failure to properly control Safeguards information. in addition, eight
loggable events have occurred between 1993 and 1996.
b.
Observations and Findinas
On October 17,1996, Maine Yankee security personnel informed the PSS that a
security administrative assistant called from home to report that safeguards
information had been left unattended on a desk in an unsecured office inside the
protected area. Although the office is located inside the protected area, it is not
locked and is accessible to persons other than security officers.
Security personnel and the PSS immediately went to the area and all safeguards
material was recovered at 5:33 pm. The licensee determined that the administrative
assistant had left the site at 3:07 pm which left the safeguards information in a
,
compromised condition for approximately two hours. The event was reported to the
NRC within one hour as required by 10 CFR 73.71. After review by Maine Yankee
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security personnel it was determined that no station personnel had been in the
security office area during the two hour period, due to the close proximity of the
security officer day room and locker room.
The Maine Yankee NRC Approved Security Plan and 10 CFR 73.21.d (2) requires in
]
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part, that while unattended, Safeguards Information shall be stored in a locked
security storage container. Failure to properly control Safeguards information on
October 17,1996, is a violation of NRC approved Security Plan and 10 CFR 73.21
(VIO 50-309/96-012-05).
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c.
Conclusion
a
The inspector identified a violation for failure to properly control Safeguards
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information. The inspector also determined that Maine Yankee properly responded to
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the event as required by the station security plan and NRC requirements. At the
completion of the inspection the licensee had not identified the root cause of this
,
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violation. This violation is notable in that there have been several instances of failure
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to properly control safeguards information in the last three years.
S7
Quality Assurance in Security and Safeguards Activities
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2
S7.1 Review of Annual Security Procram Audit
a.
Insoection Scope (71750)
The inspector reviewed the results of the annual security program as required by
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b.
Observations and Findinas
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During the inspection period, the inspector reviewed the 1996 Annual Security
Program audit that was conducted on September 9-13, and 17-18,1996, by
technical specialists from nuclear power plants in Region I that were SALP
,
,
category 1. The audit scope was well defined and the findings were well presented.
]
No major discrepancies were identified but several observations were identified
during the audit. The inspector reviewed the auditors observations and the licensee's
a
corrective actions to resolve the identified concerns. These were found to be
appropriate. These observations included a finding of the use of ro::ks to fill holes
{
under the protected area barrier, an incomplete search of a package by a security
officer, a lack of complete documentation of the Vehicle Barrier System and need to
enhance several security procedures. The audit team determined that the control of
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Safeguards Information (SI) was adequate.
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c.
Conclusion
The inspector determined that Meine Yankee, with assistance from off site security
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specialists, properly performed the required annual audit of the security program.
The audit was comprehensive with the proper involvement of the station quality
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programs department. The inspectors held discussions with the security operations
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supervisor and determined that the corrective actions were appropriate to resolve the
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observations. However, the observation concerning the control of Si material
appears to require more extensive corrective actions to resolve the problem of
continued failures in this area.
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V. Manaaement Meetinas
X1
Exit Meeting Summary
X1.1 Routine Resident inspection Exit Meetina
The inspectors presented the inspection results to members of the licensee on
October 31,1996. The licensee acknowledged the findings presented.
X1.2 Radioloaical Control Inspection Exit Meetina
The Radiological Control inspection results were presented to members of the
Licensee on September 27,1996. The licensee acknowledged the findings
presented.
X 1.3 Emeraency Preparedness insoection Exit Meetina
The Emergency Preparedness inspection results were presented to members of the
licensee on October 11,1996. The licensee acknowledged the findings presented.
X3
Manaaement Meetina Summarv
X3.1 Indeoendent Safety Assessment Team Exit Meetina
On October 10,1996, the Independent Safety Assessment Team conducted a final
exit meeting to discuss the major findings and conclusions of the team. The meeting
was held at the Wiscasset Middle School, Wiscasset, Maine, and was in two parts.
Part 1 was between the NRC and Maine Yankee and was open for public observation
only. The second part was primarily to respond to questions from the public on the
ISA process and findings.
Attached are the " handouts" provided by NRC staff and Maine Yankee. The NRC
transcripts of both parts of the meeting will be issued under separate
correspondence.
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PARTIAL LIST OF PERSONS CONTACTED
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Licensee
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R. Blackmore, Plant Manger
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J. Connell, Technical Support Department Manager
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S. Evans, Environmental Health and Safety / Emergency Preparedness, Section Head
C. Giggey, Plant Engineer
J. Grant, Plant Support
J. Hebert, Manager, Licensing and Engineering Support
G. Leitch, Vice President Operations
J. Mathieson, Onsite Emergency Preparedness Coordinator
T. Marstaller, Plant Engineer
J. McArdle, Senior Emergency Planner, Yankee Nuclear Service Division
J.' McCann, Licensing Section Head-
P. Metivier, Security Manager
J. Niles, Assistant Operations Manager
G. Pillsbury, Emergency Preparedness Training
P. Radsky, Chemistry Section Head
C. Shaw, Plant Manager (left post)
F. Smith, Chemistry Section Head
S. Smith, Operations Manager
E. Soule, Plant Engineering Manager
J. Temple, Senior Emergency Preparedness Coordinator
W. Tracy, Acting Supervisor - QA
M. Veilleau, Maintenance Manager
J. Weast, Licensing Engineer
D. Whittier, Vice President Licensing and Engineering
NRC
L. Eckert, Radiation Specialist
J. Jang, Sr. Radiation Specialist
J. Lusher, Emergency Preparedness Specialist
W, Olsen, Resident inspector
J. Yerokun, Senior Resident inspector
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INSPECTION PROCEDURES USED
IP 37551:
Onsite Engineering
IP 40500:
Effecuveness of Licensee Controls in Identifying, Resolving, and Preventing
Pr-)blems
IP 62707:
Msintenance Observation
IP 71707:
Plant Operations
IP 71750:
Plant Support Activities
IP 73753:
Inservice inspection
IP 82701:
Operational Status of the Emergency Preparedness Program
IP 83729:
Occupational Exposure During Extended Outages
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IP 83750:
Occupatior a! Exposure
lP 84750:
Radioactive Waste Trestment, Effluent and Environmental Monitoring
IP 92700:
Onsite Followup of Written Reports of Nonroutine Events at Power Reactor
Facilities
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IP 92901:
Operations Followup
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IP 92902:
Followup - Engineering
IP 92903:
Followup - Maintenance
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ITEMS OPENED, CLOSED, AND DISCUSSED
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Items Opened:
50-309/96-12-01
Failure to install Primary Vent Stack Sampling Filters as required
during conduct of maintenance in accordance with TS 5.8.a.3.
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(Section 02.1)
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50-309/96-12-02
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Unplanned Reactor Power increase to 2457 Mwt (Plant Limited
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to 2440) During RCS Delithiation on September 23,1996.
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(Section 04.1)
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50-309/96-12-03
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Documentation of air balance surveillance testing results to
demonstrate consistency with Chapter 9.13 of the FSAR.
Update of section 9.13.2.4 of the FSAR (Section R2.3)
50-309/96-12-04
Questions regarding Emergency Response Facility Ventilation
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System maintenance. Maintenance activities might have
negatively affected the ERF ventilation system (Section P8.2)
50-309/96-12-05
Failure to Properly Control Safeguards information. (Section
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S1.1)
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Items Closed:
50-309/96-007-01 URI
Emergency plant changes 96-01 and 96-02 reviewed and found
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to be in compliance with 10 CFR 50.54(q) and did not decrease
the effectiveness of the emergency plan. (Section P3.1)
Items Discussed:
50-309/96-08-02
High Energy Line Break in the Turbine Building (Section E2.1)
50-309/96-08-04
Turbine Building Flood Protection (Section E2.1)
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LIST OF ACRONYMS USED
Office for Analysis and Evaluation of Operational Data
Air Particulate Detector
Alarm Response Procedure
BAST
Boric Acid Storage Tank
CATS
Corrective Action Tracking System
Control Element Assembly
CED
Corporate Engineering Department
CFR
Code of Federal Regulations
CR
Control Room
DBS
Design Basis Screen
Emergency Notification System
Event Review Board
Emergency Response Data System
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Emergency Response Organization
Engineered Safety Feature
ESS
Emergency Support System
FES
Front End Support
gpm
Gallons Per Minute
GPO
Government Printing Office
High Efficiency Particulate Air
IFl
Inspection Follow-Up item
IFS
Inspection Follow-Up System
IMC
Inspection Manual Chapter
INCA
Incore Analysis
Instrument and Control
IPAP
Integrated Performance Assessment Process
in-Service Inspection
LCO
Limiting Condition of Operation
LER
Licensee Event Report
Management Directive
METPAC
Meteorological Post Accident Computer Model
MWt
Megawatts Thermal
Non-Cited Violation
Office of Nuclear Material Safety and Safeguards
NRC
Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Off-Site Dose Calculation Manual
Office of Enforcement
01
Office of Investigations
OSS
Operational Support System
PDT
Primary Drain Tank
PIPB
inspection Program Branch
Plant Operations Review Committee
Plant Performance Review
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PSS
Plant Shift Supervisor
PVS
Primary Vent Stack
Quality Assurance
Regional Administrator
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Radiological Environmental Monitoring Program
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RlR
Radiological incident Report
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Radiation Monitoring System
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Radiation Protection
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RP&C
Radiological Protection and Chemistry
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Systematic Assessment of Licensee Performance
Safety Parameters Display System
SOS
Shift Operating Supervisor
Technical Evaluation
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Temporary Instruction
TS
Technical Specification
Updated Final Safety Analysis Report
UOR
Unusual Occurrence Report
Unresolved item
Volume Control Tank
WorkOrder
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MAINE YANKEE HANDOUT
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INFORMATION
INDEPENDENT SAFETY
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ASSESSMENT TEAM
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OPEN PUBLIC MEETING
OCTOBER 10,1996
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MAINE YANKEE COMMFNFS ON ISA REPORT
(Talking Points Version]
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Report reflects excellent effort by the NRC and the State
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Report supports Maine Yankee's position that plant is
operating safely
[ Safe operation for over 24 years: report conprms that when issues are identifed which are safety
signtpcant, necessary actions are taken]
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ISA Report is balanced in content and reasonable in its
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subjectivity
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Maine Yankee does not have significant disagreement with
the technical facts in the report
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MAINE YANIME COMMENTS ON ISA REPORT
Many ISA issues were identified by MY prior to the
inspection
(Culture Assessment, Learning Process, Maintenance improvement Program (including a Procedure
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Adherence Initiative). Engineering Quality improvement Program, Safety Analyses improvement Plan,
Industrial Safety improvement Initiatives and Supervisory improvement Plan)
New issues raised by the ISA are receiving prompt
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attention
[NPSH, surveillance testing, timeliness ofcorrective actions, design / licensing basis issues]
NRC root.cause statements are reasonable when viewed in
.s
context
[Willdiscuss in more detaillater]
Overall, being subjected to the ISA was a significant
learning experience
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[ Regulatory thresholds, industryprocaces, opportunityfor re-calibrating interncipolicies andpractices]
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Commend all Maine Yankee personnel for their dedicated
and competent response to all challenges presented by the
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[I wanted to publicly thank themfor their dedication. Personnel at MYperform theirjobs proudly, they
endure long hours ofnever-endingpublic and regulatory scrutinv, and demonstrate that they truly care
about this plant and the safety ofthe public and that they respect to thefullest, the regulatory envannment
in which we work]
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ISA ROOT CAUSE # 1
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" Economic pressures to contain cost"
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Report correctly notes that notwithstanding these
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pressures, " management has effectively operated the
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plant within the budget constraints"
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" Management has effectively prioritized available
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resources, but financial pressures have caused the
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postponement of some needed program improvements
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and actions"
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[ Safety is always paramount duringplant operation and during budget decisions]
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[Whether we like talking about it or not, Maine Yankee has to priariti:e its activities while
ensuring that saf.ety issues are addressed as necessary]
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[ Postponed activities were not viewed at the time to have safety sigmficance; we are
recon.ridering the methods that we use to make these types ofdeci.sions]
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ISA ROOT CAUSE # 2
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" Poor problem identification as a result of complacency and a
lack of a questioning attitude"
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Maine Yankee agrees with statement in the context of
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the full report
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Agrees with NRC statement that involved areas were
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perceived by . management to
be of low safety
significance
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[I would like to emphasi:e that we do not believe that this comment applies to all
employees nor does it apply to the company as a whole - our workforce was not
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complacent regardingissuesthatpersonnelbelievedweresafetysignificant-thoseissues
were promptly addressed to the best oftheir ability]
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[We, the managers at Maine Yankee will absorb the blamefor those circumstances where
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we did not exhibit an adequate questioning arntude. It is ourjob to ensure thatpotentially
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, signtjicant and credible "what ifs"are addressedin every circumstance. In that regaral
the ISA helped us recalibrate our way ofapproaching some issues]
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MATNE YANKEE RESPONSE METHODOLOGY
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Response to the NRC ISA Report within 60 days
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Commitment to Excellence Action Plan provides an
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immediate response to ISA findings and other Maine
Tankee issues
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Provides
comprehensive
plan
for
achieving
and
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' maintaining excellent Maine Yankee performance
Resources
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Organization
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Board of Directors' Oversight
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Programs
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People
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Maine Yankee's focus is clear, and its commitment to
success is unwavering
[We are committed to providing adequate resources and running this plant safety or not at all-
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when you cut through all ofthe issuesfacing us, it is that simple!]
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NRC STAFF HANDOUT
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INFORMATION
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INDEPENDENT SAFETY
,
ASSESSMENT TEAM
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OPEN PUBLIC MEETING
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OCTOBER 10,1996
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INDEPENDENT SAFETY ASSESSMENT
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UNITED STATES
T-
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NUCLEAR REGULATORY COMMISSION
WASHINGTON, D.C. 20555-4001
.
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October 7, 1996
.....
CHAIRMAN
Mr. Charles D. Frizzle, President
Maine Yankee Atomic Power Company
329 Bath Road
Brunswick, Maine 04011
Dear Mr. Frizzle:
I am forwarding the report on the Maine Yankee Atomic Power Station by the
Nuclear Regulatory Commission's Independent Safety Assessment (ISA) team.
The
purpose of the ISA was to determine whether Maine Yankee was in conformity
with its design and licensing bases; to assess operational safety performance;
and to evaluate Maine Yankee's self-assessment, corrective actions, and plans
for improvement.
Overall performance at Maine Yankee was considered adequate for operation.
However, a number of significant weaknesses and deficiencies were identified
that will result in violations.
These weaknesses and deficiencies appear to
be related to two root causes:
economic pressures to contain costs and poor
problem identification as a result of complacency and a lack of a questioning
attitude.
The ISA review was conducted in response to findings made by the NRC's Office
of the Inspector General (0IG) in a report dated May 8,1996.
It included an
assessment of the analytic code support provided for Maine Yankee by the
Yankee Atomic Electric Company. The OIG report found, among other things,
that Maine Yankee had experienced problems with the RELAP/5YA computer code,
used for analyzing how the emergency core cooling system would function during
a small break loss-of-coolant accident (LOCA), and in response, had modified
that code.
OIG also found that these problems with the computer code had not
been reported to the NRC, as required, and that because of these problems,
Maine Yankee's use of the code was not in accordance with NRC requirements.
NRC reviews did not uncover these deficiencies.
The team was large and multi-discipliced in order to provide a thorough, in-
depth review.
Its 25 members, led by an NRC manager, included three
representatives of the State of Maine.
To ensure an independent perspective,
the NRC members were selected from NRC offices other than the Office of
Nuclear Reactor Regulation (NRR) and the NRC's Region 1.
Only persons with r)o
significant prior responsibility for regulating Maine Yankee were chosen.
The
team's management reported to me.
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The ISA team was on site at Maine Yankee between July 15 and 26, 1996, and
)
again between August 12 and 23, 1996.
During these time periods, team members
also conducted assessments at Maine Yankee's corporate headquarters in
Brunswick, Maine, and at the Yankee Atomic Electric Company offices in Bolton,
.
The ISA team reviewed the use of selected analytic codes for performing non-
,
LOCA safety analyses, as well as the capability of the safety-related support
systems to perform in accordance with the assumptions made in those analyses.
l
The review determined that the conditions of approval in NRC Safety Evaluation
Reports have been met although weaknesses in documentation and validation of
plant specific code applications are vulnerabilities which warrant your
'
attention.
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The team determined that cycle-specific core performance analyses were
'
excellent. However, weaknesses were fcund in more complicated, less
frequently performed system safety analyses.
These weaknesses did not cause
the results to exceed Maine Yankee's design and licensing bases.
However, the
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team questioned the capability of the containment spray system and the
component cooling water systems to meet the design basis assumptions for a
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LOCA initiated from greater than 2440 MWt.
These issues, along with the
1
RELAP/5YA deficiencies, will be reviewed by NRC's Office of Nuclear Reactor
Regulation.
The team identified significant deficiencies in the areas of maintenance and
engineering, as well as weaknesses in the overall approach to testing and the
corrective action program.
Specifically, the lack of routine testing of
certain safety systems resulted in the existence of a significant deficiency
of which Maine Yankee was unaware.
In addition, the ISA noted certain design
errors.
Either Maine Yankee was unaware of these errors, or it was aware of
them and had failed to take action to address them.
,
I should add that Maine Yankee deserves credit for having formed a counterpart
team of highly qualified personnel to interface with the ISA team during its
review. The existence of this team was both helpful to the ISA team's
activities and valuable as a means of ensuring that Maine Yankee learned as
much as possible from this effort.
In addition, it meant that as problem
areas were identified, Maine Yankee was in a position to devote resources
promptly to necessary corrective actions.
We have scheduled a meeting for October 10, 1996, during which we will discuss
the assessment and respond to questions you may have.
I request that
following this meeting, you determine the actions needed to ensure the long-
'
term resolution of the deficiencies noted.
I also request that by
December 10, 1996, you provide to the Commission your plans for addressing the
root causes of the deficiencies identified by the ISA.
The NRC's Region I and
its Office of Nuclear Reactor Regulation will be responsible for followup of
the issuns identified in this assessment, in terms of overseeing corrective
actions and taking any enforcement action deemed appropriate.
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3
In accordance with 10 CFR 2.790(a), a copy of this letter and the enclosure
will be placed in the NRC Public Document Room.
Should you have any questions
concerning this assessment, I would be pleased to discuss them with you.
Sincerely,
/DL
g~a ykw
7
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Enclosure:
Independent Safety Assessment Report
for Maine Yankee Atomic Power Company
cc:
See page 4
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cc w/ enclosure:
Mr. Charles B. Brinkman
Mr. Christopher R. Shaw
Manager - Washington Nuclear
Plant Manager
Operations
Maine Yankee Atomic Power Station
ABB Combustion Engineering
P.O. Box 408
)
12300 Twinbrook Parkway, Suite 330
Wiscasset, ME 04578
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,
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Rockville, MD 20852
Mr. G. D. Whittier, Vice President
,
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Thomas G. Dignan, Jr., Esquire
Licensing and Engineering
Ropes & Gray.
Maine Yankee Atomic Power Company
One International Place
329 Bath Road
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Boston, MA 02110-2624
Brunswick, ME 04011
Mr. Uldis Vanags
.
Mr. Patrick J. Dostie
State Nuclear Safety Advisor
State of Maine Nuclear Safety
State Planning Office
Inspector
.,
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State House Station #38
Maine Yankee Atomic Power Station
Augusta, ME 04333
P.O. Box 408
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,
Wiscasset, ME 04578
<
Mr. P. L. Anderson, Project Manager
Yankee Atomic Electric Company
Mr. Graham M. Leitch
,
!
580 Main Street
Vice President, Operations
Bolton, MA 01740-1398
Maine Yankee Atomic Power Station
P.O. Box 408
Regional Administrator, Region I
Wiscasset, ME 04578
U.S. Nuclear Regulatory Commission
475 Allendale Road
Mary Ann Lynch, Esquire
King of Prussia, PA 19406
Maine Yankee Atomic Power Company
329 Bath Road
First Selectman of Wiscasset
Brunswick, ME 04578
Municipal Building
U.S. Route 1
Mr. Jonathan M. Block
Wiscasset, ME 04578
Attorney at Law
P.O. Box 566
Mr. J. T. Yerokun
Putney, VT 05346-0566
Senior Resident Inspector
Maine Yankee Atomic Power Station
Mr. James R. Hebert, Manager
U.S. Nuclear Regulatory Commission
Nuclear Engineering and Licensing
P.D. Box E
Maine Yankee Atomic Power Company
Wiscasset, ME 04578
329 Bath Road
Brunswick, ME 04578
Friends of the Coast
P.O. Box 98
Edgecomb, ME 04556
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EXECUTIVE SUMMARY
Background
In December 1995, the Union of Concerned Scientists forwarded anonymous
allegations to the State of Maine, and the State submitted the allegations to
the NRC. The allegations were that Yankee Atomic Electric Company knowingly
'1
performed inadequate analyses to support an increase in the rated thermal
power at which Maine Yankee Atomic Power Station (MYAPS) may operate.
After
performing a technical review, the NRC Office of Nuclear Reactor Regulation
(NRR) issued a confirmatory order on January 3, 1996, limiting power operation
at the plant to the original licensed power level of 2440 MWt.
i
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The NRC Office of the Inspector General (0lG) completed an inquiry into this
allegation on May 8,1996.
0IG established that MYAPS had experienced
.
problems with, and made modifications' to, the RELAP/5YA computer code which
.
was used in the emergency core cooling analysis fcr a small-break loss-of-
,
coolant accident.
OIG also reported weaknesses in the NRC review and followup
activities which contributed to NRC failure to detect these deficiencies.
In
response to these findings, as well as to respond to concerns by the Governor
of Maine about the safety and the effectiveness of regulatory oversight of
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MYAPS, the NRC Chairman initiated an independent safety assessment of MYAPS.
'
This assessment was to be performed by a team comprised of staff who were
!
independent of any recent or significant regulatoiy oversight responsibility
c
for MYAPS. Additionally, the assessment was to be coordinated with the State
of Maine to facilitate participation by State representatives consistent with
the Commission's policy on cooperation with States at commercial nuclear power
plants (57 FR 6462, February 25, 1992).
{
Licensing and Design-Basis
.
Maine Yankee was in general conformance with its licensing-basis although
significant items of non-conformance were identified.
The licensing-basis was
understood by the licensee but lacked specificity, contained inconsistencies,
and had not been well maintained.
The use of analytic codes for safety analyses was very good. Cycle specific
core performance analyses were excellent.
More complicated, less frequently
performed safety analyses contained weaknesses, but the analyses were found to
be acceptable based on compensating margin.
Conditions of use specified in
j
the safety evaluation reports were found to be satisfied, but not documented.
l
The quality and availability of design-basis information was good overall.
Despite uncorrected and previously undiscovered design problems, the design-
basis and compensatory measures adequately supported plant operation at a
power level of 2440 MWt.
However, the team could not conclude, and the
licensee did not demonstrate, that at a power of 2700 MWt the design-basis
assured adequate NPSH for the containment spray pumps and the heat removal
,
capability of the component cooling water system in the event of a loss-of-
coolant accident.
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Operations
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Performance in the area of operations was very good, with strengths noted in
the areas of operator performance during routine and transient operating
conditions; shift turnovers and pre-evolution briefs; use of risk information
to assure safe operations; and the involvement of management in day-to-day
e
operations.
Weaknesses were noted in the area of "workarounds" and
i
compensatory measures which unnecessarily burdened the operators or
complicated their response to transient conditions. Additionally, log keeping
practices and post-trip reviews lacked rigor.
Maintenance and Testing
i
Performance in the area of maintenance was good overall however, testing was
weak.
The results of the review of equipment reliability for the auxiliary
feedwater, emergency feedwater, high pressure safety injection, and emergency
diesel generator systems showed mixed equipment performance.
Strengths were
i
noted in the areas of knowledge and use of risk methodologies for planning,
prioritizing, and scheduling work; the control and limited use of temporary
,
sealants; and a motivated and dedicated work force. Although material
'
condition was considered good overall, a number of significant material
'
!
condition deficiencies were noted as was a decline in material condition
i
following the 1995 steam generator tubing out age.
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Inadequacies in the scope of testing programs were identified, as were
weaknesses in the rigor with which testing was performed and in the evaluation
of testing results to demonstrate functionality of safety equipment. A lack
of a questioning attitude and stressed resources resulted in the use of poor
surveillance procedures and ineffective evaluation of surveillance test data.
.
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Engineering
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The quality of engineering work was mixed but considered good overall.
Strengths were noted in the capability and experience of the engineering
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staff, day-to-day engineering support of maintenance and operations, in the
quality of most calculations, and in the routine use and application of
.
analytic codes.
However, engineering was stressed by a shortage of resources,
j
and there was a tendency to accept existing conditions.
Specific weaknesses
]
were noted with inconsistent identification and resolution of problems,
j
inadequate testing, and work on some calculations and analytic codes.
f
Self Assessment and Corrective Actions
Weaknesses were identified in the areas of problem identification and
'
resolution.
While licensee self-assessments were generally good, they
.
occasionally failed to identify weaknesses or incorrectly characterized the
'
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significance of the findings. Additionally, some corrective actions were not
timely and others were ineffective, leading to repetitive problems.
Licensee
planning was generally effective, although some weaknesses were found in the
overall implementation of improvement plans.
Some economic pressures resulted
in limitations on resources, which impaired the licensee's ability to complete
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improvement projects that affected plant safety.
Equipment problems were not
resolved and improvement programs were not effectively implemented because
the licensee perceived them to be of low safety significance.
Root Causes and Overall Conclusions
While overall performance at Maine Yankee was adequate for operation, a number
of deficiencies were identified by the team in each of the areas assessed.
These deficiencies, which included weak identification and resolution of
problems; weak scope, rigor, and evaluation of testing; and declining material
condition stemmed from two closely related root causes.
These root causes
were (1) economic pressure to be a low-cost energy producer has limited
available resources to address corrective actions and some plant improvement
upgrades and (2) there is a lack of a questioning culture which has resulted
in the failure to identify or promptly correct significant problems in areas
perceived by management to be of low safety significance.
The economic pressures discussed in Section 4.3 resulted in limitations on
resources and interfered with the licensee's ability to complete projects and
other efforts that would improve plant safety and testing activities.
Examples include the failure to adequately test safety related components
(Section 3.2.4); the long-standing deficient design conditions, such as the
undersized atmospheric steam dump valve (Sections 3.1.3.1 and 3.3.1) and
environmental qualification issues (Section 2.3.9); and the lack of effective
improvement programs, such as the design basis reconstitution program
(Sections 3.3.3 and 4.3.3).
These and other examples discussed in the report
illustrate the licensee's willingness to accept existing conditions, many of
which became operator workarounds (Section 3.1.1.1).
Examples of issues which illustrate complacency and the failure to identify or
promptly correct significant problems, include previously undiscovered
deficient conditions of the service water and auxiliary feedwater water
systems (Section 3.2.2); inadequacies in ventilation systems (Section 2.3.7);
post-trip reviews which lacked rigor and completeness (Section 3.1.2.7);
emergency operating procedures that may not adequately address an inadequate
core cooling event and a steam generator tube rupture under certain conditions
(Section 3.1.3.1); lack of a questioning attitude during test performance and
evaluation that was not conducive to discovering equipment problems, but
rather to accepting equipment performance (Sections 2.2.1, 3.2.2, 3.2.4); and
licensee self-assessments that occasionally failed to identify weaknesses, or
incorrectly characterized the significance of findings (Section 4.1).
In
addition, some corrective actions were not timely and others were ineffective,
leading to repetitive problems (Section 4.2).
vii
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UNITED STATES NUCLEAR REGULTORY COMMISSION
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INDEPENDENT SAFETY ASSESSMENT TEAM
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OF
MAINE YANKEE ATOMIC POWER STATION
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PUBLIC MEETING OCTOBER 10,1996
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SELECTION OF MAINE YANKEE
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ALLEGATIONS REGARDING RELAP/5YA
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OFFICE OF INSPECTOR GENERAL INQUIRY
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STATE OF MAINE CONCERNS
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INDEPENDENT SAFETY ASSESSMENT
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LARGE EXPERIENCED TEAM
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INDEPENDENT OF NRR AND REGION I
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PARTICIPATION BY STATE OF MAINE
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MAINE YANKEE INDEPENDENT SAFETY ASSESSMENT
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MISSION
1.
Provide an independent assessment of the conformance of Maine Yankee
Atomic Power Station to its design and licensing bases including
appropriate reviews at the site and corporate office.
2.
Provide an independent assessment of operational safety performance
providing risk perspectives, where appropriate.
'
3.
Evaluate the effectiveness of licensee self-assessment, corrective actions,
and improvement plans.
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4.
Determine the root cause(s) of safety significant findings and draw
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conclusions on overall performance.
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Maine Yankee
Independent Safety Assessment Team
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Edward L. Jordan
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Team Manager
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Ellis W. Merschoff
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Team Leader
Region 11
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Uldis Vanags
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Ola B. West
Patrick Dostie
Ad*d"eg on i
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David Decrow
State Representatives
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Kriss M. Kennedy
Ronald Lloyd
Thomas O. Martin
Alan L Madison
Jack E. Rosenthal
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OPS / Training
Maint./ Testing
Eng. Design / Tech.
Management & Organization
Analytic Code Support
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AEOD
Region IV
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Larry Bell
Russell Bywater
John Boardman
Harold Christensen
G. Norman Lauben
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Region ill
Region il
John Kauffman
Peter Prescott
George Hausman
Leonard Ward
AEOD
Region lli
Contractor
Contractor
Robert Christie
Cyril Crane
Contractor
Contractor
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George Cha
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Contractor
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Michael Shlyamberg
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STATE PARTICIPATION
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TECHNICAL TEAM - DAY-TO-DAY PARTICIPATION IN EACH OF
THE FIVE FUNCTIONAL AREAS BEING ASSESSED.
e
ULDIS VANAGS
e
PATRICK DOSTIE
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DAVID DECROW
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PROCESS TEAM - OBSERVE THE PROCESS AT KEY
MILESTONES TO ASSURE ISAT IS FAIR, BALANCED, AND
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OBJECTIVE.
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PETER WILEY
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DR. FORREST REMICK
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CITIZEN'S GROUP - PERIODIC BRIEFINGS FOR GOVERNOR AND
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CITIZEN'S GROUP TO KEEP THEM INFORMED OF PROGRESS.
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DR. DON ZILLMAN
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MR. ROGER HEWSON.
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MS. ELIZABETH ARMSTRONG
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DR. EDWARD LAVERTY
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MR. THOMAS BROUSSARD
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LICENSEE SUPPORT ORGANIZATION
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SENIOR LEVEL COUNTERPARTS
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ADMINISTRATIVE
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EXTENSIVE RESPONSE LIBRARY
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EFFECTIVE LINK TO LINE ORGANIZATION
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THOROUGH EXTENT OF CONDITION REVIEWS
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SAFETY ASSESSMENT SCHEDULE
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JUNE 17-JULY 12
TEAM PREPARATION
JULY 15
PUBLIC ENTRANCE MEETING
JULY 15-26
FIRST ONSITE EVALUATION PERIOD
,
AUGUST 12-23
SECOND ONSITE EVALUATION PERIOD
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OCTOBER 8
ISSUE REPORT
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OCTOBER 10
PUBLIC EXIT MEETING
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SAFETY ASSESSMENT ACTIVITIES
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WALKDOWN SYSTEMS
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EXTENDED CONTROL ROOM OBSERVATIONS
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VERTICAL SLICE REVIEW
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HIGH PRESSURE SAFETY INJECTION
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PROGRAM / PROCESS / PROCEDURE REVIEW
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ANALYTIC CODE REVIEW
HORIZONTAL REVIEW TO SER
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VERTICAL SLICE REVIEW STEAM LINE BREAK
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INTERVIEWS
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SAFETY ASSESSMENT STANDARDS
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REGULATIONS - MEASURE CONFORMANCE
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ASSESSMENT - MEASURE MARGIN OF SAFETY
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SUPERIOR
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ACCEPTABLE
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PROBABILISTIC RISK ASSESSMENT - PROVIDE PERSPECTIVE
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NRC ASSESSMENT STANDARDS
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SUPERIOR
GOOD
ACCEPTABLE
Safety
Properly Focused
Normally Well Focused Acceptable
Performance
Programs
Effective Control
Some Deficiencies Exist Instances of
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Insufficient Control
Self Assessment
Effective
Some Issues Not
May not Occur
!
Identified
Until Problem is
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Apparent
Corrective Actions
Comprehensive
Some Not Complete
Not Thorough
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Root Cause
Recurring Problems
Normally Thorough
Do Not Probe
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Eliminated
Deeply
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SAFETY ASSESSMENT RESULTS
OVERALL PERFORMANCE ADEQUATE FOR OPERATION
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DESIGN AND LICENSING BASIS - GENERALLY IN
CONFORMANCE
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OPERATIONS - VERY GOOD
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MAINTENANCE - GOOD
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TESTING - ACCEPTABLE
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ENGINEERING - GOOD
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ACCEPTABLE
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LICENSING AND DESIGN BASIS
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LICENSING BASIS
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- LACKS SPECIFICITY
> CONTAINS INCONSISTENCIES
> NOT WELL MAINTAINED
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USE OF ANALYTIC CODES
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> CYCLE SPECIFIC - EXCELLENT
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> COMPLEX, INFREQUENTLY USED - WEAK
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DESIGN BASIS
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> GOOD QUALITY
- GOOD AVAILABILITY
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> ADEQUATELY SUPPORTS 2440 MWt
> OPERATION AT 2700 MWt NOT DEMONSTRATED
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LICENSING / DESIGN BASIS
OPERABILITY ISSUES RAISED
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COMPONENT COOLING PIPING INSIDE CONTAINMENT
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REACTOR WATER STORAGE TANK LEVEL TRANSMITTERS
EQUIPMENT QUALIFICATION FOR SUBMERGENCE
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VENTILATION
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LOGIC CIRCUITRY
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CONTAINMENT SPRAY PUMP
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CHECK VALVE TESTING
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SAFETY ASSESSMENT
OPERATIONS
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OVERALL PERFORMANCE VERY GOOD
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STRENGTHS
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- USE OF RISK INFORMATION
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- MANAGEMENT INVOLVEMENT
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> SHIFT TURNOVERS
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> PRE EVOLUTION BRIEFS
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WEAKNESSES
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> WORKAROUNDS AND COMPENSATORY MEASURES
- POST TRIP REVIEWS
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> LOG KEEPING
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MAINTENANCE
OVERALL PERFORMANCE GOOD
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STRENGTHS
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> KNOWLEDGE /USE OF RISK
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> MOTIVATED / DEDICATED WORK FORCE
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> CONTROL OF TEMPORARY REPAIRS
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- QUALITY OF MAINTENANCE
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WEAKNESSES
!
- DECLINING MATERIAL CONDITION
- INCONSISTENT EQUIPMENT RELIABILITY
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- - - .- . . - . - -. - .
- .
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SAFETY ASSESSMENT
TESTING
OVERALL PERFORMANCE ACCEPTABLE
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TESTING WEAKNESSES
INADEQUATE SCOPE
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>
WEAK RIGOR
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MTAK EVALUATIONS
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TESTING STRENGTHS
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>
>
INSERVICE TESTING
CONTAINMENT LEAK RATE TESTING
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!
_
-
- -
-
- -
- - - - - -
-
-
- - - -
- -
-
- -
- - - - .
- - .
- - .
- . . - _ _ _ _
- .
- - . - .-. - -
_. -
"
SAFETY ASSESSMENT
ENGINEERING
!
OVERALL PERFORMANCE WAS MIXED
e
QUALITY OF ENGINEERING WORK WAS GOOD.
- QUALIFIED CAPABLE STAFF
- GOOD ELECTRICAL DESIGN WORK
- SUPPORT TO OPERATIONS AND MAINTENANCE
> SUPPORT PROVIDED BY YANKEE ATOMIC
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LIMITED OWNERSHIP
,
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> EQUIPMENT QUALIFICATION
> FIRE PROTECTION
- TESTING
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INUONSISTENT IDENTIFICATION AND RESOLUTION OF
PROBLEMS
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> VENTILATION
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> ATMOSPHERIC DUMP VALVE
!
> AUXILIARY FEED PUMP
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18
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- ------
-
. - - - -
-
- -
- -
- - - - - - - - . . . - . _ - - _ _ - - - - - _ . - - - -
...!
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EFFECTIVENESS OF SELF ASSESSMENT, CORRECTIVE ACTIONS,
AND IMPROVEMENT PLANS
,
OVERALL EFFECTIVENESS WAS ACCEPTABLE
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SELF ASSESSMENT
> INTERNAL / EXTERNAL EFFECTIVENESS MIXED
- OVERSIGHT COMMITTEES EFFECTIVE
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- FRAGMENTED PROBLEM IDENTIFICATION PROCESS
!
CORRECTIVE ACTION PROGRAM
> FRAGMENTED PROCESS
!
> TRENDING AND TIMELINESS WEAK
[
> OCCASIONALLY INEFFECTIVE
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IMPROVEMENT PLANS
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- MANY INDIVIDUAL PLANS
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- NO INTEGRATED PLAN
!
> RESULTS MIXED
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!
19
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-
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. . .
. _ _. __
_
_
_
..
_
. _ _ _ _ . _ _
. .
. _ _ _ _ _ . _ .
.
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.
!
ROOT CAUSES OF SIGNIFICANT FINDINGS
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ROOT CAUSE 1
Economic pressure to be a low-cost energy producer has limited
'
available resources to address corrective actions and some plant
improvement upgrades. Management has effectively prioritized
available resources, but financial pressures have caused the
postponement of some needed programs and actions.
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>
,
!
20
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-
-
-
- - -
_
_
.
_
..
.--
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-
-
.
.
ROOT CAUSES OF SIGNIFICANT FINDINGS
.
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ROOT CAUSE 2
1
There is a lack of a questioning culture which has resulted in the
failure to identify or promptly correct significant problems in areas
perceived by management to be of low safety significance.
Management appears complacent with the current level of safety
performance and there does not appear to be a clear incentive for
improvement.
.
21
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