:on 850605,personnel Overexposure Occurred. Calculations Indicate Dose of 10.6 Rems to Skin & 0.03 Rem to Whole Body.Control & Disposal of Protective Clothing Revised to Prevent Recurrence of Incident| ML20133J034 |
| Person / Time |
|---|
| Site: |
McGuire  |
|---|
| Issue date: |
08/02/1985 |
|---|
| From: |
Day J DUKE POWER CO. |
|---|
| To: |
|
|---|
| Shared Package |
|---|
| ML20133J026 |
List: |
|---|
| References |
|---|
| LER-85-021, LER-85-21, NUDOCS 8508090626 |
| Download: ML20133J034 (4) |
|
text
.
NRC Form 300 U.S. NUCLE 173 KELULAT@2V COMM13SICN 3 838 APPROVED OMS NO 3160 4 104
~
LICENSEE EVENT REPORT (LER)
F ACILITY NAME til DOCKET NUMSER (2)
PAGE (3i McGuire Nuclear Station - Unit 1 0[510tol0l l l 1 lOFl0 l4 flTLE tel Personnel Exposure EVENT DATE (Si LER NUMBER tel REPORT DATE 471 OTHER F ACILiTIEs INVOLVED 16)
MONTH DAY YEAR V5AR N(
[v
'O A
e 0 15101010 1 1 I 0l6 0l 5 8 5 8l5 0l2l1
~
0l 1 0l8 0l2 8l 5 eistogoici l l Twis REPORT is sueuiTTED PURSUANT TO THE REOUiREuf NTs Or to Crm 6 renece one er me,e e raee."...a,> iill r
o,,,,,,,,,
"oo' ai 6
2a.0mi 2a.06 ci la73i.H2H )
73.7 mi POVWE R 20 4061eH1H4 60 38(cH11 60 73seH2Het 73 71tel LEVEL O i 00 2a.06i.mm So mcH2)
So 73ieH2H.i.i X
i gnEgspugajg Iio 20 406 sil1Huel 60.734eH2Hd 60 73teH2HemH Al 366Al 20 406'sMilliol 60 73EeH2Hul 60.73teH2HvanHBI 20 406(eH1Het 60 73ieH2Hml 60.73isH2 Hat LICENSEE CONTACT FOR TMis LE R (121 NAME TELf PMONE NUMBER ARE A CODE Jerry Day - Licensing 7 0 l4 3 7 i 3l t 7 l0 l3 l3 i
COMPLETE ONE LINE FOR E ACM COMPONENT F AILURE DESCRISED IN THit REPORT (131 m
VA C
AEP C
REPORTA LE
CAUSE
SYSTEY COMPONENT S'
CAUSE
SY ST E M COMPON E NT 7
yO NPR yg pp g l
i I I I I I I
I I I I I I I
I I I I I I I
I I I I I I SUPPLEMENTAL REPORT E XPECTED 114+
MONTM DAY vfAR SL 6 mis $rON 4ES III mes como are EXPECTEQ Sv0ws$10N DA TE!
NO l
l l
J.".$YR ACT (Lem.t to 74Jo speces a e. sooro=>eere y rdreen snap e space ryoe.,,trea I,aes/ (16' On June 5, 1985, a radioactive particle was discovered under the upper left arm of a technician involved in steam generator tube plugging who was exiting containment.
The particle was removed and later analyzed.
Initial dose calculations indicated a dose of 10.6 Rem to the skin and 0.030 Rem to the whole body, which represents an overexposure to the skin for the quarter pursuant to 10 CFR 20.101a. A review of methodology and assumptions of tne initial dose calculation has resulted in revised dose calculations which yield lower values for the dose which do not represent an overexposure.
The control and disposal of all protective clothing has been revised to prevent this type of incident from reoccurring.
The original calculation was based upon conservative methodology and assumptions about the exposure. The revised calculation is based upon more realistic assumptions. The health of the technician and the safety of the plant were unaffected by this incident.
8508090626 850802 i$%n PDR ADOCK 05000369
PDR uc e. 6 (9 8 D
r i
NXC Form 364A U S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION apeRO <EO oms NO 3 iso-oio4 EXPIRES 8/3185 FJ.CILtTV NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
- "iVS v5'a McGuire Nuclear Station -Unit 1 o[5l0l0l0l3l6l9 8l 5 0l2l1 0l1 0l 2 OF 0l4 TEXT W more space a requered, use edderwrut NRC form 366Ksl(17)
On June 5,1985 at 2200, a radioactive particle was discovered under the upper left arm of a technician who had been assisting in the plugging of a steam generator tube and had partially entered (head and arms) the steam generator.
The particle was removed and analyzed. The particle was found to have 1.219 micro Curies of Cobalt-60. On June 10, 1985, the dose was calculated to be 10.6 Rem to the skin and 0.030 Rem to the whole body. This is the dose at 7 mg/cm(2) skin depth averaged over 1 cm(2) and assumes contact with the skin for the two full hours of use of the protective clothing.
Subsequently, the dose was recalculated for more realistic assumptions, and as being delivered averaged over the dermal layer, as well as at 7 mg/cm(2).
Changing any single parameter to a more realistic value (time, exposure depth, or movement) yields a value that is not an overexposure.
Below are the results of several calculations using more realistic assumptions:
Time Skin Area Skin Depth Dose (hrs) cm (2) mg/cm(2)
Rem Literal worst case 2
1 at 7 10.6 4-125 mg/cm(2) 2 1
4-125 1.9 4-40 mg/cm(2) 2 1
4-40 5.3 Statistically likely 1
1 at 7 5.3 Most likely transfer
.5 1
at 7 2.65 1 cm movement of particle on skin 2
2 at 7 5.3 Proposed 10 CFR 20 2
10 at 7 1.06 Calculating the dose at 7 mg/cm(2) is at a thin slice location and represents a two dimensional calculation.
It is more realistic to calculate dose over a volume (three dimensional).
The time of exposure is also in question. Two hours is the maximum possible time of exposure. This conservatively assumes the particle was in the protective clothing, transferred immediately when the technician put on the protective clothing, and did not move once transferred. Since no particle motion was assumed, the dose was calculated over one square centimeter; minimal particle motion (one centimeter) would have distributed the dose as not to involve an overexposure.
Based on the above results, Duke Power concludes that no overexposure occurred.
NRC FORV 344A
1 NRC Form 364A U S. NUCLEGR REGULOTOQV COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVED OMB NO 3150-0104 EXPIRES 8711 @5 FACILITU NAME (Il DOCKET NUMBER (21 LER NUMBER 163 PAGE13)
"$0p.
,'7#J u*a McGuire Nuclear Station - Unit 1 ol5j0l0l0l3l6l9 8l5 0l2l1 0l1 0l3 OF 0l4 1EKT In more spece a reeuwed, use eda;tenalNRC form 366Ks)(17)
.Beginning in April, 1985 personnel contaminations occurred as a result of micro-scopic particles containing only Cobalt-60. At this time an investigation was started to determine the source of the Cobalt-60. The following possibilities were evaluated:
1.
All pure Cobalt-60 sources on site were lead tested but no sources were found to be leaking.
2.
All new steel on site used in construction was surveyed but no contaminated material was found.
3.
Detailed grid surveys of the plant were performed. No activity was above background.
4.
Surveys using maslin cloth (oil cloth) were performed. All activity was below background.
It is believed that the Cobalt-60 is coming from activated stellite in the Reactor Coolant System. Due to leakage or maintenance on primary system components the activated stellite (Cobalt 60) is picked up on the protective clothing. During laundering of protective clothing most contamination is removed. However, the Cobalt-60 particles are insoluble and can be suspended in the wash water and then redeposited on the protective clothing.
Corrective Action
The following corrective actions were initiated after the original personnel contaminations:
Extensive frisking (80 man-hours per day) of all protective clothing.
Disposal of all cloth coveralls and hoods. New coveralls and hoods purchased. Prior to mass disposal only protective clothing used in high contamination jobs had been disposed of as radwaste.
Increased the number of personnel frisking stations within the plant.
Frisking the inside of protective clothing by purchasing special (yellow) coveralls to be worn in very high contamination and high temperature areas.
More use of plastic and disposable protective clothing where possible.
Requisition of an automatic laundry monitor to eliminate technician error.
The individual was removed from furhter activities involving radiation exposure for the remainder of the quarther. The incidnet has been reviewed with appropriate personnel at other Duke stations.
NmC FORM 366A E9 03)
r NRC Form 364A U.S NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AerRovEo ous NO 3 iso-oio4 E X PIR E S 8,11 '85 F#.CILITY NAME (1)
DOCKET NUM8ER (2)
LER NUMBER (6)
PAGE (3)
"$Q,P
-,17Jf30 v<^a McGuire Nuclear Station 0 l5 l0 l0 l0 l3 l6 l 9 81 5 0l2l1 011 Ol4 OF g l4 TEKT IM more space os requeed, use ed&hono!NRC Form 366A's) l17)
Safety Analysis
The exposure had no effect on any safety related system and the health and safety of the public were not affected.
The exposure of the technician was calculated with realistic assumptions and did not involve an overexposure. The health of the tecnician was not affected by this event.
i NRC FORv Josa IS 833
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000369/LER-1985-001, :on 841229,daily Health Physics Surveillance of Waste Gas Decay Tank Not Completed within 24 H Interval. Caused by Personnel Error.Use of Duties Checklist Required & Documentation of Duties Will Be Reviewed |
- on 841229,daily Health Physics Surveillance of Waste Gas Decay Tank Not Completed within 24 H Interval. Caused by Personnel Error.Use of Duties Checklist Required & Documentation of Duties Will Be Reviewed
| 10 CFR 50.73(a)(2)(1) | | 05000369/LER-1985-002-01, :on 850113,required Quarterly Surveillance Not Performed within Allowable Interval.Caused by Personnel Error.Fuel Oil Transfer Pump Performance Test for Each Diesel Will Be Added to Computer Listing |
- on 850113,required Quarterly Surveillance Not Performed within Allowable Interval.Caused by Personnel Error.Fuel Oil Transfer Pump Performance Test for Each Diesel Will Be Added to Computer Listing
| 10 CFR 50.73(a)(2)(i) | | 05000369/LER-1985-003-01, :on 850120,erroneous Signals to Reactor Protection Sys Created Likelihood of Spurious Trip.Caused by Freezing Temps in Area.On 850121,jumper Installed on Bistable Circuit to Thaw Instruments |
- on 850120,erroneous Signals to Reactor Protection Sys Created Likelihood of Spurious Trip.Caused by Freezing Temps in Area.On 850121,jumper Installed on Bistable Circuit to Thaw Instruments
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000369/LER-1985-003, Advises of Delay of Commitment in LER 85-003 to Reroute Instrument Impulse Lines & to Heat Trace & Insulate by Dec 1985,due to Design & Matl Lead Times.Implementation of Mods Delayed Until 1986 Outage | Advises of Delay of Commitment in LER 85-003 to Reroute Instrument Impulse Lines & to Heat Trace & Insulate by Dec 1985,due to Design & Matl Lead Times.Implementation of Mods Delayed Until 1986 Outage | | | 05000369/LER-1985-004-01, :on 850128,reactor Tripped on lo-lo Steam Generator Level When Main Feedwater Pump Tripped on Low Suction Pressure Signal.Caused by Failure of Pneumatic Pressure Transmitter.Components Replaced |
- on 850128,reactor Tripped on lo-lo Steam Generator Level When Main Feedwater Pump Tripped on Low Suction Pressure Signal.Caused by Failure of Pneumatic Pressure Transmitter.Components Replaced
| | | 05000369/LER-1985-005-01, :on 850201,determined Plant Outside Design Analyses Assumptions,Based on Westinghouse Response Re Negative Flux Rate Trip Setpoint.Bistable Setpoint Reduced to 2.5% Rated Thermal Power |
- on 850201,determined Plant Outside Design Analyses Assumptions,Based on Westinghouse Response Re Negative Flux Rate Trip Setpoint.Bistable Setpoint Reduced to 2.5% Rated Thermal Power
| 10 CFR 50.73(a)(2) | | 05000369/LER-1985-006-01, :on 850205,reactor Tripped on High Negative Flux Rate Signal.Cause unknown.Post-trip Review Performed & Electronic Recorders Used to Monitor Possible Spikes |
- on 850205,reactor Tripped on High Negative Flux Rate Signal.Cause unknown.Post-trip Review Performed & Electronic Recorders Used to Monitor Possible Spikes
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000369/LER-1985-007-03, :on 850205,two ESF Actuations Occurred During Work on Reactor Protection & Nuclear Instrumentation Sys Channels.Caused by Procedures Allowing Simultaneous Sys Work.Procedures Revised |
- on 850205,two ESF Actuations Occurred During Work on Reactor Protection & Nuclear Instrumentation Sys Channels.Caused by Procedures Allowing Simultaneous Sys Work.Procedures Revised
| 10 CFR 50.73(a)(1), Submit an LER 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000369/LER-1985-008-01, :on 850206,discovered That Reactor Trip Switchgear Wiring Did Not Satisfy Separation Criteria for safety-related Circuits.Caused by Administrative/Procedural Deficiency.Procedures Revised |
- on 850206,discovered That Reactor Trip Switchgear Wiring Did Not Satisfy Separation Criteria for safety-related Circuits.Caused by Administrative/Procedural Deficiency.Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000369/LER-1985-009-01, :on 850219,estmated 1 Cubic Ft of Contaminated Spent Resin Released from Vent.Resin Discovered on 850220 on Roof of Auxiliary Bldg & Other Bldgs.Caused by Personnel Error |
- on 850219,estmated 1 Cubic Ft of Contaminated Spent Resin Released from Vent.Resin Discovered on 850220 on Roof of Auxiliary Bldg & Other Bldgs.Caused by Personnel Error
| | | 05000369/LER-1985-010-01, :on 850320,keyswitch for Door on Reactor Side of Containment Personnel Airlock in Bypass Position.Caused by Procedural Deficiency.Procedures Will Be Changed to Ensure Switches Returned to Active Position |
- on 850320,keyswitch for Door on Reactor Side of Containment Personnel Airlock in Bypass Position.Caused by Procedural Deficiency.Procedures Will Be Changed to Ensure Switches Returned to Active Position
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000369/LER-1985-011-01, :on 850409,samples Taken from Cold Leg Accumulator a Prior to Unit Shutdown Revealed Low Boron Concentration.Caused by Component Failure.Boron Concentration Returned to within Specs |
- on 850409,samples Taken from Cold Leg Accumulator a Prior to Unit Shutdown Revealed Low Boron Concentration.Caused by Component Failure.Boron Concentration Returned to within Specs
| 10 CFR 50.73(a)(2)(1) | | 05000369/LER-1985-012-01, :from 850214-0425,fire Doors Normally Locked Closed Were Unlocked & Not Verified Closed Daily Nor Was Fire Watch Posted.Caused by Administrative/Procedural Deficiency.Required Surveillance Implemented |
- from 850214-0425,fire Doors Normally Locked Closed Were Unlocked & Not Verified Closed Daily Nor Was Fire Watch Posted.Caused by Administrative/Procedural Deficiency.Required Surveillance Implemented
| | | 05000369/LER-1985-013-01, :on 850502,during Refueling,Gearcase Lubricating Grease Found in Electrical Compartments of Limitorque Motor Operated Valve Actuators 1VX-1A & 1VX-2B. Caused by Error During Previous Maint Work |
- on 850502,during Refueling,Gearcase Lubricating Grease Found in Electrical Compartments of Limitorque Motor Operated Valve Actuators 1VX-1A & 1VX-2B. Caused by Error During Previous Maint Work
| | | 05000369/LER-1985-014-01, :on 850507,core Alterations Started W/O Completion of Required Surveillance on Source Range Neutron Flux Monitors While in Mode 6.Caused by Administrative/ Procedural Deficiency.New Procedure Planned |
- on 850507,core Alterations Started W/O Completion of Required Surveillance on Source Range Neutron Flux Monitors While in Mode 6.Caused by Administrative/ Procedural Deficiency.New Procedure Planned
| | | 05000369/LER-1985-015-02, :on 850508,auxiliary & Reactor Bldg Side Door Lower Airlock Seals Deflated,Causing Loss of Containment Integrity.Caused by Maladjustment of Airlock Door Pin Limit Switches Combined W/Design Deficiency |
- on 850508,auxiliary & Reactor Bldg Side Door Lower Airlock Seals Deflated,Causing Loss of Containment Integrity.Caused by Maladjustment of Airlock Door Pin Limit Switches Combined W/Design Deficiency
| | | 05000369/LER-1985-016-01, :on 850508,discovered That Temp Compensation Chart Not Incorporated in Hydrogen Analyzer Operation Emergency Procedure.Caused by Procedural Deficiency.Temp Compensation Charts Incorporated in Procedure |
- on 850508,discovered That Temp Compensation Chart Not Incorporated in Hydrogen Analyzer Operation Emergency Procedure.Caused by Procedural Deficiency.Temp Compensation Charts Incorporated in Procedure
| | | 05000369/LER-1985-017-01, :on 850515,diesel Generator 1A Experienced Invalid Automatic Start Due to Unit Blackout Signal.Caused by Electrical Disturbance to Power Transmission Sys During Severe Storm & Listed Design Deficiency |
- on 850515,diesel Generator 1A Experienced Invalid Automatic Start Due to Unit Blackout Signal.Caused by Electrical Disturbance to Power Transmission Sys During Severe Storm & Listed Design Deficiency
| | | 05000369/LER-1985-018-01, :on 850525,valve 1RV-429 in Containment Ventilation Cooling Water Sys Outside Containment Found Open,Allowing Flow Path Between Auxiliary Bldg & Upper Containment Through Inside Containment Valve |
- on 850525,valve 1RV-429 in Containment Ventilation Cooling Water Sys Outside Containment Found Open,Allowing Flow Path Between Auxiliary Bldg & Upper Containment Through Inside Containment Valve
| | | 05000369/LER-1985-019-01, :on 850530,cable Transits Penetrating Units 1 & 2 Reactor Bldg Walls Discovered to Be Fire Barriers.Caused by Oversight During Development of Fire Barrier Insp Procedure.Procedures Revised |
- on 850530,cable Transits Penetrating Units 1 & 2 Reactor Bldg Walls Discovered to Be Fire Barriers.Caused by Oversight During Development of Fire Barrier Insp Procedure.Procedures Revised
| | | 05000369/LER-1985-020-01, :on 850607,diesel Generator 1B Experienced Two Invalid Automatic Starts.Caused by Power Distribution Sys Disturbances Due to Severe Weather.Start Sys Will Be Modified |
- on 850607,diesel Generator 1B Experienced Two Invalid Automatic Starts.Caused by Power Distribution Sys Disturbances Due to Severe Weather.Start Sys Will Be Modified
| | | 05000369/LER-1985-021, :on 850605,personnel Overexposure Occurred. Calculations Indicate Dose of 10.6 Rems to Skin & 0.03 Rem to Whole Body.Control & Disposal of Protective Clothing Revised to Prevent Recurrence of Incident |
- on 850605,personnel Overexposure Occurred. Calculations Indicate Dose of 10.6 Rems to Skin & 0.03 Rem to Whole Body.Control & Disposal of Protective Clothing Revised to Prevent Recurrence of Incident
| | | 05000369/LER-1985-021-01, Forwards LER 85-021-01 Re Personnel Exposure,Initially Determined to Be Overexposure.Revised Calculation Indicates No Overexposure Occurred | Forwards LER 85-021-01 Re Personnel Exposure,Initially Determined to Be Overexposure.Revised Calculation Indicates No Overexposure Occurred | | | 05000369/LER-1985-022-01, :on 850623,unplanned ESF Actuation Occurred on Loss of Both Main Feed Pumps Signal.Caused by Voltage Transient When Trend Chart Recorder Reinserted.Recorder Will Be Replaced |
- on 850623,unplanned ESF Actuation Occurred on Loss of Both Main Feed Pumps Signal.Caused by Voltage Transient When Trend Chart Recorder Reinserted.Recorder Will Be Replaced
| | | 05000369/LER-1985-023-01, :on 850703,violation of Electrical Channel Separation Requirements by Temporary Cable Routing Discovered.Caused by Administrative/Procedural Deficiency. Cable Removed from Blue Channel Cable Tray |
- on 850703,violation of Electrical Channel Separation Requirements by Temporary Cable Routing Discovered.Caused by Administrative/Procedural Deficiency. Cable Removed from Blue Channel Cable Tray
| | | 05000369/LER-1985-024-01, :on 850723,determined That Operability Test Not Performed on Station Standby Battery Charger.On 850813, Found That Standby Charger Placed in Svc Twice Supplying Vital Loads on Channels 2 & 4 |
- on 850723,determined That Operability Test Not Performed on Station Standby Battery Charger.On 850813, Found That Standby Charger Placed in Svc Twice Supplying Vital Loads on Channels 2 & 4
| | | 05000369/LER-1985-025-01, :on 850909,train Chillers & Air Handling Unit for Control Ventilation Area Sys Tripped.Caused by Design Deficiency Allowing Both Chillers to Become Inoperable Due to Blown Fuse.Fuse Replaced.Wiring Reviewed |
- on 850909,train Chillers & Air Handling Unit for Control Ventilation Area Sys Tripped.Caused by Design Deficiency Allowing Both Chillers to Become Inoperable Due to Blown Fuse.Fuse Replaced.Wiring Reviewed
| | | 05000369/LER-1985-026-01, :on 850911,vendor-employed Minor Exposed in Excess of Quarterly Dose Limit of 125 Mrem.Caused by Individual Misrepresenting Age to Work in Radiation Control Area.Birth Dates Will Be Verified |
- on 850911,vendor-employed Minor Exposed in Excess of Quarterly Dose Limit of 125 Mrem.Caused by Individual Misrepresenting Age to Work in Radiation Control Area.Birth Dates Will Be Verified
| | | 05000369/LER-1985-027-01, :on 850911,pressurizer Heater Group 1B Inoperable While Diesel Generator 1A Inoperable.Caused by Personnel Error.Generator Returned to Operable.Rept Will Be Reviewed W/Personnel |
- on 850911,pressurizer Heater Group 1B Inoperable While Diesel Generator 1A Inoperable.Caused by Personnel Error.Generator Returned to Operable.Rept Will Be Reviewed W/Personnel
| | | 05000369/LER-1985-028-01, :on 850919,environmentally Sealed Valcor Model 526 Inside Containment Valve Failed.Caused by Ruptured Seal as Result of Improper Installation.Four Valves Resealed & Returned to Svc.New Design Being Studied |
- on 850919,environmentally Sealed Valcor Model 526 Inside Containment Valve Failed.Caused by Ruptured Seal as Result of Improper Installation.Four Valves Resealed & Returned to Svc.New Design Being Studied
| | | 05000369/LER-1985-029-01, :on 851001,Westinghouse Notified Util That Reanalysis of Peak Containment Pressure Calculation Resulted in Greater Value than Internal Pressure of 15 Psig.Emergency Procedure for Nd Spray Initiation Revised |
- on 851001,Westinghouse Notified Util That Reanalysis of Peak Containment Pressure Calculation Resulted in Greater Value than Internal Pressure of 15 Psig.Emergency Procedure for Nd Spray Initiation Revised
| 10 CFR 50.73(a)(2)(vi) | | 05000369/LER-1985-030-01, :on 851009,valve 1RN-33 Found in Locked Closed Position Instead of Locked Open Due to Reversed Local Valve Position Indicator.Cause Unknown.Valve Opened & Properly Labeled |
- on 851009,valve 1RN-33 Found in Locked Closed Position Instead of Locked Open Due to Reversed Local Valve Position Indicator.Cause Unknown.Valve Opened & Properly Labeled
| | | 05000369/LER-1985-031-01, :on 851017,Train B Chiller for Control Area Ventilation/Chilled Water Sys Tripped on Low Yc Flow While Train B Sys Inoperable.Cause Could Not Be Determined. Pressure Switch Repaired & Tubes Cleaned |
- on 851017,Train B Chiller for Control Area Ventilation/Chilled Water Sys Tripped on Low Yc Flow While Train B Sys Inoperable.Cause Could Not Be Determined. Pressure Switch Repaired & Tubes Cleaned
| | | 05000369/LER-1985-032-01, :on 851018,QA Surveillance Revealed That Chemical & Vol Control Sys Valves 1NV-223 & 2NV-223 Not Partially Stroked.Caused by Lack of Relevant Procedures. Partial Stroke Requirement Will Be Deleted |
- on 851018,QA Surveillance Revealed That Chemical & Vol Control Sys Valves 1NV-223 & 2NV-223 Not Partially Stroked.Caused by Lack of Relevant Procedures. Partial Stroke Requirement Will Be Deleted
| | | 05000369/LER-1985-033-01, :on 851030,momentary Blackout on Train B Occurred.Caused by Nuclear Control Operator Inadvertently Opening Diesel Generator Breaker.Procedures for Blackout Implemented.Collars Installed on Generator |
- on 851030,momentary Blackout on Train B Occurred.Caused by Nuclear Control Operator Inadvertently Opening Diesel Generator Breaker.Procedures for Blackout Implemented.Collars Installed on Generator
| | | 05000369/LER-1985-034-01, :on 851102,reactor/turbine Trip on Steam Generator 1A lo-lo Level Occurred.Caused by Loss of Instrument Air Due to Rupture of Welded Seam on Flexible Pipe on Discharge Air Compressor B |
- on 851102,reactor/turbine Trip on Steam Generator 1A lo-lo Level Occurred.Caused by Loss of Instrument Air Due to Rupture of Welded Seam on Flexible Pipe on Discharge Air Compressor B
| | | 05000369/LER-1985-035-01, :on 851030,B&W Fuel Assemblies Determined Incorrectly Stored Side by Side in Spent Fuel Pool.Caused by Inadequate Personnel Review of Tech Spec.Assemblies Placed in Checkerboard Pattern |
- on 851030,B&W Fuel Assemblies Determined Incorrectly Stored Side by Side in Spent Fuel Pool.Caused by Inadequate Personnel Review of Tech Spec.Assemblies Placed in Checkerboard Pattern
| | | 05000369/LER-1985-036-01, :on 851119,reactor Tripped Due to Feedwater Pump Turbine Trip on High Discharge Pressure.Caused by Rod Control Sys Not Lowering Power Enough During Turbine Runback.Failed Fuse Will Be Replaced |
- on 851119,reactor Tripped Due to Feedwater Pump Turbine Trip on High Discharge Pressure.Caused by Rod Control Sys Not Lowering Power Enough During Turbine Runback.Failed Fuse Will Be Replaced
| | | 05000369/LER-1985-037-01, :on 851210,Train a ESF Actuation Occurred Due to Actuation of Slave Relay in Reactor Protection Sys.Caused by Personnel Error.Safeguards Safety Injection Signal & Sequencer 1A Reset & Pumps Secured |
- on 851210,Train a ESF Actuation Occurred Due to Actuation of Slave Relay in Reactor Protection Sys.Caused by Personnel Error.Safeguards Safety Injection Signal & Sequencer 1A Reset & Pumps Secured
| | | 05000369/LER-1985-038-01, :on 851222,reactor Tripped Due to Turbine Trip from 93% Power.Caused by Ground Fault within Motor Operated Disconnect (MOD) on Main Power Busline 1B.Unit Stabilized & MOD Repaired |
- on 851222,reactor Tripped Due to Turbine Trip from 93% Power.Caused by Ground Fault within Motor Operated Disconnect (MOD) on Main Power Busline 1B.Unit Stabilized & MOD Repaired
| | | 05000369/LER-1985-039-01, :on 860101,discovered That Spent Fuel Pool Ventilation Performance Test Not Performed by Required Date of 851210.Caused by Personnel Error.Test Performed for Exhaust Fan 1A |
- on 860101,discovered That Spent Fuel Pool Ventilation Performance Test Not Performed by Required Date of 851210.Caused by Personnel Error.Test Performed for Exhaust Fan 1A
| | | 05000369/LER-1985-039, :on 851210,spent Fuel Ventilation Performance Test Not Performed by Required Date.Caused by Personnel Error.Personnel Responsibility Will Be Assigned for Each Performance Test |
- on 851210,spent Fuel Ventilation Performance Test Not Performed by Required Date.Caused by Personnel Error.Personnel Responsibility Will Be Assigned for Each Performance Test
| |
|