ML20132A984

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Insp Rept 50-483/96-11 on 961013-1123.Violations Noted.Major Areas Inspected:Licensee safety-conscious Operations,Sound Engineering Practices & Appropriate Performance of Maint, Surveillance & Plant Support Activities
ML20132A984
Person / Time
Site: Callaway Ameren icon.png
Issue date: 12/12/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20132A953 List:
References
50-483-96-11, NUDOCS 9612160407
Download: ML20132A984 (16)


See also: IR 05000483/1996011

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-483

License No.:

NPF-30

Report No.:

50-483/96-11

Licensee:

Union Electric Company

Facility:

Callaway Plant

Location:

Junction Highway CC and Highway O

Fulton, Missouri

Dates:

October 13 through November 23,1996

Inspectors:

D. G. Passehl, Senior Resident inspector

F. L. Brush, Resident inspector

Approved By:

W. D. Johnson, Chief, Project Branch B

ATTACHMENT:

Supplemental Information

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9612160407 961212

PDR

ADOCK 05000483

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PDR

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EXECUTIVE SUMMARY

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Callaway Plant

NRC Inspection Report 50-483/96-11

Operation.s

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The .:spectors identified that the component cooling water system normal operating

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procedure did not provide adequate guidance for system operation. The failure of

the procedure to provide adequate guidance was a violation (Section O3.1).

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The licensee identified that an operator inadvertently sent a blended flow of borated

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water to the reactor coolant system rather than the spent fuel pool. The failure to

follow the spent fuel pool normal operating procedure was a noncited violation

(Section 04.2).

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The licensee identified that an equipment operator incorrectly placed a worker

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protection tag on and pulled the closing power fuses for the centrifugal charging

Pump A supply breaker. This was a noncited violation of the workman's protection

assurance tagging procedure (Section 04.3).

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The quality assurance department performed an effective review of the plant

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shutdown and cooldown for the refueling outage (Section 07.1).

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Enaineerina

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The inspectors identified that the component cooling water system Traire A

temperature was below the lower limit specified in the Final Safety Analysis Report

(Section E1.1).

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Report Details

Summarv of Plant Status

The reactor began this inspection period shutdown for Refueling Outage 8.

On October 12,1996, an unplanned engineered safety features auxilialy feedwater

actuation occurred. The operating main feedwater pump tripped on high discharge

pressure. All systems responded as required.

On November 11,1996, operators closed the main generator output breaker to end

Refueling Outage 8. The refueling outage was completed in 31 days.

Later on November 11,1996, at approximately 15 percent reactor power, a feedwater

isolation occurred which caused a turbine trip. In addition, high vibrations experienced on

reactor coolant Pump B, following the turbine trip, required the operators to shut down the

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reactor.

On November 12,1996, operators placed the unit back on line after plant personnel

balanced the pump. On November 17,1996, the plant reached full power.

l. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

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and safety-conscious. Problems that occurred during shutdown (Section 01.2) and

startup (Section 02.1) are described below.

Plant status, operating problems, and work plans were appropriately addressed

during daily turnover and plan-of-the-day meetings. Plant testing and maintenance

requiring control room coordination were properly controlled.

01.2 Inadvertent Auxiliarv Feedwater Actuation

a.

Insoection Scoce (71707)

The inspectors reviewed the circumstances surrounding an inadvertent engineered

safety features auxiliary feedwater actuation.

b.

Observations and Findinas

On October 12,1996, during the plant shutdown for tha refueling outage, an

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engineered safety features auxiliary feedwater actuation occurred. The operating

main feedwater pump tripped on high discharge pressure and caused a motor driven

auxiliary feedwater system actuation.

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Control room personnel were performing a control rod drop time test in accordance

with Procedure ETP-SF-STOO1," Control Rod Drop Time Test," Revision O. In order

to support this testing, plant operators realigned the main feedwater system to

prevent automatic actuation of the feedwater system isolation valves and other

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components. The realignment resulted in isolation of the main feedwater system

from the main feed pump discharge check valves to the main feedwater isolation

valves. Main feedwater Pump A was aligned to recirculate to the main condenser.

With the feedwater system in this lineup, pressurizing of the feedwater system

occurred from the combination of system residual heat and some smallleakage

through feedwater heater extraction steam isolation valves. This caused actuation

of pressure switches for high discharge pressure of main feedwater Pump A.

Actuation of the pressure switches tripped the operating main feedwater pump and

caused the auxiliary feedwater actuation.

Plant operator response was appropriate. All safety equipment performed as

designed. The licensee convened an Event Review Team to investigate the facts

and possible causes. The licensee identified a number of corrective actions that will

be reviewed when the inspectors evaluate the associated Licensee Event Report.

c.

Conclusions

The inspectors concluded that the licensee's initial response to the unanticipated

motor driven auxiliary feedwater actuation was satisfactory.

01.3 Plant Startuo Observations

a.

Inspection Scope (71707)

The inspectors observed portions of the reactor startup following the refueling

outage,

b.

Observations and Findinas

The licensee conducted thorough pre-evolution briefings. Operator self checking

was good. Shift personnel used proper communications. The shift supervisor

exhibited good command and control. Licensee management was present in the

control room for major evolutions associated with the startup. Management

exhibited good involvement. The inspectors verified compliance to the Technical

Specifications and Final Safety Analysis Report requirements by reviewing logs,

touring main control boards and reviewing status boards.

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Operational Status of Facilities and Equipment

O2.1 Inadvertent Steam Generator Hi-Hi Level and Turbine Trio

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a.

Insoection Scoce (71707)

The inspectors reviewed the licensee's response to an inadvertent hi-hi steam

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generator level turbine trip and a plant shutdown required by Technical

Specifications due to high vibrations on reactor coolant Pump B.

b.

Observations and Findinas

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On November 11,1996, with the reactor at approximately 15 percent power, an

inadvertent hi-hi level on Steam Generator A occurred which resulted in a turbine

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trip. Following the turbine trip, a motor-driven auxiliary feedwater system actuation

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and a feedwater isolation system actuation occurred. All systems responded as

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required.

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The event occurred while the operators were attempting to stabilize steam

generator levels following closure of the feedwater regulating bypass valves.

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Following the turbine trip, vibrations on reactor coolant Pump B increased to just

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over 15 mils with a rate of increase greater than two 2 mils in one hour.

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The operators entered procedure OTO-BB-00002," Reactor Coolant Pump Off-

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Normal," Revision 8. The operators tripped the reactor coolant pump and shut

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down the plant to Mode 3 as required by Procedure OTO-BB-00002 and Technical

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Specification 3.4.1.1.

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The licensee convened an Event Review Team to investigate the facts and possible

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causes. The licensee identified a number of corrective actions that will be reviewed

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when the inspectors evaluate the associated Licensee Event Report.

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03

Operations Procedures and Documentation

O3.1 Inadeauste Component Coolina Water System Normal Operatina Procedure

a.

Inspection Scooe (71707)

The inspectors reviewed normal operating Procedure OTN-EG-00001," Component

Cooling Water System," Revision 14. This was a result of an inspector concern

about system operation.

b.

Observations and Findinas

During a tour of the plant, the inspectors noted that the component cooling water

flow rate to the lube oil coolers for centrifugal charging Pump A and safety injection

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Pump A was above the normal range delineated on their respective flow

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instruments. Additionally, the component cooling water temperature at the outlet of

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the lube oil coolers for these pumps was approximately 50 F. The minimum

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component cooling water temperature in the Final Safety Analysis Report

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operability analysis for the components serviced by component cooling water.

Section 9.2.2.2.3 was 60'F. Section E1.1 of this report discusses the licensee's

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The component cooling water system is comprised of two independent safety

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related trains. Each train, in addition to its safety related loads, could be aligned to

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provide cooling water to nonsafety related components in the service loop. At the

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time of discovery, Train B was in service providing cooling water to the service

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loop. Train A was in service to support earlier operation of centrifugal charging

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Pump A. With centrifugal charging Pump A secured, component cooling water

Train A was not required to be in operation.

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Procedure OTN-EG-1, Step 2.7, stated that, during normal operation, the maximum

component cooling water flow should not exceed 110 percent of the flow listed in

Attachment 1 of the procedure. The basis for the 110 percent value was unclear.

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The attachment only listed minimum component cooling water flows. The table did

not provide a range of flows for the components. During normal system operation,

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the component cooling water system flow through the various components listed in

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the attachment routinely exceeded 110 percent of the minimum value. Additionally,

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the flow sometimes also exceeded the " green band" on the local flow instruments.

During the inspectors' tour on November 12,1996, the inspectors found the

component cooling water flow from the centrifugal charging Pump A lube oil cooler

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to be pegged high on a local instrument. This was above the " green band" upper

limit of 34,500lbm/hr on the local instrument. The minimum flow listed in

Attachment 1 of Procedure OTN-EG-1 was 27,500lbm/hr. The actual flow through

the tube oil cooler exceeded 27,500 lbm/hr by more than 10 percent.

The inspectors identified that the procedure did not adequately address component

cooling water system operation with respect to component flow and temperature

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during normal plant operation. Procedure OTN-EG-OOOO1 was inadequate in that it

did not give information required for proper operation of the component cooling

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system as required by Technical Specification 6.8.1.a. This is a violation of

Technical Specification 6.8.1.a (483/9611-01).

The licensee was reviewing the engineering flow balance for the system to verify

the throttle positions for component cooling water valves that regulate flow to

various safety related equipment. During the initial review, the licensee believed

that no operability concerns existed.

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c.

Conclusions

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The inspectors concluded that the procedure for operating the component cooling

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water system was inadequate.

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04

Operator Knowledge and Performance

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O4.1 Refuelina operations

a.

Insoection Scope (71707)

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The inspectors observed fuel assembly movement during core offload.

b.

Observations and Findinas

Communications between personnel on the refueling machine, in the control room,

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and at other stations were good. Personnel actions were conservative when

moving fuel assemblies. Foreign material exclusion controls around the reactor

cavity and on the refueling machine were satisfactory.

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04.2 Inadvertent Iniection of Borated Water to the Reactor Coolant System

a.

Jnspection Scope (71707)

The inspectors reviewed an event in which a reactor operator inadvertently injected

borated water into the reactor coolant system.

b.

Observations and Findinas

On November 20,1996, while intending to inject blended makeup flow to the spent

fuel pool, the reactor operator injected the flow to the reactor coolant system.

After several minutes the reactor operator noticed the volume control tank level

start to increase and secured the flow. Reactor coolant system average

temperature decreased approximately 1.3 F as a result of the borated water

addition.

The reactor operator's immediate action was to dilute the reactor coolant system

with 263 gallons of makeup water to restore temperature. There were no other

adverse effects on the reactor coolant system.

The licensee initiated an investigation of the event using the corrective action

process. The inspectors found that the licensee's ir:itial and followup corrective

actions were appropriate.

The inspectors reviewed the procedure for filling the spent fuel pool. Normal

Operating Procedure OTN-EC-OOOO1," Fuel Pool Cooling and Cleanup System,

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Revision 11, Step 5.8.9, required that the operator select hard close on the

following handswitches when filling the spent fuel pool with blended flow:

BG-HIS-1108, volume control tank outlet header BGFCV0110B handswitch

BG-HIS-1118, volume control tank inlet header BGFCV0111 B handswitch

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Instead of taking the handswitches to hard close, the operator went to hard open by

mistake. This opened the volume control tank outlet and inlet header Valves

BGFCV0110B and BGFCV0111B, respectively. The opening of these valves

established the flow to the reactor coolant system through normal charging.

The failure to adhere to Procedure OTN-EC-00001 Step 5.8.9 is considered a

violation of the licensee's operating procedures. This licensee-identified and

corrected violation is being treated as a noncited violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (483/9611-02),

c.

Conclusions

The inspectors concluded that the failure to transfer borated water to the spent fuel

pool was due to personnel error. The licensee's actions were appropriate.

04.3 Worker Protection Tao Placed on the Wrona Comoorsnt

a.

Inspection Scope (71707)

The inspectors reviewed an unplanned Technical Specification 3.5.2 entry when an

equipment operator pulled the closing power fuses for centrifugal charging Pump A

supply Breaker NB0104. The equipment operator was supposed to pull the closing

power fuses for spent fuel pool cooling Pump A supply Breaker NG0104.

b.

Observations and Findinas

While intending to place a worker protection tag on closing power fuses for spent

fuel pool cooling Pump A supply Breaker NG0104, an equipment operator

incorrectly placed the worker protection tag on the closing power fuses for

centrifugal charging Pump A supply Breaker NB0104. This action made centrifugal

charging Pump A inoperable and placed the plant in a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> shutdown action

Statement per Technical Specification 3.5.2.

When the equipment operator pulled the closing power fuses for centrifugal

charging Pump A supply Breaker NB0104, the control room received an engineered

safety features actuation system alarm. Control room personnel realized that the

equipment operator pulled the wrong closing power fuses and contacted the

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equipment operator. Control room personnel directed the equipment operator to

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replace the closing power fuses for centrifugal charging Pump A. The licensee

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started the centrifugal charging pump to ensure operability and exited the Technical

Specification Action Statement. The charging pump was inoperable for

approximately 9 minutes.

The licensee initiated an investigation of the event using the corrective action

process.

The licensee identified the following causes:

Failure to perform dual verification of the tag. The equipment operator did

not arrange for a secrand person to verify that the tag was on the correct

component.

Misreading of the component identification number.

Failure to read the noun description of the component being tagged.

Administrative Procedure ODP-ZZ-00310, " Workman's Protection Assurance

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Tagging", Revision 2, Step 4.1.10.3, required that the method and order specified

on the tagout control sheet be followed when hanging tags.

The tagout control sheet for Workman's Protection Assurance 21271, Tag 2,

specified that a tag be hung on closing power fuses for spent fuel pool cooling

Pump A supply breaker. Failure to adhere to this requirement is considered a

violation of the licensee's administrative procedures. This licensee-identified and

corrected violation is being treated as a noncited violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (483/9611-03).

c.

Conclusions

The inspectors concluded that the failure to pull the correct fuses was due to

personnel error. The inspectors found that the licensee's initial and followup

actions were appropriate.

07

Quality Assurance in Operations

07.1 Review of Quality Assurance Deoartment Surveillance of Plant Shutdown and

Cooldown

a.

Inspection Scope (71707)

The inspectors reviewed the quality assurance department's Surveillance

Report SP96-084 for a surveillance conducted from October 11,1996, through

October 14,1996. Quality assurance personnel performed observations of control

room activities during shutdown of the plant from Mode 1 to Mode 6 in preparation

for Refueling Outage 8.

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b.

Observations and Findinas

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Quality assurance personnel provided a good assessment of the major evolutions

that occurred during the shutdown. Quality assurance personnel observed control

rod drop time testing, the new methods employed for the plant cooldown using all

steam dumps and pressurizer auxiliary spray, and drain down of the reactor coolant

system to 6 inches below the reactor vessel flange.

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Quality assurance personnel found good use of procedures, shift turnover meetings,

pre-evolution briefings, and communications. In addition, they verified compliance

with Final Safety Ant. lysis Report and Technical Specification requirements through

work control database reviews, log reviews, and walkdowns of the main control

boards. Quality assurance personnel also identified observations that were

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appropriately documented for followup.

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c.

Conclusions

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The quality assurance department's review of the plant shutdown and cooldown for

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the refueling outage was good.

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11. Maintenance

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M1

Conduct of Maintenance

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M 1.1 General Comments - Maintenance

a.

Insoection Scooe (62703)

The inspectors observed all or portions of the following work activities:

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Work Document W174699- Replace Reactor Coolant Pump D internals;

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Work Document P402569- Replace Reactor Coolant Pump D motor;

Work Document C557751 - Replace Main Feedwater Pump B discharge

check valve;

Work Document C557753- Replace Main Feedwater Pump A discharge

check valve;

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Work Document C580902- Remove Low Pressure Feedwater Heater 2A

vent head and tube bundle;

Work Document C580884- Remove Low Pressure Feedwater Heater 2C

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vent head and tube bundle;

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Work Document C580890-Install Low Pressure Feedwater Heater 2C tube

bundle; and

Work Document C580908- Install Low Pressure Feedwater Heater 2A tube

bundle.

b.

Observations and Findinas

The inspectors found the work performed under these activities to be professional

and thorough. All work observed was performed with the work packages present

and in active use. The inspectors frequently observed supervisors and system

engineers monitoring job progress, and quality control personnel were present when

required. Housekeeping and foreign material exclusion controls were satisfactory.

M1.2 General Comments - Surveillance

a.

Insoection Scope (61726)

The inspectors observed all or portions of the following test activities:

Surveillance Procedure OSP-EJ-00003, Containment Recirculation Sump

Inspection

Surveillance Procedure OSP-EN-P001 A,Section XI - Containment Spray

Pump Operability

Surveillance Procedure MSM-AB-QVOO1, Main Steam Safety Valve Testing

b.

Observations and Findinas

Surveillance testing observed during this inspection period was conducted

satisfactorily in accordance with the licensee's approved programs and the

Technical Specifications.

M8

Miscellaneous Maintenance issues

M8.1 (Closed) Violation 483/95006-01: the licensee failed to orevent the entry of

foreion materialinto safetv-related systems as identified below:

On April 4,1995, the licensee identified a latex glove inside safety injection

system to reactor coolant system check Valve B88949A(483/95006-01al.

On April 20,1995, after the sumps had been inspected and made available

for service the NRC inspectors identified multiple pieces of foreign materialin

the containment emergency sumps (483/95006-01b).

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The inspectors observed foreign material exclusion practices during the refueling

outage and noted only minor problems, in addition, the inspectors accompanied

licensee personnel on the final closecut inspection of the containment recirculation

sumps. The inspectors found the sumps to be very clean.

Ill. Enaineerina

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Conduct of Engineering

E1.1

Comoonent Coolina Water System Water Temoerature and Flow

a.

Insoection Scope (37551)

The inspectors noted that the component cooling water system Train A temperature

was below the lower limit of 60 F specified in the Final Safety Analysis Report.

Additionally, the inspectors noted that the component cooling water flow rate to the

lube oil coolers for centrifugal charging Pump A and safety injection Pump A was

above the normal range delineated on their respective flow instruments. The

inspectors reviewed the licensee's response to these issues.

b.

Observations and Findinas

During a tour of centrifugal charging pump Room A, the inspectors noted that the

temperature of the component cooling water coming from the lube oil heat

exchanger on centrifugal charging Pump A was approximately 50*F. The

component cooling water temperature from safety injection Pump A was also at

approximately 50 F.

Also, the inspectors found the component cooling water flow from the centrifugal

charging Pump A and safety injection Pump A lube oil coolers to be above the

" green band" limit on the localinstruments. Normal Operating Procedure

OTN-EG-1, Revision 14, " Component Cooling Water," did not provide adequate

operating instructions to ensure the component cooling water system was properly

operated with respect to component flow and temperature. Section 03.1 discusses

the operational aspects of this issue.

The lower limit for component cooling water temperature in the Final Safety

Analysis Report, Section 9.2.2.2.3, was 60 F. The inspectors asked the licensee if

the low water temperature could affect the operability of the components serviced

by component cooling water. The licensee did not believe there was an immediate

operability concern based on other in-house design information in addition to the

Final Safety Analysis Report.

The licensee performed a safety evaluation which concluded that the various

components would be operable as long as the component cooling water

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temperature remained above 40 F. The licensee determined that, during periods of

cold weather, the CCW temperature would go below 60 F when operating in the

Mode 1 lineup. Following the safety evaluation, the licensee changed the minimum

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component cooling water temperature in the Final Safety Analysis Report from 60 F

to 40 F.

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The licensee was performing additional evaluations on the effect of high flow rates

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and cool water temperatures on the components serviced by component cooling

water.

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Conclusions

The inspectors concluded that the component cooling water system was not being

operated as described in the Final Safety Analysis Report due to an inadequate

procedure. The Final Safety Analysis Report was revised to reflect the allowed

minimum component cooling water system temperature.

E2

Engineering Support of Facilities and Equipment

E2.1

Review of Facility Conformance to Updated Final Safety Analvsis Report

Commitments

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A recent discovery of a licensee operating their f acility in a manner contrary to the

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Final Safety Analysis Report description highlighted the need for a special focused

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review that compares plant practices, procedures, and/or parameters to the Final

Safety Analysis Report description. While performing the inspections discussed in

this report, the inspectors reviewed the applicable portions of the Final Safety

Analysis Report that related to the areas inspected. The following inconsistency

was noted between the wording of the Updated Safety Analysis Report and the

plant practices, procedures, and/or parameters observed by the inspectors.

As discussed in Section E1.1, the inspectors identified that a discrepancy existed

between the as-built component cooling water system operation and the Final

Safety Analysis Report.

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IV. Plant SuDDort

R2

Status of RP&C Facilities and Equipment

R2.1 Containment Buildina Closecut inspection

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inspection Scope (71750)

The inspectors performed a reactor containment building housekeeping and materiel

condition inspection prior to the plant entering Mode 4 following Refueling

Outage 8.

b.

Observations and Findinas

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The inspectors found that the licensee's cleanup of the reactor containment buil ding

was satisfactory. Overall, most areas of containment were clean and free of debris,

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although the inspectors noted a small number of tie wraps, duct tape, screws, wire

and other similar items. The items were not of sufficient size and quantity to affect

safety related equipment during a design basis accident. The licensee removed

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these items during the closeout tour.

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Also, the inspectors noted boric acid crystal buildup on three valves in the safety

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injection system test lines. The licensee cleaned the valves and, after the plant was

taken to normal operating temperature and pressure, reinspected the valves. There

was no sign of additional leakage.

c.

Conclusions

The inspectors did not note any items or issues that could have affected safety

related equipment operation.

V. Manaaement Meetinos

X1

Exit Meeting Summary

The exit meeting was conducted on November 25,1996. The licensee did not

express a position on any of the inspection findings documented in this report and

did not identify any information as proprietary.

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ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. D. Affolter, Manager, Callaway Plant

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J. D. Blosser, Manager, Operations Support

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H. D. Bono, Supervising Engineer, Licensing Fuels and Site Licensing

G. J. Czeschin, Superintendent, Training

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M. S. Evans, Superintendent, Health Physics

G. A. Hughes, Supervising Engineer, independent Safety Engineering Group

K. W. Kucchenmeister, Superintendent, Design Engineering

J. V. Laux, Manager, Quality Assurance

J. A. McGraw, Superintendent, Nuclear Engineering Systems

C. D. Naslund, Manager, Nuclear Engineering

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D. W. Neterer, Shif t Supervisor

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J. T. Patterson, Shift Supervisor

J. R. Peevy, Manager, Emergency Preparedness and

Organizational Support

G. L. Randolph, Vice President, Nuclear Operations

M. A. Reidmeyer, Engineer, Quality Assurance

R. R. Roselius, Superintendent, Chemistry and Rad Waste

M. E. Taylor, Assistant Manager, Work Control

W. A. Witt, Superintendent, Technical Support

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The above personnel attended the exit meeting. In addition to these personnel, the

inspectors contacted other personnel during this inspection period.

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lNSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-483/9611-01

VIO

Inadequate component cooling water normal operating

procedure (Section O3.1)

50-483/9611-02

NCV

Failure to follow procedure during boric water transfer to

spent fuel pool (Section 04.2)

50-483/9611-03

NCV

Failure to adhere to tagout procedure (Section 04.3)

Closed

50-483/9506-01

VIO

Failure to prevent foreign materials from entering safety

related systems (Section M8.1)

50-483/9611-02

NCV

Failure to follow procedure during boric water transfer to

spent fuel pool (Section 04.2)

50-483/9611-03

NCV

Failure to adhere to tagout procedure (Section 04.3)

l