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MONTHYEARML20138B2131985-10-0404 October 1985 Confirmatory Action Ltr Re 851004 Telcon Concerning Return of Facility to Power Operations After 851002 Reactor Trip. Util Must First Conduct Root Cause Analysis of Trip & Provide Briefing to NRC Before Return to Power Project stage: Other ML20133K5131985-10-11011 October 1985 Notification of Significant Meeting on 851016 W/Util Onsite to Discuss Root Cause Assessment & Readiness for Resumption of Power Operations Following 851002 Reactor Trip Project stage: Meeting ML20133K5891985-10-14014 October 1985 Forwards Action List Providing Util Plan to Resolve Concerns Stemming from 851002 Transient,Per 851010-11 Meetings.Listed Commitments Scheduled for Completion Prior to Restart. Schedule for long-term Items Will Be Submitted by 851118 Project stage: Meeting ML20133K7191985-10-18018 October 1985 Forwards Supplemental Info Re 851002 Transient,Per NRC Request During 851016 Meeting.Info Includes Main Feed Pump Trip Determination,Hpi a Flow Anomaly,Cooldown of RCS, Cooldown Rate,Tech Specs & Revised Action List Project stage: Supplement ML20133P8511985-10-25025 October 1985 Forwards Summary & Supplemental Info Re 851002 Transient, Per 851025 Telcon.Items in Plan Include pre- & post-startup Actions to Determine Root Cause of Event & Initiation of Corrective Programs Project stage: Supplement ML20134A8371985-11-0101 November 1985 Forwards Addendum to Attachment 5,Part Ii,Rev 1 to Auxiliary Feedwater/Main Feedwater Failure Analysis Contained in Project stage: Other ML20138R0971985-11-13013 November 1985 Forwards Rev 2 to Attachment 2 & Addendum NRC-5150 Re HPI a Flow Anomoly,Rev 1 to Attachment 5,Parts I & II Re Auxiliary Feedwater/Main Feedwater Failure Analysis & Attachment 8 Re Oil Levels on safety-related Pumps Project stage: Other ML20138R9291985-11-15015 November 1985 Forwards Latest Rev to Action List,Describing Program Plan to Resolve Concerns Stemming from 851002 Transient.All Startup Required Items Completed.All Power Escalation Items Will Be Completed by Full Power Operation Project stage: Other ML20137H9361985-12-23023 December 1985 Responds to Violations Noted in Insp Rept 50-312/85-30. Corrective Actions:Instrumentation & Control Procedure I.103 Revised to Include Multiplier Link Change Instructions & Pegging Steam Pressure Controller Setpoints Reduced Project stage: Other 1985-10-04
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M8851999-10-0808 October 1999 Informs of Staff Determination That Listed Calculations Should Be Withheld from Public Disclosure,Per 10CFR2.790, as Requested in 990909 Affidavit ML20211J7731999-08-31031 August 1999 Forwards Insp Rept 50-312/99-03 on 990802-06.No Violations Noted.Insp Included Decommissioning & Dismantlement Activities,Verification of Compliance with Selected TS & Review of Completed SEs ML20211H7481999-08-13013 August 1999 Forwards Amend 126 to License DPR-54 & Safety Evaluation. Amend Changes Permanently Defueled Technical Specification (PDTS) D3/4.1, Spent Fuel Pool Level, to Replace Specific Reference to SFP Level Alarm Switches with Generic Ref 3F0799-22, Provides Update & Rev to Submittal Made by Util Ltr with Regard to EAL Classification Methodology for Unit 3.Reponses to NRC Staff Questions Provided as Attachment D to Ltr & Reflects Discussions Held1999-07-13013 July 1999 Provides Update & Rev to Submittal Made by Util Ltr with Regard to EAL Classification Methodology for Unit 3.Reponses to NRC Staff Questions Provided as Attachment D to Ltr & Reflects Discussions Held ML20210H9541999-07-0707 July 1999 Informs NRC of Change to Rancho Seco Decommissioning Schedule,As Described in Licensee Post Shutdown Decommissioning Activities Rept ML20209D2501999-06-24024 June 1999 Informs That Util Has Revised All Sections of Rancho Seco Emergency Plan (Rsep),Change 4,effective 990624 ML20196G0431999-06-22022 June 1999 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Smud Rancho Seco Nuclear Generating Station ML20195D1851999-05-27027 May 1999 Forwards Rancho Seco Annual Rept, IAW Plant Permanently Defueled TS D6.9.4 & D6.9.6b.Rept Contains Shutdown Statistics,Narrative Summary of Shutdown Experience,Er Info & Tabulation of Facility Changes,Tests & Experiments ML20195B8511999-05-27027 May 1999 Forwards Change 4 to Rancho Seco Emergency Plan, Incorporating Commitments Made to NRC as Outlined in NRC .Emergency Plan Includes Two Listed Supporting Documents ML20207E9181999-05-27027 May 1999 Informs That Effective 990328,NRR Underwent Reorganization. within Framework of Reorganization,Div of Licensing Project Mgt Created.Reorganization Chart Encl ML20206U7411999-05-18018 May 1999 Provides Summary of 990217-18 Visit to Rancho Seco Facility to Become Familar with Facility,Including Onsite ISFSI & Meeting with Representatives of Smud to Discuss Issues Re Revised Rancho Seco Ep,Submitted to NRC on 960429 ML20206M1611999-05-10010 May 1999 Forwards Listed Proprietary Calculations to Support Review of Rancho Seco ISFSI Sar.Proprietary Encls Withheld ML20206E8591999-04-12012 April 1999 Provides Info Re High Total Coliform Result in Plant Domestic Sewage Effluent Prior to Confluence with Combined Effluent.Cause of High Total Coliform Result Was Broken Flow Rate Instrument.Instrument Was Repaired on 990318 ML20204H6751999-03-19019 March 1999 Forwards Insp Rept 50-312/99-02 on 990309-11.No Violations Noted.Portions of Physical Security & Access Authorization Programs Were Inspected ML20204E4031999-03-16016 March 1999 Submits Rept of Status of Decommissioning Funding for Rancho Seco,As Required by 10CFR50.75(f)(1).Plant Is Currently in Safstor, with Operating License Scheduled to Expire in Oct 2008 ML20204E6661999-03-11011 March 1999 Forwards Rancho Seco Exposure Rept for Individuals That Received Greater than 100 Mrem During 1998,IAW TS D6.9.2.2 & NRC Regulatory Guide 1.16 ML20204E6441999-03-11011 March 1999 Forwards Individual Monitoring Repts for Personnel That Required Radiation Exposure Monitoring During 1998 ML20207L1711999-03-10010 March 1999 Informs of Staff Determination That Supporting Calculations & Drawings Contained in Rev 2 of Sar, Should Be Withheld from Public Disclosure,Per 10CFR2.790 NL-99-002, Submits Info About Property Insurance for Rancho Seco Nuclear Generating Station,Iaw 10CFR50.54(w)(3)1999-03-10010 March 1999 Submits Info About Property Insurance for Rancho Seco Nuclear Generating Station,Iaw 10CFR50.54(w)(3) ML20207D4431999-03-0101 March 1999 Forwards Annual Radioactive Effluent Release Rept, for Rancho Seco Nuclear Generating Station for 1998 ML20207H6181999-02-18018 February 1999 Provides Attached Metrix & Two Copies of Rancho Seco ISFSI Sar,Rev 2 on Compact Disc,As Requested in 990209 Meeting. First Rounds of RAIs Dealt Primarily with Use of Cask as Storage Cask.Without Compact Disc ML20203D0761999-02-10010 February 1999 Ltr Contract:Task Order 37 Entitled, Technical Assistance in Review of New Safety Analysis Rept for Rancho Seco Spent Fuel Storage Facility, Under Contract NRC-02-95-003 ML20155D4431998-10-27027 October 1998 Forwards Amend 3 to Rancho Seco Dsar,Representing Updated Licensing Basis for Operation of Permanently Shutdown & Defueled Rancho Seco Nuclear Facility During Permanently Defueled Mode.With Instructions & List of Effective Pages NL-98-032, Forwards Certified Copies of Listed Nuclear Liability Endorsements for Util1998-09-30030 September 1998 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Util ML20237A6031998-08-0707 August 1998 Forwards Insp Rept 50-312/98-03 on 980706-09.No Violations Noted ML20237A9481998-08-0303 August 1998 Forwards Smud 1997 Annual Rept, IAW 10CFR50.71(b),which Includes Certified Financial Statements ML20236Q9461998-07-15015 July 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-312/98-02 ML20236J6331998-06-30030 June 1998 Forwards Response to Violations Noted in Insp Rept 50-312/98-02.Corrective Actions:Util Revised RSAP-1003 to Clarify District Security Staff Responsibilities Re Handling & Review of Criminal History Info ML20236E8211998-06-0303 June 1998 Forwards Insp Rept 50-312/98-02 on 980519-21 & NOV Re Failure to Review & Consider All Info Obtained During Background Investigation.Areas Examined During Insp Also Included Portions of Physical Security Program ML20217G8391998-04-20020 April 1998 Forwards Copy of Rancho Seco Monthly Discharger Self-Monitoring Rept for Mar 1998 IR 05000312/19980011998-03-25025 March 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-312/98-01 on 980205 ML20217F1891998-03-18018 March 1998 Forwards Signed Original & Amend 7 to Rancho Seco Long Term Defueled Condition Physical Security Plan & Rev 4 to Long Term Defueled Condition Training & Qualification Plan.Encls Withheld,Per 10CFR2.790 ML20217G6661998-03-18018 March 1998 Forwards Discharge Self Monitoring Rept for Feb 1998, Which Makes Note of One Wastewater Discharge Permit Violation ML20217H0451998-03-18018 March 1998 Submits Rancho Seco Exposure Rept for Individuals Receiving Greater than 100 Mrem During 1997,per TS D6.9.2.2 & Guidance Contained in Reg Guide 1.16.No One Exposed to Greater than 100 Mrem in 1997 ML20216K1091998-03-11011 March 1998 Forwards NRC Form 5 Individual Monitoring Repts for Personnel Who Required Radiation Exposure Monitoring,Per 10CFR20.1502 During 1997.W/o Encl ML20217N9531998-03-0505 March 1998 Responds to Violations Noted in Insp Rept 50-312/98-01. Corrective Actions:Radiation Protection Group Wrote Potential Deviation from Quality (Pdq) 97-0082 & Assigned Radiation Protection Action to Determine Cause & CAs ML20203H7001998-02-25025 February 1998 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1997, IAW 10CFR50.36a(a)(2) & TS D6.9.3.Revs to Radiological Environ Monitoring Manual & off-site Dose Calculation Manual,Encl ML20202G0131998-02-12012 February 1998 Forwards Certified Copies of Listed Nuclear Liability Endorsements & Master Worker Policy Certificate of Insurace for Facility NL-98-006, Submits Annual Rept of Property Insurance Levels for Rsngs, IAW 10CFR50.54(w)(3)1998-02-12012 February 1998 Submits Annual Rept of Property Insurance Levels for Rsngs, IAW 10CFR50.54(w)(3) ML20202C4641998-02-0505 February 1998 Forwards Insp Rept 50-312/98-01 on 980105-08 & Notice of Violation.Insp Included Decommissioning & Dismantlement Work Underway,Verification of Compliance W/Selected TS & Main & Surveillance Activities Associated W/Sfp ML20199A5881997-11-10010 November 1997 Responds to NRC Re Violations Noted in Insp Rept 50-312/97-01.Corrective Actions:Reviewed SFP Water Temp & Instrument Calibr Records,Generated Otr 97-001 to Document out-of-tolerance Instrument & Generated Pdq 97-0064 ML20198R9501997-11-0505 November 1997 Requests Interpretation of or Rev to NUREG-1536, Std Review Plan for Dry Cask Storage Sys, Re Compliance W/ 10CFR72.236(e) & 10CFR72.122(h)(4) for Dry Fuel Storage Casks ML20198K5391997-10-21021 October 1997 Forwards Insp Rept 50-312/97-04 on 970922-25 & Notice of Violation.Response Required & Will Be Used to Determine If Further Action Will Be Necessary ML20217D3101997-09-25025 September 1997 Forwards Update of 1995 Decommissioning Evaluation, for Rancho Seco Nuclear Generation Station & Annual Review of Nuclear Decommissioning Trust Fund for Adequacy Re Assumptions for Inflation & Rate of Return ML20211F0991997-09-23023 September 1997 Forwards One Certified Copy of Mutual Atomic Energy Liability Underwriters Nuclear Energy Liability Insurance Endorsement 120 for Policy MF-0075 for Smud Rancho Seco Nuclear Facility ML20198G8141997-08-22022 August 1997 Forwards Amend 125 to License DPR-54 & Safety Evaluation. Amend Permits Smud to Change TS to Incorporate Revised 10CFR20.Amend Also Revises References from NRC Region V to NRC Region IV ML20151L0281997-07-29029 July 1997 Provides Response to NRC Request for Addl Info Re TS Change,Relocating Administrative Controls Related to QA to Ufsar,Per NUREG-0737 ML20149E5031997-07-10010 July 1997 Second Partial Response to FOIA Request for Documents. Forwards Records Listed in App C Being Made Available in Pdr.Records in App D Already Available in PDR ML20148P5161997-06-30030 June 1997 Second Partial Response to FOIA Request for Documents.App B Records Being Made Available in PDR ML20141A1721997-06-17017 June 1997 Forwards Insp Rept 50-312/97-03 on 970603-05.No Violations Noted.Areas Examined During Insp Included Portions of Physical Security Program 1999-08-31
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEAR3F0799-22, Provides Update & Rev to Submittal Made by Util Ltr with Regard to EAL Classification Methodology for Unit 3.Reponses to NRC Staff Questions Provided as Attachment D to Ltr & Reflects Discussions Held1999-07-13013 July 1999 Provides Update & Rev to Submittal Made by Util Ltr with Regard to EAL Classification Methodology for Unit 3.Reponses to NRC Staff Questions Provided as Attachment D to Ltr & Reflects Discussions Held ML20210H9541999-07-0707 July 1999 Informs NRC of Change to Rancho Seco Decommissioning Schedule,As Described in Licensee Post Shutdown Decommissioning Activities Rept ML20209D2501999-06-24024 June 1999 Informs That Util Has Revised All Sections of Rancho Seco Emergency Plan (Rsep),Change 4,effective 990624 ML20196G0431999-06-22022 June 1999 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Smud Rancho Seco Nuclear Generating Station ML20195B8511999-05-27027 May 1999 Forwards Change 4 to Rancho Seco Emergency Plan, Incorporating Commitments Made to NRC as Outlined in NRC .Emergency Plan Includes Two Listed Supporting Documents ML20195D1851999-05-27027 May 1999 Forwards Rancho Seco Annual Rept, IAW Plant Permanently Defueled TS D6.9.4 & D6.9.6b.Rept Contains Shutdown Statistics,Narrative Summary of Shutdown Experience,Er Info & Tabulation of Facility Changes,Tests & Experiments ML20206M1611999-05-10010 May 1999 Forwards Listed Proprietary Calculations to Support Review of Rancho Seco ISFSI Sar.Proprietary Encls Withheld ML20206E8591999-04-12012 April 1999 Provides Info Re High Total Coliform Result in Plant Domestic Sewage Effluent Prior to Confluence with Combined Effluent.Cause of High Total Coliform Result Was Broken Flow Rate Instrument.Instrument Was Repaired on 990318 ML20204E4031999-03-16016 March 1999 Submits Rept of Status of Decommissioning Funding for Rancho Seco,As Required by 10CFR50.75(f)(1).Plant Is Currently in Safstor, with Operating License Scheduled to Expire in Oct 2008 ML20204E6441999-03-11011 March 1999 Forwards Individual Monitoring Repts for Personnel That Required Radiation Exposure Monitoring During 1998 ML20204E6661999-03-11011 March 1999 Forwards Rancho Seco Exposure Rept for Individuals That Received Greater than 100 Mrem During 1998,IAW TS D6.9.2.2 & NRC Regulatory Guide 1.16 NL-99-002, Submits Info About Property Insurance for Rancho Seco Nuclear Generating Station,Iaw 10CFR50.54(w)(3)1999-03-10010 March 1999 Submits Info About Property Insurance for Rancho Seco Nuclear Generating Station,Iaw 10CFR50.54(w)(3) ML20207D4431999-03-0101 March 1999 Forwards Annual Radioactive Effluent Release Rept, for Rancho Seco Nuclear Generating Station for 1998 ML20207H6181999-02-18018 February 1999 Provides Attached Metrix & Two Copies of Rancho Seco ISFSI Sar,Rev 2 on Compact Disc,As Requested in 990209 Meeting. First Rounds of RAIs Dealt Primarily with Use of Cask as Storage Cask.Without Compact Disc ML20155D4431998-10-27027 October 1998 Forwards Amend 3 to Rancho Seco Dsar,Representing Updated Licensing Basis for Operation of Permanently Shutdown & Defueled Rancho Seco Nuclear Facility During Permanently Defueled Mode.With Instructions & List of Effective Pages NL-98-032, Forwards Certified Copies of Listed Nuclear Liability Endorsements for Util1998-09-30030 September 1998 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Util ML20237A9481998-08-0303 August 1998 Forwards Smud 1997 Annual Rept, IAW 10CFR50.71(b),which Includes Certified Financial Statements ML20236J6331998-06-30030 June 1998 Forwards Response to Violations Noted in Insp Rept 50-312/98-02.Corrective Actions:Util Revised RSAP-1003 to Clarify District Security Staff Responsibilities Re Handling & Review of Criminal History Info ML20217G8391998-04-20020 April 1998 Forwards Copy of Rancho Seco Monthly Discharger Self-Monitoring Rept for Mar 1998 ML20217H0451998-03-18018 March 1998 Submits Rancho Seco Exposure Rept for Individuals Receiving Greater than 100 Mrem During 1997,per TS D6.9.2.2 & Guidance Contained in Reg Guide 1.16.No One Exposed to Greater than 100 Mrem in 1997 ML20217F1891998-03-18018 March 1998 Forwards Signed Original & Amend 7 to Rancho Seco Long Term Defueled Condition Physical Security Plan & Rev 4 to Long Term Defueled Condition Training & Qualification Plan.Encls Withheld,Per 10CFR2.790 ML20217G6661998-03-18018 March 1998 Forwards Discharge Self Monitoring Rept for Feb 1998, Which Makes Note of One Wastewater Discharge Permit Violation ML20216K1091998-03-11011 March 1998 Forwards NRC Form 5 Individual Monitoring Repts for Personnel Who Required Radiation Exposure Monitoring,Per 10CFR20.1502 During 1997.W/o Encl ML20217N9531998-03-0505 March 1998 Responds to Violations Noted in Insp Rept 50-312/98-01. Corrective Actions:Radiation Protection Group Wrote Potential Deviation from Quality (Pdq) 97-0082 & Assigned Radiation Protection Action to Determine Cause & CAs ML20203H7001998-02-25025 February 1998 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1997, IAW 10CFR50.36a(a)(2) & TS D6.9.3.Revs to Radiological Environ Monitoring Manual & off-site Dose Calculation Manual,Encl NL-98-006, Submits Annual Rept of Property Insurance Levels for Rsngs, IAW 10CFR50.54(w)(3)1998-02-12012 February 1998 Submits Annual Rept of Property Insurance Levels for Rsngs, IAW 10CFR50.54(w)(3) ML20202G0131998-02-12012 February 1998 Forwards Certified Copies of Listed Nuclear Liability Endorsements & Master Worker Policy Certificate of Insurace for Facility ML20199A5881997-11-10010 November 1997 Responds to NRC Re Violations Noted in Insp Rept 50-312/97-01.Corrective Actions:Reviewed SFP Water Temp & Instrument Calibr Records,Generated Otr 97-001 to Document out-of-tolerance Instrument & Generated Pdq 97-0064 ML20198R9501997-11-0505 November 1997 Requests Interpretation of or Rev to NUREG-1536, Std Review Plan for Dry Cask Storage Sys, Re Compliance W/ 10CFR72.236(e) & 10CFR72.122(h)(4) for Dry Fuel Storage Casks ML20217D3101997-09-25025 September 1997 Forwards Update of 1995 Decommissioning Evaluation, for Rancho Seco Nuclear Generation Station & Annual Review of Nuclear Decommissioning Trust Fund for Adequacy Re Assumptions for Inflation & Rate of Return ML20211F0991997-09-23023 September 1997 Forwards One Certified Copy of Mutual Atomic Energy Liability Underwriters Nuclear Energy Liability Insurance Endorsement 120 for Policy MF-0075 for Smud Rancho Seco Nuclear Facility ML20151L0281997-07-29029 July 1997 Provides Response to NRC Request for Addl Info Re TS Change,Relocating Administrative Controls Related to QA to Ufsar,Per NUREG-0737 NL-97-030, Forwards Endorsement 132 to Nelia Policy NF-0212 & Endorsement 118 to Maelu Policy MF-0075 for Smuds Rsngs1997-05-13013 May 1997 Forwards Endorsement 132 to Nelia Policy NF-0212 & Endorsement 118 to Maelu Policy MF-0075 for Smuds Rsngs ML20138F5321997-04-28028 April 1997 Forwards Response to RAI Re License Amend 192,updating Cask Drop Design Basis Analysis,Per NRC 960510 Request for Addl Info on 960318 Application NL-97-027, Forwards Certified Copies of Listed Nuclear Liability Endorsements for Utility1997-04-17017 April 1997 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Utility ML20137W8091997-03-20020 March 1997 Forwards Biennial Update to Rancho Seco Post-Shutdown Decommissioning Activities Rept ML20137S3571997-03-19019 March 1997 Provides Notification of Use of Revised Quality Manual for Activities Re Rancho Seco ISFSI ML20137D0981997-03-18018 March 1997 Submits Rancho Seco Exposure Rept for Individuals Receiving Greater than 100 Mrem During 1996.Provided IAW TS D6.9.2.2 & Guidance Contained in NRC Reg Guide 1.16.No One Exposed to Greater than 100 Mrem in 1996 ML20137D1221997-03-18018 March 1997 Submits,Iaw 10CFR20.2206 & TS D6.9.2.1,1996 NRC Form 5 Individual Monitoring Repts for Personnel Requiring Radiation Exposure Monitoring Per 10CFR20.1502 During 1996. W/O Encl NL-97-012, Submits Rept of Listed Current Levels of Property Insurance for Plant,Iaw 10CFR50.54(w)(3)1997-02-11011 February 1997 Submits Rept of Listed Current Levels of Property Insurance for Plant,Iaw 10CFR50.54(w)(3) ML20138L1091997-01-29029 January 1997 Informs of Schedule Change Re Decommissioning of Rancho Seco.Incremental Decommissioning Action Plan,Encl NL-97-005, Forwards Certified Copies of Listed Nuclear Liability Endorsements for Utility1997-01-22022 January 1997 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Utility NL-96-056, Forwards Certified Copies of Listed Nuclear Liability Endorsements for Util1996-12-16016 December 1996 Forwards Certified Copies of Listed Nuclear Liability Endorsements for Util ML20134E0041996-10-23023 October 1996 Forwards Response to NRC GL 96-04, Boraflex Degradation in Spent Fuel Pool Storage Racks ML18102B6871996-08-0606 August 1996 Informs That Util Will Revise Loading & Unloading Procedures & Operator Training as Necessary ML20149E4491994-05-16016 May 1994 Forwards 1993 Annual Rept of Sacramento Municipal Utility District,For Info ML20149E3971994-05-10010 May 1994 Forwards Re Updated Decommissioning Cost Estimate for Rancho Seco & Attached Rept by Tlg Engineering,Inc. W/Svc List ML20059H6731994-01-20020 January 1994 Forwards Revised Rancho Seco Quality Manual, Reflecting Current Rancho Seco Pol Phase Nuclear Organization Changes ML20059E1221994-01-0303 January 1994 Forwards Amend 7 to Long Term Defueled Condition Physical Security Plan.Encl Withheld (Ref 10CFR73) ML20059C1681993-12-22022 December 1993 Forwards Suppl Info to Support Review & Approval of 930514 Proposed License Amend 186 Re Nuclear Organization Changes, Per NRC Request 1999-07-07
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L5431990-09-20020 September 1990 Requests Exemptions from Certain Requirements of 10CFR50.47(b) & 50,App E & Proposes New Emergency Plan That Specifically Applies to Long Term Defueled Condition ML20059J9161990-09-13013 September 1990 Notification of Change in Operator/Senior Operator Status for R Groehler,Effective 900907 ML20059J9221990-09-13013 September 1990 Responds to Generic Ltr 90-03, Relaxation of Staff Position in Generic Ltr 83-28,Item 2.2,Part 2, 'Vendor Interface for Safety-Related Components.' No Vendor Interface Exists for Spent Fuel Pool Liner NL-90-442, Forwards Endorsements 13 to Nelia Certificate N-49 & Maelu Certificate M-49,Endorsements 91 & 92 to Maelu Policy MF-75 & Endorsements 103 & 104 to Nelia Policy NF-2121990-09-12012 September 1990 Forwards Endorsements 13 to Nelia Certificate N-49 & Maelu Certificate M-49,Endorsements 91 & 92 to Maelu Policy MF-75 & Endorsements 103 & 104 to Nelia Policy NF-212 ML20059G0791990-09-0606 September 1990 Forwards Supplemental Fitness for Duty Performance Data, Omitted from 900725 Rept Re Random Drug Testing Results ML20059E0031990-08-30030 August 1990 Forwards Semiannual Radioactive Effluent Release Rept,Jan- June 1990, Corrected Repts & Revs to ODCM ML20059C2491990-08-27027 August 1990 Advises That M Foster & B Rausch Leaving Util Effective on 900810 & 17,respectively & Will No Longer Require Active Operator Licenses ML20056B2591990-08-20020 August 1990 Forwards Long-Term Defueled Condition Security Training & Qualification Plan. Encl Withheld (Ref 10CFR2.790) ML20056B2961990-08-10010 August 1990 Discusses 900731 Meeting Re Future of Util & Closure & Decommissioning of Facility.Request for Possession Only License Pending Before Commission ML20058Q2811990-08-0909 August 1990 Forwards Updated Listing of Commitments & long-range Scope List Items Deferred or Closed by Commitment Mgt Review Group Since Last Update ML20058N0911990-08-0707 August 1990 Notifies of Minor Change in List of Tech Specs Applicable in Plant Defueled Condition.Determined That Surveillance Requirements Table 4.1-1,Item 63 Not Required to Be Included in List of Tech Specs Applicable in Defueled Condition ML20056A1131990-07-30030 July 1990 Apprises of Status of Plans to Use 3 of 4 Emergency Diesel Generators as Peaking Power Supplies & Responds to Questions in .Util Obtained Authorization for Operation of Diesel Generators for No More than 90 Days Per Yr ML20056A2041990-07-30030 July 1990 Provides Response to NRC Bulletin 90-001, Loss of Fill Oil in Transmitters Mfg by Rosemount. Pressure & Differential Pressure Transmitters 1153 & 1154 Do Not Perform Any safety-related Function in Current Plant Mode ML20055J0311990-07-25025 July 1990 Forwards fitness-for-duty Performance Data for Facility from 900103-0630 ML20055J0331990-07-25025 July 1990 Notifies of Change in Operator/Senior Operator Status. Operators Terminating Employment & No Longer Require License ML20055H8081990-07-24024 July 1990 Forwards Decommissioning Financial Plan for Plant,Per 10CFR50.33(k)(2) & Requests Interim Exemption Re Requirement to Have Full Decommissioning Funding at Time of Termination of Operation,Per 10CFR50.12 ML20055H7561990-07-24024 July 1990 Requests Exemption from Performing Annual Exercise of Emergency Plan,Activation of Alert & Notification Sys & Distribution of Public Info Brochures,Per 10CFR50.12 Requirements ML20055F8421990-07-13013 July 1990 Forwards Application for Proposed Decommissioning of Plant. Util Needs Relief from Equipment Maint,Surveillance,Staffing & Other Requirements Not Necessary to Protect Public Health & Safety During Defueled Condition ML20055G9821990-07-12012 July 1990 Advises That Environ Exposure Controls Action Plan Will Be Provided by Sept 1990,per Insp Rept 50-312/90-02 ML20055E5111990-07-0606 July 1990 Notifies of Change in Operator/Senior Operator Status for D Rosenbaum & M Cooper,Effective 900622 & 29,respectively ML20055C3541990-02-14014 February 1990 Forwards Updated Response to Insp Rept 50-312/88-30. Calculations for Liquid Effluent Monitors Completed & in Use & Rev to Reg Guide 4.15 in Procedure RSAP-1702 Scheduled to Be Completed & Implemented by Apr 1990 ML20055C3511990-02-14014 February 1990 Forwards Addl Info Re 900306 Response to NRC Bulletin 88-003, Inadequate Latch Engagement in Hfa Type Latching Relays Mfg by Ge. Util Will Replace Only Relays Found Not to Meet Insp Criteria ML20248H2571989-10-0606 October 1989 Responds to NRC Re Addendum to Safety Evaluation Supporting Amend 92 to License DPR-54 Re Reactor Vessel Vent Valve Testing.No Testing of Reactor Vessel Vent Valves Will Be Performed ML20248H2391989-10-0606 October 1989 Requests Exemption from Requirements of 10CFR26 Re Fitness for Duty Programs Based on Present & Future Operational Configuration ML20248A8271989-09-25025 September 1989 Requests Permission to Submit Next Amend to Updated FSAR W/Decommissioning Plan Submittal.Extension Will Allow District to Incorporate Plant Closure Status in SAR Update to Reflect Plant Conditions Accurately ML20248D4611989-09-13013 September 1989 Responds to 890906 Request for Assessment of Util Compliance W/Ol & Associated Programs & Commitments,Per 10CFR50.54(f). Staffing Requirements for Emergency Preparedness Will Not Be Violated & Future Shortfalls Will Be Remedied ML20247G1991989-09-11011 September 1989 Requests Extension for Time Period Equivalent to That of Current Shutdown.Extension Would Result in Revised Final Expiration Date of Not Earlier than 900318.Plant Would Not Be Brought Above Cold Shutdown W/O NRC Prior Concurrence ML20247H3551989-09-0707 September 1989 Informs That Util Stands by Commitments of 890621 & 0829 Re Implementation of Closure Plan in Safe & Deliberate Manner in Compliance W/License & W/All Applicable Laws & Regulations ML20247H5541989-09-0101 September 1989 Responds to Violations Noted in Insp Rept 50-312/89-14. Corrective Actions:Stop Order on Fuel Movement Issued & Action Plan Generated on 890908 to Address Broader Issues 05000312/LER-1988-010, Forwards Rev 1 to LER 88-010,due to Change in Commitment Date for re-evaluating Fire Zones.Date Changed to 901001. Zones re-evaluated in Conjunction W/Mods to Fire Detection Annunciator Sys1989-08-23023 August 1989 Forwards Rev 1 to LER 88-010,due to Change in Commitment Date for re-evaluating Fire Zones.Date Changed to 901001. Zones re-evaluated in Conjunction W/Mods to Fire Detection Annunciator Sys ML20246A4011989-08-16016 August 1989 Forwards Rev 5 to Inservice Testing Program Plan. Changes Identified Consistent W/Guidance Provided by Generic Ltr 89-04 NL-89-593, Forwards Plant Closure Organizational Charts & Administrative Procedure RSAP-0101,per 890802 Request1989-08-15015 August 1989 Forwards Plant Closure Organizational Charts & Administrative Procedure RSAP-0101,per 890802 Request ML20245H4781989-08-10010 August 1989 Requests Exemption from Generic Ltr 89-07, Power Reactor Safeguards Contingency Planning for Surface Vehicle Bombs Because on 890607,util Board of Directors Ordered That Plant Cease Operation ML20245H1781989-08-0909 August 1989 Notifies of Change in Operator/Senior Operator Status. J Dailey & J Reynolds Terminated Employment on 890721 & 890802,respectively ML20245L1831989-08-0808 August 1989 Informs That Official Correspondence Must Be Directed to Listed Individuals Due to Reorganization of Util Following 890606 Election ML20247L9221989-07-26026 July 1989 Provides Revised Response to NRC Re Violations Noted in Insp Rept 50-312/88-33.Corrective Action:Portable Shield Walls Inspected Every 6 Months to Ensure All Safety Factors Met & Area Surveys Conducted on Weekly Basis ML20247M4121989-07-24024 July 1989 Requests Exemption from 10CFR50,App E,Section IV.F.2 to Allow Util Not to Perform Annual Emergency Plan Exercise for 1989.Request Results from Transitional Mode of Plant from Operating Plant to Plant Preparing for Decommissioning NL-89-541, Requests That Completion Date for Addl Training of Personnel Involved in Performing Work on Environ Qualified Equipment Be Extended from 890616 to 8912151989-07-14014 July 1989 Requests That Completion Date for Addl Training of Personnel Involved in Performing Work on Environ Qualified Equipment Be Extended from 890616 to 891215 ML20246P4011989-07-14014 July 1989 Informs That Evaluation of Contracts & Agreements Identified No Restrictions on Employee Ability to Provide Info About Potential Safety Issues to NRC NL-89-547, Forwards Amend 110 to License DPR-54,issued on 890609, Identifying Discrepancy in Tech Spec Page X (Table of Contents) Which Does Not Reflect Changes Approved in Amend 1061989-07-0606 July 1989 Forwards Amend 110 to License DPR-54,issued on 890609, Identifying Discrepancy in Tech Spec Page X (Table of Contents) Which Does Not Reflect Changes Approved in Amend 106 ML20246A9751989-06-30030 June 1989 Advises That Concerns Addressed in Generic Ltr 89-08 Inapplicable,Since Util Intends to Defuel Reactor.Generic Ltr Will Be Reviewed Prior to Placing Facility in heatup-cooldown Operational Mode for Return to Power ML20246A5171989-06-30030 June 1989 Forwards Rancho Seco Closure Plan, Per 890621 Request for Addl Info Re Plan CEO-89-289, Notifies of Change in Operator/Senior Operator Status.Listed Operator/Senior Operator Terminated Employment on Listed Effective Date1989-06-27027 June 1989 Notifies of Change in Operator/Senior Operator Status.Listed Operator/Senior Operator Terminated Employment on Listed Effective Date NL-89-526, Lists Discrepancies Noted in Amend 109 to License DPR-54,per 890615 Discussion W/S Reynolds.Tech Specs Encl1989-06-22022 June 1989 Lists Discrepancies Noted in Amend 109 to License DPR-54,per 890615 Discussion W/S Reynolds.Tech Specs Encl ML20245H4181989-06-21021 June 1989 Discusses Util Plans Re Overall Closure of Plant,Per 890615 Meeting W/Nrc.Util Will Request Appropriate Changes to Tech Specs to Reflect Defueled Mode & Will Evaluate & Request Changes to Emergency Plan ML20245D9281989-06-21021 June 1989 Discusses Activities Underway Re Plan for Closure of Plant Discussed During 890615 Meeting W/Region V.Util Intends to Continue Use of Essential Programs,Such as Preventive Maint Program,For Sys within Scope of Closure Process ML20245A0981989-06-16016 June 1989 Responds to NRC Bulletin 89-001, Failure of Westinghouse Steam Generator Tube Mechanical Plugs. No Westinghouse Plugs Used at Plant ML20248B5751989-06-0202 June 1989 Advises That Util Anticipates That Final Analysis of Thermal Striping Will Conservatively Support Surge Line Lifetime Significantly Longer than June 1994 Date,Per NRC Bulletin 88-011, Pressurizer Surge Line Thermal Stratification NL-89-468, Submits Justification for Absence of Functional Testing Requirement in Proposed Tech Spec 4.14(f) Re Snubber Svc Life Monitoring,Per 890517 Request1989-05-30030 May 1989 Submits Justification for Absence of Functional Testing Requirement in Proposed Tech Spec 4.14(f) Re Snubber Svc Life Monitoring,Per 890517 Request ML20247N2601989-05-25025 May 1989 Requests Guidance Re Whether NRC Concurs W/Arbitrator Order Concerning Employee Access to Plant 1990-09-06
[Table view] |
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esuun SACRAMENTO MUNICIPAL UTILITY DISTRICT 6201 S Street. P O Bow 15830. Sacramento. CA 95813. (916) 452 3211 AN ELECTHic SYSTEM SERVING THE HE ART OF CALIFOHNIA RJR 85-520 October 18, 1985 DIRECTOR OF NUCLEAR REACTOR REGULATION ATTENTION HUGH L THOMFSON JR DIREC10R DIVISION OF LICENSING k U S NUCLEAR REGULATORY COMMISSION 3
WASHINGTON D C 20555 DOCKET NO 50-312 LICENSE NO DPR-54 NRC REQUESTED SUPPLEMENTAL INFORMATION FROM TRAN51EN1 0F OCTOBER 2, 1985 During the October 16, 1985, meeting at Rancho Seco with our staffs and NRC Region V, the District agreed to provide the NRC with supplemental information concerning the transient of October 2,1985. The attachments provide the District's assessment and conclusions to date in the four areas highlighted by the NRC review team. Also included as an attachment is the latest revision of the District's " Action List" sent to you on October 14, 1985 (RJR 85-514).
The District supplied this list as part of its program plan ". . . to investigate and correct the causes associated with . . . " the October 2nd event. The attachemnts are:
1 MAIN FEED PUMP TRIP DETERMINATION: Results of the District's deternIInation of the probable cause of the main feed pump trip event.
II HPI "A" FLOW AN0MALY: Analysis and investigation of the mechanisms creating the apparent flow anomaly upon initiation of high pressure injtetton in "A" line.
III COOLDOWN OF THE RCS: A quantitative discussion of the cooldown rate experienced by the RCS during the transient.
IV C00l.00WN RATf m AND TECH SPEC 1: The District's interpretation of the RCS cooldown vs. Tech Spec limits and t.ooldown curves.
V ACTION TIS _T: Latest revision which provides the current status of the District's program plan to resolve issues of the October 2,1985, transient.
If you require additional information or have any questions concerning any of
}heaboye,contactJerryDelezenskiofmystaff.
A Dgr\
R. J. RODRIGUEZ \ 5 ,
ASSISTANTGENERAL)fANAGER, NUCLEAR Attachments l
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t
\
ATTACHMENT 1 TOOCTOBER 18, 1985, NRC LETTER I. MAIN FEE 0 PUMP TRIP DETERMINATION During the October 2,1C35, trcnsient.
A. SYMPTOM:
The control panel A main feed pump trip indicator and the plant computer system indiceced the A main feed pump was tripped shortly after loss o' condenser vacuum and 19 seconds before the mactor trip. The 3 main feed pump was indicated tripped 30 seconds af ter '.no A main feed pump trip indication. The cause of these r,ain feed. pump trips was not immediately apparent.
B. INVESTIGATION:
Positive indication enabling conclusive identification of the cause, or causes, of the trip of both main feedwater pump-drive turbines was not available. Therefore, the investigation plan consisted of an examination of the "as found" condition of tne feedwater pumps / drive turbines including controls, analysis l of the data recorded during the event, consideration of Operator l statements about transient events, review of drawings and vendor equipment manuals, review of certain modifications and assistance of manufacturers' field engineers. The investigation plan was composed of the following steps:
- 1. Identification of main feed pump / drive turbine trip devices.
- 2. Examination of trip device "as found" conditions for clues about trip causes.
- 3. Proposal of several trip hypotheses.
- 4. Proof or disproof of hypotheses.
- 5. Development of conclusions.
In order to identify all main feed pump / drive turbine trip devices, an engineering review of drawings, schematics, vendors' manuals, manufacturers' records, and plant records was conducted. An angineer from Westinghouse (manufacturer of the drive turbine) examined the physical installation at Rancho Seco to identify any trip devices not documented, looking specifically for a low vacuum trip device. None were found. The following is a list of
r
[
e 2
trip devices:
- 1. Bearing Lube Oil Pressure Low
- 2. ThrustBearingWear(ForwardandReverse)
- 3. PumpDischargePressureHigh(InstantaneousTrip) 4 Pump Discharge Pressure High (Delayed Trip)
- 5. Overspeed
- 6. Manual
- 7. Governor Oil Pressure Low (This device initiates feed pump trip alarms and causes the throttle and stop valves to close.
The pump / turbine is not tripped by this device.)
Examination of trip device "as found" conditions was performed and the set point of each device identified above, The trip devices were also examined for proper interconnection in the control system and for any degradation. The trip devices for both pumps were found to be in the " normal" (not tripped) state.
The B MFP Discharge Pressure High (Delayed Trip) trip device set point was found set 35 psi lower than the normal set point. Wiring for the trip devices was found to conform to the drawlags and no undocumented trip devices were found.
The Operators on shift during the transient were pooled by the Plant Superintendent concerning actuation of a manual trip. The findings of this poll were:
- 1. The A MFP was definitely not tripped by actuation of the manual trip.
- 2. Manual trip of the 8 MfW is still under study.
Five hypotheses have been proposed and evaluated as discussed below:
- 1. Pump Discharge Pressure High Trip actuated by a pressure spike in the pump discharge. The pressure spike was attributed to pressure oscillations Induced by loss of condenser vacuum, increased pump discharge pressure from increased pump speed, and water hammer caused by closure of a feedwater block valvo.
This hypothesis was disproved by engineering analysis and evaluation. The maximum pressure attributable to the afore.
3 mentioned pressure components was determined to be about 1300 psig, the trip is set at 1650 psig. Pump speed necessary to attain the pressure trip setpoint was deter-mined to be about 5200 RPM. Actual maximum pump '.pced attained by the A MfP (determined by interpolating available data) was about 4100 RPM.
- 2. Thrust Bearing Wear Trip actuated by movement of the pump / turbine shaft. Shaft movement was attributed to flow and pressure oscillations causing unbalanced resultant forces from the turbine rotor and pump impeller. This should have caused the thrust bearing wear signal to " seal in". The thrust bearing wear trip did not require reset prior to resetting the MfP turbine. This investigation con-tinues.
- 3. Overspeed Trip actuated by excessive pump / turbine speed. The overspeed was attributed to unloading of the pump impeller caused by steam entering the pump suction, or reduced flow through the pump. Heat for vaporizing feed-water liquid was supplied by condensation of pegging steam.
This was evaluated by an engineering calculation. The calculation concluded that feedwater would remain a compressed liquid after heating attributed to desuperheating and con-densing pegging steam. Evaluation of other overspeed phenomenon, including proper trip of the device, is continuing.
4 Low Vacuum Trip actuated by loss of condenser vacuum.
A low vacuum trip device has not been identified. Investigation of transient effects on the pump / turbine assembly is continuing.
- 5. Governor Oil Pressure Low switch actuated by causing the throttle and stop valves to close and generation of a computer
" pump tripped" signal. This apparent trip of the A MfP is attributed to a decay in turbine governor oli pressure.
Actuation of the governor low oil pressure switch does not cause actuation of the AUTO STOP oil dump solenoid, thus, the A MfP drive turbine was not, in fact, tripped. This hypothesis is supported by the following:
- 1. Pump speed momentarily increased about 400 RPM about two minutes after the pump was indicated to have tripped.
- 2. The Operators were not abic to reset the puup.
- 3. Two lub oil pumps for the A MfP were found running after the plant was stabilized.
4 C. CONCLUSION:
At this time we are not proposing a conclusion to the cause of the trip of the main feed pump turbines. Investigations are continuing as described above and additional phenomenon are being explored with assistance from INPO dnd other utilities that have similar pump drives and controls. We util comunicate to NRC any new findings that develop from our continuing investigation.
l
ATTACHMENT 11 IIPI "A" FLOW ANOMALY following the transient of October 2nd, Control Room operators reported that indicated flow through the "A" High Pressure Injection (HPI) line had dropped to zero when the control valves for the other three HP! lines were opened in unison, Review of the data gathered by one of the plant computers confirmed the report and showed that the condition lasted for about 30 seconds. Post transient investigation also revealed that this same phenomenon occurred during a trip in 1984 involving a shorted inverter. At that time Control Room operators assuned that the abnormal indication was related to the inverter problem.
Troubleshooting of the phenomenon has proceeded in six distinct phases. ,
in Phase 1, proper function of all devices in the instrumentation loop was verified.
In Phase 2, a test was written and performed which duplicated the phenomenon and allowed for collection of additional data under controlled conditions, in Phase 3, calculations, based on the data collected in Phase 2, showed that a large reduction in flow would be expected as a result of the transient flow conditions and piping system geometry. However, this calculated flow drop was not as large as that which was actually experience, it should be noted that tha system alignment at the time the abnormal condition occurred was for normal Reactor Coolant System Make-up with post trip HP! addition and not in the line-up that the system would automatically assume during a Safety features Actuation.
Phase 4, consisted of examination of the affccted control valve and flow element by radiography in order to provide additional assurance that an intermittent, partial flow blockage in the valve or erosion of the flow elements did not exist. These examinations showed the 1 equipment to be in good condition.
Phase 5, consists of another test procedure, approved by the Plant Review Committee but not yet performed, that will demonstrate again that this flow phenomenon occurs only during nanual HPl and not during Safety features Actuated HPl. Proper HPl flow under Safety features condition was demonstrated in June of this year during routine refueling interval surveillance testing. flow resistance of this flow path and a parallel HP! flow path will be compared.
Phase 6, consists of further refining the calculations performed in Phase 3 using data collected in Phase 5 testing.
The compiled results from the exhaustive investigation detailed above will demonstrate that a transient hydraulic pht:nomenon resulting from the "as built" piping configuration occurs during manual HPI but does not af fect balanced Safety features initiated HP! flow.
ATTACllMENT Ill C00LDOWN Of Tile RCS A quasi steady state energy balance has shown good agreement between the RCS heat removal based on the observed cooldown, and the heat removal from the OTSGs based on Auxiliary Feedwater Flow and 0TSG level.
Additionally, good agreement was found between the heat removal from the OTSGs based on Auxiliary Feedwater flow and 0TSG 1evel, and the assumed steam loads. The assumed steam loads include the ,
Auxiliary feedwater Pump Turbine and the 4A Feedwater Heater relief I valves as the major steam loads.
Preliminary results are attached. The results will be checked in accordance with our calculation procedures before finalization.
Final results should be available before October 22, 1985. This calculation will formalize the rough calculations done inmediately following the transient,
1 CALCULATION SHEET
$~ SSACRAMENTO M U DMUNICIPAL UTILITY DISTRICT C 6201SStreet.P,0 Bo=15830.SacramentoCA950521830(9161452 3211 l ORIGINATOR *^
- t**:
- C DATE
! / Y 'b C ALC. NO. 3 ~ f ~ l i I ^ l E SUBJECT * '#
- ('I
- a' CHECKED I< / 7 \' SHE E T l_ OF __2 I
PRELIMINARY RESULTS s .
o Average AFW flows between 01:36 and 01:43
. A 172,000 lb/hr
> B 186,000 lb/hr - -
e o OTSG Water Inventory Change between 01:36 and 01:43
~~
A 3,120 lb 19 8 3,570 lb '
Steaming Rate W 1 = WA ry ut, A 145,000 lb/hr
'o 77 8 155,000 lb/hr
'I
_ _ _ , , _. ,n .w , -- , . - - * -- - - - * * - * ' '
,e Change in steam mass between 01:36 and 01:43 l, (Pressure 945 4 622 psig) . .
}z-
" uts = 9,260 lb ao -
si Total steam usage W2 " W1 + />Ms -
s' ' '
t>t 23
,o W2 = 379,000 lb/hr , ,
t is
,, kNOWN Steam Loads se
,g Hoggers, Air ejectors Gland Steam, Aux Feed Pump Turb, Pegging Steam to 4A ~
to 370,000 lb/hr (85% of this is pegging steam). . . l Unaccounted for steam losses , ,
"I 9,000 lb/hr 34{
Sl
,, This is within the uncertainty of the calculation.
- i .
two teac ie se
CALCULATION SHEET
$SMUD SACRAMENTO MUNICIPAL UTILITY DISTRICT ( i 6201SStreet.P O Bon 15830.SacrameentoCA9585218301916) 452 3211 ORIGIN A TOR ________________.__._______DATE _ _ _ _ _ _ _ _ _ _ _ . _ CALC. NO _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _
SUBJECT _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ . . _ . _ . . . _ _ _ _ _ - CHECKED _ _ . . _ . _ _ _ _ _ . _ _ . _ _ _ _ . . . . _
__ __ _ .___ _ _ . _ _ _ _ . . . _ _ _ - _ . . _ _ _ _ . _ _ _ . _ SHEET _2 _
_ OF _ 2 _ __ ._ _ .
2 3
PRIMARY SIDE HEAT BALANCE
. All numbers for 7 minute period from 01:36 to 01:43
, Heat removed from OTSG's (based on AFW flows and 0TSG level change)
'l 0
sg
= 42.5 MBtu
,,l Decay Heat Input =7.4 MBtu Pump Heat Input =9.6 MBtu l
,)l
j Heat from cooling RCS water =16.35MBtu is: ,
i.! Heat from immersed metal =7.85MBtu
,a
,,! Heat frcn pressure boundary metal ~4 MBtu Net Heat removed from RCS ry ai! Q= 45.2 MBtu l
[( This agrees within 6%
J4 25 28; 27 2RI 2S Jo 11 12 11 14 1%
3e SM'/O ,419e to 64
ATTACHMENT IV C00LD0WN TECHNICAL SPECIFICATION The Rancho Seco Technical Specifications contain two limits on cooldown of the primary system. Technical Specification 3.1.2.4 states, "The pressurizer heatup and cooldown rates shall not exceed 100* F. in any 1-hour period." This limit applies only to the pressurizer and is based on an ASME Code fatigue analysis performed on that vessel. This specification was clearly not exceeded during the October 2, 1985, transient.
Technical Specification 3.1.2.2 provides a curve (Figure 3.1.2-2) of allowable system pressure as a function of temperature for normal heatup and cooldown operation. Operation in accordance with this curve ensures the requirements of 10 CFR 50 Appendix G are satisfied. Technical Specification 3.1.2.2 also states that the cooldown rate stated on the above figure (100* F/ hour when T > 270* F) shall not be exceeded. Information from the Babcock & Wilcox Company indicates that this cooldown rate is applicable only below 550' F. This information is being provided to the Rancho Seco Operators as guidance for interpreting this Technical Specification. The G;tober 2, 1985, transient involved a cooldown from 550' F of approximately 70* F in about 20 minutes. This equates to a cooldown rate in excess of the Technical Specification limit and the District will satisfy the reporting requirements of 10 CFR 50.35.
The extension of the 100* F/ hour requirement of beyond the temperature range (363' F) indicated on Figure 3.1.2-2 is to maintain consistency between reactor coolant system operation and the original design functional requirements. The October 2, 1985, transient did not result in the reactor cold leg temperature entering the range of the pressure limitations on Figure 3.1.2-2. Therefore, the requirements of 10 CFR 50 Appendix G were not violated. The violation of the 100* F/ hour limit has an insignificant effect on the current fatigue life of the plant but has been logged for consideration in future accumulative cycle fatigue analysis.
In accordance with current Rancho Seco Emergency Operation Procedures, this transient resulted in operator action to reduce primary system pressure in accordance with Figure 1 of Procedure E05. The trainstent was evaluated by the Babcock and Wilcox Company and determined not to meet the conditions of possible pressure boundary degradation and the system was returned to normal Hot Standby status.
LEGEND: SU-. Startup R: quired LT = Lcng T rm STATUS DATE 10-18-85 -
PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS jWR No./NCR/ COMRENTS ETC.
'I Post Trip Report J. Field SU In Progress NA Draf t completed. In Review to be finalized 10/21.
II Root Cause Analysis S. Crunk SU Completed NA' Reviewed by Management Review Team.
III Aux FW ICS Control
- a. Verify calibration of N. Brock SU Completed 104969, 104972 Completed 10/07/85 appropriate modules. 104973, 104974 104975
- b. Reset of Aux FW Valves- B. Spencer SU Completed NA Crews were trained.
On MFWP Reset.
- c. Revise procedures for B. Spencer SU Completed NA Temporary change to III.b. Operating Procedure A.51 done 10/13/85. .
t
- d. Evaluate design of AFW V. Lewis ST In Progress NA valve reset on restart of MFW Pump or RCP.
4 I
J
~- . . _ . , . - . . , , . . , . _. -
LEGEND: SU = Startup R: quired LT = Lcng Term STATUS DATE 10-18-85 -
PE = Power Escalation DCTOBER 2, 1985 TRANSIENT TIME 1600 NA =.Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS
- ETC'.
IV HPI "A" Inject Line flow indication
-a. Write and perform J. Field SU Results NA Results to be approved Special Test Procedure. Approval 10/18.
Required
- b. Perform calibration N. Brock SU Completed 105228 Completed 10/04/85.
check of FT-23807. Found OK.
- c. Resolve flow anomaly and J. Field SU Requires S-5103 NCR assigned to D. Abbott.
prepare Summary Report. Disposition (To be completed 10/22.)
V Pegging Steam Controls
- a. Determine adequacy of J. Field SU Completed NA Nuclear Engineering pegging steam setpoints (S. Rutter) Support and FW heater relief valve setpoints.
- b. 1. Verify setpoints of R. Lawrence SU Completed 104541, 104544 All setpoints as per 2nd and 4th Point 104542, 104543 Process Standards.
heater shell. relief 104562, 104563 valves.
- 2. Reset 4th point R. Lawrence SU 104581, 104583 Revised setpoint values heater shell reliefs 104582, 104584 per V a.
to new setpoint values.
L _
LEGEND; SU = Startup Required LT = Lcng Term STATUS DATE 10-18-85 -
PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1600 HA = Not Applicable ST = Short Term - ACTION LIST - '
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
Y c. Verify setpoints of all R. Lawrence PE Planning Will require use of hydro secondary system relief assist on valves without valves which could recent setpoint history.
cause rapid cooldowns/
other FW heater shell rel ief s.
- d. Determine appropriate R. Lawrence LT To be done as part of PM periodic test program program upgrade.
(i.e., either PM or SP Program) and implement same for all secondary relief valves.
- e. Resolve report of MSR J. Field SU Completed NA Resolved that MSR Reliefs Reliefs lifting after did not lift.
Rx/ Turbine trip.
- f. Establish criteria for V. Lewis LT process setpoint -
determination.
- g. Review plant for proper V. Lewis LT application of criteria.
- h. Add setpoints for R. Colombo LT AP.152 FSL-32243, 32244, and 32453 to Process Standa rds.
L- .-_.,_ _ ._._. . . . _
LEGEND: SU = Startup R; quired LT = Leng Term STATUS DATE 10-18-85 PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
VI "A" Main Feedwater Pump seal water and controls
- a. Repair linkage on N. Brock SU Completed 104965 Completed "immediate" controller. repairs 10/02/85.
Completed 105378 Proper pin installed.
- b. Check common mode N. Brock LT Reviewing NA Looking for common mode failure possibility on relations to VI a.
controller linkage.
VII Main Feed Pump Trip Event
- a. Perform test to duplicate J. Field SU Written NA Deferred pending results of low vacuum condition. Other investigations.
- b. Install monitoring N. Brock SU Planning NA See X.a.
instrumentation.
- c. Verify "as built" wiring C. Linkhart SU Completed 102722 Plant drawings accurately of "A" FWP trip circuits. show "as built" configuration.
- d. Check setpoints of trip N. Brock PE Hold 102716, 102721 Requires WR 102716 to be devices. 102718, 103272 closed out.
102720, 103273 u _ _ _ _ _ _
LEGEND: SU = Startup R2quir:d LT = Lcng Tcrm STATUS DATE 10-18-85 -
PE = Power Escalation DCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST.-
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
VII e. Compile history of FW N. Brock ST Completed NA pump control problems.
- f. Check end play on main R. Lawrence SU Completed 102719 Acceptable.
shaft of "A" MFW Pump.
- g. Obtain L0 sample from R. Lawrence SU Completed 103269, 102719 Normal.
"A" and "B" MFW Pump and have analysis performed.
- h. Verify "as built" wiring C. Linkhart SU Completed 105686 Acceptable; elementaries of "B" FWP trip circuits. are correct. S-5119 written.
- i. Install Trip Circuit C. Linkhart LT Preparing Requires pump out of
, Alarm Lights. ECNs service.
VIII Main Condenser Loss of Vacuum Event
- a. Update drawings to R. Lawrence SU Completed R-0177 reflect "as built" conditions of MSR relief sealing steam.
- b. Revise procedure (s) to B. Spencer SU Completed NA Temporary change to show MSR relief sealing Operating Procedure A.49 steam valves, written.
L
LEGEND: SU = Startup R:quirzd LT = Lcng Tcrm STATUS DATE 10-18-85 -
PE = Power Escalation DCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
VIII c. Determine whether B. Spencer SU Completed NA Temporary change to sealing steam procedures Operating Procedure A.49 are adequate and usable. written.
- d. Review / analyze perform- J. Field LT Holding NA Long term item.
ance of the gland steam condenser.
- e. Investigate when/why MSR B. Spencer SU Completed NA Investigation unable to sealing steam valve was to ascertain when/why closed. valve was closed.
- f. Determine whether MSR R. Lawrence LT Complete NA Review shows adequate Relief Sealing Steam for restart.
System works as designed. .
- g. Initiate WR for rework R. Lawrence LT Schedule 104113 Next refueling.
of leaking MSR relief valve.
- h. Resolve setpoint error S. Carmichael SU Work 105116 of main turbine low vacuum trip.
- 1. Correct / upgrade docu- R. Lawrence LT mentation for maintenance on turbine trip block.
L
t LEGEND: SU = Startup R quired LT = Lcng Tcrm STATUS DATE 10-18-85 -
PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
VIII j. Include placement / B. Spencer SU In Progress removal of MSR relief valve covers in procedures,
- k. Fabricate new MSR relief R. Lawrence ST Being Designed valve covers.
- 1. Include main turbine R. Colombo ST trip setpoints in Process Standards.
- m. Develop design improve- V. Lewis LT ment to reduce leakage of MSR relief valves.
IX Condensate /FW Oscillation J. Field SU Completed NA Input to Event Report.
X ICS Tuning
- a. Prepare ICS/Feedpump N. Brock PE In STP to PRC 10/18/85.
tuning STP. Preparation
- b. Perform tuning as plant N. Brock PE Engineering conditions permit. Required
- c. aTc Control N. Brock LT Engineering L
LEGEND: SU = Startup R:quir:d LT = Lcng Tcrm STATUS DATE 10-18-85 -
PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
XI Valve Identification Program
- a. Develop list of selected B. Spencer SU Completed To include Operating systems for Operations ,
Procedures A.37, walkdown. A.49,A.41, A.42, A.50, A.46, A.34, A.38, A.40, A.51, A.47, A.28, A.39, A.53, A.6. ___.
- b. Operations crew to walk B. ' Spencer SU Completed down systems to identify valves not on prints.
- c. Prepare NCRs on findings B. Spencer SU In Progress NCRs written. Temporary and revise procedures as changes to procedures to be necessa ry. completed 10/18.
- d. Update drawings and B. Spencer LT In Progress DCNs to be generated.
place ids on valves.
- e. QA Surveillance H. Canter SU Completed No's. 492, 488 XII "B" Feedwater Line Leak R. Lawrence SU Completed 104548, 104564 Report addressing the Reactor Building. 104560, 104572 cause and the repair done.
102095, 104569 Material meets applicable 104567, S-5090 code.
S-5111 L
i LEGEND: SU = Startup R: quired LT = Lcng Term STATUS DATE 10-18-85 -
PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
XIII P-319 Bearing Failure
- a. Pump Repair R. Lawrence SU Completed SP run and passed on 10/10/85.
- b. Maintenance History R. Lawrence SU Completed Surveillance History and Cause of Failure / Post Repair Test Corrective Action
- c. QA Surveillance J. Jewett SU Completed No. 485
- d. Provide oiling B. Rausch SU Completed TS 85-1033 To include safety related instructions pumps. How to determine level . How to maintain oil level . Pump specific instructions.
- e. Past practice on LO B. Spencer SU In Progress Level.
- f. Investigate whether R. Lawrence SU Completed
" Normal" level was changed.
- g. 48-Hour Endurance Run J. Field SU 48 Hr. Run Awaiting performance of SP.
Completed 4
. h. Identify all safety R. Lawrence SU Completed NA related pumps which utilize slinger rings.
L
r LEGEND: SU = Startup Required LT = Lcng Tcrm STATUS DATE 10-18-85 -
PE = Power Escalation DCTOBER 2, 1985 TRANSIENT TIME 1600 NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
XIII 1. Oil level indication for V. Lewis SU Completed Determine proper P-318, 319 configuration.
J. Root Cause S. Crunk SU Completed- Included as subsection of Item II.
- k. Inspect rings in pumps R. Lawrence SU In Progress which have been previously disassembled.
XIV Loss of Aux Steam Event
- a. Prepare Report M. Nickerson .:0 Completed TS 85-1021
- b. Root Cause S. Crunk LT To be NA RC 85-021 Completed .
11/30/85
- c. Investigate Aux Boiler C. Linkhart SU Completed NA Power Supply.
- d. I and C analysis of N. Brock LT To be XIV c. Completed 11/15/85 L
LEGEND: SU o Startup Requir:d LT = Leng Tcra STATUS DATE 10-18-85 -
PE = Power Escalation DCTOBER 2, 1985 TRANSIENT TIME 1600 ,
NA = Not Applicable ST = Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
XV Training
- a. Lessons Learned F. Thompson LT Reviewing NA
- b. Training on Item III.b B. Spencer SU Completed NA SO 20-85 (Instructions /
Recommendation)
- c. Training on pumps / motor M. Hieronimus SU In Progress NA oiling
~
XVI Procedure Adequacy 1
- a. E0Ps D. Comstock SU In Progress NA
- b. Normal Procedures D. Comstock LT In Progress NA
- c. Identify operator actions M. Hieronimus LT Active NA Requires input / feedback
, not specifically Program from A0's, EA's, etc.
addressed in procedures. Memo to SS of 10-10-85
" Problem Feedback Report."
- d. Monitor operation D. Comstock PE Prepared NA QA surveillance planned.
procedures during SU. Validation of procedures will be performed.
I~
- e. Evaluate operator D. Comstock SU Completed NA performance during the
- trip.
t
1
-LEGEND: SU = Startup Required LT = Lcng Term STATUS DATE 10-18-85
- PE = Power Escalation OCTOBER 2, 1985 TRANSIENT TIME 1500 NA = Not Applicable ST - Short Term - ACTION LIST -
DESCRIPTION RESPONSIBILITY SCHEDULE STATUS WR No./NCR/ COMMENTS ETC.
XVII Health Physics / Emergency Plan
- a. Health Physics aspects. F. Kellie SU Completed FWK 85-202 No Health Physics impact.
- b. Emergency ~ Plan B. Spencer SU Completed NA Emergency Plan did not utilization. M. Heironimus require activation.
to B. Spencer memo XVIII RCS Overcooling
- a. Tech Spec Review R. Colombo SU Completed NA
- b. B and W Evaluation J. Field SU Completed NA B and W letter, SMUD-85-222, dated Oct. 4, 1985, " Structural Integrity of Pressure Boundary Components are Suitable for Continued Power Operation.
XIX Preventive Maintenance Program for Non-safety Related Equipment
- a. Description of existing R. Lawrence SU Completed NA N. Brock'and C. Linkhart program. to provide IC/ Elect input.
- b. Planned improvements. R. Lawrence LT Requires NA N. Brock and C. Linkhart 11/30/85 to provide IC/ Elect input.
response to NRC.
l