05000354/LER-1996-025, Forwards LER 96-025-00.Commitments Listed Including Work Order Initiated to Install Recording Instrumentation to Determine Actual Line Dynamics During Next RCIC warm-up

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Forwards LER 96-025-00.Commitments Listed Including Work Order Initiated to Install Recording Instrumentation to Determine Actual Line Dynamics During Next RCIC warm-up
ML20135F397
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 12/06/1996
From: Bezilla M
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20135F400 List:
References
LR-N96408, NUDOCS 9612130028
Download: ML20135F397 (2)


LER-1996-025, Forwards LER 96-025-00.Commitments Listed Including Work Order Initiated to Install Recording Instrumentation to Determine Actual Line Dynamics During Next RCIC warm-up
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv), System Actuation
3541996025R00 - NRC Website

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"*O psgG Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 l

Nuclear Business Unit DEC 061996 I

LR-N96408' 1

U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 I

i

Dear Sir:

HOPE CREEK GENERATING STATION DOCKET NO. 50-354 I

UNIT NO. 1 LICENSEE EVENT REPORT NO. 96-025-00 i

This Licensee Event Report entitled, " Engineered Safety Feature Actuation - Reactor Core Isolation Cooling System Isolation," is i

being submitted pursuant to the requirements of l

10CFR50.73 (a) (2) (iv).

i Sincerely, g?ll p '

Mark Bezilla General Manager -

Hope Creek Operations l

l t

Attachment i

JPP SORC Mtg.96-111 l

C Distribution LER File

\\N 6y 4

120085 9612130028 961206 PDR ADOCK 05000354, S

PDR Thepwerisinyourfunds.

95-2168 HEV 694

.. _, _ -.... _ _ _ _ _. _. _ _ _.... _ _... _. _ _ _.. _ _.. ~. _.. _. _. _ _. _.. - _.. _. _ _ _ _ _ _

e.

DEC 061996 Attachment A i

The following items represent commitments that Public Service Electric.& Gas (PSE&G)- made to the Nitclear Regulatory Commission (NRC) relative to this LER (354/96-025-00).

The commitments are

.as-follows:

l A work order (961126200) has been initiated to install l

recording instrumentation to determine actual line dynamics 1

during the next RCIC warm-up.

This work is scheduled to be completed during the next forced / planned cold shutdown of l

the plant.

A plan will be developed to perform a RCIC system walkdown to evaluate the adequacy of the flow venturi installation.

This plan will be completed by February 28, 1997.

This t

walkdown will be completed no later than the next refueling i

outage.

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