Marked-up Allegation Investigation Repts 4-84-A-06/21 & 172, Rev 3,re Allegations A-126 & A-291 Concerning Tomkins- Beckwith Not Maintaining Matl Traceability on Supplemental Steel Used W/Pipe Hangers & SupportsML20133A068 |
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Waterford |
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08/29/1984 |
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NRC |
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ML17198A272 |
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References |
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RTR-NUREG-0787, RTR-NUREG-787 4-84-A-06-21-01, 4-84-A-6-21-1, A-126, A-291, NUDOCS 8510020125 |
Download: ML20133A068 (2) |
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Category:INVESTIGATION REPORTS
MONTHYEARML20211H0291986-08-0101 August 1986 Synopsis of Investigation Rept 4-84-043(S).Major Areas Investigated:Alleged Knowledge of Util President & Senior vice-president Nuclear Operations of Util Internal Investigation of Marijuana Use,Prior to 841120 ML20209G8531985-03-14014 March 1985 Inquiry Rept Q4-84-049.Major Areas Investigated:Allegations Re Intimidation of Util Employee by Util Const Manager. Inquiry Closed.Portions Deleted ML20195F3471985-02-26026 February 1985 Partially Withheld Investigation Rept 4-84-043.Contradictory Statements by Jm Cain,Rs Leddick & RP Barkhurst Noted. Major Areas Investigated:Alleged Concealment of Drug Abuse by Reactor Operators ML20210U8751985-02-13013 February 1985 Investigation Rept 4-83-030 on 831215.Major Areas Investigated:Allegations Re Improper Torquing of Bolts Associated W/Emergency Diesel Generator by Licensee.Torque Values Not Listed for Specific Bolts ML20133A0681984-08-29029 August 1984 Marked-up Allegation Investigation Repts 4-84-A-06/21 & 172, Rev 3,re Allegations A-126 & A-291 Concerning Tomkins- Beckwith Not Maintaining Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports ML20132G4301984-08-29029 August 1984 Allegation Investigation Repts 4-84-a-06/21 & 172,Rev 3,re Allegations A-126 & A-291 Concerning Tompkins-Beckwith Not Maintaining Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports.No Potential Violations Noted ML20137A3841984-08-17017 August 1984 Inquiry Rept Q4-84-036 on 840803.Area of Inquiry:Util Receipt of Falsified Applicant Resume ML20132H0931984-07-18018 July 1984 Allegation Investigation Repts 4-84-A-06/8,30 & 32,Draft 2 Re Allegations A-113,A-135 & A-137 Concerning Need for Review of Concrete Placement Records,Based on Ebasco Svcs, Inc 821209 Memo & Problems Noted in Nonconformance Repts ML20132H1051984-07-17017 July 1984 Allegation Investigation Repts 4-84-a-06/8,30 & 32,Draft 1 Re Allegations A-113,A-135 & A-137 Concerning Need for Review of Concrete Placement Records Based Ebasco Svcs,Inc 821209 Memo & Problems Noted in Nonconformance Repts ML20137U8471984-07-11011 July 1984 Allegation Investigation Repts 4-84-A-06/21 & 172,Rev 2 Re Allegations A-126 & A-291 Concerning Tompkins-Beckwith Failure to Maintain Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports ML20132G3991984-07-11011 July 1984 Marked-up Allegation Investigation Repts 4-84-A-06/21,172, Rev 2,re Allegations A-126 & A-291 Concerning Tompkins- Beckwith Not Maintaining Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports ML20132G6711984-07-11011 July 1984 Marked-up Allegation Investigation Repts A-84-A-06/8,30 & 32 Re Allegations A-113,A-135 & A-137 Concerning Need for Review of Concrete Placement Records,Based on Ebasco Svc,Inc 821209 Memo ML20137V0011984-07-10010 July 1984 Allegation Investigation Repts 4-84-A-06/21 & 172,Rev 1 Re Allegations A-126 & A-291 Concerning Tompkins-Beckwith Failure to Maintain Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports ML20132G4131984-07-10010 July 1984 Marked-up Allegation Investigation Repts 4-84-A-06/21 & 172, Rev 1,re Allegations A-126 & A-291 Concerning Tompkins- Beckwith Not Maintaining Matl Traceability on Supplemental Steel.No Potential Violations Noted ML20137T5021984-06-27027 June 1984 Marked-up Allegation Investigation Repts 4-84-A-06/21 & 172, Rev 0 Re Allegations A-126 & A-291 Concerning Tompkins- Beckwith Failure to Maintain Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports ML20137T6871984-06-27027 June 1984 Allegation Investigation Repts 4-84-A-06:21 & 172,Rev 0 Re Allegations A-126 & A-291 Concerning Tompkins-Beckwith Failure to Maintain Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports ML20137V6341984-06-25025 June 1984 Rev 0 to Allegation Investigation Repts 4-84-A-06/114,184b, 184f,184o & 184p Re Allegations A-226,A-306b,A-306f,A-306o & A-306p Concerning Traceability Requirements of Permanent Attachment Matl Welded to Class 1 & 2 Piping ML20137T3751984-06-20020 June 1984 Draft 2 of Allegation Investigation Rept 4-84-A-06 Re Allegations A-126 & A-291 Concerning Failure to Maintain Matl Traceability on Supplemental Steel Used W/Pipe Hangers & Supports.No Potential Violations Noted ML20132E1461984-06-0606 June 1984 Rev 1 to Allegation Investigation Rept 4-84-A-06-53 Re Allegations A-158 & A-272 Concerning Issues Raised in Ebasco 830609 Memo on Ja Jones Const Co Qa/Qc Documentation. Expanded Review Performed by Util Adequate ML20140G5891984-02-24024 February 1984 Supplemental Inquiry Rept Q4-83-015(S) Re Alleged Intimidation of QC Personnel.Portions Deleted ML20140G5761983-11-0101 November 1983 Inquiry Rept Q4-83-015 Re Alleged Intimidation of QC Personnel.Portions Deleted ML20140G5701983-03-17017 March 1983 Inquiry Rept Q4-83-006 Re Util Harassment of QC Inspector. Portions Deleted ML20140G5571982-10-0808 October 1982 Inquiry Rept Q4-82-023 Re Alleged Discriminatory Hiring Practice at Facility.Portions Deleted ML20140G5501982-08-17017 August 1982 Inquiry Rept Q4-82-014 Re Alleged Discrimination by Tompkins-Beckwith,Inc.Portions Deleted 1986-08-01
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000382/19990201999-10-21021 October 1999 Insp Rept 50-382/99-20 on 990815-0925.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support Activities IR 05000382/19990141999-10-19019 October 1999 Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Major Areas Inspected:Operator Requalification Training Program PNO-IV-99-038A, on 990929,restart of Waterford 3 Occurred. Cause Identified as Failed Seal Water Heat Exchanger Baffle. New Battle & Seal Assembled Were Installed & Reactor Coolant Pump 2B Was Returned to Svc Satisfactorily1999-10-0101 October 1999 PNO-IV-99-038A:on 990929,restart of Waterford 3 Occurred. Cause Identified as Failed Seal Water Heat Exchanger Baffle. New Battle & Seal Assembled Were Installed & Reactor Coolant Pump 2B Was Returned to Svc Satisfactorily IR 05000382/19990181999-09-29029 September 1999 Insp Rept 50-382/99-18 on 990830-0902.Violations Noted.Major Areas Inspected:Implementation of NRC-approved Fire Protection Program IR 05000382/19990191999-09-27027 September 1999 Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted. Major Areas Inspected:Plant Support PNO-IV-99-038, on 990910,operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.New Baffle & Seal Assembly Were Installed & Plant Was Returned to Power Operations on 9908101999-09-15015 September 1999 PNO-IV-99-038:on 990910,operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.New Baffle & Seal Assembly Were Installed & Plant Was Returned to Power Operations on 990810 IR 05000382/19990151999-09-14014 September 1999 Insp Rept 50-382/99-15 on 990719-23 with in Ofc Insp Until 0819.No Violations Noted.Major Areas Inspected:Assessment of 10CFR50.59 Safety Evaluation Program & Review of Previous Insp Findings Involving Tornado Missile Protection IR 05000382/19990071999-09-0808 September 1999 Insp Rept 50-382/99-07 on 990601-11.Noncited Violations Identified.Major Areas Inspected:Operations IR 05000382/19990161999-09-0101 September 1999 Insp Rept 50-382/99-16 on 990704-0814.Noncited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support PNO-IV-99-032A, on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plant Sd.New Baffle & Seal Assembly Was Installed1999-08-12012 August 1999 PNO-IV-99-032A:on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plant Sd.New Baffle & Seal Assembly Was Installed IR 05000382/19990101999-08-11011 August 1999 Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Major Areas Inspected:Solid Radioactive Waste Mgt & Radioactive Matl Transportation Programs PNO-IV-99-032, on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plan Shutdown.Resident Inspectors Will Monitor1999-08-0303 August 1999 PNO-IV-99-032:on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plan Shutdown.Resident Inspectors Will Monitor IR 05000382/19990131999-07-15015 July 1999 Insp Rept 50-382/99-13 on 990523-0703.Noncited Violations Noted.Major Areas Inspected:Aspects of Operations,Maint, Engineering & Plant Support Activities IR 05000382/19990121999-06-21021 June 1999 Insp Rept 50-382/99-12 on 990524-27.No Violations Noted. Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000382/19990111999-06-18018 June 1999 Insp Rept 50-382/99-11 on 990524-28.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radwaste Effluent Mgt Program,Status of Effluent Radiation Monitors & Counting Room Instruments ML20196C9461999-06-15015 June 1999 Notice of Violation from Insp Completed on 990422.Violation Noted:Licensee Failed to Consider Info Contained During Background Investigation Before Granting Temporary Unescorted Access to Contractor Employee IR 05000382/19990091999-06-0303 June 1999 Insp Rept 50-382/99-09 on 990411-0522.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20209B8581999-05-25025 May 1999 EN-98-046A:on 990524,staff Withdrew Proposed Civil Penalty in Amount of $110,000 Issued to Licensee.Action Based on Severity Level III Problems Associated with ECCS & Afws IR 05000382/19990061999-05-18018 May 1999 Insp Rept 50-382/99-06 on 990405-09.Non-cited Violations Identified.Major Areas Inspected:Issue Previously Identified During Architect Engineering Insp Which Documented NRC Insp Rept 50-382/98-201 IR 05000382/19990051999-05-10010 May 1999 Insp Rept 50-382/99-05 on 990228-0410.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support ML20206F4801999-05-0303 May 1999 Insp Rept 50-382/99-08 on 990405-07.One Apparent Violation Noted & Being Considered for Escalated Eas.Major Areas Inspected:Plant Support Including Licensee Access Authorization Program IR 05000382/19990041999-04-0909 April 1999 Insp Rept 50-382/99-04 on 990301-19.One Violation Occurred & Being Treated as Noncited Violation.Major Areas Inspected: Review of Licensee Implementation of Facility ISI Program & Followup Review of Reactor Trip Breaker Performance IR 05000382/19990021999-04-0505 April 1999 Insp Rept 50-382/99-02 on 990117-0227.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support Activities IR 05000382/19990031999-03-26026 March 1999 Insp Rept 50-382/99-03 on 990308-12.Violations Noted.Major Areas Inspected:Radiation Protection Program Focusing on RF09 Refueling Outage Activities IR 05000382/19990011999-03-0303 March 1999 Partially Deleted Insp Rept 50-382/99-01 on 990125-29 & 0208-12 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Plant Support ML20207F1581999-03-0303 March 1999 Notice of Violation from Insp on 990125-29 & 0208-12. Violation Noted:Inspector Determined That Waterford Audits SA-98-025.1 & SA-98-036.1,dtd 980916,were Conducted by Individuals Not Independent of Program Mgt Being Audited IR 05000382/19980181998-12-21021 December 1998 Insp Rept 50-382/98-18 on 981018-1128.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000382/19980151998-11-24024 November 1998 Insp Rept 50-382/98-15 on 980906-1017.No Violations Noted. Major Areas Inspected:Aspects of Operations,Maint, Engineering & Plant Support Activities PNO-IV-98-054, on 981117,plant Shutdown Greater than 72 H Due to Unidentified Leak.Investigations by Licensee Verified That Leakage Occurred from RCP 2b Seal Area1998-11-19019 November 1998 PNO-IV-98-054:on 981117,plant Shutdown Greater than 72 H Due to Unidentified Leak.Investigations by Licensee Verified That Leakage Occurred from RCP 2b Seal Area IR 05000382/19980131998-11-17017 November 1998 Insp Rept 50-382/98-13 on 980831-0901 & 981005-08.No Violations Noted.Major Areas Inspected:Maint Using Guidance of Temp Instruction 2515/137, Insp of Medium-Voltage & Low-Voltage Power Circuit Breakers ML20155D0561998-10-29029 October 1998 Insp Rept 50-382/98-17 on 981005-08.Violations Noted. Major Areas Inspected:Routine Review of Radiation Protection Program Activities ML20155D0411998-10-29029 October 1998 Notice of Violation from Insp on 981005-08.Violation Noted: Inspectors Identified That Radiation Surveys to Evaluate Extent of Radiation Levels Had Not Been Performed Prior to Operations Personnel Entering Area ML20155D5111998-10-27027 October 1998 Partially Withheld Insp Rept 50-382/98-16 on 980914-18. Violations Noted.Major Areas Inspected:Licensee Physical Security Program.Portions Withheld (Ref 10CFR2.790) ML20155D5021998-10-27027 October 1998 Notice of Violation from Insp on 980914-18.Violation Noted: Performance Tests of Protected Area Detection Sys Identified That Two Detection Zones Did Not Meet Design Criteria to Detect Test Individuals ML20154L0831998-10-0909 October 1998 Notice of Violation from Insp on 980726-0905.Violation Noted:On 980721,NRC Inspectors Found Door 206,vital Area Portal,Unlocked & Not in Alarm at Central Alarm Station ML20154L1281998-10-0909 October 1998 Insp Rept 50-382/98-14 on 980726-0905.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support PNO-IV-98-045, on 980926,Unit 3 Declared Unusual Event of Hurricane Warning in St Charles Parish.River Bend Station Continued to Operate at Full Power Since Hurricane Force Winds Were Not Predicted in Vicinity of Site1998-09-28028 September 1998 PNO-IV-98-045:on 980926,Unit 3 Declared Unusual Event of Hurricane Warning in St Charles Parish.River Bend Station Continued to Operate at Full Power Since Hurricane Force Winds Were Not Predicted in Vicinity of Site PNO-IV-98-040, on 980917,licensee Commenced Shutdown of Reactor in Order to Replace Pressurizer Code Safety Valve That Had Been Experiencing Increased Leakage.Licensee Plans to Restart Facility on 9809231998-09-18018 September 1998 PNO-IV-98-040:on 980917,licensee Commenced Shutdown of Reactor in Order to Replace Pressurizer Code Safety Valve That Had Been Experiencing Increased Leakage.Licensee Plans to Restart Facility on 980923 IR 05000382/19980121998-08-21021 August 1998 Insp Rept 50-382/98-12 on 980614-0725.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000382/19992011998-07-27027 July 1998 Insp Rept 50-382/99-201 on 990511-0619.No Violations Noted Major Areas Inspected:Engineering IR 05000382/19980101998-07-20020 July 1998 Insp Rept 50-382/98-10 on 980622-26.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Access Authorization,Alarm Stations,Protected Area Access Control of Personnel & Packages & Vehicles ML20236P2431998-07-10010 July 1998 Notice of Violation from Insp on 980503-0613.Violation Noted:On 980521,AP UNT-005-013 Was Not Implemented in That Impairment to Fire Door D150 Was Not Controlled IR 05000382/19980091998-07-10010 July 1998 Insp Rept 50-382/98-09 on 980503-0613.Violations Noted.Major Areas Inspected:Aspects of Operations,Maint,Engineering & Plant Support Activities.Fire Door in Reactor Auxiliary Bldg Was Observed to Be Open W/No Controls in Place ML20249A9611998-06-16016 June 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $100,000.Violation Noted:Licensee Identified That Calculated Peak Fuel Cladding Temp Would Have Exceeded 2200 F Using Licensing Basis Analysis & HPSI Flow ML20151R9131998-06-0909 June 1998 EN-98-046:on 980616,notice of Proposed Imposition of Civil Penalty in Amount of $110,000 Issued to Licensee.Action Based on Level III Problem Involving HPSI Flow Issues at Waterford-3 Facility IR 05000382/19980081998-05-29029 May 1998 Insp Rept 50-382/98-08 on 980322-0502.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20248F6801998-05-29029 May 1998 Notice of Violation from Insp on 980322-0502.Violation Noted:Licensee Failed to Establish Adequate Procedures for Operation of EDG When in No or Low Electrical Loading Condition in That No Specific Guidance Provided IR 05000382/19980991998-04-24024 April 1998 SALP Rept 50-382/98-99 for 961201-980321 ML20217B6731998-04-21021 April 1998 Notice of Violation from Insp on 980201-0321.Violation Noted:On Past Occasions,Engineer Operated Governor Valve on Emergency Feedwater Turbine W/O Direction or Concurrence of Shift Superintendent or Control Room Supervisor ML20217B6981998-04-21021 April 1998 Insp Rept 50-382/98-06 on 980201-0321.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering 1999-09-08
[Table view] |
Text
6 REVISION 3 08/29/84 SSER Task: Allegation A-126, A-291 Reference No.: 4-8.4-A-06/21, 172 Characterization: It is alleged that Tompkins-Beckwith (T-B) did not maintain material traceability on the supplemental steel used with pipe hangers and supports. The supplemental steel refers to additional steel used to install pre-fabricated pipe hangers and supports.
Assessment of Alleration: Bergen-Patterson (B-P) furnished pre-fabricat ad 9 piping supports anc hangers. EBASCO furnished the supplemental structural 3 steel for use by T-B during installation of the piping hangers and supports. y.
The supports and supplemental material were designed to Seismic Category I J requirements. 10CFR50,AppendixBqualityassurancerequirementsfillows identificationofanitemtobemaintainedbyrecordstrcea/ jotheitem.
As a result, Certificates of Compliance furnished by the verified (
- that the material furnished was properly certified in accordance with the 3 applicable ASTM Specifications.
The EBASCO Material Inspection Receiving Report (MIRR) was used to verify B that the correct material was received. A Requisition on Warehouse (ROW) was used by T-B to obtain release of the material from EBASCO. %
The initial T-B program was established to provide traceability of the paint to be used on the supplemental steel. A material control number p .
was steel stenciled on each item listed on the R0W. If the material was i cut into smaller pieces, the number was to be transferred accordingly, e R
After number stamping, the material was painted by a subcontractor. 2, Different colored paint was used with yellow signifying non-safety b non-permanent material. The other colors used designated safety related 5*
l material. $
In 1978, -T-B agreed to a contract change with EBASCO to extend the paint material traceability system to also include steel traceability. Because the change came after the original program had been in operation, a number of implementation problems occurred and providing full steel traceability proved difficult.
In late 1983, the contract between EBASCO and T-B was changed to reflect a decision by EBASCO to abandon attempts to provide supplemental structural steel traceability using material control numbers. The supplemental structural steel certification program continued to be in effect as it had been throughout the project.
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REVISION.1 06/21/84 SSER Task: Allegations A-149; A-151; A-152; and A-153 Reference Number: 4-84-A-06/44/46/47/48 Characterization: The allegation is that four nonconformance reports (NCRs) were signed by QC inspectors performing work prior to their being certified.
It is further alleged that one NCR shows a lack of inspection reports for installation of seismic Category I stairs.
Assessment of Allegation: In a review of records for this allegation, the NRC staff identified seven NCRs in an EBASCO QAIRG letter that contained deficiencies that were undetected in previous record reviews. Four of these NCRs (W3-5563, W3-5564, W3-5565 and W3-5973) were the ones alleged to contain inspections performed by J. A. Jones QC inspectors prior to their certifica-tions. The other three were addressed in Allegation A-416. These NCRs were reviewed to answer any deficiency and to evaluate the disposition and corrective action required should the allegation prove true. Review of the Ebasco QC inspectors certifications were also performed to assure qualification of the applicable inspecting personnel.
NCR W3-5563, dated January 24, 1983, involved bolting on the bridge crane of the fuel handling building (FHB). It was signed-off by a J. A. Jones Construction Company trainee prior to that person's certification as a Level I inspector. Attachments to NCR W3-5563 indicated that the trainee inspected the work on August 27 and 28, 1979 and on November 6, 1979. The individual in question was certified as a trainee on July 9, 1979 and certified as a Level I inspector on November 7, 1979. Original bolting deficiencies were documented in an NCR in 1979. The bolting inspection was originally signed off in the presence of a Level II inspector, who countersigned the inspection reports on february 4, 1983.
The recommended disposition was signed on January 31, 1983, and corrective action was completed in accordance with recommended disposition and signed off on February 4,1983.
The corrective action taken was not appropriate. Reinspection should have been performed by a certified inspector and properly signed-off by EBASCO QC.
The incident was reported to NRC as PRI Report 111, and later designated as SCD 78.
NCR W3-5564 dated January 24, 1983, involved lack of records to verify the inspection of bolting and welding by J. A. Jones on Seismic Category I stairs between elevations -34.75 and -8.0' in the Fuel Handling Building.
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l The recommended disposition included inspection of welds and bolted connections by:EBASCO QC. The disposition was signed c:, February 2,1983 and revised on March 15, 1983, since the inspection revealed that several of the
- bolted connections were loose and that in most of the connections, the bolts L had not been tightened sufficiently to bring the mating surfaces in full contact."
~
l All bolting was completed and inspected on September 23, 1983. Welding
't - repairs for four welds were completed and inspected on July 26, 1983. The NCR was signed off by the QAE on November 7, 1983. Dispositioning of the NCR was I not acceptable in regard to inspection of welds without removing the paint.
The' paint precludes adequate visual inspection of the welds.
The' NRC staff also checked the deficiency for reportability in regard to L. 10CFR50.55(e). The stairs were determined to be in an area where they could not affect safety-related structures, systems, or components if they failed and therefore this deficiency was not reportable.
-NCR W3-5565, dated January 24, 1983, involves witnessing and acceptance of reeving of the FHB bridge crane by a QC inspector trainee who was not im certified as a Level I inspector at the time of inspection.
' The QC inspector was certified as a trainee for Structural and Reinforcing Steel'on July 9, 1979 and.for Level I, Concrete, Structural and Reinforcing ,
" Steel, on November 7, 1979. Inspections were performed on August 15, 17 20
- 21, and 22, 1979.
L The reconinended disposition was for E8ASCO QC to reinspect the work by
- j. a certified inspector- and process the required documentation.
The manufacturer adjusted, checked and tested the crane during January 1983.
The certification was signed off by a start up engineer on January 24, 1983 (late entry on warning bell made February 4,1983). Although the staff reviewed the start up engineer's certification and found it adequate, the inspection ,
performed by the QC inspector was not in the file. Final corrective action 11, 1983. The deficiency was was concluded reported to the NRC and as signed PRI-III off by(the QAE on Julylater designated as SCD-78).
NCR W3-5973, dated March 28, 1983, involved the welding inspection of a FHB tornado door frame which was performed by an inspector prior to his being certified as a QC inspecter, Structural / Reinforcing Steel Level I or a Visual Inspector. He was certified as a level I, Structural / Reinforcing Steel on August 24, 1977, and Visual Inspector on October 18, 1977. The inspection was made during the period August 3, 1977 through October 14, 1977. Also, there were no inspection reports for weld repairs made on welds on the door ;
frame. The weld repairs were a result of. work done to plumb the door frame as documented in an NCR in 1977.
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A l- M/ 6' The recommended disposition was to reinspect'the weld areas and document the results. If repairs were required, they were to be made in accordance with applicable procedures and reinspected. Since no weld repairs were required, the final corrective action was "use-as-is."
Review of the certifications of the responsible inspectors showed no deficiencies other than those above.
The NRC staff's review of this issue indicated that the allegation is valid regarding inspection by personnel prior to their certification, and incomplete records identified in these NCRs, but the deficiencies noted in the records reviewed will not affect plant safety. Evaluation / inspection of the issues identified no hardware problems, except for NCR W3-5564, where it was found
.that a set of FHB stairs had several bolting connections which were loose, and that in most connections the bolts had not been tightened to bring the mating surfaces in full contact. Inspection of the stairs showed that they were not located in an area where their failure would have caused damage to safety-related equipment. The records reviewers had considered the generic aspects of inspector certification. The reviewers pointed out discrepancies in regard to inspector certification and incomplete or missing records. The NRC staff concludes that this allegation has no safety significance or generic implications.
m Potential Violation: Each NCR represents a violation of contractor procedure requirements that, in turn, represents violation of 10 CFR 50, Appendix B, Criterion XVI. '
Actions Required: None.
References
- 1. Letter from G. Hill to J. Cyzrko dated June 6,1983,
Subject:
Review of Seismic Class I Concrete Records.
- 2. NCR W3-5563, dated January 24, 1983.
- 3. NCR W3-5564, dated January 24, 1983.
- 4. NCR W3-5565, dated January 24, 1983.
- 5. NCR W3-5973, dated March 28, 1983.
- 6. NCR W3-1728, dated November 5, 1979.
- 7. NCR W3-545, dated August 3, 1977
- 8. Certifications of Inspectors involved with NCRs.
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- 9. EBASCO Procedures WOC-101 and 169.
- l. 10. -EBASCO Drawings LOV 1564 G-850.and 1564 3845.
- . 11. ANSI N45.2.6-1973
,, i Statement' Prepared by:
1 Reviewed By:
Team Leader Date a
Reviewed By:
Site Team Leader (s) Date Approved By:
Task Mantgement Date
.-