ML20133H174

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Insp Rept 50-289/85-19 on 850531-0628.Violation Noted: While Reactor Coolant Pump Id Operating,Valve NU-V-96D Not Open
ML20133H174
Person / Time
Site: Crane Constellation icon.png
Issue date: 07/17/1985
From: Conte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20133H133 List:
References
50-289-85-19, NUDOCS 8508090217
Download: ML20133H174 (40)


See also: IR 05000289/1985019

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U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No.

50-289/85-19

Docket No.

50-289

License No.

DPR-50

Priority --

Category C

Licensee:

GPU Nuclear Corporation

Post Office Box 480

Middletown, Pennsylvania

17057

Facility At:

Three Mile Island Nuclear Station, Unit 1

Inspection At:

Middletown, Pennsylvania

Inspection Conducted: May 31, 1985 - June 28, 1985

Inspectors:

N. Blumberg, Lead Reactor Engineer, Region I

J. Bryant, Senior Resident Inspector (Oconee), Region II

B. Burgess, Project Inspector, Region III

E. Gray, Lead Reactor Engineer, Region I

D. Haverkamp, Technical Assistant for TMI-1 Restart,

Region I

  • T. Peebles, Senior Resident Inspector (Turkey Point),

Region II

M. Schaeffer, Reactor Engineer, Region I

R. Urban, Reactor Engineer, Region I

P. Wen, Reactor Engineer, Region I

F. Young, Resident Inspector (TMI-1), Region I

Contractor

Personnel:

  • B. Gore, Research Scientist, Battelle PNL

J. Huenefeld, Research Engineer, Battelle PNL

  • Participation was limited, generally, to site familiariza-

tion training and facility orientation.

Approved By:

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Date

  1. TMI-1 Restart Staff

Division.of Reactor Projects

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Inspecticn Summary:

This special safety inspection (448 hours0.00519 days <br />0.124 hours <br />7.407407e-4 weeks <br />1.70464e-4 months <br />) reviewed shift activities and hot

shutdown plant activities in preparation for TMI-1 restart. Specific items

reviewed included Commission conditions for TMI-1 restart, an inadvertent

safety injection actuation, surveillance testing preparatory to restart, steam

generator and restart hearing license condition implementation, postulated

loss of feedwater transient at the facility, corporate activities in the

quality assurance end modification control areas, removal of diesel generator

interpole connectors, facility systems and equipment readiness for restart,

TMI-1 replica simulator design questions, and licensee action on previous

inspection findings.

Inspection Results:

Licensee management and quality assurance department personnel continued their

detailed involvement in plant activities. Overall, procedures were properly

implemented with a deliberate step-by-step approach, however, one instance was

identified in which an isolation valve was not restored to its open position

(violation, paragraph 2.2).

In addition, an inadvertent safety injection

actuation was caused by personnel errors, apparently due to those individuals'

unfamiliarity with the surveillance procedure. Overall, surveillance data

reflected operations within technical specifications limits.

The licensee

complies with applicable steam generator and restart hearing license condi-

tions, although the TMI-1 Restart Staff experienced some difficulties in

ascertaining compliance with certain conditions for various reasons. Adequate

procedures cover a loss of feedwater transient, and they implement many of the

conditions and commitments that resulted from the restart hearing. The licensee

has continued to implement initiatives in the modification control program.

Licensee corrective actions in response to the potential for diesel generator

interpole connector cracking were deliberate, well thought out and responsive

to NRC concerns.

The licensee resolved both previous and recent NRC issues

with respect to making plant equipment physically ready to restart, and there

were no physical obstacles to restart of the facility as of the close of the

inspection period.

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OETAILS

1.0 Introduction

1.1 Commission Conditions to Restart of TMI-1

By Memorandum and Order CLI-85-09, dated May 29, 1985, the Commis-

sion issued a decision that lifted the effectiveness of previous

orders directing that Three Mile Island Unit I (TMI-1) remain shut

down.

That action by the Commission permitted TMI-1 to resume

operation, subject to satisfactory completion of the conditions

imposed in the May 29, 1985 Order.

CLI-85-09 described the various

considerations, bases and reasons that were related to their deci-

sion to permit TMI-1 operation.

However, as described in CLI-85-09,

the Commission noted that TMI-1 has been shut down for over six

years.

The Commission believed that:

" ...because of this consideration alone that the power level

should be raised gradually to ensure that all components of the

facility still function properly, and that there is an adequate

opportunity to operate the plant at low power levels....

Furthermore, because the facility has not operated for six

years, the Commission has determined that licensee's perfor-

mance during the period of startup and power ascension, begin-

ning with initial criticality, should be carefully monitored

and thoroughly evaluated. During this time period, and any

time period thereafter the staff feels to be appropriate, the

staff is to provide more oversight to TMI-1 than it would

normally give an operating reactor."

As further stated in CLI-85-09, the Commission imposed in their

decision the following two conditions:

"(1) To ensure a safe return to operation, licensee is to

submit a power ascension schedule, with hold points as

necessary at appropriate power levels, to the NRC staff

for staf f's approval .

The plant cannot be restarted prior

to staff approval of such a schedule; and

(2) The NRC staff prior to restart is to provide to the

Commission for its information a general description of a

program to provide increased NRC oversight at TMI-1...."

The licensee's power ascensicn schedule for restart of TMI-1 was

described in a letter, dated May 31, 1985, from H. D. Hukill, Direc-

tor, TMI-1, to Dr. T. E. Murley, Regional Administrator, NRC

Region I.

That letter provided a description of the detailed

sequence of the restart power ascension test program, scheduled to

take 99 days.

In addition, the licensee committed to obtain verbal

authorization from the Region I Regional Administrator prior to

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proceeding beyond six specified hold points. The NRC staff's review

and acceptance of the power ascension schedule and hold points for

TMI-1 restart were documented in a letter, dated June 3, 1985, from

T. E. Murley to H. D. Hukill, thus satisfying the first of the two

above-stated Commission conditions.

The NRC staff's augmented inspection program for TMI-1 restart was

described in a memorandum, dated June 5, 1985, from W. J. Dircks,

Executive Director for Operations, for the Commissioners. That

memorandum discussed the steps being taken to monitor restart

activities more aggressively in order that the staff can verify in a

reasonable period of time that operational activities are being

ctrried out satisfactorily.

Those steps include the establishment

of a saparate organization (TMI-1 Restart Staff) to manage and

coorainate the NRC efforts.

This organization is directed by a

seafor NRC manager and is composed of three separate staff compo-

sents (resident inspection staff, operational assessment staff and

support staff), as depicted in Figure 1.

The unique component of

the restart staff is the operational assessment staff which is

comprised of NRC inspectors from Regions II and III and NRC contrac-

tor operator licensing examiners from Battelle Pacific Northwest

Laboratory (PNL) and EG&G, Idaho.

These individuals (all of whom

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have experience with B&W reactors) will be assigned to observe the

conduct of control room operators and licensed activities performed

in other plant areas. The functions of the TMI-1 Restart Staff were

described generally in the June 5, 1985 memorandum, and the scope of

augmented NRC inspection coverage during the various phases of the

licensee's restart program is as depicted in Figure 2, thus satisfy-

ing the second of the above Commission conditions.

1.2 TMI-1 Restart Staff Activities and Facility Operations Summary

The NRC TMI-1 Restart Staff functions and respinsibilities have been

delineated further by various other NRC memorarda, which emphasize

the staff's primary responsibility to provide increased direct

inspection and monitoring to assure the safe operation of TMI-1.

In

summary, the TMI-1 Restart Staff was established to substantially

augment the normal NRC resident and regional inspection activities

(1) to provide increased NRC awareness and understanding of the

safety of TMI-1 startup operations, (2) to provide timely NRC staff

response to operational problems or events that may occur during

this period, and (3) to provide a sound technical basis for deter-

mining the effectiveness of licensee management controls for safe

facility operation.

In anticipation of the potential for TMI-1 criticality on June 11,

1985, as permitted by the Commission's Restart Order (CLI-85-09),

the Restart Staff began around-the-clock (24-hour) shift operations

coverage at 3:30 a.m., on June 6, 1985.

The NRC's augmented inspec-

tion program for TMI-1 restart, including planned staffing and.

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Region I

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Resident inspectors

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Startup Testing

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Project Engineers

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FIGURE 1

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FINAL HEATUP AND SURVEILLANCE TESTING (5 DAYS)

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40% POWER TESTING (5 DAYS)

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CORRECTIVE MAINTENANCE / MANAGEMENT REVIEW (10 DAYS)

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responsibilities, was discussed by T. E. Murley, NRC Region I

Regional Administrator, during a media briefing at the NRC's

Middletown Office at 10;00 a.m. on June 6, 1985. At 4:21 a.m. on

Junn 7, 1985, one of the reactor coolant pumps was started to

commence the heatup of the reactor coolant system (RCS), and the RCS

temperature reached 200'F at 7:09 a.m. on June 7,1985.

Subsequently, on June 7,1985, the U.S. Court of Appeals for the

Third Circuit in Philadelphia, Pennsylvania, announced its decision

to stay the Commission Restart Order (CLI-85-09). After a determi-

nation by the TMI-1 Restart Staff that the licensee would not be

conducting significant startup testing activities, the 24-hour shift

inspector coverage was terminated at 3:00 p.m. on June 7, 1985.

The

RCS heatup was continued until the plant reached normal hot shutdown

conditions (about 530'F and 2150 psig). The RCS was maintained in

that condition for the remainder of the inspection period to com-

plete licensed operator familiarization training at " hot plant"

conditions, pending further action by the Court of Appeals.

Inspec-

tion coverage was maintained throughout this period by the resident

and support staff components of the Restart Staff.

2.0 Shift Inspection Activities

2.1 Routine Review

As a result of the NRC decision of May 29, 1985, in favor of TMI-1

Restart and in anticipation of an expected June 11, 1985 criticality

date, Region I implemented its augmented inspection coverage as

described in paragraphs 1.1 and 1.2.

The TMI-1 operational assessment staff shift inspectors observed

pre-operational activities to determine the adequacy and effective-

ness of operating personnel performance based on a review of the

indicators listed below:

Operators are attentive and responsive to plant parameters and

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conditions.

Plant evolutions and testing are planned and properly author-

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ized.

Procedures are used and followed as required by plant policy.

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Equipment status changes are appropriately documented and

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communicated to appropriate shift personnel.

The operating conditions of plant equipment are effectively

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monitored, and appropriate corrective action is initiated when

required.

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Backup instrumentation, measurements, and readings are used as

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appropriate when normal instrumentation is found to be defec-

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tive or out of tolerance.

Logkeeping is timely, accurate, and adequately reflects plant

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activities and status.

Operators follow good operating practices in conducting plant

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operations.

Operator knowledge / actions are as a result of performance-

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oriented training.

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Shift inspector findings are addressed below and in paragraph 9.4.

2.2 Valve Lineup Verification

When performing reactor coolant system (RCS) valve lineup verifica-

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tion (dayshift on June 7, 1985) the inspector noticed that Reactor

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Coolant Pump (RCP) 10 No. 1 Seal Leakoff Manual Isolation Valve

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MU-V-960 was shut. With this valve shut, the RCP-10 No. 1 seal

leakoff was isolated.

Continued operation under normal operating

pressure / temperature for an extended period of time with this valve

lineup may result in damage to the seal package, which includes two

other seals. The RCP seal package is important because it forms the

RCS pressure boundary. At the time the lineup verification was

performed, RCP-10 was in operation requiring the pump's seal to be in

operation.

The auxiliary operator who was assisting the inspector in

the valve lineup verification immediately notified the Unit I control

room.

The shift foreman instructed the auxiliary operator to open

MU-V-960. When the valve was open, high range leakoff indication in

the control room increased from 0.7 gpm to approximately 4.25 gpm.

The licensee's Plant Operations Department personnel immediately began

to review this event to determine if any damage had occurred to

RCP-10 seal package.

They documented that review in Plant Incident

Report (PIR) No.1-85-05, dated June 13, 1985.

The pump vendor, Westinghouse, was notified of this event and the

vendor recommended that the plant be cooled down and an inspection

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be performed of the pump's seal package. While the plant was being

cooled down, the No. 2 seal appeared to reseat itself at approxi-

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mately 700 psig.

Because both the No. 1 and No. 2 seals were then

functioning properly, the licensee concluded that there was no

safety concern with the continued operation of RCP-10.

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the plant was returned to normal hot shutdown operating temperature

and pressure without excessive leakage past the No. 2 seal.

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The licensee's review determined that MU-V-960 was inadvertently left

closed sometime on the previous (midnight) shift on June 7, 1985

after performing seal leakoff flow verification (seal bucket

checks).

This flow verification evolution (which required two valve

manipulations and restoration to normal) was performed by auxiliary

operators under licensed senior reactor operator supervision but with

no specific written procedures.

The involved operators acknowledged

the possibility that they left the valve shut. Operating Procedure

1104-2, " Makeup and Purification System," requires that MU-V-960 be

open during normal operations. Therefore, the inspector considered

this to be contrary to Technical Specification 6.8.1 (289/85-19-01).

The licensee's review also noted that specific guidance had not been

given to the operators regarding proper RCP seal flow verification.

As part of the licensee's own review and corrective action, Procedure

Change Request (PCR) No. 1-05-85-0384 was initiated to add specific

procedural steps to perform " bucket checks" on RCPs.

This PCR is in

the review and approval process.

In addition, the licensee's review noted that the control room

operators had not recognized the problem from information indicated

by the RCP seal leakoff flow recorder in the control room.

The

licensee's review concluded that the control room operators should

have observed and questioned the difference between the low range

leakoff value and the high range leakoff value while starting the

RCPs.

The licensee is making a change to the CR0 log to require

recording of both high and low range flow indications each shift to

help provide additional assurance that operators verify proper seal

flow indication.

The Operations Manager has provided information regarding this

violation and the corrective actions to all shifts to be reviewed by

all crew members.

The inspector reviewed the above corrective actions and concluded

that licensee personnel immediately obtained procedural compliance

and that the licensee had taken adequate corrective measures for

this violation.

2.3 Borated Water Storage Tank Temperature

During the midshift on June 7, 1985, the shift inspector noted a

Borated Water Storage Tank (BWST) high temperature alarm in the

control room.

The inspector questioned the control room operator

about the alarm in regard to meeting a design requirements of

keeping the BWST less than 90*F.

Discussions with the shift supervi-

sor revealed that the BWST heat tracing might be adversely affecting

the adjacent temperature instrument.

The shift supervisor, however,

noted that '.he average temperature indicated by two other BWST

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temperature instruments was less than 90 F.

These instruments

provided input to the plant computer and were not located near the

tank's heat tracing.

The shift inspector referred this matter to the resident inspector

who discussed this item with plant operations and plant engineering

representatives. The inspector noted that the temperature was very

close to the limit and was concerned whether the temperature indica-

tar was giving the operator a true indication of tank temperature.

Based on the inspector's discussions with plant engineering per-

sonnel, the BWST heat tracing temperature was set at 110*F, consis-

tent with the setting on adjacent chemical control tanks.

Sub-

sequently, licensee representatives reset the heat tracing for the

BWST at 50*F.

At this temperature the heat tracing on this tank

would not affect the indication of the tank temperature.

The

resident inspector concluded that BWST temperature at the time of the

observation was in accordance with safety analysis assumptiens and

Technical Specification requirements and considered that the shift

inspector's concern was resolved.

2.4 Summary of Findings

In general, shift inspector observations confirmed that the operators

were attentive to their duties.

They were responsive to symptoms of

abnormal conditions although there was an isolated lapse of atten-

tiveness related to RCP seal leak-off flow indication.

They appro-

priately planned evolutions and they, in general, properly imple-

mented procedures. There was an isolated case of a mispositioned

valve that went unrecognized for over a shift time period but this

was not indicative of a programmatic problem or improper implementa-

tion of the operating system restart valve lineup effort.

The

operators were knowledgeable of plant design and kept themselves

updated on plant activity during each shift.

3.0 _ Plant Operations During Preparation for Star _ tup

3.1 Routino Review

The resident inspectors periodically inspected the facility to

determine the licensee's compliance with general operating require-

ments of Section 6 of the Technical Specifications (TS) in the

following areas:

review of selected plant parameters for abnormal trends;

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plant status from a maintenance / modification viewpoint includ-

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ing plant housekeeping and fire protection measures;

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control of ongoing and special evolutions, including control

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room personnel awareness of these evolutions;

control of documents including log-keeping practices;

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implementation of radiological controls; and,

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implementation of the security plan including access control,

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boundary integrity and badging practices.

The inspectors focused on the following areas:

control rocm operations during regular and backshift hours

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including frequent observation of activities in progress and

periodic reviews of selected sections of the shift foreman's

log and control room operator's log and selected sections of

other control room daily logs;

areas outside the control room; and,

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selected licensee planning meetings.

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The inspectors identified no conditions adverse to nuclear safety or

inconsistent with regulatory requirements. Additional findings are

noted below.

3.2 partial Emergency Safeguards Actuation

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An unplanned partial actuation of emergency safeguards (ES) compo-

nents occurred at 10:04 a.m. on June 26, 1985 due to personnel

error. While conducting quarterly surveillance testing of reactor

building cooling and Isolation system logic channels, an operator

failed to reset one group of ES components as specified by steps in

the procedure.

This resulted in the unexpected start of the

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emergency diesel generator, makeup pump 1A and decay heat pump 1A,

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and operation of two ES valves (decay heat valve 4A and makeup

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valve 18).

In addition, two fans in the reactor building stopped

due to the ES actuation. The diesel and pumps were secured about

one minute after their initiation and other components were promptly

aligned to their normal operating configurations.

No actual safety

injection resulted, due to the ES valve lineup for the test; all

components functioned as designed; and there was no equipment

damage.

The licensee made proper notifications in accordance with

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10 CFR 50.72.

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Following this occurrence, on June 26, 1985, the inspector reviewed

the plant operations that were in progress and the various personnel

actions that contributed to the unexpected partial ES actuation.

The inspector discussed these matters with the shift foreman and the

cognizant plant engineer (procedure owner) who were both present in

the control room when the surveillance test was being performed.

The inspector considered that the apparent cause of personnel error

was due to several individuals' (control room operator, shift foreman

and cognizant plant engineer) unfamiliarity with the surveillance

test which is required to be performed quarterly during normal plant

operation but was performed only a few times during the previous

years of plant shutdown.

The error apparently was caused, specif-

ically, by the operator's (and others') lack of detailed understanding

of the system response when procedural steps were performed in a

sequence other than that specified by the surveillance procedure.

Also, a communications problem was apparent when the operator

requested, and was too hastily granted, approval for releasing an ES

bypass pushbutton.

However, the consequences (unexpected ES actua-

tion) were obvious to the operator when the error was made.

The

operator response to the initiation was both prompt and correct, and

the remainder of the surveillance test was performed without further

incident.

The inspector observed the shift supervisor relief turnover after

this occurrence and considered the information exchange to be

accurate and thorough as related to the subject event.

The licensee

followup actions to this occurrence were incomplete at the end of

the inspection, in that a 30 day Licensee Event Report (LER) was

being prepared in accordance with 10 CFR 50.73.

This item will

remain unresolved pending NRC review of that report (289/85-LO-01).

3.3 Shif t Supervisor _ Meeting with Plant Management

In preparation for the pending startup, facility management in the

operations and startup testing organization met with shift supervi-

sors on June 4, 1985.

The purpose of the meeting was two-fold:

to

summarize the planned evolutions for the low power physics testing

and power escalation programs; and to discuss with the shift super-

visors cautionary items or lessons learned from other plants which

restarted after long term shutdowns (summarized in an internal

memorandum, dated May 22, 1985, from the Operations and Maintenance

Director,THI-1).

(The review of other plant problems subsequent to

long term shutdown was a Itconsee commitment by letter, dated May 7,

1985, in response to the most recent NRC Systematic Assessment of

Licensoo Performance.) The meeting was also attended by the Direc-

tor, TMI-1.

The NRC's TMI-1 Restart Manager was invited and

attended this meeting.

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Licensee management exhibited initative in conducting the meeting.

It was a frank and open discussion of what was expected of shift

supervisors in terms of overall control of safe operations of the

facility and what shift supervisors could expect of facility manage-

ment in minimizing unnecesary distractions to the overall goal of

safe operation of the facility.

Operations areas or concerns

warranting close attention by the shift supervisors were highlighted

by management along with test sequences that could appear somewhat

complex if not carefully planned by the shift conducting the test.

Various shift supervisors expressed concern over the number of

monitoring organizations who will appear from time to time in the

control room or who are on shif t.

The concern was based on the

groups indirectly demanding excessive attention from shift person-

nel through questioning, discussion, etc.

Licenseo management

reiterated the need for suc5 monitoring, and they required that

management be informed of any interference of shift personnel duties

with respect to the safe operation of the facility.

The inspector had no further comments.

3.4 Summary of Findings

Overall, persornel stationed in the control room exhibited overall

control of daily activities, including problem areas that needed

resolution.

The planning meetings stressed attentiveness to proceed

safely with daily activities, including surveillance and maintenance,

and to resolve any inter-departmental interface problems.

Licensee

upper management and quality assurance department personnel continued

their detailed involvement in site activities.

4.0 Surveillance Testing in_. Preparation for Restart

The inspector reviewed the surveillance test results of selected compo-

nents/ systems to verify that the test procedures were properly approved

and adequately detailed to assure performance of satisfactory surveil-

lance; test instrumentation required by the procedure was calibrated; the

results satisfied Technical Specifications (TS) and procedural acceptance

criteria, or were otherwise properly dispositioned.

The following tests were reviewed:

4.1 Control Rod

4.1.1

Rod _ Drop Time

The rod drop measurement was performed in accordance with

procedure SP 1303-11.1, " Control Rod Drop Time." The

inspector verified by review of the test results performed

on June 9, 1985, that all control rods reached a 75*4

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insertion in less than 1.66 seconds as required by the TS.

The inspector also reviewed several visicorder traces and

verified that the drop time had been interpreted

correctly.

4.1.2

Rod Position Indication

The licensee performed control rod drive (CRO) absolute

(API) and relative position indication (RPI) surveillance

calibration in accordance with procedure SP 1302-5.13,

Revision 6.

Rod position indications were cross checked

among API, RPI and zone reference position.

Deviations

among zone reference position, API and RPI were all within

5% for each rod.

The associated asymmetric rod alarm and

fault were also tested and found acceptable.

4.1.3

Control Rod Program Special Check

The licensee performed control rod exercise in accordance

with procedure SP 1301-9.2, " Control Rod Program Special

Check," on June 9, 1985.

The test results showed that the

rod position indication meter and the corresponding computer

rod position printout correctly responded for each rod

motion. Although the power and instrumentation cables

were not physically checked in this surveillance, the

above test indirectly showed that the cables have been

properly connected.

4.2 Inadequate Core Cooling Monitoring

4.2.1

Saturation Margin Monitor

The inspector reviewed the saturation margin monitor

monthly functional test results (SP 1303-11.52, completed

May 13, 1985).

Test results indicate that the performance

of the saturation margin monitors is in accordance with

applicable TS and restart hearing commitments.

4.2.2

Backup Incore Thermocouple Readout System (BIR0)

_

The BIRO refueling calibration (SP 1302-22) was perfurmed

on August 14, 1984. All thermecouple (T/C) performances

were acceptable except K-12.

The faulty T/C was replaced

by T/C H-13 and a subsequent test performed on March 14,

1985 indicated its acceptance.

The inspector also re-

viewed the recent monthly BIRO T/C check (SP 1302-21).

Test data confirmed that the BIRO's operability was in

accordance with restart hearing commitments.

.

_

.

.

12

4.3 Reactor Coolant System (RCS) Leak Rate

The inspector reviewed the RCS leak rate surveillance (SP 1303-1.1)

results performed on June 8-9, 1985. The surveillance results

indicated that all calculated leakages were well within TS limits.

However, the calculated unidentified leakage was a negative value

from (-) 0.21 to (-) 0.26 gpm which was consistent with previous

surveillance results from (-) 0.21 to (-) 0.29 gpm taken during the

Hot Functional Test during the period April 10-19, 1985. This

anomally was caused by an RCS evaporative loss term that is permitted

to be used by TMI-1 Technical Specifications. The validity of the

l

evaporative loss term (0.27 gpm) has been referred to NRR to determine

'

whether a change to the TS is appropriate (289/84-08-02).

4.4 Reactor Protection System (RPS)

4.4.1

RC Flux Flow

The RPS channels for the reactor DNB protection based on

flow and axial imbalance trip were calibrated in accor-

dance with procedure SP 1302-5.4 on June 5, 1985. The

calibration results for eight flow transmitters

(RC14-A-DPT1 through 4 and RC14-B-DPT1 through 4) and both

RC flow loops (A and B) were found acceptable. The

associated flux / imbalance / flow trip bistables were checked

per SP 1303-4.1, "RPS Functional." The actual gain

adjustment factor for the flow buffer amplifier will be

verified / adjusted when the unit reaches appropriate power

levels.

4.4.2

Reactor Trip on loss of Feedwater (FW)/ Main Turbine Trip

The RPS channels for the reactor trip on loss of FW or main

l

turbine trip were calibrated in accordance with procedure

SP 1302-5.34, " Reactor Trip on Loss of Feedwater/ Main

Turbine Trip," Revision 0.

The instrument loop test data

of May 9, 1984, indicated that the switch setpoint for

pressure switches PS 919 and PS 924 did not meet the

acceptance criteria. Both pressure switches were cali-

brated and retested, and the final values were within the

acceptance criteria of the TS and met commitments made as a

result of the restart hearing.

.

.

.

.

.

_ _ _ _ - _

_ _ _ _ _ .

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13

4.5 Pressurizer Heaters Emergency Power Test

The licensee performed the subject test in accordance with procedure

SP 1303-11.55, " Pressurizer Heaters Emergency Power Functional

Test," Revision 0, on March 20, 1985. This test demonstrated that

1) pressurizer heater groups 8 and 9 transferred from their normal

power bus to the emergency power bus and energized and 2) following

an ES signal the heaters tripped and were not able to be re-applied

while an ES signal was present.

The test results satisfied the

requirement of TS 4.6.3 and restart hearing commitments.

4.6 Other System / Component Testing

'

In addition to the above, various other surveillance test data were

reviewed to ' assure that test results met the TS acceptance criteria.

Approximately 20*4 of the licensee's surveillance procedures were

<

reviewed covering a majority of refueling and annual surveillances,

and selected more-frequent tests. No conditions adverse to nuclear

safety or inconsistent with regulatory requirements were identified.

5.0 TMI-1 Restart License Conditions Review

The inspector conducted a . review and inspection to assure that the

licensee met those continuing and currer.tly applicable (for criticality)

license condifions issued or proposed as a result of or related to the

TMI-I steam generator' repair hearing ~and the restart hearing.

The review

included a verification, as applicable, that an NRC inspection adequately

certified compliance with the Jicense condition.

The inspector verified

that each license condition wa~s met, or the condition was reviewed for

current acceptability to ass'ure that the licensee continued to comply

even with the passage of time due to restart delays.

The license conditions verified based on the review during past inspec-

tions were:

2.C.5 (also see below), 2.C.8(1), 2.C.8(5), Proposed 2.C.9(a),

(b), (1), (m), (n), (r), (t), Proposed 2.C.13(c).

The license conditions

that were verified during this inspection are listed below along with

inspector findings.

5.1 Steam Generator Chemistry Program (LC 2.C.5)

In conjunction with the review of outstanding issues in NUREG 1019,

" Steam Generator Repair Safety Evaluation Report" (and Supplement),

the inspector reviewed the licensee's secondary water chemistry

monitoring program.

The inspector determined that the licensee

program did include a sampling schedule for critical parameters.

The licensee procedures were found to include requirements for

recording and plotting critical parameters.

The program contained -

basic steps to address corrective actions if chemistry parameters

_ _ _ _ _ _ _ _ _ _

.

.

14

4

were determined to be out of specification.

Based on this review of key

procedures, the inspector concluded that the licensee had met

license condition 2.C.S.

Applicable inspections supporting the above noted findings are:

NRC

Inspection Reports 50-289/84-07, 84-16 and 85-17.

5.2 Primary to Secondary Leak Rate Shutdown Limit (LC 2.C.8(2))

The license condition requires that the plant be shut down if primary

to secondary leakage is greater than 0.1 gpm (6 gph) above baseline.

The inspector held discussions with licensee representatives regarding

licensee implementation of the LC issued by Technical Specification

Amendment 103, dated December 21, 1984.

The purpose of these discus-

sions was to ascertain the specific actions by which the licensee

would meet the license condition as described in licensee letter

(Serial No. 5211-85-2070), dated June 8, 1985 and by related OTSG

hearing commitments (Topical Report 008, Revision 3).

The inspector noted that the licensee's procedure (Surveillance

Procedure (SP) 1301-1) lacked specificity of licensee actions upon

an indication of primary to secondary leakage in excess of 6 gph

above baseline (.5 gph) and noted that operations would be permitted

for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> with leakage between 6 and 12 gph.

In response, licensee representatives expressed concern about

additional thermal cycles on the primary system, resulting from

unnecessary plant shutdowns caused by a primary to secondary leak

rate indication that may be unrelated to actual leakage because of

transient conditions.

Further, licensee representatives expressed

uncertainty over how the indication of this leak rate would respond

on a day-to-day basis considering measurement inaccuracies, power

level changes or other factors unknown because of noncritical testing.

(The indication of primary to secondary leak rate is a mass balance

calculation between RCS concentration using the Xe-133 isotope as

input to the OTSG and measuring the OTSG output of Xe-133 by way of

the condenser off gas system - a condenser off gas grab sample

provides additional accuracy of primary to secondary leak rate.)

The inspector acknowledged the licensee's concerns and their posi-

tion on the factors affecting the primary to secondary leak rate

calculation.

However, after subsequent discussions, licensee

representatives agreed to re-review the SP 1301-1 procedural actions

after they gained experience and data from the power escalation

program to see if any changes were warranted.

The inspector con-

cluded that the license condition was enforceable as it was stated

.

.

15

and the SP procedural steps were not needed for enforceability.

The

acceptability of the implementing procedure is unresolved pending

completion of licensee action as stated above and subsequent NRC

Region I review (289/85-19-01).

5.3 Liquid Radwaste Separation of Units (Proposed LC 2.C.9.(d))

This proposed license condition requires that isolation of liquid

transfer line interconnections between Units 1 and 2 shall be

maintained. TMI-1 SP 1303-11.48, " Unit 1/ Unit 2 Isolation Verifica-

tion" is used quarterly by the licensee to ensure that all process

piping connecting Unit 1 and Unit 2 liquid radwaste systems is

isolated.

The inspector verified that SP 1303-11.48 was current (June 4,

1985), there were no exceptions or deficiencies, and all signoffs

were complete.

The licensee has satisfied this proposed license

condition.

5.4 Shift Manning Requirements (Proposed LC 2.C.9.(e) through (k))

Theseproposedlicenseconditionsrequirethelicenseetomeei

various minimum staffing requirements, shift rotation, and reporting

requirements (289/82-BC-54).

They are minimum conditions imposed by

the Licensing Board based on the evidentiary record.

The require-

ments of NRC. regulations on shift manning, which in some respects

are more restrictive than these proposed license conditions, are

also applicable.

TMI-1 Administrative Procedure (AP) 1029, " Conduct of Operations,"

Section 5.7 addresses Proposed License Conditions 2.C.9(e) through

(j). TMI-1 Operations Surveillance Procedure OPS-S-286 addresses

Proposed License Condition 2.c.9(k) concerning annual reporting

requirements to the Commonwealth of Pennsylvania and the NRC staff

when insufficient individuals are enrolled in the licensee's train-

ing program. Both of the above procedures were reviewed by the

inspector.

These proposed license conditions have been satisfied.

5.5 Conservative Indication of Saturation Margin (Proposed LC 2.C.9(o))

This proposed license condition requires the TMI-1 emergency proce-

dures to direct operations to rely on redundant saturation indica-

tions that are closest to saturation in determining if the high

pressure injection (HPI) system flow can be throttled until the

backup display system for the incore thermocouples (BIRO) is made

fully safety grade and environmentally qualified (289/83-BC-17).

-

,

.

16

The licensee submitted letters to the NRC staff, dated May 21, 1985

and June 28, 1985, that certify the backup incore thermocouple system

is fully safety grade and environmentally qualified.

Therefore,

this proposed license condition is met.

The qualification of the

BIRO will be further reviewed by NRC Region I to resolve a previous

inspection finding (289/84-06-03).

Abnormal Transient Procedure 1210-10 requires the determination of

saturation margin by conservative indication of redundant saturation

margin monitor instruments (for each RCS loop, used with reactor

coolant pump on) or either of two hand calculation methods.

The hand

calculation methods use either the BIRO or plant computer display of

the five highest incore thermocouples along with safety grade (except

for computer point readout on one pressure channel) RCS pressure

instrument. The inspector noted that, for the RCP off situation, the

most conservative of the hand calculation methods was not specified.

That becomes moot because the licensee certified, subsequent to

inspector questioning, that the BIRO was environmentally qualified

(previous correspondence certified seismic qualifications).

During the review of ATP 1210-10 the inspector noted that the

computer point for pressure instrument 963 was used in the hand

calculation of saturation margin and he further noted that the

instrument string error analysis did not include that computer point

in the 963 instrument loop.

That error analysis was the basis for

staff certification of a TMI-1 Restart Hearing Appeal Board decision

to certify that the instrument error was less than 20 F.

Subsequent

to inspector questioning, licensee representatives performed an

additional analysis and reported that the instrument error was

still less than 20 F.

The inspector concluded that the licensee met

LC 2.C.9(o).

5.6 Interim Measures for Non Safety Grade Emergency Feedwater (Proposed

LC 2.C.9(p))

This proposed license condition requires that an auxiliary operator

be dispatched to the emergency feedwater (EFW) flow control valve

area upon any EFW auto-start condition in order to take manual

control of the valve, if needed; this individual will perform no

other duties until the control room operators verify EFW flow to the

steam generators (289/83-BC-20, previously reviewed and closed).

The inspector reviewed various emergency and alarm procedures.

Within these procedures, various steps relating to EFW initiation

direct the operator to go to Abnormal Transient Operating Guideline

(ATOG) Procedure 1210-10, " Abnormal Transients, Rules, Guides, and

Graphs." Section 2.0 of that Procedure addresses the requirements

of this proposed license condition.

Therefore, this LC is satis-

fied.

___ _

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._

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,

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17

5.7 Emergency Power for Pressurizer Heater (Proposed LC 2.C.9(q))

i

The proposed license condition requires the reactor to be

subcritical or in a hot standby condition prior to connecting the

4

pressurizer heaters to the emergency power supply (289/83-BC-21,

1

previously reviewed and closed).

The inspector again reviewed emergency procedures'1202-2, " Station

Blackout" and 1202-29, " Pressurizer System Failure." Both proce-

i

dures continue to contain guidance to the operators concerning

pressurizer heater connection to the emerger.cy power supply. The

guidance in these procedures satisfies this proposed license condi-

tion.

i

5.8 Restricted Positions and Personnel (Proposed LC 2.C.9(s) and (u))

Proposed License Condition 2.C.9(s) requires that the licensee not

,

'

use TMI-2 pre-accident licensed operators and certain management

personnel in the operations or key management positions of TMI-I as

specified in the Commission Order CLI-85-02, dated February 25,

1985.

In May 1985, NRC Region I management initiated discussions with

,

licensee management regarding their plans to implement this condi-

tion. At the outset of those discussions, it became clear that the

licensee needed to define certain phases or aspects of the condition

based on the hearing record for lack of more specific guidance in

'

CLI-85-02.

The licensee finalized those plans in June 1985 with an

acceptable disposition by the TMI-1 Restart. Staff as noted below.

The licensee initially identified the restricted positions at the

TMI-1 site by marking (yellow highlight) those positions on a May 1,

1985 Organizational Position Listing.

Their bases for identifica-

tion of. restricted positions (in response to the wording of

'

CLI-85-02) included:

licensed operators for TMI-1 including engi-

.

neers and training instructors or other personnel who had licenses

to be maintained; key managers in the operations or training of

operators and those managers in the oversight of operations at the

TMI-1 site; and non-managerial positions involved in the direct

operation or independent oversight of operations at the TMI-1 site.

The inspector identified the following positions as potentially

applicable to the CLI-85-02 restriction which were not included in

the licensee's initial listing:

auxiliary operators, shift techni-

cal advisers, TMI-I QA audit personnel, startup and test manager,

and simulator development :anager.

The licensee representatives

acknowledged the inspector's comments ard incorporated these addi-

tional positions in their restricted position listing.

Also, the licensee identified those preaccident personnel who were

considered to be restricted based on the wording of CLI-85-02.

Their bases for identification were those personnel who filled the

specific positions listed by the restrictions of CLI-85-02 and those

pre-accident licensed TMI-2 operators and trainees on shift. At the

.~

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,

18

outset of discussions in this area, licensee representatives

.

'

. expressed uncertainty as to the time period for the term " pre-

accident." Since the license condition had its roots in uncertain-

-

ties about individual performance related to the TMI-2 leak rate

i.

falsification issue, licensee representatives proposed a start time

for the preaccident period as the date of the first RCS leak rate

calculation at TMI-2 (March 22, 1978).

In verbal consultation with

cognizant individuals of the Office of Nuclear Reactor Regulation

Staff, the TMI-1 Restart Staff (1) verified the completeness of the

list of TMI-2 licensed operators in the licensee's listing, and (2)

J

. accepted the licensee's proposed start date for the preaccident

period with respect to identifying those TMI-2 licensed operators and

trainees who potentially were involved in the TMI-2 RCS leak rate

'

falsification.

The TMI-1 Restart Staff also concluded that the

licensee representatives made a reasonable search of records to

identify trainees on shift during the preaccident period (March 22,

1978 to March 28,.1979).

These records were:

training department

records, personnel files, accident generated documents listing

assigned personnel, shift schedules, and legal department records.

The licensee finalized their " confidential" listing of restricted

positions and restricted personnel in a memorandum, (Serial No.

'

5211-85-1254, Revision 1), dated June 20, 1985, from H. Hukill,

Director, TMI-1, to C. Smyth, TMI-1 Licensing Manager. The memoran-

j

dum also required that the Director, TMI-1 will periodically

assure that restricted personnel are not among the TMI-1 licensed

i

operator candidate classes.

The licensee confirmed that this document

will be available for periodic NRC inspections to demonstrate

'

continued compliance with the license condition. As a result of

,

that memorandum, the TMI-1 Restart Staff verified that restricted

'

personnel are not in restricted TMI-1 site organization positions as

defined above. Accordingly, the staff concluded that the licensee

met the restricted personnel condition of CLI-85-02 (proposed LC

2.C.9(s)).

Subsequent to the finalization of licensee implementation plans, two

individuals were identified to the TMI-1 Restart Staff as being in

unique positions.

In one case a restricted individual is presently

a consultant in the training department.

Licensee representatives

,

took the position that this individual was not employed by GPUN at

,

TMI-1, the individual's work received considerable GPUN management

review, and he was not in a restricted position as defined above.

The TMI-1 Restart Staff considered acceptable the licensee's deter-

mination that the individual could continue in that position while

meeting the CLI-85-02 restriction.

i

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19

In another case, a former engineer signed an affidavit stating that

he was aware of the CLI-85-02 restriction and that the restriction

was not applicable to him. His basis was that, as a trainee during

the defined preaccident period, he never stood watch in the control

room and was never a part of the operating crew.

Based on the

personal knowledge of TMI-1 Restart Staff inspectors and their

recollection of the individual and his duties, it was considered

acceptable for the licensee not to include this individual in the

list of restricted individuals (also meeting the CLI-85-02 require-

ment of "on shift for training").

With respect to the above, the TMI-1 Restart Staff concluded that

the licensee met proposed LC 2.C.9(s).

Another proposed license condition restricted the two primary

individuals who responded for the licensee to the TMI-2 Accident

Notice of Violation. The above referenced organizational position

listing (May 1, 1985) does not have these individuals listed. Also,

based on the personal knowledge of the TMI-1 Restart Staff inspec-

tors, these individuals are not used to operate TMI-1 or represent

the licensee in TMI-1 matters. Accordingly, the TMI-1 Restart Staff

concluded that the licensee met proposed LC 2.C.9(u).

5:9 Natural Circulation Testing / Training (Proposed LC 2.C.10(a))

The proposed license condition requires, in part, that natural

circulation training be completed prior to exceeding 5% power in

accordance with licensee commitments made in response to TMI Task

Action Plan (TAP) Item I.G.I.

These commitments were made, in part,

in licensee letters, dated May 6, 1981 and April 5, 1983, regarding

the special low power test program and the TMI-1 Restart Test

Specification (Revision 1), respectively.

The inspector discussed licensee implementation plans for the

Natural Circulation Training while below 5% power and reviewed the

approved Lesson Plan No. 11.2.01.281, Revision 0, dated May 23,

1985, " Natural Circulation." Essentially, the licensee plans two

transitions from forced circulation (use of reactor coolant pumps)

along with observation of key parameters (in accordance with Operat-

ing Procedure 1102-16, and Abnormal Transient Procedure 1210-10) and

the recovery from natural circulation. The control room will have

two additional training stations each with a cathode ray tube (CRT)

for display of the RCS pressure-temperature (P-T) plot and one CRT

for parameters display.

Personnel from the training stations will

be rotated to the control panel for actual instrumentation observa-

tion. A training instructor will be at each station and at the

panels guiding the operator through observations pertinent to the

1

indication of natural circulation cooling effectiveness.

1

.

.

20

The inspector noted that the lesson plan was practically oriented

and consistent with the applicable operating procedures.

The

theoretical presentation will be complemented with practical factors

affecting natural circulation cooling. effectiveness such as steam

generator water . level or using emergency feedwater versus normal

feedwater.

The inspector concluded that the licensee is adequately prepared to

.

provide performance oriented training to licensee personnel during

the low power physics test program meeting the related commitments

for TAP I.G.1 and requirements of LC 2.C.10(a).

The inspector acknowledged licensee plans to perform makeup training

after the NRC 5% power hold point for those operators who might be

absent during the low' power physics test program.

The inspector

stated that an NRC staff review would be conducted to assure each

shift (including shift supervisors) was adequately trained on natural

circulation until individual operator makeup training could be

provided later in the power escalation program.

5.10 Previous License Condition Inspection Finding (289/83-14-04)

NRC Inspection Report No. 50-289/83-14 documented the review of

outstanding preoperational and startup testing for various modifica-

tions within the scope of the staff's TMI-1 certification process.

Various tests were keyed to criticality, 5*s power, or completion of

the power escalation program.

The status of those tests is listed

below. Those tests ~ requiring critical and at power conditions were

incorporated as license conditions. The TMI-1 Restart Staff

inspection program will verify the proper completion of all

applicable license conditions as noted above. Accordingly, this

inspector follow item is closed.

The following licensee actions were to be completed prior to reactor

criticality:

Functionally test the emergency feedwater flow indication

--

system and cavitating venturies (TP 233/3 and 233/4 - NRC

Inspections 50-289/84-01 and 84-14) - complete;

--

Functionally test the high pressure injection cross connect and

cavitating venturi modifications (TP 655/1 - NRC Inspections

50-289/84-18, 84-22 and 84-31) - complete; and,

Safety system valve / breaker lineup position verification

--

(various licensee procedures - NRC Inspections 50-289/84-15 and

84-17) - complete.

. _ .

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l

The following licensee actions should be completed prior to exceed-

ing 5% reactor power:

Pressurizer heater emergency power /RCS pressure control func-

--

tional testing (SP 1303-11.55 - NRC Inspection 50-289/83-25) -

complete; and,

--

Functionally test the emergency feedwater backup instrument air

modification (TP 700/2 - Proposed LC 2.C.10(c)).

The following licensee actions should be completed prior to comple-

tion of the power ascension program:

.

Functionally test anticipatory reactor trips on loss of

--

!

feedwater/ turbine trip and automatic initiation of emergency

feedwater modification (TP 800/2, 8, 9 - Proposed LC

,

2.C.10.b.(d), and (f)); and,

--

Implementation of training and power ascension testing per Task

Action Plan Item I.G.1 (Proposed LC 2.C.10(a)).

When the Office of Nuclear Reactor Regulation issues the license amend-

ment which incorporates the above noted " proposed" license conditions,

l

the TMI-1 Restart Staff will determine whether there are any changes to

l

the license conditions that would invalidate this review.

6.0 Loss of Main Feedwater with Actuation of the Steam Leak Rupture Detection

System

l

The purpose of this limited review was to determine the initial antici-

pated response of TMI-I equipment and personnel to a complete loss of

main feedwater to the once through steam generators (OTSGs) with an

inadvertant actuation of the steam leak rupture detection system (SLRDS).

This postulated scenario would be similiar to the event initiation se-

quence that occurred at the Davis-Besse facility on June 9, 1985.

6.1 Areas Inspected

The inspectors reviewed the following documents:

--

TMI-1 Operations Plant Manual;

--

TMI-1 Final Safety Analysis Report;

o

--

TMI-1 Restart Hearing Atomic Safety and Licensing Board Partial

Initial Decision (Plant Design and Procedures and Separation

Issues), Volume 1; and,

,

--

Sequence of Events - Davis-Besse Event of June 9, 1985, and

related documentation.

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22

The following procedures were reviewed by the inspectors:

--

Abnormal Transient Operating Guidelines (ATOG) (ATP) 1210

Series;

--

Loss of Feed to One Steam Generator, EP 1202-26, Revision 10;

and,

Total Loss of ICS/NNI Power, EP 1202-40, Revision 5.

--

The following piping and instrument drawings were reviewed by the

inspectors:

--

C-302-081, Revision 25, Feedwater;

C-302-011, Revision 26, Main Steam; and,

--

C302-082, Revision 3, Emergency Feedwater.

--

The following elementary electric diagrams were reviewed by the

inspectors:

--

SS-208-110, Revision 9, 6900 V Switchgear 1A2;

--

SS-208-105, Revision 0, 6900 V Switchgear;

--

SS-209-755, Revision 4, DC and Miscellaneous;

SS-209-756, Revision 4, DC and Miscellaneous;

--

SS-208-421, Revision 6, 480 V Control Center;

--

--

SS-209-143, Revision 7, DC and Miscellaneous;

--

SS-209-144, Revision 6, DC and Miscellaneous;

--

SS-208-425, Revision 6, 480 V Control Center; and,

--

SS-208-524, Revision 1, 480 V Control Center.

In addition to the above reviews, the inspectors had discussions

with various licensee representatives.

The inspectors physically walked down the EFW system to determine if

there were any deficiencies present. One issue was raised by the

inspectors as a result of this walk down.

It concerned preventive

maintenance (PM) on the EFW system strainers and check valves.

The

inspectors determined that the strainers had been removed and PM was

conducted on the check valves. The inspectors reviewed the Pump and

.

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23

Valve Inservice Testins sIST) Program and determined that all the

check valves were periodically tested to provide assurance of the

operability of these valves during their service life.

6.2 Expected Sequence of Events

Assuming all Technical Specification safety related equipment was

operable including the emergency feedwater system with the reactor

at 100?s power, the inspector postulated a sequential loss of main

feedwater pumps (MFP) with a subsequent (but unrelated) actuation of

the steam line rupture detection system.

Due to the loss of one MFP

an automatic power runback would occur due to the integrated control

system control logic.

The power reduction might cause RCS TAVE to

rise thereby causing pressurizer level and subsequently RCS pressure

to rise to the reactor trip setpoint. A challenge to the PORV may

occur depending on plant-specific conditions.

Subsequently the

second MFP is lost (reason unknown).

(This delayed loss of

feedwater is conservative since the complete loss of MFP causes a

reactor trip due to pressure switch in the MFP turbine hydraulic

system, installed as a result of the TMI-1 restart hearing.) The

complete loss of MFP not only initiates a reactor trip but it also

initiates emergency feedwater (EFW) due to differential pressure

switches scensing across the MFP.

The applicable operating / emergency

procedures guide the operators to feed both OTSG's and assure adequate

primary to secondary heat transfer for reactor core cooling.

Since

EFW initiated due to the loss of MFW, control of the feedwater

regulating valves, EF-V30A/B, is automatic to 30" on the startup

range.

Further, by proposed license conditions, existing procedures

require that an auxiliary operator be dispatched to the EF-V30's to

take manual control as directed by the control room if safety grade

flow instrumentation indicates a loss of EFW.

'

Both 50?4 capacity (but each sufficient for post accident decay heat

loads) safety grade motor driven emergency feedwater pumps (EFPs)

and one 100*6 capacity turbine driven (non-safety grade) EFP will

receive the auto-start signals. To produce this signal, the actua-

tion system is arranged into two trains.

Each train contains two

control grade differential pressure switches (one for each MFP) or

sensors indicating a loss of all reactor coolant pumps. This circuit

is designed so that a single failure will not prevent the EFW

system from functioning.

If, for an unknown reason, the turbine

driven EFP would trip due to an overspeed condition, each motor

driven EFP would provide enough feedwater to an OTSG.

The EFW control valves fail open on the unlikely loss of all instru-

ment air (backed up by a safety grade two hour passive air bottle

I

arrangement).

Loss of ICS power to EF-V30A/B is backed up by a safety

grade automatic controller.

If in the unlikely event that the EF-V30's

L

l

t

. -

-

_ _ - -

- ._.

.

-

.

-

.

-

_-

-.

,

.

24

stick closed, recent modifications (for the long term upgrade of

EFW) provide for a mechanical (operator local control) bypass around

the EF-30's until the Cycle 6 (refueling after restart) startup.

Abnormally low water levels in the OTSGs should not occur but if it

does there is no isolation of the main steam isolation valve or EFW

flow control valve.

(No EFW discharge isolation valves exist except

for flow check valves.) The steam line rupture detection system

(SLRDS) responds only from low pressures (less than 600 psig) in

pairs of steam line piping and actuation affects only main feedwater

to the affected (ruptured) OTSG.

(The isolation of EFW by SLRDS was

removed as a result of the TMI-1 restart hearing.)

In case emergency feedwater is unavailable (beyond design basis

event) the high pressure injection (HPI) system (makeup pump to RCS)

is required by procedure to be used in a feed and bleed cooling

mode.

The HPI pumps have a shutoff head above maximum systen

operating pressure.

6.3 Conclusion

Based on this limited review, the inspector concluded that the

present design of TMI-1 would preclude a serious abnormal event

occurring from a loss of all main feedwater with a spurious SLRDS

actuation.

First, actuation of the SLRDS merely isolates main

feedwater, not emergency feedwater.

Second, the EFW system is

diverse and comprised of two safety grade motor driven pumps and one

turbine driven pump.

Third, recent EFW system modifications provide

two separate alternate paths of emergency feedwater into each OTSG

if the standard paths are unavailable; this lineup would have to be

accomplished by local manual action until after the next refueling

outage.

Finally, the HPI system is capable of supplying water to the

reactor for a feed and bleed mode of cooling if emergency feedwater

was not available.

The HPI pump shutoff head is above maximum system

operating pressure.

7.0 Corporate Inspection

During this inspection, the resident inspector conducted an inspection at

the licensee's corporate office (Parsippany, New Jersey) to follow up on

specific outstanding issues.

7.1 Allegation Regarding Vendor Surveillance Representative

On November 21, 1984, the Director of Quality Assurance reported to

the resident inspector that the licensee received a second allegation

concerning a vendor surveillance representative. The allegation,

similar to the allegation documented in NRC Inspection Report 50-289/

84-33, was received from a vendor representative.

It was alleged

.

. _ _ _ _ _ - _ . -___ _ _

_

_

_

_.

-_

_

-

'

.

.

-

25

.

that the same vendor surveillance representative offered to perform

,

consulting and contract services for the vendor for personal gain.

The licensee initiated another investigation to address the recent

allegation.

The inspector reviewed the documentation associated with the investiga-

tion.

The allegation by the vendor was made orally in casual

passing to a GPUNC auditor.

The vendor characterized the allegation

,

as one individual's word against another individual's word and

^

not worth pursuing.

Because the vendor did not desire to pursue the

3

allegation, the allegation could not be fully substantiated.

However,

the licensee's investigation included a telephonic contact of all

vendors that the licensee's vendor surveillance representative had

,

audited during the period in question.

The licensee's investigation did not uncover any more alleged

improperties by the vendor surveillance representative.

However,

licensee management d?cided to reassign the individual for various

performance-related reasons to another position which does not

require auditing of vendors.

In addition, the inspector reviewed corporate procedure

1000-POL-1010.2, Revision 0, effective November 15, 1982, " Code of

Business and Conflict of Interest Statement," with the Director of

Quality Assurance and other key managers. The procedure requires

certain GPUN employees to sign a statement revealing any outside

interests that would conflict with GPUN corporate objectives.

Prior

y

to this time, vendor surveillance representatives were not required

' , ~

to sign this statement.

Through dicussions with licensee represen-

tatives and a review of selected records, the inspector determined

that vendor surveillance representatives are now required to sign

the " Conflict of Interest Statement," as commited to by a licensee

representative in NRC Inspection Report 50-289/84-33.

Based on the above review, the inspector concluded that there were no

nuclear safety implications or conditions adverse to quality.

7.2 Fire Protection Modification Preliminary Engineering Design Review

(PEDR)

As part of a continued review of licensee's activities in the area

of Plant Modificaticns, the inspector attended a Preliminary

..

4

.

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. . . , . .

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, - . -

-

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. .

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.

26

Engineering Design Review (PEDR) Meeting on 10 CFR 50, Appendix R

(Fire Protection Modification). The PEDR reviewed their vendor's

evaluation on overall approach to Appendix R compliance.

The TMI-I Appendix R evaluations being performed by Gilbert / Common-

wealth have been consolidated into a single report entitled "Appen-

dix R Circuit Evaluation Summary Report." This report includes a

presentation of the level of fire protection required for compliance

with 10 CFR 50, Appendix R, selection of systems and components

required, evaluation of required circuits, and development of

proposed modifications.

The sections. dealing with the above sub-

jects provide an overview of the approach to meeting 10 CFR 50,

Appendix R at TMI-1. Most of this work is scheduled to be performed

during the next refueling outage.

The meeting was held at the GPU Corporate Office and was attended by

representatives from corporate engineering, maintenance and

construction, licensing, plant engineering and representatives from

Gilbert / Commonwealth.

(Since plant operations representatives were

unable to attend, the PEDR will be continued at a later date to

obtain operations department comments.) During this portion of the

PEDR, the project engineer presented the work on a system by system

basis.

This portion of the PEDR appeared to address all aspects of

the modifications from the regulatory requirements viewpoint.

The

inspector noted that the meeting demonstrated that there was still a

significant amount of work to be done during cycle 6 refueling as

well as some more engineering work.

In general, the inspector considered the PEDR to be a useful mechan-

ism to identify problems encountered during modification installa-

tion.

8.0 Diesel Generator Interpolar Connecting Strap Failure (Part 21 Report)

8.1 Background

The 10 CFR 21 report, dated June 3, 1985, by the Louis Allis Company

describes the failure of one interpolar connector in an emergency

diesel generator at the Calvert Cliffs Nuclear Station.

Region

based inspectors reviewed licensee corrective actions at Calvert

Cliffs Nuclear Station on June 6, 1985, as documented in reports

50-317/85-13 and 50-318/85-11. The 10 CFR 21 report identifies

TMI-1 as having two diesel generators (Colt order #205672) with

interpolar connectors.

Figure 3 (attached) is a sketch of the

TMI-Calvert Cliffs interpolar connector area and shows the signifi-

cant fatigue cracking found on the Calvert Cliffs diesel genera-

tor.

9

P

.

Laminated Iron

/

Pole Plate

l

Interpolar

Connedting Strap (Cu)

Catastrophic

.

Fatigue

Crack

,. :

Location

',<y

,e '

Weld

. . -

Damper

Bar (Cu)

Shorting

/

, , . .

Strap (Cu)

("'

g

'

j

f

.

<

,

/

Braze '

Cracked through Near Center

of Length on Eight Straps

at Calvert Cliffs

Structural

Bar

Diesel Generator Alternator

(Am6rtisseurWinding)

.

FIGURE 3

_

_

_

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-

.

. _ _

. - _ .

_

_

- _ _ - . _ - .

.

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.

27

'

8.2 Field Observations

On June 7, 1985 the same two region based inspectors reviewed

licensee corrective actions for the diesel generators at TMI-1. The

.

'

review included the method of strap removal, condition of the straps

with respect to fatigue cracking, and the licensee's evaluation of

,

potential electrical effects of strap removal.

Inspector observa-

4

tions included portions of the strap removal process, associated

quality control inspection, liquid penetrant testing and the result-

ing generator conditions.

The TMI-1 maintenance procedure for job ticket CG908 provided

details for removal of the interpolar straps including protection

,

from chips or filings and it provided for post maintenance testing

which included vibration analysis and normal Technical Specification

i

surveillance testing. The procedure provided for a cut location that

would leave a maximum stub, 1/2" long.

The inspector reviewed the

t

Calvert Cliffs fatigue crack location (as noted on Figure 3) on the

shorting strap with the TMI-1 preventive maintenance manager. As a

result, the licensee concluded that the stub length of the shorting

straps on generator "A" should be cut as close as possible to the

pole plate.

The inspector later observed cuts made to remove connecting straps

from generator "A" and noted the cut position to be properly located

to not leave a stub.

Followup of this concern by the resident inspector on June 12, 1985

resulted in the observation that the stubs previously remaining on

generator "B" were removed.

The interpolar connecting straps, as-removed from generator "B",

were examined by the inspector and found to not have midlength

cracking. The same observation, as confirmed by liquid penetrant

examination was made by licensee QC inspection personnel on straps

from generator "A".

The liquid penetrant examination report of June

4

L

10, 1985 for generator "A"

showed the general presence of weld

discontinuities, two cracked areas on the shorting straps and one

crack near the centerline of the weld.

However, the inspector

>

concluded that significant fatigue cracking, similar to that of the

Calvert Cliffs interpolar connecting straps, did not occur on the

TMI-1 straps although some cracking had initiated.

The TMI-1

maintenance actions provided for prevention of future fatigue

cracking in this area by removal of the interconnecting straps and

shorting strap stubs.

No conditions adverse to nuclear safety or inconsistent with regula-

tory requirements were identified.

i

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28

8.3 Electrical Engineering Evaluation

The inspector reviewed the licensee's engineering evaluation on the

effect, if any, of removing the interpolar connecting straps linking

the damper windings on the two emergency diesel generators, EG-Y-IA

and EG-Y-IB at the facility. The information considered by the

licensee evaluation included correspondence from the generator

manufacturer (Louis Allis letter to Colt Industries, Fairbanks Morse

Engine Division, dated June 3,1985) anc' the engineering evaluation

done at Calvert Cliffs, (Facility Change Request (FCR) 85-1025,

dated May 26, 1985).

The inspector reviewed these evaluations and concurred with these

licensees, after subsequent discussions with the generator manufac-

turer, that the removal of the interpolar connecting straps will

have no measurable affect on voltage and frequency regulation when

accepting or dropping loads.

Further, no changes involving relay

coordination were warranted. Additionally, the inspector concluded

that the removal of these interpolar connecting straps slightly

changed (increased) the negative sequence reactance and the

quadrature substransient reactance which would result in reduced

fault current for an unbalanced three phase load.

The connecting

straps make the damper winding circuitry continuous by shorting the

damper bars on the field pole faces from one pole to the next. This

arrangement is advantageous when synchronous generators of dissimilar

sizes are run in parallel; a mode that dnes not occur at TMI because

it would constitute a violation of Technical Specification require-

ments.

The inspector reviewed the data obtained from the Diesel Generator

Surveillance Procedure 1303-4.16, Revision 31, dated May 7, 1985,

and the Preventive Maintenance Procedure E-1 " Vibration Analysis for

Rotating Equipment," Revision 4, dated July 4,1981, subsequent to

the removal of the connecting straps to assure the generators

performed their intended functions satisfactorily.

No conditions adverse to nuclear safety or inconsistent with regula-

tory requirements were identified.

8.4 Conclusion

The inspectors concluded that GPUN had adequately evaluated the

effects of the removal of the interpolar connecting straps and took

appropriate followup action. The licensee was responsive to the

vendor supplied information and NRC identified concerns.

Based on

operating history of 14 similar diesels without the interpolar

connectors, the review of the licensee-identified factors involved

in this issue, input from the manufacturer, and observations of the

inspectors, the licensee satisfactorily completed preventive /

corrective actions (289/85-PT-01).

This completes the review

of the subject Part 21 report at TMI-1.

'

e

.

29

9.0 Restart Readiness

During the inspection, the resident inspectors assisted by region based

inspectors continued the review of equipment (started in NRC Inspection

No. 50-289/85-12) in selected areas to assess the readiness of the plant

for startup.

The selected areas inspected included safety related build-

ing spaces; outstanding licensee identified items in the surveillance,

maintenance and modification areas; outstanding NRC inspection findings;

and selected valve lineups.

The objective was to identify equipment

operability problems that could adversely affect safe operation of the

facility.

The results of this review are documented below.

9.1 Safety Related Building Spaces

Periodically, the inspector reviewed safety related building spaces

to identify any loose equipment, scaffolding, or other problems such

as fire hazards / housekeeping that could adversely affect the opera-

bility of safety related equipment in adjacent areas. The inspec-

tion also included a review of the following procedures and internal

correspondence which provide administrative control of such miscel-

laneous equipment stored in safety related areas.

--

Maintenance Procedure (MP) 1401-18, Revision 0, June 3, 1985,

Equipment Storage Inside Class 1 Buildings

MP 1440-Y-3, Revision 1, February 25, 1985, Scaffold Inspection

--

--

Inter-office Memorandum (Serial No. 3300-85-130), June 21,

1985, from the Manager Plant Engineering to Operations and

Maintenance Director, " Scaffolding Remaining Inside Class 1

Buildings During Plant Power Operations."

Selected areas of the following safety related buildings were in-

spected:

reactor building; auxiliary building; fuel handling

building; intermediate building; diesel generator building; and

control building.

In general, equipment storage was satisfactory and in accordance

with the above referenced procedures and memorandum. However, at

the beginning of the inspection period, the inspector identified

some areas of concern with respect to loose equipment on rollers,

loose scaffolding and loose floor grating. At that time, the

licensee was in the process of correcting these known deficiencies

in preparation for the pending June 11, 1985 criticality date.

._ _

, - .

.

30

Mechanical Engineering was in control of assuring that stored

equipment was properly tied down and residual scaffolding to remain

in place whs identified and restrained to criteria established by the

licensee.

~

Unrestrained equipment without rollers was located and positioned on

the floor at a safe distance to not adversely affect safety related

equipment if it fell over.

Equipment on rollers was restrained with

wire rope. Scaffolding was rigid and restrained to the building

walls using wire rope and cement anchors.

Loose equipment on top of

platforms or brackets was minimized and were assumed to fall and

therefore kept at a safe distance from the safety related equipment.

Fire protection engineers were actively involved in analyzing

adverse fire hazard loadings in safety related areas due to scaf-

folding platforms. There were no adverse conditions in building

spaces with respect to stored equipment or housekeeping.

As of June 28, 1985 there were no conditions adverse to nuclear

safety.

9.2 Outstanding Licensee Identified Items

The inspector reviewed selected portions of the licensee's appli-

cable corrective action tracking systems to determine if any adverse

condition for safety related equipment operability existed.

The

inspector's review included tracking systems for open maintenance

job tickets, open exceptions and deficiencies (E&Ds) associated with

technical specification surveillances, and open plant modification

incomplete work list items.

The inspector reviewed the open job tickets and discussed all work

that had been classified as priority one, two and three. At the

completion of the review, only one job was classified as priority

one.

This job remained open only due to administrative closecut of

associated paperwork. Of the priority two and three work, the

inspector determined that the work required by these jobs would not

have an adverse affect on the plant safety if not performed prior to

returning the plant to operations.

The inspector reviewed approximately 20% of the technical specifica-

tion surveillances to ensure that the required test was performed

within the proper frequency and that test data obtained met the

procedures acceptance criteria.

In addition, the inspector reviewed

all E&Ds noted by the licensee for all current surveillances.

From

this sampling the inspector determined that the licensee was properly

conducting required surveillances and none of the noted deficiencies

or exceptions would adversely affect plant safety.

.

,

.

31

This review identified approximately 25 of 60 E&Ds outstanding

because'of needed_ procedure changes.

The inspector questioned

licensee representatives as to why so many procedure changes were

needed since the surveillance program has been implemented during the

long term shutdown.

In response, licensee personnel characterized

the changes as improvements or typographical error corrections not

affecting TS acceptance criteria or operability. Based on a limited

review, the inspector confirmed the licensee representatives' state-

ments.

The need for surveillance procedural improvements will

continue to be routinely reviewed by NRC Region I.

The incomplete work items list (IWL) was reviewed. The inspector

discussed the IWL with licensee representatives.

The licensee

adequately resolved or addressed each item on the IWL to ensure that

no adverse condition would exist due to an item remaining open. The

inspector also discussed with the licensee how or if modifications

would continue if the plant restarted.

The licensee stated the

number of modifications during plant operations would be limited.

For the control room and the reactor building, the licensee stated

that no modification work would be performed unless specifically

authorized by plant management.

The inspector found no condition that would adversely affect plant

safety in these areas.

9.3 Outstanding Inspection Findings

In conjunction with a licensee representative, the inspector re-

viewed the Region I file of outstanding inspection findings to

identify any equipment operability problems adversely affecting safe

operation of the facility.

The licensee representative identified

those items ready for review or tentative dates when items would be

ready for review.

No conditions adverse to nuclear safety were

identified.

.

9.4 Valve Lineup Verifications

As-part of the validation of the TMI-1 readiness for restart, the

NRC TMI-1 Restart Staff independently verified the position of

,

l

safety-related valves. The shift inspectors, with the aid of

auxiliary operators, verified the position of valves listed in the

'

following operating procedures:-

l

Operating Procedure (0P) 1104-1, Core Flood System;

--

OP 1104-2, Makeup and Purification;

--

,

OP 1104-4, Decay Heat Removal System;

--

4

l

OP 1104-5, Reactor Building Spray; and,

--

I

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32

OP 1101-3, Containment Integrity and Access Limits.

--

In general, the valve lists were determined to be accurate and

valves checked were in their proper position.

However, MU-V-950 was

found mispositioned, as discussed in section 2.0 of this report.

Due to the continued delay of restart (U.S. Court of Appeals for the

Third Circuit stay of the Commissions restart decision), this effort

was stopped but the review would normally include additional safety

related systems.

No conditions were identified that would preclude safe operation of

the facility.

10.0 TMI-1 Replica Simulator

Region I staff reviewed the concerns described in a letter, dated April

5,1985 from Mrs. Marjorie M. Aamodt to the Chairman, Atomic Safety and

Licensing Board, regarding alleged design problems with the training

simulator (TMI-I Replica Simulator) being installed at TMI-1.

The letter

indicated that the capabilities of the simulator have been undermined as

a result of some decisions by GPUN management in opposition to the advice

of engineers assigned to the project.

The letter also stated that Mrs.

Aamodt had the name of an engineer who resigned because of these deci-

sions.

Subsequent to staff discussions with Mrs. Aamodt, the wife of the engi-

neer was contacted.

She indicated that her husband (the subject engi-

neer) was unavailable for two to three months because of travel. The

information the wife provided was somewhat different from the information

provided by Mrs. Aamodt in her letter.

For example, the wife indicated

that:

her husband's decision to leave GPUN employment was totally for

--

personal reasons;

--

her husband's feeling was that GPUN was doing a good job on the

simulator project; and,

--

she believes the contrasting information may have came from a next

door neighbor.

Region I intends to discuss this matter with the engineer when he is

available in two or three months.

This area is unresolved pending NRC staff discussions with the former

GPUN engineer (289/85-19-02).

,

. _ - . . - .

-

-

- - - - -

-

, - . -

._

_

.-

-

-

_ . -

_

,. .

.

33

a

j

11.0 Follow-Up on Previous Inspection Findings

.

The following items were reviewed to assure that the licensee took

l

adequate corrective action in a timely manner and/or met their commit-

ments as stated in applicable inspection reports.

4

11.1 (Closed) Inspector Follow Item (289/82-BC-01 through 06): NRC

Region I staff to review for adequacy hot functional test procedures

(TP 600 series and below) low physics test procedures (TP 700

series) and power esculation test procedures (TP 800 series) and

'

related licensee test results evaluation.

i

The review of the preoperational (up to hot functional testing) test

4

procedures and test results evaluation was completed as documented

in NRC Inspection Report 50-289/85-16.

The review for technical

adequacy of the TP 700 and TP 800 series procedures was intially

+

completed as documented by NRC Inspection Reports 50-289/84-01,

84-06 and 84-14. A re-review of the current revisions of these

procedures was completed in Inspection Report 50-289/85-18.

Imple-

mentation of these test procedures along with a review of licensee

i

test result evaluations will be followed as a part of the TMI-1

l

Restart Staff' inspection program and specific inspection plans.

.

11.2 (Closed) Inspector Follow Item (289/82-BC-54, 61, 63 and 83-BC-17

j

and 83-14-04):

Specific licensee conditions to be incorporated into

the TMI-1 Restart Hearing License Amendment.

Detailed review of all applicable and proposed license conditions is

documented in paragraph 5.0.

r

11.3 (Closed) Inspector Follow Item (289/83-BC-15):

Restart License

,

Condition on Probation Period for Licensee's Training Qualification

[

,

and Requalification Test Program.

This proposed license condition (2.C.12) subjects the licensee's

training program to an in depth audit by independent auditors ap-

)

proved by the Director of the Office of Nuclear Reactor Regulation

'

(NRR).

By letters, dated October 1, 1982 and May 3, 1983, the

licensee provided NRR information related to the qualification of

.

their proposed auditor (Data Design Laboratories, Inc. (DDL)). By

E

letter, dated April 9, 1984, the Director of NRR approved DDL as the

board mandated independent auditor.

In accordance with this licensee

,

'

condition, the probationary period was to last two years after

'

- restart of the unit. The work of the auditor will be subject to

further NRR review.

In response to Board concerns that generated this proposed licensee

condition, Region I continued to conduct licensed and non-licensed

i

training inspections on at least an annual basis and in some cases

more frequently supplemented by special reviews such as the Operator

.

5

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34

,

Readiness Inspection (50-289/84-05).

The resident inspectors have

l

periodically factored these concerns into their routine inspections.

'

The planned shift inspector coverage is oriented toward looking at

operator performance that is a result of performance oriented

,

training.

This inspection coverage (except the shift assignments)

will continue during the two year probation period.

In summary, the licensee properly implemented commitments made and license

conditions existing or proposed as a result of the TMI-1 restart hearing.

12.0 Exit Interview

.

The inspectors discussed the inspection scope and findings with licensee

management at the exit interviews conducted on June 7 and June 28, 1985.

The following licensee personnel attended the final exit meeting:

J. Colitz, Plant Engineering Director, TMI-l

--

T. Dunn, Quality Assurance / Operations /Radiologia1 Control Supervisor

--

H. Hukill, Director of TMI-1

--

C. Incorvati, GPUN, TMI Audits Supervisor

--

R. Neidig, TMI-1 Communications

--

C. Smyth, TMI-1 Licensing Manager

--

R. Toole, Operations & Maintenance Director, TMI-I

--

As discussed at the meeting, the inspection results are summarized in the

.

cover page of the inspection report.

The licensee representatives

indicated that none of the subject matter discussed contained proprietary

information. With the issuance of a licensee letter certifying the

,

safety grade qualification of the BIRO system, the inspector noted that

there were no obstacles (physical or administrative) to the safe restart

of the unit.

Unresolved Items are matters about which information is required in order

to ascertain whether they are acceptable items, violations or deviations.

Unresolved item (s), discussed during the exit meeting, are documented in

paragraphs 3.2, 5.2 and 10.0.

Inspector Follow Items are matters which were established to administra-

tively follow open issues based on licensee or staff commitments frem the

TMI-1 restart hearing.

Inspector follow item (s), discussed during the

exit meeting, are documented in paragraphs 5.0 and 11.0.

t

.. *

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No.

50-289/85-19

Docket No.

50-289

.

License No.

DPR-50

Priority --

Category C

Licensee:

GPU Nuclear Corporation

Post Office Box 480

Middletown, Pennsylvania

17057

Facility At:

Three Mile Island Nuclear Station, Unit 1

Inspection At:

Middletown, Pennsylvania

Inspection Conducted:

May 31, 1985 - June 28, 1985

Inspectors:

N. Blumberg, Lead Reactor Engineer, Region I

J. Bryant, Senior Resident Inspector (Oconee), Region II

B. Burgess, Project Inspector, Region III

E. Gray, Lead Reactor Engineer, Region I

0. Haverkamp, Technical Assistant for TMI-1 Restart,

Region I

  • T. Peebles, Senior Resident Inspector (Turkey Point),

Region II

M. Schaeffer, Reactor Engineer, Region I

R. Urban, Reactor Engineer, Region I

P. Wen, Reactor Engineer, Region I

F. Young, Resident Inspector (TMI-1), Region I

Contractor

>

Personnel:

  • B. Gore, Research Scientist, Battelle PNL

J. Huenefeld, Research Engineer, Battelle PNL

  • Participation was limited, generally, to site familiariza-

tion training and facility orientation.

Approved By:

Aw

7/r7 /Y

h

[R. Conte,TMI-1RestaQManager

Date

TMI-1 Restart Staff

Division of Reactor Projects