ML20057E742

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Insp Repts 50-324/93-33 & 50-325/93-33 on 930801-0903. Violations Noted.Major Areas Inspected:Maint Observation, Surveillance Observation,Operational Safety Verification, three-year Plan & Unit 1 Outage/Restart
ML20057E742
Person / Time
Site: Brunswick  
Issue date: 10/01/1993
From: Christensen H, Prevatte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20057E732 List:
References
50-324-93-33, 50-325-93-33, NUDOCS 9310130107
Download: ML20057E742 (31)


See also: IR 05000324/1993033

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NUCLEAR REGULATORY COMMISSION

UNITED STATES

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REGION 11

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101 MARIETTA STREET, N.W., SUITE 2900

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ATLANTA, GEORGIA 303234199

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Report Nos.:

50-325/93-33 and 50-324/93-33

Licensee:

Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

Docket Nos.:

50-325 and 50-324

License Nos.: DPR-71 and DPR-62

Facility Name:

Brunswick 1 and 2

Inspection Conducted: August 1 - September 3, 1993

Lead Inspector:

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R. LT Preva{Q, Sen'ior ResiderA Inspector

Daye/igned

Other Inspectors:

P. M. Byron, Resident Inspector

M. T. Janus, Resident Inspector

G. A. Harris, Project Engineer

y asnyk, Physical Security Inspector

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Approved By:.

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41."0. Christe'nsen, Chief

Dite Signed

Reactor Projects Section IA

Division of Reactor Projects

SUMMARY

Scope:

This routine safety inspection by the resident inspector involved the areas of

maintenance observation, surveillance observation, operational safety

verification, Three-Year Plan, Unit 1 outage / restart, onsite review committee,

Engineered Safety Feature System walkdown, action on previous inspection

findings, and review of licensee event reports, and Employee Concerns Program.

Results:

In the areas inspected, a violation was identified in the area of personnel

access control, paragraph 4.

A licensee identified non-cited violation was

identified in the area of incorrect valve installations on the diesel

generators, paragraph 2.

Additionally, weaknesses were identified in the

areas of procedural guidance for resetting gain adjustment factors (GAFs) on

average power range monitors, paragraph 4, and poor e rk planning and

coordination during air leakage testing on the main generator, paragraph 2.

Unit 1 - Remained in a forced outage that began April 21, 1992.

Unit 2 - Operated at 100% power for the reporting period.

9310130107 931001

PDR

ADOCK 05000324

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • K. Ahern, Manager - Operations Supp1rt and Work Control

R. Anderson, Vice-President - Brunswick Nuclear Project

G. Barnes, Manager - Operations, Unit 1

E. Blackmon, Manager - Radwaste/ Fire Protection

M. Bradley, Manager - Brunswick Project Assessment

  • H. Brown, Plant Manager - Unit 1 (Acting)

R. Godley, Supervisor - Regulatory Compliance

  • R. Grazio, Manager - Nuclear Engineering Department
  • J. Heffley, Manager - Maintenance, Unit 2

G. Hicks, Manager - Training

  • C. Hinnant, Director of Site Operations

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P. Leslie, Manager - Security

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  • J. Leviner, Manager - Nuclear Systems Engineer
  • W. Levis, Manager - Regulatory Affairs
  • R. Lopriore, Manager - Maintenance, Unit 1

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G. Miller, Manager - Technical Support

  • C. Robertson, Manager - Environmental & Radiological Control
  • J. Titrington, Manager - Operations, Unit 2

C. Warren, Plant Manager - Unit 2

  • G. Warriner, Manager - Control and Administration

E. Willett, Manager - Project Management

Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, office personnel and security force

members.

  • Attended the exit interview.

Acronyms and initialisms used in the report are listed in the last

paragraph.

2.

Maintenance Observation (62703)

The inspectors observed maintenance activities, interviewed personnel,

and reviewed records to verify that work was conducted in accordance

with approved procedures, Technical Specifications, and applicable

industry codes and standards. The inspectors also verified that:

redundant components were operable; administrative controls were

followed; tagouts were adequate; personnel were qualified; correct

replacements parts were used; radiological controls were proper; fire

protection was adequate; quality control hold points were adequate and

observed; adequate post-maintenance testing was performed; and

independent verification requirements were implemented. The inspectors

independently verified that selected equipment was properly returned to

service.

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Outstanding work requests were reviewed to ensure that the licensee gave

priority to safety-related maintenance. The inspectors observed /

reviewed portions of the following maintenance activities:

LPRM Cable Replacement

The inspector observed the troubleshooting activities associated with

the LPRM cable replacement modification PM 92-049. Work associated with

this modification involved the replacement of 124 coaxial cables, the

replacement of 16 LPRM detectors and changeout of under vessel hardline

cables with new hardline cables that were compatible with new

connectors. The LPRM cables required replacement due to degradation

that resulted in low insulation resistance values. The new cables were

designed to require minimal maintenance and are qualified for a 40 year

operating life.

After the new cables were installed, the cable connectors were left

uncovered and exposed to the drywell atmosphere. The high humidity in

the drywell atmosphere resulted in moisture collecting between the cable

wire core and insulator. The presence of moisture reduced the cable

insulation resistance below acceptable values. The licensee contacted

the cable and detector vendor and they both agreed that the low

resistance valves were caused by moisture intrusion.

It was then

decided that the moisture in each cable would be removed by heating and

vacuuming techniques.

Simultaneously, resistance readings were taken on

cable lengths between the control room cabinets and drywell penetration

and pedestal locations. The readings were compared against acceptable

values.

The licensee conducted the troubleshooting activities using OSPP-NE002,

Special Process Procedure, SRM, IRM, and LPRM Preinstallation and Post

Installation Testing, Rev. 3.

The procedure requires a nominal

resistance value of IXE10 ohms and a minimal resistance of IXE8 ohms.

In addition, values as low as IXE6 ohms are acceptable with system

engineer concurrence. At penetration QC6, fifteen of the seventeen

connectors were found to have lower than desired resistance readings

(i.e, IXE10 ohms).

It was believed that the damage was due to flexing

of the hardline cable during installation. The licensee plans to

replace the penetration during the next refueling outage.

The licensee concluded, after discussions with GE, that the resistance

readings for QC6 hardline cables were acceptable based on the margin

that exists in the LPRM calculations.

In addition, to the above

procedure, EER 90-0349 evaluated insulation resistance readings that

were lower than acceptance values. The EER stated that the IXE10 ohm

acceptance value was extremely conservative and that LPRM insulation

resistance values found to be greater than IXE9 ohms should be

considered acceptable. GE concurred with the conclusions of this EER

during a recent telecon with the licensee.

The inspector reviewed the

EER and considered it acceptable.

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The inspector, along with the system engineer, reviewed warehouse

storage conditions for the LPRM cables.

Recently, a cable was withdrawn

from its storage location and could not be used due t: moisture

intrusion. The system engineer accompanying the inspector noted that he

had earlier observed some cables stored in plastic bags which were not

sealed. The cables observed during this inspection were found sealed in

plastic to prevent air and moisture intrusion.

Preventive Maintenance on Diesel Generator No. 2

On August 3, DG No. 2 was taken out of service to perform the 18 month

preventive maintenance inspection, 0-MST-DG0500R, and other minor

inspections of maintenance activities. As stated in the previous

monthly inspection report (50-325,324/93-30), the diesel's main and

thrust bearings were examined for symptoms of frictional heating similar

to that observed on DG No. 1.

No discoloration was observed. A

boroscopic examination of the diesel's cylinders did not reveal any

damage. The examination did reveal some polishing in the 4R and 6R

cylinders.

On August 3, the licensee discovered that the newly installed 2-MUD-V101

jacket water head tank drain valve was installed in the reverse

direction as indicated by the flow arrow on the valve body. This item

was documented by the licensee in ACR 93-260.

Previous maintenance on DG No. I had found the jacket water temperature

control valve installed in the reverse direction. A review of this

second event found that the direct replacement instructions had required

the installation of two welded couplings % line with the valve.

The

licensee discovered that the craft perso.:.wl had used an unapproved

alternate installation method to reduce the number of welds by

eliminating the two couplings. These discrepancies were discovered and

corrected immediately by the licensee prior to declaring the diesel

operable.

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On August 3, during an investigation of lube oil flange leakage on DG

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No. 2 valve 2-LO-RV11, the licensee discovered that the engine driven

lube oil pump relief valve had been installed in the vertical instead of

horizontal position. The above valve was removed and reinstalled in the

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correct position. The system engineer performed an analysis to

determine the effect oc diesel engine operability of the misoriented

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relief valve. The analysis determined that the valve did not affect the

operability of the diesel engine.

The inspector reviewed and agreed

with this analysis. The relief valve had been in the incorrect position

since the previous diesel generator outage in June, 1993.

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While performing post maintenance housekeeping duties in the vicinity of

the DG No. 2 starting air system, workers heard air escaping from the

system. An investigation by maintenance personnel revealed that a cover

plate gasket on the control air filter had blown out. Discussions with

the diesel maintenance supervisor revealed that this event has occurred

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several times since the recent installation of the control air filter

modification.

The inspector questioned the system engineer to determine if the correct

gasket was being used for the application. The system engineer was

unable to conclusively answer this question. The inspector then

reviewed the procurement process for the cover plate gasket. A parts

quality classification and commercial grade dedication evaluation report

was reviewed and the installed gasket was found to be correct for this

application. The licensee contacted the vendor who confirmed the

licensee's conclusions.

It was determined that the gasket had failed

because the cover plate had not been adequately torqued. An inspection

of this system also revealed that a gasket for check valve V-58 was

leaking.

This gasket was also replaced.

During an attempt to conduct the operability run, the diesel generator

would not start due to improper valve alignment of the control air

filters. The valves were realigned and the diesel started as required.

The inspector reviewed the clearance restoration instructions and found

that they were incorrect in that the restoration instructions had

required valves to be shut in both filter dryer trains. The inspector

verified that valve misalignment had occurred during system restoration

after the above gasket replacement.

The licensee reviewed the appropriate procedures used to perform the

diesel maintenance and clearance preparation tasks. The deficiencies

were identified and immediately corrected. Additionally, the licensee

convened special sessions of STAR refresher training to remind personnel

of the need to conduct activities that are important to safety in a

careful and accurate manner.

TS 6.8.1.a, requires that written procedures shall be established,

implemented and maintained covering activities such as maintenance and

clearances. The instructions for the installation of DG valves, 2-MUD-

V101, 2LO-RVll, and DG No. I jacket water temperature control valve, and

the DG No. 2 control air filter restoration instruction were inadequate.

The failure to have adequate valve installation and clearance

restoration instructions is a violation of TS 6.8.1.a.

This violation

will not be subject to enforcement action because it meets the criteria

specified in Section VII.B of the Enforcement Policy, NCV 93-33-02.

Nuclear Service Water System Leaks

The inspector, in Inspection Report 325,324/93-20, discussed a leak and

repairs on the Unit I nuclear service water system piping. The leak was

repaired and returned to service on July 30. After returning the system

to service, a new leak of approximately I dpm was identified on a six

inch welded flange approximately three feet after the vital header taps

off the main nuclear header. A temporary soft patch was placed over

this leak until permanent repairs could be accomplished.

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On August 13, an additional small leak, approximately 80 dpm, developed

in the 1 C conventional SW pump discharge line to the nuclear header

near the pump isolation valve. The licensee removed the Unit I nuclear

water system from service on August 26 and performed code repairs on

both of the above leaks. This work was completed and the system was

returned to service on August 31.

The inspector visually inspected each of the above leaks, the temporary

patch, and the repairs. A visual inspection was performed on the

repairs for the first leak which resulted in the replacement of a three

foot section of concrete lined carbon steel piping with copper nickel

piping. An inprocess inspection found that the defects had been removed

on the second leak and a code class weld repair had been performed. The

workmanship and quality of both efforts were examined and determined to

be satisfactory.

The inspector additionally performed a followup inspection on the

backfill over the piping repairs completed in July on the nuclear

service water system.

The efforts were satisfactorily completed without

problems.

Cracks in Core Support Shroud

The licensee previously identified cracks in the Unit I reactor vessel

core shroud in the heat affected zones of the H-3 and H-4 welds. This

was discussed in Inspection Report 325,324/93-30. The licensee took a

boat sample from each affected weld area to determine the initiating

cause. A Region II specialist was on site during the week of August 16

to review the UT data and the preliminary analysis of the boot sample.

The results of his inspection are contained in Inspection Report

325,324/93-34. The H-3 and H-4 weld boat samples were taken between

August 19 and 21. The boat samples were obtained by the electric

discharge machinery process and were 0.80 inches deep.

On August 24, GE informed the licensee that inspection of the H-3 boat

sample revealed that the crack passed all the way through the boat

sample. This finding invalidated the assumptions contained in the

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bounding analysis which the licensee had previously received because

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crack depth was found to be greater that 0.80 inches and exceeded the

0.40 inches obtained by UT examination.

On August 26, the licensee met with the NRC to discuss their recent

findings and revised plans to determine the crack depth. GE discussed

their analysis and the NRC questioned the validity of several

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assumptions used in the analysis. The NRC stated that a more

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substantive analysis would be required to justify plant restart and

operation. The licensee stated that they plan to use robotics to

perform further UT examinations.

The licensee has contracted with GE to build three devices similar to

the one used on the foreign BWR (KKM in Switzerland) described in GE

RICSIL 054. Two units will be used for data gathering and the third

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will be available as a spare. The licensee has contracted with KKM to

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obtain the service of a UT operator experienced in this procedure to

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perform the H-3 UT. The anticipated delivery for these machines is

September 15. The licensee anticipates that it will take approximately

ten days to setup, perform the UT examination, and evaluate the data.

The licensee plans to take an additional boat sample or samples as

needed to validate the UT results. They anticipate an extensive

analysis to support a justification for continued operation and have

developed a means of implementing a permanent repair. An overall outage

schedule delay of approximately four weeks is anticipated.

The inspector has observed and been involved in the above activities on

a daily basis and will continue to follow this issue and the licensee's

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actions until it is resolved, Inspector Followup Item:

IFI 325,324/

93-33-03.

Main Generator Seal Oil Leak

On August 17, an Air Leakage Test on the Unit 1 main generator was

performed using Administrative Instruction AI-117, Rev. O, Guidance for

Troubleshooting Safety Related Equipment. This test was part of a pre-

operational test of the main generator prior to unit startup. Test

instructions were written on a Troubleshooting Change Form (TCF)93-105

and approved by operations. The TCF was reviewed and discussed with

operations personnel, however a detailed pre-job briefing was not

performed.

In preparation for the test, valve and electrical lineups were completed

by operations personnel, temporary air valve, gauges were installed and

turbine lube oil and seal oil systems were started.

After informing the control room, maintenance personnel opened service

air valve 1-HC-b-03 to purge and pressurize the main generator. This

purging effort was to be maintained for approximately four hours.

During the purging effort the maintenance engineer noticed that the

sight glass for the hydrogen seal oil float trap was full. The engineer

became concerned because during previous testing, oil had backed up into

the hydrogen detraining section and had flooded the generator.

Because

of this concern, the maintenance engineer pressurized the generator to

operate the float trap. As air entered the generator the pressure began

to slowly increase.

Two maintenance personnel monitored sight glasses in low point drains

from the generator, exciter, and hydrogen detraining sections. The TCF

erroneously instructed maintenance to throttle close the float trap

bypass valve when the air pressure reached 10 psig.

The 10 psig value

was based on conversations with the vendor. At approximately 7 psig,

the engineer noticed that the sight glass was approximately half full

and steady. The maintenance crew did not take immediate action to

reduce pressure or close the float trap bypass valve because the sight

glass level was not decreasing. The pressurization of the generator was

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sufficient to force the oil into the air detraining section, out the

vent and onto the floor. This resulted in approximately 150 gallons of

oil spilling on the turbine building floors at elevations 55', 38' and

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20' and a small amount of oil seeping outside the turbine building at

ground elevation.

Subsequent investigation by the licensee revealed the TCF instructions

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required the float trap valve bypass (1-S0-H-05) to be manipulated by

the maintenance personnel to maintain oil level in the sight glass.

However, during this test, this valve was under clearance and the crew

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members were not authorized to manipulate the valve. Another

contributing factor to this event was the need to complete the test in

an expeditious manner due to the unavailability of travelling support

maintenance crew members to assist if problems were discovered as a

result of the test.

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The licensee is currently conducting a root cause analysis of the

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incident.

Investigations by the inspector revealed several deficiencies

in the conduct of this maintenance activity. These deficiencies

included inadequate communication between maintenance and operations

personnel, inaccurate procedural instructions, misinterpretation of

clearance procedure requirements, and inadequate scheduling and

coordination of work activities. The licensee is currently identifying

and implementing corrective actions to prevent a recurrence of this

event. The licensee documented this event in ACR 93-275. The above

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occurrence, though not safety-related, indicates a weakness in work

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planning, coordination and procedures. The inspector will review the

licensee's ACR and root cause analysis to determine the adequacy of

corrective actions for this item.

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Surveillance Observation (61726)

The inspectors observed surveillance testing required by Technical

Specifications. Through observation, interviews, and record review the

inspectors verified that: tests conformed to Technical Specification

requirements; administrative controls were followed; personnel were

qualified; instrumentation was calibrated; and data was accurate and

compl ete. The inspectors independently verified selected test results

and proper return to service of equipment.

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The inspectors witnessed / reviewed portions of the following test

activities:

2-MST-RWCU 22M

RWCU High Differential Flow Trip Unit Channel

Calibration

2-PT-24 1-2

Service Water Pump and Discharge Valve

Operability Test

2-MST-RHR 26M

Residual Heat Removal / Core Spray Low Reactor

Pressure Permissive Trip Unit Channel

Calibration

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The inspector noted that procedures were available and used during the

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above tests. Maintenance personnel also appeared to be knowledgeable on

all aspects of the observed tests.

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Violations and deviations 'were not identified.

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Operational Safety Verification (71707)

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The inspectors verified that Unit 1.and Unit 2 were operated in

compliance with Technical Specifications and other regulatory-

requirements by direct observations of. activities, facility-tours,

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discussions with personnel, reviewing of records and independent

verification of safety system status.

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The inspectors verified that control room manning requirements of

10 CFR 50.54 and the Technical Specifications were met. Control

operator, shift supervisor, clearance, STA, daily and standing

instructions and jumper / bypass logs were reviewed to obtain information

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concerning operating trends and out of service safety systems to ensure

that there were no conflicts with Technical Specification Limiting

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Conditions for Operations.

Direct observations of control room panels

and instrumentation and recorded traces important to safety were

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conducted to verify operability and that operating parameters were

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within Technical Specification limits. The inspectors observed shift

turnovers to verify that system status continuity was maintained. The

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inspectors also verified the status of selected control room

annunciators.

Operability of a selected Engineered Safety Feature division was

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verified weekly by ensuring that:

each accessible valve in the flow

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path was in its correct position; each power supply and breaker was

closed for components that must activate upon initiation signal; the RHR

subsystem cross-tie valve for each unit was closed with the power

removed from the valve operator; there was not leakage of major

components; there was proper lubrication and cooling water available;

and conditions did not exist which could prevent fulfillment of the

system's functional requirements.

Instrumentation essential to system

actuation or performance was verified operable by observing on-scale

indication and proper instrument valve lineup, if accessible.

The inspectors verified that the licensee's HP policies and procedures

were followed. This included observation of HP practices and a review

of area surveys, radiation work permits, posting and instrument

calibration.

The inspectors verified by general observations that:

the security

organization was properly manned and security personnel were capable of

performing their assigned functions; persons and packages were checked

prior to entry into the PA; vehicles were properly authorized, searched

and escorted within the PA; persons within the PA displayed photo

identification badges; personnel in vital areas were authorized;

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effective compensatory measures were employed when required; and

security's response to threats or alarms was adequate.

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The inspectors also observed plant housekeeping controls, verified

position of certain containment isolation valves, checked clearances and

verified the operability of onsite and offsite emergency power sources.

Alternate Safe Shutdown Drill

An Alternate Safe Shutdown (ASSD) drill was conducted on the morning of

August 19. The drill was observed by the licensee, individuals from the

Nuclear Assessment Department (NAD), and a regional and resident

inspector. The drill was conducted to evaluate the ability of operators

to safely shutdown the plant using 0-ASSD-02 Alternate Safe Shutdown

Procedure, Rev. 12. The drill scenario required operators to simulate

an evacuation of the control room due to a fire.

The inspector observed the operators performing the functions of shift

supervisor, reactor building operator, and remote shutdown panel

operator.

In addition, two drill evaluators were observed and

evaluated. The inspector noted that only one evaluator had been

assigned to evaluate two operators. At the beginning of the drill this

did not provide adequate coverage since both operators were performing

actions rapidly and simultaneously as dictated by the drill scenario.

The inspector and the evaluators experienced some difficulty following

drill evolutions due to infrequent briefings provided by the operators

and the inability to listen to sound-powered phone conversations between

operators positioned at various stations throughout the plant.

At times the inspector observed an operator perform steps in the

procedure without waiting for adequate feedback from evaluators. The

evaluators did not consistently provided feedback to the operators to

simulate plant response to the operators' actions.

For example, the

ASSD procedure required operators to cooldown the plant by opening

safety relief valves, but evaluators were observed giving incorrect

plant responses to changes in reactor water level and reactor pressure.

The inspector also observed that an evaluator was not present while an

operator completed a procedural step to secure shutdown cooling. The

inspector verified that the operator completed the step successfully.

The drill, while realistic, did not contain faults or equipment

malfunctions to create abnormal conditions requiring the shift

supervisor to demonstrate problem solving, decision making and exercise

command and control skills or the ability to reestablish communications.

Inclusion of these faults would have enabled evaluators to better assess

the crew's ability to safely shutdown the plant under changing

conditions. However; the inspector noted that the shift supervisor

demonstrated good command and control throughout the drill. The

licensee informed the inspector that the ASSD job performance measures,

which are use to evaluate an operator's ability to perform a significant

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operational or safety task, contain faults and malfunctions. The

resident inspector concluded that the drill was conducted adequately and

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that the operators demonstrated the ability to shutdown and cooldown the

plant.

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Hurricane Preparedness

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The inspector previously identified, in Inspection Report 325,324/93-27,

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a weakness in the licensee's review of Lessons Learned from Hurricane

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Andrew. The licensee re-addressed this issue by reviewing the major

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items, concerns, and structures in the Turkey Point report and

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determining their applicability to Brunswick. They then developed plans

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and compensatory measures to address these items. The inspector

reviewed the licensee's revised procedures and concluded that they

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addressed the potential hurricane effects on non-safety structures,

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equipment, and buildings important to the operation of the plant. The

licensee's initial efforts on this issue as reported in the previous

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monthly inspection report was not considered thorough.

However, after

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discussing the issue with the licensee in detail, their reassessment and

response was considered aggressive.

In addition, an INP0 assist visit

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which focused on hurricane preparedness was held the week of August

23rd, and included participation by members of the Turkey Point EP

staff. The licensee stated that the visit was very beneficial.

Several

supporting procedures are in the process of, or are scheduled to be

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revised based on the results of this visit.

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On August 26, during the INP0 assist visit, an emergency preparedness

exercise was conducted using a hurricane scenario. The inspector

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observed portions of this exercise and noted that the drill progressed

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smoothly with good communications and response actions by all team

members. The inspector also noted that some difficulties and confusion

existed over when to call in relief team members and suspend all outside

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activities. These deficiencies were also identified by the licensee and

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will be formally proceduralized in the future revisions of the

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procedure. The licensee concluded that the drill was a good test of the

revised procedures and plan to incorporate lessons from this drill and

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the observations of INPO team members into a planned revision of the

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hurricane preparedness procedures.

On August 30, 1993, the licensee had an opportunity to put into practice

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some of the lessons learned in hurricane preparedness when Hurricane

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Emily approached the general vicinity. The site was placed under a

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hurricane watch on August 29. The inspector reviewed the licensee's

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Emergency Response Plan and Procedures to insure that they were

preparing for the imminent approach of Hurricane Emily. At that time,

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the hurricane was approximately 350 miles from the site.

The licensee

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implemented their plan with Administrative Instruction AI-68, Brunswick

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Nuclear Plant Response to Severe Weather Warnings, Revision 9, and

Abnormal Operating Procedure A0P-13.0, Operation During Hurricane, Flood

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Conditions, Tornado, or Earthquake, Revision 11. The inspectors

observed all licensee preparations made for the storm and found them to

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be satisfactory. Outside equipment was tied down or removed if it had

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the potential to become a missile or overturn and damage other

equipment. Teams were established for Control Room, Plant, TSC, and OSC

manning if required. The inspector performed site-wide inspections and

attended the licensee's preparation and status meetings to ensure that

the site was being prepared for the storm. The inspector performed

operational tests of the NRC cellular telephone and HF radio system on

August 30. As a precautionary measure, Region II dispatched a four

wheel drive vehicle with three support personnel to the site at 11:00 AM

on August 30. Region II manned the Emergency Response Center at the

Atlanta Regional office at 4:00 PM and the site was manned for around-

the-clock coverage with two resident inspectors. On the morning of

August 31, all indications were that Hurricane Emily would pass to the

East of the site and approximately 100 miles out to sea on a NNW track.

At that time, a decision was made to send the Regional Response

personnel to the Surry Plant in Virginia.

The storm passed the area and

hit the North Carolina coast near Cape Hatteras late on August 31. The

hurricane watch was terminated at 11:00 am on August 31.

i

U2 Non-conservative Settina of APRM Gain Ad.iustment Factors

In conjunction with the Brunswick power up-rate project, the

licensee conducted a sodium tracer injection test on July 2, to

determine the calibration constants for the main steam flow

elements. The meter differential for the main steam flow elements

had not been revised since the initial calibration, and the

current value was believed to be inaccurate due to wear on the

nozzle plate over the past 15 years. The sodium tracer test data

was to be used to determine the feedwater flow rate.

The new

feedwater flow rate was then to be used to determine new

calibration constants for the main steam flow elements. This

would ensure that feedwater flow indication and main steam flow

indications were in agreement.

The testing and analysis was conducted by GE. The Unit 2 testing

was conducted on July 2, with the unit operating at 100% indicated

power. The unit remained operating at 100% indicated power until

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July 14, when preliminary test results were released by GE. The

1

preliminary results indicated a non-conservative inaccuracy in

feedwater flow of 1.094%. This inaccuracy corresponded to an

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increase in core thermal power of approximately 1.08%.

In

response to these results, the licensee initiated a reduction in

power from 2436 MWth to 2405 MWth, which corresponds to an actual

reactor power of less than 100% indicated. As a result of the

reduction in power, a new core thermal power reading of 2409 MWth

now corresponds to 100% power. An administrative limit of 2405

was chosen until the plant process computer could be changed to

incorporate the new information based on the test results.

Standing Instruction (SI)93-166 was established to ensure that

core thermal power would be limited to less than or equal to an

indicated 2405 MWth. The plant continued operation in this manner

until the appropriate changes to the process computer were made on

August 5.

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On August 5, while in the process of implementing the corrections

to the plant process computer, the licensee discovered that they

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had operated with non-conservative Average Power Range Monitor

(APRM) Gain Adjustment Factor (GAF) settings since the power

reduction 23 days earlier on July 14.

During the implementation

of the change in data points for the process computer, it was

discovered that the APRM GAFs had not been adjusted to correspond

with the new thermal power limit of 2409 MWth as the equivalent to

100% reactor power.

The GAF values in use were still based on the

old thermal power limit of 2436 MWth which was no longer valid.

During the time in question, while the unit operated with the APRM

GAF settings, the error went unnoticed by plant operators,

corporate maintenance engineers, plant nuclear engineers. During

this period, operators performed the required daily periodic test,

PT 1.11, Core Performance Parameter Check. The purpose of this

test is to obtain basic core parameters required by Technical

Specifications (TS) and to calibrate the APRM channels to read

greater than or equal to actual core thermal power. This test

required the operators to obtain a P1 edit of the process computer

program. The P1 edit provides the operator with a current listing

of various monitored parameters and safety limit setpoints. The

display also provides the operators with proper settings for the

APRM GAFs. The plant process computer generates these APRM GAF

settings based on a calculation using the plant's license thermal

power limit (reference value) of 2436 MWth. The test required the

operators to only verify that at least two APRM GAF settings are

less than or equal to 1.00.

The event occurred because plant personnel failed to recognize

that other parameters, such as APRM GAF setpoints, are effected by

changes to the core thermal power limit.

It was also noted that

plant procedures do not address or provide a methodology to

prevent this problem. The licensee corrected this item and issued

Standing Instruction SI 93-172 which limits thermal power to 99.5%

until the feedwater flow instrumentation can be calibrated. The

licensee also documented this issue in Adverse Condition Report

(ACR) B-93-261. The resolution of the ACR will identify the root

cause of the problem and provide corrective action to prevent

reoccurrence.

The inspector will follow up on the ACR to ensure

that the issue is properly addressed.

The item is identified as a weakness in attention to detail.

The licensee has identified that the failure to adjust the APRM

GAFs did not adversely affect the APRM setpoints input to the RPS.

The licensee has determined that the APRM setpoints were still

within TS allowable limits. The inspector independently verified

that the APRM trip setpoints were within TS tolerances.

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Access Control

During review of the licensee's security event logs, adverse condition

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reports, and discussion with licensee security personnel, several

concerns were discovered in the area of personnel access control. These

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concerns are discussed below.

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On August 2,1993, a member of the security force returned from medical

leave which started on June 17, 1993, a total of 47 days. Although the

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officer's badge was placed in " lost" status, blocking it from being

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used, a security supervisor erroneously reinstated the badge into the

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security computer. This was done despite the fact that the officer had

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not completed required chemical testing. The officer entered the

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protected area at 7:55 am until another security force member discovered

the error and the officer was removed from the protected area at

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8:34 am.

CP&L Screening Practices and Procedures 107, Screening For Level 1

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Employment, Reinstatement, dated April 22, 1993, requires completion of

chemical testing and review of the individual's activities by a

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supervisor for absences greater then 30 days. Contrary to the above,

the individual did not complete chemical testing until approximately

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11:30 am, three hours after entry into the protected area; and a

required summary of activities form was not completed until the

following day.

1

This is somewhat mitigated in that this individual's spouse is also a

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security officer, and the individual met with security management

personnel approximately three times during the period of the abse ?

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The individual remained in the random drug testing pool, but wac not

selected for random testing.

i

10 CFR 73.71(c)(1) requires these types of events to be logged within 24

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hours of their occurrence. The licensee did not log this event until

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after NRC inspectors discussed the event with members of the security

staff.

In a previous event, badge P2284 was issued 63 days after pre-access

drug screening which is required within 60 days. This was due to

personnel error which was discovered during a Quality Assurance Audit

and was properly logged.

4

This failure to properly control access to the protected area based on

requirements of 10 CFR Part 26, The Fitness For Duty Rule, failure to

adhere to the licensee's procedure, and failure to log the event in a

timely fashion is a violation of regulatory requirements. This is a

Violation: Failure to Control Plant Access (325,324/93-33-01).

Two additional events were identified which did not place the licensee

in violation but allowed the potential for violation and required

corrective action.

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On July 7,1993, a security force member failed Ceneral Employee

Training and had his badge placed in lost status at 1136 hours0.0131 days <br />0.316 hours <br />0.00188 weeks <br />4.32248e-4 months <br />. Without

the knowledge of licensee security personnel, the security contract

force chief utilized this officer at the vehicle access gate, exterior

to the protected area. This post is manned by two security force

members, one armed, one unarmed. This officer acted as the armed

officer,. but was not considered a member of the response team. On

July 12, 1993, licensee security personnel became aware of the situation

and the officer was removed from the post. During his time on duty, the

officer's security training had not expired, no violation took place.

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The licensee reviewed computer records which showed the officer's badge

in lost status. On July 12, 1993, the officer passed the GET training

and the badge was reactivated. Licensee security staff and contractor

management personnel agreed that poor judgement was exhibited by the

contractor security chief, who had a disciplinary letter placed in his

file. Security contractor personnel were advised to contact licensee

personnel for guidance in non-routine situations.

Licensee Adverse Condition Report B-93-217 dated July 9, 1993, discusses

a situation where an individual's badge was placed in lost status due to

expiration of GET training. After completing training, the individual

attempted to enter the protected area but his badge was still

deactivated. The access control officer electronically unlocked the

turnstile and allowed access into the protected area. The officer

immediately noted the error due to the advisory on the computer screen

at the entry post and removed the individual from the protected area.

'

Although no violation took place, the officer demonstrated poor

judgement.

The licensee has implemented several corrective measures to address the

types of problems discussed above.

In order to identify individuals

with the potential for being away from a continued observation program

for more then 30 days, or individuals who require chemical testing the

licensee has implemented a program to suspend access on badges that have

not been used within 30 days. A "do not issue" tag is placed on the

badge and the badge is deactivated in the security computer.

In order

to have the badge reactivated the employee must have a form completed

which shows that an ascertaining of activities has been accomplished by

the supervisor. Additionally, the employee must complete chemical

testing if required.

One violation and no deviations were identified.

5.

Three-Year Plan

The inspector reviewed the licensee's monthly management report for

July,1993. The significant accomplishments for the month of July

included implementation of the procedure for preparation, review,

approval, and performance of post modification tests; development of a

formal training program for procedure control; completion of final

evaluations for additional site facilities; and completion and submittal

of a proposed site staffing plan.

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Overall,17 action steps and project phases were completed during July.

Three initiatives were completed early and four late activities were

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also completed. Completion of five initiative actions and two project

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phases were delayed. _The design and installation of the non-segregated

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bus modification was delayed due to equipment failures during laboratory

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testing. The initiative addressing an interim modification process was

delayed because it was expanded to include all minor modifications. The

root cause analysis overview training was delayed to accommodate the

addition of new supervisors that will result from recent organizational

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changes. Review of the overall status showed that 27 initiatives and 65

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projects are currently in progress.

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The licensee, in a letter to the Regional Administrator dated August 27,

1993, noted that a revision of the three year. plan was underway and

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noted that the submittal planned for September,1993, would be delayed

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until December, 1993.

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In the inspector's July inspection report (325,324/93-30),.it was noted

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that the plans for the Work Control Center and Hands on Training Center

had been approved and were in the bid process. The inspector was

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informed in early August that corporate management had placed these

projects on hold and was having an outside consultant conduct an

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additional review of these plans. :The inspector will continue to follow'

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these and other three year projects as they progress.

6.

Unit 1 Outage / Restart

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(Closed) D-1 STSI Items

The licensee has committed to have all the Unit 1 STSI items, with the

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exception of the 26 STSI items associated with.the service water pumps

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and related hardware, completed. prior to restart. These items will be

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completed during the scheduled pump replacement. This project will be

completed by November 1994. On. June 30, 1993, 1038 STSI items were

required to.be completed prior to restart. The licensee had completed

787 of these at the end of the inspection period and plans to complete

the remaining 251 items by September 10.

Based on the licensee's

efforts and the remaining items being scheduled, this item is closed for

Unit 1.

(0 pen) Reduction in Unit 1 Corrective Maintenance Backlog

The following are the corrective maintenance backlog categories, goal,

and status as of August 31 and progress in the past month:

Indication

Goal

Status 8/31

Chanae In

Past Month

Focus systems

<650

480

-31

(on line WR/J0s)

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Indication

Goal

Status 8/31

Change In

Past Month

(cont'd)

Focus Systems

<80

216

-141

(Priority 1-4

WR/J0s)

Other Systems

<80

121

-70

(Priority 1-4

WR/J0s)

Control Room

<5

37

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Annunciators

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Operator Work

<25

65

-34

Arounds

Permanent

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0

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Caution Tags

STSI Items

<26

251

-277

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Temporary Mods

<20

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-4

A review of the above items indicates that good progress has been made

over the past month. The licensee currently has 1404 WR/J0s scheduled

to be completed prior to Unit I restart. The WR/J0s work off rate

averaged approximately 46 items per day for the past month. During the

same time period, approximately 7 items were added per day. At the

current work off rate, it is anticipated that these items should be

completed about October 1, 1993. This appears to be an achievable goal

since the curre:)t schedule shows all work complete on September 28. The

inspector will continue to track this item until restart.

License _e Scif-Assessment for Unit 1 Restart

The licensee Nuclear Assessment Department planned to conduct a two

phase assessment of Unit I readiness for restart.

Phase I of this

assessment was conducted from August 23 through August 27. The Phase II

assessment will focus on 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> control room observations and will be

conducted during startup and power ascension up to 100% reactor power.

The Phase I assessment team consisted of 13 CP&L personnel, 2

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consultants,1 INPO individual and an employee of another utility.

The

assessment focused on the areas of operations, maintenance, E&RC, and

Engineering / Technical Support. Special emphasis was placed on

determining the adequacy of management involvement, coaching and

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communications, lessons learned from the startup of Unit 2, backlog

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reduction, corrective action effectiveness, the attitude and morale of

station personnel, the use and effectiveness of the integrated schedule,

plant material condition and housekeeping, and startup readiness.

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The inspector held informal discussions with members of the assessment

team and attended two team meetings and the assessment debrief to plant

management on August 27, 1993. The assessment identified that plant

equipment and personnel were ready for restart after the following items

were completed:

integrated startup plan submitted to the NRC on November 30, 1992

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e commitments to NRC contained in CP&L letter to NRC dated July 23,

1992 are met (CIP)

e PN31 reviews for Unit 1

Unit I restart targets identified in the June 9, 1993 meeting with

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the NRC are met for WR/J0s on focus systems, corrective

maintenance, temporary modifications, control room annunciators,

permanent caution tags, and STSIs

elements for Unit I startup and power ascension needed for rod

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pull are met

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The team did identify a potential issue involving a lack of CP&L

presence and control over refueling floor activities. They also noted

that even though significant progress had been made, additional

improvement was still needed in the area of work control and scheduling.

They additionally noted that added emphasis by NED was needed in design

ownership and configuration management. Overall, the team stated that

significant plant work improvement had been made in process, people, and

equipment readiness since Unit 2 restart.

The inspector reviewed the

assessment and, based on plant observations and evaluations, has reached

a similar conclusion. The inspector will continue to follow, review,

and evaluate Phase II of the NAD assessment during Unit I restart.

(Closed) NRC Bulletin 93-02, Debris Plugging of Emergency Core Cooling

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Suction Strainers. This bulletin, issued on May 11, 1993, identified a

previously unrecognized potential contributor to a loss of net positive

suction head for Emergency Core Cooling System (ECCS) following a Loss-

of Coolant Accident (LOCA). The bulletin requested that licensees

identify any fibrous filter material not designed to withstand a LOCA

installed inside primary containment, take immediate compensatory

measures required to ensure functional capability of the ECCS, and take

prompt action to remove any such material.

Licensees were requested to

respond in writing within thirty days stating whether these actions had

been or would be completed. The licensee's response to NRC Bulletin 93-

02 was addressed in a letter to NRR dated June 10, 1993.

In this

letter, the licensee stated that they had completed the requested

actions, that fibrous filter material not designed to withstand the

effects of a LOCA are not installed or stored inside of primary

containment during power operation, and that a primary containment

walkdown prior to closure following major outages is performed to ensure

that non-designed equipment / materials are removed or stored in a safe

manner. This licensee response has been reviewed by NRR and was

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acknowledged in an August 6, 1993, letter. The NRR letter states that,

based on a review of the submitted material, the licensee's actions are

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considered complete.

Additionally, the inspector recently witnessed the licensee's ECCS

suction strainer inspection in the Unit I torus. Divers did not find

any indications of debris plugging or strainer degradation. The

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inspector also reviewed Administrative Instruction AI-127, Drywell

Inspection and Closecut, Revision 1, and verified that it includes steps

requiring the removal of temporary filters prior to drywell closure.

The inspectors routinely perform a pre-closure drywell and torus

walkdown following each outage to verify all extraneous, non-qualified

material (i.e. fibrous filter material) used for the outage has been

removed prior to unit start up.

M ed on a review of the licensee

response, the recent strainer ingection results, and the above

mentioned procedure, this issue is considered losed.

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(Closed) Hardened Wet Well Vent - Unit 1

The design for the Hardened Wetwell Vent system to be installed at the

Brunswick site in response to NRC Generic Letter 89-16 was previously

discussed in NRC Inspection Report 325,324/92-37. The design was

installed and tested on Unit 2 prior to the unit's restart in April of

this year. The inspection related activities associated with Unit 2 are

discussed in NRC Inspection Report 325,324/93-10.

The installation of the Unit 1 Hardened Wetwell Vent system,

including all piping components and rupture disks, was completed

on July 20. The tie to the non-interruptable air line was

completed on July 23 with installation of the vent line being

completed in several stages. The piping components for the system

were assembled in sections, and each section was hydrostatically

tested for leakage prior to being installed in the system.

Following final assembly of the various sections of vent line, the

entire vent line was tested with low pressure air to verify the

mechanical joint tightness and the pressure integrity of the final

installed vent line. This test was completed on July 23.

The inspector reviewed the design package and the as-built

drawings and followed the installation activities as they were

completed.

Following the installation of the system, the

inspector reviewed the system design and conducted a walkdown of

the installed vent line system with the modification engineer

verifying that the installed system was built in accordance with

requirements specified in the design package. During the

walkdown, the engineer pointed out some of the differences between

the system installed on Unit I and that which was previously

installed on Unit 2.

These changes in the installed piping were

minor in nature and primarily consisted of the addition of a valve

in the nitrogen supply line to the two Containment Atmospheric

Control (CAC) valves that are part of the system. The addition of

this valve allowed for the pressure and leakage testing of this

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line to be completed in sections, rather than one entire run. The

benefits of such an addition were based on the experience gained

in testing the installed design on Unit 2.

As part of the design review effort, the inspector reviewed the

data from tests that were performed on the ventline system. This

included pre-installation and post-installation piping and system

tests. No discrepancies or deficiencies were identified. The

licensee has not completed the following tests: AT-1A, CAC V216

and CAC V7 Valve Operation and Logic Test; AT-10, Hardened Wetwell

Vent Radiation Monitor Operational Test; AT-3, Local Leak Rate

Test 1-CAC-V216; and AT-40, Nitrogen System Hardened Wetwell Vent

Valve Operational Test. The inspector will follow and review the

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results of these tests. The inspector also reviewed the

procedural changes associated with this modification. For Unit 1,

there were 32 document changes associated with the installation,

operation and testing. The inspector reviewed this list of

document changes and noted that of the 32 changes, only 9 were

required to be completed prior to declaring the system operable.

The licensee had completed and approved eight of the nine required

changes necessary for system operability. A final change to

Operating Procedure OP 46, Instrument and Service Air System has

been written and reviewed, but has not been approved. The

inspector, as part of the routine inspection plan, will follow the

licensee's efforts in the completion of these activities.

The inspector verified that the plant modification / design

information for the Hardened Wetwell Vent has been incorporated

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into the plant simulator and operation of the system is currently

included in the training program.

Based on the above, this item

is closed.

Violations and deviations were not identified.

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7.

Onsite Review Committee (40500)

The inspectors attended selected Plant Nuclear Safety Committee meetings

conducted during the period. The inspectors verified that the meetings

were conducted in accordance with Technical Specification requirements

regarding quorum membership, review process, frequency and personnel

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qualifications. Meeting minutes were reviewed to confirm that decisions

and recommendations were reflected in the minutes and followup of

corrective actions were completed.

There were no concerns identified relative to the PNSC meetings

attended. The resolution of safety issues presented during these

meetings was considered to be acceptable.

8.

Engineered Safety Feature System Walkdown (71710)

The inspector conducted a detailed walkdown of Unit 2 Loop A core spray

system. The core spray system protects the reactor core by directly

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spraying cooling water on top of the fuel assemblies from sparger rings

located just above the reactor core. This action removes decay and

residual heat from the core and thus maintains cladding temperatures and

oxidation within acceptable limits.

The inspector did not observe any significant material condition

deficiencies. The valve lineup procedure, when compared with the as-

found configuration and applicable drawings, did not reveal any

discrepancies. No system caintenance discrepancies were noted.

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Observed leaks were properly captured and routed to drains. All

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significant components were properly labelled and identifiable. All

control board and local instrumentation were indicating properly. No

discrepancies were observed with the electrical lineup of the system.

No discrepancies were identified with the support systems needed to

ensure operability (i.e., electrical, ventilation, etc.).

Violations and deviations were not identified.

9.

Action on Previous Inspection Findings (92701) (92702)

(Closed) IFI 325/93-10-07, Followup on Potential Disc and Stem

Separation on Valves 1-Ell-F017 A and B.

In a 1989 LER, the licensee

had identified the occurrence of a disc to stem separation on the RHR

outboard low pressure coolant injection valve 2-Ell-F017A. This had

occurred due to inadequate engagement of the disc to stem locking pin.

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This Unit 2 valve was repaired in 1989.

In 1992, the licensee

identified a noise emanating from the Unit 1,1-E11-F017B valve that

indicated disc to stem separation. The licensee opened and inspected

this valve and found that valve disc to stem separation had also

occurred. This was due to an inadequate tack weld on the locking pin,

caused by the lack of adequate material being applied close enough to

the locking pin to prevent it from backing out due to vibration.

Based

on the above, the inspector expressed concern about the adequacy of the

)

weld on 1-Ell-F017A and 2-Ell-F017 A and B since the same welding

procedure was used to prevent the locking pin from backing out and

causing disc to stem separations. The licensee interviewed the welders

who performed these tasks and on each of the above valves. The welders

stated that they had " puddled" the weld material as close to the locking

pin as physically possible and that they clearly understood the purpose

,

of the tack weld.

The licensee has determined that a major contribution to this event was

that this valve was not designed for but was being used to throttle RHR

flow to maintain acceptable cooldown rates. The vibration created by

this throttling had caused the locking pin to loosen and back out. The

licensee has replaced the RHR 03 and RHR 24 valves with globe valves in

both RHR loops for Unit I and plans to perform the same modification on

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Unit 2 during the next outage. After these modifications, the RHR 03

and RHR 24 valves will be used to throttle flow and the RHR 17 valve

will be maintained in its normal open position. Under this condition,

the vibration would not be present and the above failure potential would

be considerably reduced. The pin location in the valve does not allow

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visibility under X-ray conditions.

Since disassembly of this valve

would require a significant amount of work and personnel radiation

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exposure, the licensee has decided not to open the valve for visual

inspection. The inspector accepted the licensee's evaluation and

conclusions for this item. Based on the above, this item is closed.

(Closed) IFI 325,324/90-07-01, ECCS Analog Trip Unit Power Source

Upgrade.

PM 82-030 and 82-031 were implemented in 1985 and 1983,

respectively, as a means of preventing spurious ECCS actuations. To

further increase system reliability, two additional modifications, PM

85-020 and 85-021, were planned. These modifications were proposed due

to the remote possibility that problems could re-occur with the battery

out of service and the battery charger re-energizing automatically as

part of a diesel start and load.

In addition, the licensee conducted an

analysis to show that the probability of this condition was extremely

remote and that previously installed modifications and procedures were

in place to prevent spurious ECCS actuations. After an examination of

the problem by NED, the project has been canceled based on the low

probability of the initiating event and the low marginal contribution to

plant safety. The inspector agreed with this conclusion. This item is

considered closed.

(Closed) Violation 325,324/92-35-02, Inadequate Procedures With Regard

to Clearance Process. This violaticn involved the failure of a

clearance to communicate the loss of reactor water level instrumentation

to the control operators. The event occurred when a clearance was

implemented to permit the installation of the digital feedwater

modification. The reactor water level control system and the level

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strip chart recorder were deenergized by this clearance. This recorder

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provided the input to the high flow level annunciator on the RTGB. This

deleted the only alarm available to the operators.

The clearance did

not provide for any temporary alarm and did not contain any steps to

inform the operators that no alarm was available. Since the test

function of the annunciator was still operable and no tag was on the

annunciator window, all operators were not aware that this function had

been lost. This was a contributing factor to an event that involved

excessive drain down of the reactor vessel water level. The licensee

corrective actions were to install a temporary alarm, revise the

applicable procedure OP-17, Residual Heat Removal System Operating

Procedure, Revision 47, to require a second operator monitor RPV level

changes, and issue a standing instruction to require that two operators

monitor critical activities such as lowering reactor water level.

In

addition, the licensee has proposed a plant betterment project that will

provide for ERFIS alarms of reactor water level and temperature at

shutdown conditions.

NED has been assigned responsibility to develop

this change. A review of the modification process by the licensee

determined that adequate guidance is included for plant conditions. A

memo from the engineering supervisor to all NED personnel reiterated the

need to follow the established guidelines. The licensee, as stated in

their response to this item, implemented an outage Risk Management

Procedure BSP-56, Revision 0, on March 5, 1993. The inspector, through

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documentation review and discussions with licensee personnel, verified

that all stated corrective actions for this item have been completed.

(Closed) URI 325,324/93-27-02, Inadequate Surveillance Procedure and

Post Modification Testing. This item is discussed in detail in Report

No. 50-325,324/93-30 and was identified as a non-cited violation

50-325,324/93-30-01.

(0 pen) VIO 325,324/93-27-03, Failure to follow procedures for

controlling excessive overtime.

This item was closed in error in

Inspection Report 50-325,324/93-30, and is reopened.

10.

Review of Licensee Event Reports (92700)

(Closed) LER 1-92-26, RPS Actuation on Low Reactor Water Level. On

October 2,1992, Unit I was in cold shutdown for a maintenance outage

with the RWCU out of service and the RHR system Loop B in shutdown

cooling. Reactor water level was being controlled by allowing the

control rod drive system cooling water flow to increase level to

approximately 240 inches above the core and then reducing reactor level

to 200 inches by rejecting level to the radwaste system. The normal

reactor water level hi/lo annunciator was out of service due to

installation of the modification of digital feedwater control.

The reactor operator began lowering reactor water level. During the

course of the drain down, he began to read a trip report. The reactor

operator did not monitor reactor water level that had decreased to the

trip setpoints for tre reactor protection system. The RPS actuation

resulted in primary containment isolation system group isolations 2

(drywell floor and equipment drain valves), 6 (primary containment

atmospheric valves), and 8 (shutdown cooling). The loss of shutdown

cooling resulted in a minimal increase in reactor water temperature.

The licensee conducted a root cause analysis of the event and

implemented corrective action for the identified weaknesses. The direct

cause of the event was the inattention of the reactor operator during

the performance of a critical license activity.

A Site Incident Investigation Team (SIIT) investigation was initiated by

the licensee. Their investigation concluded that the root cause was a

lack of clear management standards governing conduct of control room

activities and the control and sequencing of outage projects. A number

of recommendations were proposed by this team.

Operations reviewed its policy of holding shift information briefings

during watch standing periods and to more clearly define what types of

information are appropriate for such briefings. As a result, a room

outside the control room proper has been designated for pre-job

briefings, reactive meetings, etc.

In addition, a memo has been

generated that better describes the content and conduct of shift

information briefings. The inspector reviewed the memo and found it

provided adequate guidance.

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Two violations were issued under NOV 92-35-02. The corrective action

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for these violations were reviewed. One of these violations is closed

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in this report in paragraph 9.

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The licensee initiated EWR-9089 to provide alarms for reactor water

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level and reactor temperature that can be adjusted to alarm depending on

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what the desired level and temperature would be during the outage. _The

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licensee discovered that its ERFIS system has this capability. This

betterment modification has been proposed to be in operation by December

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of 1993.

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The licensee has developed and approved BSP-56, BNP Outage Risk

Management, Revision 0.

This procedure was the product of the

licensee's effort to better manage and assess the risk of certain work

activities during outage conditions. The inspector reviewed the

procedure and found that its instructions were adequate. As stated

above, the lack of a hi/lo annunciator was a result of the modification

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on the digital feedwater control system. . A procedure was developed to

ensure that the system conditions are appropriate prior to the

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installation of the modification. The licensee has developed

Modification Administration Procedure, MAP-006, Modification Acceptance

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Test Preparation, Review, Approval, and Performance. This procedure

contains prerequisites that address plant and system initial conditions

prior to installing and testing a new plant modification. The

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operations procedure for plant modification review, Operations Review of

Plant Modifications, Direct Replacement Packages, Technical

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Specification Changes and Procedure Changes as a result of Technical

Specification Changes, Revision 15, currently has requirements included

that ensure that the design documents state what plant conditions are

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required for modification installation.

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A memorandum to all control room operators was issued that described

those parameters (i.e. reactor power, reactor water level...) that the

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reactor operators may not affect without giving prior notice to the unit

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SRO. The memorandum also reiterated that the unit SR0 must be in

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control of and direct all control room activities. The memorandum was

incorporated into 01-01, Operating Principals and Philosophy, Volume 7,

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Revision 049. The inspector verified that the instructions were

adequate and had been incorporated into the proce6ere.

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A control room activity study was conducted in January and February

1993, to identify work control and maintenance activities that distract

from operations oversight ability. The study provided reccmmendations

in work control, command and control, professional conduct, control room

equipment, control room noise distractions and other recommendations. A

major finding in the study identified the need to lessen the

administrative burden of the SCO. This was accomplished by relocating

those work activities to a work control center. On-going observation of

control room activities by resident and regional inspectors has shown

this to be an effective method of reducing the administrative burden of

the SCO.

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While attempting to recover from a loss of shutdown cooling, the 1-Ell-

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F017B LPCI Outboard Injection Valve, failed to reopen. ~A component

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failure analysis was performed by Technical Support to determine the

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reason for the failure of the valve. The failure analysis revealed that

actuator failure was caused by the disintegration of the nylon gear

inserts in the motor drive intermediate pinion and shaft assembly. Work

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requests were written to disassemble, clean, inspect, and repair this

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valve and other high speed SMB-5T actuators. A preventive maintenance

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request was submnted to have the nylon gear inserts replaced every four

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fuel cycles.

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(Closed) LER l-92-11 Primary Conta'inment Monitoring System Inoperable

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Due to Relay Failure. On April 6,1992, a partial-Group 6 isolation

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occurred that resalted in the inoperability of ali of the primary

containment atmosphere radiation monitors and the Division I primary

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containment hydrogen / oxygen analyzer.

Inoperability of the primary

containment atmospheric radiation monitors was a condition outside of

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that addressed in TS 3.4.3.1, Reactor Coolant Leakage / Leakage Detection

Systems. Consequently TS 3.0.3 was invoked requiring Unit I to be

placed in Hot Shutdown within six hours and cold shutdown within the

following thirty hours. The cause of the event was the failure of the

normally energized 1-CAC-3B relay coil due to aging. The 115V-AC relay

model number CR120A was manufactured by General Electric. The licensee

replaced the failed relay and conducted a comprehensive study using

Nuclear Plant Reliability Data System, Operating Experience reports,

EDBS, drawings, and maintenance history to determine failure causes and

useful life periods. As of this writing, 54 relays have been replaced

in Unit 2 (March, 1993) and 39 in Unit 1.

Four remaining relays are

scheduled for installation prior to the Unit I startup. A preventive

maintenance route has been written to replace other relays on a

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scheduled frequency. This LER is considered closed.

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(Closed) LER l-93-005, Standby Gas Treatment (SBGT) Design Has Resulted

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in Throttle Valve Logic Allowing Flow Beyond Technical Specification

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Limits. On February 14, 1993, testing of the Unit 1 SBGT using Special

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Procedure 1-SP-93-014, " Flow Throttling of SBGT Filter Trains," found

that unthrottled flow of a single train would exceed the TS rated flow

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limit of 3300 cfm. The as found flow for IA SBGT was 4050 cfm and

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IB SBGT was 3950 cfm. The licensee determined that with the excess

flow, the heater was inadequate to roduce the humidity to 70 percent.

ACR 93-014 was written to document this problem.

Analyses were performed to investigate the effects of the higher flow

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rates.

It was determined that the SBGT can be safely operated up to

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4200 cfm without violating its design basis functions. The analysis

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also determined that the minimum heater capacity to reduce humidity to

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70 percent was 16.7 kw under normal voltage conditions. This ensures

that the TS value of 15.2 kw would be achieved under degraded voltage

conditions. This is documented in EER 93-0327.

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The licensee had a vendor perform a test on Iodine-131 removal

efficiency determination of absorbent samples for SBGT 1A.

Results of

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analysis and testing confirmed that the system as installed will provide

the required absorber efficier.cy at the higher flow rate. This analysis

was documented in a March 6, 1993, NUCON Report No. 13CP154/21.

Calculation BNP-E-8.031, Revision 0, determined that SBGT heater output

under degraded conditions is 17.8 kw. Calculation OSBGT-0006,

Revision 0, determined that a heat addition of 16.7 kw is required to

lower the relative humidity from 100 to 70 percent for 4200 cfm SBGT

fl ow.

The inspector reviewed the above documents and determined that they were

adequate. The licensee increased the heater output by changing the

wiring configuration from a delta to a wye wiring scheme. This was

accomplished by Plant Modifications92-105 and 92-106. The licensee has

determined that the as found condition would meet the unit design

requirements.

In addition, the inlet valves were adjusted to provide

throttling. This was accomplished by stops and the adjustment of limit

switches.

The inspector's review of the listed documents verifies that the

licensee completed the listed corrective actions and this item is

closed.

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11.

Employee Concerns Program

The inspector reviewed the licensee's employee concern Quality Check

program which was created to provide employees an alternate path from

their supervisor and normal line management to express safety concerns

or allegations. As part of this inspection, the inspector reviewed the

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program implementing procedure and discussed the program / process with

the site Quality Check Representative.

Survey reports of Quality Check

activities were also reviewed.

See attachment for questions addressed

during this inspection.

The licensee had established several methods for submission of employee

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concerns which included employee interviews, telephone, or by submission

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Quality Check

of Quality Check Report (QCR) forms in one of several,litidentiality of

Station lockboxes. The inspector was informed that co

the submitter was maintained. The Manager - Quality Check was

responsible for reviewing the QCRs and identifying nuclear safety issues

or other matters requiring management attention.

Employee concerns were

classified in one of three categories

Nuclear Safety issues or

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lassification of a " Case" which

technical / quality issues received

required an investigation and s a fe of action. Other concerns, such

as personnel issues, resulted i

clw sfication of Management

Information Items (MIIs) or Not ~

.,f Information. Only Cases and MIIs

required a formal response from line management. After review by the

Manager - Quality Check, the concern was then transferred to Quality

Check forms and routed to assigned evaluators / investigators.

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12.

Exit Interview (30703)

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The inspection scope and findings were summarized on September 3, 1993,

with those persons indicated in paragraph 1.

The inspectors described

the areas inspected and discussed in detail the inspection findings in

the summary. Dissenting comments were not received from the licensee.

Proprietary information is not contained in this report.

Item Number

Description / Reference Paraaraoh

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93-33-01

Violation: Failure to Control Plant Access,

paragraph 4.

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93-33-02

NCV: Inadequate maintenance procedures,

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paragraph 2.

93-33-03

IFI:

Followup on core shroud activities,

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paragraph 2.

13.

Acronyms and Initialisms

ACR

Adverse Condition Report

APRM

Average Power Range Monitor

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ASSD

Alternate Safe Shutdown Drill

BNP

Brunswick Nuclear Project

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BWR

Boiling Water Reactor

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CAC

Containment Atmospheric Control

CP&L

Carolina Power & Light Company

DG

Diesel Generator

DPM

Drips Per Minute

E&RC

Environmental & Radiation Control

ECCS

Emergency Core Cooling System

EDBS

Engineering Data Base System

EP

Emergency Preparedness

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ERFIS

Emergency Response Facility Information System

EWR

Engineering Work Request

GAF

Gain Adjustment Factor

GE

General Electric Company

GET

General Employee Training

HF

High Frequency

HP

Health Physics

INP0

Institute of Nuclear Power Operations

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LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LPCI

Low Pressure Coolant Injection

LPRM

Local Power Range Monitor

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NAD

Nuclear Assessment Department

NED

Nuclear Engineering Department

NOV

Notice of Violation-

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NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

OSC

Operations Support Center

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PA

Protected Area

PM

Plant Modification

PNSC

Plant Nuclear Safety Committee

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PSIG

Pounds Per Square Inch Gauge

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PT

Periodic Test

QC

Quality Control

RHR

Residual Heat Removal

RICSIL

Rapid Information Communication Service Info. Letter

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RPS

Reactor Protection System

RPV

Reactor Pressure Vessel

RTGB

Reactor Turbine Gauge Board

RWCU

Reactor Water Cleanup

SBGT

Standby Gas Treatment

SCO

Senior Control Operator

SI

Standing Instruction

SIIT

Site Incident Investigation Team

SR0

Senior Reactor Operator

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STA

Shift Technical Advisor

STSI

Short Term Structural Integrity

SW

Service Water

TCF

Troubleshooting Change Form

TS

Technical Specification

TSC

Technical Support Center

UT

Ultrasonic Testing

WR/JO

Work Request / Job Order

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Attachment 1

EMPLOYEE CONCERNS PROGRAMS

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PLANT NAME: Brunswick

LICENSEE: CP&L

DOCKET f: 50-325.50-324

NOTE: Please indicate yes or no as applicable and add comments in the space

provided.

A.

PROGRAM:

1.

Does the licensee have an employee concerns program? Yes

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2.

Has NRC inspected the program? No. Originally scheduled for

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Sept. 7 but deferred. Manager of Quality Check informally

discusses current issues with the Senior Resident Inspector on a

monthly basis.

B.

SCOPE: (Indicate all that apply.)

1.

Is it for:

a. Technical? Yes

b. Administrative? Yes

c. Personnel issues? Yes

2.

Does it cover safety as well as non-safety issues? Yes

3.

Is it designed for:

a. Nuclear safety? Yes

b. Personal safety? Yes

c. Personnel issues - including union grievances? Yes

4.

Does the program apply to all licensee employees? Yes

5.

Contractors? Yes

6.

Does the licensee require its contractors and their subs to have a

similar program? No

7.

Does the licensee conduct an exit interview upon terminating

employees asking if they have any safety concerns? Yes.

Part of

BSP-37, Employee Checkout Instructions.

C.

INDEPENDENCE:

1.

What is the title of the person in charge? Manager, Quality Check

2.

To whom do they report? Manager, Nuclear Assessment Department

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3.

Are they independent of line management? Yes

4.

Does the ECP use third party consultants? Uses outside

departments within CP&L corporate and currently has a program

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assessment being performed by outside consultant however it does

not normally use outside consultants as part of the program

5.

How is a concern about a manager or vice president followed up? A

review of the concern is conducted by the next level of

management. Concerns directed against the Manager, Nuclear

Assessment Department are immediately forwarded to Senior _Vice

President, Nuclear Generation Group.

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D.

RESOURCES:

1.

What is the size of the staff devoted to this program? Four. One

manager and three site representatives.

2.

What are ECP staff qualifications (technical training,

interviewing training, investigator training, other)?

Interviewing training including OJT. Experienced QA/QC personnel

in this position.

E. REFERRALS:

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1.

Who has followup on concerns (ECP staff, line management, other)?

Concern is identified, reviewed and classified by ECP staff

members and then forwarded to line management personnel for

investigation and resolution.

F. CONFIDENTIALITY:

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1.

Are the reports confidential? Yes

2.

To whom is the identity of the alleger made known (senior

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management, ECP staff, line canagement, other)? Senior management

and ECP staff

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3.

Can employees:

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a. be anonymous? Yes

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b. report by phone? Yes

G. FEEDBACK:

1.

Is feedback given to the alleger upon completion of the followup?

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Yes. Verbal communication of results/ resolution.

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2.

Does program reward good ideas? Yes. Good ideas are rewarded

with a letter of appreciation from the President or Chief

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Operating Officer.

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3.

Who, or at what level, makes the final decision of resolution?

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Manager, Quality Check

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4.

Are the resolutions of anonymous concerns disseminated? No, only

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to submitter.

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H. EFFECTIVENESS:

1.

How does the licensee measure the effectiveness of the program?

The licensee has no formal measure of program effectiveness.

2.

Are concerns:

a. Trended? Yes. Monthly status of number received and total

YTD; semi-annual report to senior management.

b. Used? Yes

3.

In the last three years how many concerns were raised? 107

Of the concerns raised, how many were closed? 106

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What percentage were substantiated? The licensee does not

substantiate concerns.

4.

How are followup techniques used to measure effectiveness (random

survey, interviews,other)? A random survey conducted by senior

management.

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5.

How frequently are internal audits of the ECP conducted and by

whom? Internal audits are very infrequent; only one in the very

beginning of the program.

I. ADNINISTRATION/ TRAINING:

1.

Is ECP prescribed by a procedure? Yes

2.

How are employees, as well as contractors, made aware of this

program (training, newsletter, bulletin board, other)? Initial-

GET training, bulletin boards, ECP boxes located throughout the

plant, posters, and brochures.

ADDITIONAL COMMENTS:

(Including characteristics which make the program

especially effective, if any.)

The inspector reviewed the licensee's program procedures, the CP&L Nuclear

Projects Quality Check Program and BSP-37 Brunswick Site Procedure Employee

Checkout Instructions, and has verified that the licensee meets the intent of

the program. Currently, BSP-37 is undergoing revision to clarify and formally

proceduralize parts of the program as it is currently implemented.

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