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Results
Other: 05000312/LER-1985-019, :on 851002,reactor Trip Occurred & RCS Temp Decreased to Approx 70 F.Caused by Excessive Steam Loads Due to Two Open Relief Valves on Feedwater Heater 4A.HPI Flow Manually Initiated to Maintain Pressure, 05000312/LER-1985-023, :on 851205,reactor Trip Occurred on High RCS Pressure.Caused by Underfeeding of Main Feedwater Sys During Flow Scaling Procedure.Integrated Control Sys Modules Examined & Refurbished, ML20134A837, ML20137H936, ML20138B213, ML20138R097, ML20138R929
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MONTHYEARML20138B2131985-10-0404 October 1985 Confirmatory Action Ltr Re 851004 Telcon Concerning Return of Facility to Power Operations After 851002 Reactor Trip. Util Must First Conduct Root Cause Analysis of Trip & Provide Briefing to NRC Before Return to Power Project stage: Other ML20133K5131985-10-11011 October 1985 Notification of Significant Meeting on 851016 W/Util Onsite to Discuss Root Cause Assessment & Readiness for Resumption of Power Operations Following 851002 Reactor Trip Project stage: Meeting ML20133K5891985-10-14014 October 1985 Forwards Action List Providing Util Plan to Resolve Concerns Stemming from 851002 Transient,Per 851010-11 Meetings.Listed Commitments Scheduled for Completion Prior to Restart. Schedule for long-term Items Will Be Submitted by 851118 Project stage: Meeting ML20133K7191985-10-18018 October 1985 Forwards Supplemental Info Re 851002 Transient,Per NRC Request During 851016 Meeting.Info Includes Main Feed Pump Trip Determination,Hpi a Flow Anomaly,Cooldown of RCS, Cooldown Rate,Tech Specs & Revised Action List Project stage: Supplement ML20133P8511985-10-25025 October 1985 Forwards Summary & Supplemental Info Re 851002 Transient, Per 851025 Telcon.Items in Plan Include pre- & post-startup Actions to Determine Root Cause of Event & Initiation of Corrective Programs Project stage: Supplement 05000312/LER-1985-019, :on 851002,reactor Trip Occurred & RCS Temp Decreased to Approx 70 F.Caused by Excessive Steam Loads Due to Two Open Relief Valves on Feedwater Heater 4A.HPI Flow Manually Initiated to Maintain Pressure1985-10-29029 October 1985
- on 851002,reactor Trip Occurred & RCS Temp Decreased to Approx 70 F.Caused by Excessive Steam Loads Due to Two Open Relief Valves on Feedwater Heater 4A.HPI Flow Manually Initiated to Maintain Pressure
Project stage: Other ML20134A8371985-11-0101 November 1985 Forwards Addendum to Attachment 5,Part Ii,Rev 1 to Auxiliary Feedwater/Main Feedwater Failure Analysis Contained in Project stage: Other ML20138R0971985-11-13013 November 1985 Forwards Rev 2 to Attachment 2 & Addendum NRC-5150 Re HPI a Flow Anomoly,Rev 1 to Attachment 5,Parts I & II Re Auxiliary Feedwater/Main Feedwater Failure Analysis & Attachment 8 Re Oil Levels on safety-related Pumps Project stage: Other ML20138R9291985-11-15015 November 1985 Forwards Latest Rev to Action List,Describing Program Plan to Resolve Concerns Stemming from 851002 Transient.All Startup Required Items Completed.All Power Escalation Items Will Be Completed by Full Power Operation Project stage: Other ML20137H9361985-12-23023 December 1985 Responds to Violations Noted in Insp Rept 50-312/85-30. Corrective Actions:Instrumentation & Control Procedure I.103 Revised to Include Multiplier Link Change Instructions & Pegging Steam Pressure Controller Setpoints Reduced Project stage: Other 05000312/LER-1985-023, :on 851205,reactor Trip Occurred on High RCS Pressure.Caused by Underfeeding of Main Feedwater Sys During Flow Scaling Procedure.Integrated Control Sys Modules Examined & Refurbished1986-01-0202 January 1986
- on 851205,reactor Trip Occurred on High RCS Pressure.Caused by Underfeeding of Main Feedwater Sys During Flow Scaling Procedure.Integrated Control Sys Modules Examined & Refurbished
Project stage: Other 1985-10-04
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION a
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1450 MARIA LANE, SUITE 210 p
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,o WALNUT CREEK, CALIFORNI A 94596
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October 11, 1985 NOTICE OF SIGNIFICANT MEETING l
Name of Licensee:
Sacramento Municipal Utility District Name of Facility:
Rancho Seco Docket No. :
~50-312 Date and Time of Meeting: October 16, 1985, 9:30 am*
Location of Meeting: Rancho Seco Site, Herald, California
Conference to discuss the root.cause assessment and readiness for resumption of power operations fcilowing the reactor trip which occurred on October 2, 1985.
NRC Attendees:
J. B. Martin, Regional Administrator D. F. Kirsch, Acting Director, Division of Reactor Safety and Projects A. E. Chaffee, Chief, Reactor Projects Branch L. F. Miller, Jr., Chief, Reactor ProjectsSection II F. J. Miraglia, Jr., Deputy Director, Division of Licensing, NRR R. H. Vollmer, Deputy Director, IE Licensee Attendees: D. K. K. Lowe, General Manager R. J. Rodriguez, Assistant General Manager, Nuclear Other SMUD Staff NOTE: Attendance at this meeting by NRC personnel other than those listed above should be made known by October 15, 1985, 12:00 noon via a telephone call to L. F. Miller, FTS 463-3869.
- Tentative, subject to change Distribution:
DEDROGR, V. Stello Director, IE - J. M. Taylor Director, Inspection Programs, IE - J. G. Partlow Director, Div. of Emergency Preparedness and Eng. Response, IE - E. L. Jordan Director, Division of Quality Assurance, Vendor and Technical Training Center Programs - B. K. Grimes Director, Erforcement Staff, IE - J. A. Axelrad Director and Chief Counsel, Regional Operations and Enf., ELD - J. Lieberman Director, Division. of Licensing, NRR - H. Thompson Chief, Licensing Reactor Branch 3 Division of Licensing, NRR, G. Knighton 8510220000 851011 PDR ADOCK 05000312 PDR S
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