ML20056D147

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Insp Repts 50-327/93-23 & 50-328/93-23 on 930606-0710. Violations Noted.Major Areas Inspected:Plant Operations, Plant Maint,Plant Surveillance,Evaluation of Licensee self- Assessment Capability & LER Closeout
ML20056D147
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 07/21/1993
From: Holland W, Kellogg P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20056D132 List:
References
50-327-93-23, 50-328-93-23, NUDOCS 9308050034
Download: ML20056D147 (39)


See also: IR 05000327/1993023

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA STREET. N.W., SUITE 2900

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ATLANTA, GEORGIA 30323-0199

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Report Nos.:

50-327/93-23 and 50-328/93-23

Licensee: Tennessee Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

Docket Nos.:

50-327 and 50-328

License Nos.: DPR-77 and DPR-79

Facility Name:

Sequoyah Units 1 and 2

Inspection Conducted: June 6 through July 10, 1993

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Lead Inspector:

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W. 17

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D&tre Signed

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Inspectors:

S. M. Shaeff r Resident Inspector

A. R. Long, Resident Inspector

S. E. Sparks, Project Engineer

P. A. Balmain, Resident Inspector, Vogtle

K. D. Ivey, Resident Inspector, Watts Bar

W. K. Poertner, Resident Inspector, Oconee

C. A. Hughey, Resident Inspector, Grand Gulf

R. C. Haag, Senior Resident Inspector, Summer

P. C. Hopkins, Resident Inspector, Catawba

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P. G. Humphrey, Resident Inspector, Watts Bar

J. F. Melfi, Resident Inspector, Trojan

L. Garner. Project Engineer

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Approved by:

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PauyJ. Kellogg

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Date SYgned

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ects

SUMMARY

Scope:

Routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, evaluation of licensee

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self-assessment capability, licensee event report closecut, and followup on

previous inspection findings. During the performance of this inspection, the

resident inspectors conducted several reviews of the licensee's backshift or

weekend operations.

9308050034 930721

PDR

ADOCK 05000327

PDR

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This report also addresses special inspections conducted in the areas of

backlog and operations. These two areas were identified by the licensee as

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needing attention. in their submittal of the Sequoyah Restart Plan to the NRC.

Results:

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In the area of Operations, a weakness was identified regarding an assistant

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unit operator being inattentive while on duty (paragraph 3.a (1)).

In the area of Operations, a violation was identified for failure to ensure

that all fuel handling was performed in accordance with Site Standard Practice

-12.1 (paragraph 3.a (2)).

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In the area of Operations, a non-cited violation was identified for failure to

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notify the NRC as required by Technical Specification Limiting Condition for

Operation 3.7.11.1 ACTION b.2.a (paragraph 3.f (6)).

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In the area of Safety Assessment / Quality Verification, a violation was

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identified for frilure to adequately implement corrective action for

identification and removal of foreign material in the reactor vessel prior to

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the Unit 1 Cycle 6 core reload (paragraph 4.b).

Reviews of licensee assessments by a senior management oversight group,

Nuclear Assurance, and an operational restart readiness team resulted in a

conclusion that the licensee's ongoing self assessments are providing

meaningful input to site and corporate management regarding restart plan

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acceptability and implementation (paragraph 6).

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In the area of Safety Assessment / Quality Verification, a violation was

identified for failure to promptly identify the procedure problem associated

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with LER 327/92-21 during corrective action for LER 327/92-03 (paragraph 7.b).

Reviews of licensee outage performance were conducted in several functional

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areas during the period (paragraph 3.g).

The licensee's continuing excellent

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performance in maintaining outage person-rem dose expenditure and personnel

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contamination events well below projected goals was considered to be a

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strength in the radiological controls area. Also, system engineering

activities associated with backlog reviews was considered as good. However,

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reviews in the operations, maintenance, and safety assessment / quality

verification areas were mixed. These areas had regulatory issues which-

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resulted in identification of violations discussed in this report.

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Inspections, to date, indicate that the licensee is addressing backlog issues

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in the manner described in the Sequoyah Restart Plan. However, several

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restart plan inconsistencies were noted by the inspectors during this period.

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They were:

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Need for clarification on how emergent issues (issues after May 1, 1993)

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were being reviewed.

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Need for clarification of how post restart issues would be prioritized.

(The process for this item had not been presented to the inspectors when

the inspection period ended.)

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Need for senior plant management to better communicate expectations to

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BRC, lower levels of management, and system engineers regarding

execution of the restart plan (uniform clarification of restart criteria

to all).

This observation was considered to take on added importance

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later in the inspection period based on the inspectors comments during

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the last week of this period.

Several plan enhancements or corrections were accomplished during this

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inspection period. The inspectors consider that the licensee needs to

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formally incorporate these enhancements or corrections into the plan and

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formally communicate this information to the NRC (paragraph 9.a).

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The inspectors concluded, based on licensee assessments, review of operations

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standdown meetings, and general observations during the period that general

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operator performance regarding attention to detail and sensitivity to not

living with past problems is improving (paragraph 9.b).

A review of licensee previous commitments concluded that the licensee has

implemented a comprehensive and effective program to track and respond to

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commitments (paragraph 10).

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • R. Fenech, Site Vice President
  • D. Keuter, Vice President, Nuclear Readiness

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  • K. Powers, Plant Manager

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  • J. Baumstark, Operations Manager
  • L. Bryant, Maintenance Manager
  • M. Burzynski, Nuclear Engineering Manager

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  • M. Cooper, Restart Plan Coordinator
  • D. Driscoll, Site Quality Assurance Manager
  • T. Flippo, Acting Site Support Manager

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  • J. Gates, Outage Manager

C. Kent, Chemistry and Radiological Control Manager

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  • D. Lundy, Technical Support Manager

R. Rausch, Modifications Manager

  • R. Shell, Site Licensing Manager

J. Smith, Regulatory Licensing Manager

  • R. Thompson, Compliance Licensing Manager
  • J. Ward, Engineering and Modifications Manager

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  • N. Welch, Operations Superintendent

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  • K. Whittenberg, Public Relations Manager

NRC Employees

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R. Crlenjak, Chief, DRP Branch 4

P. Kellogg, Chief, DRP Section 4A

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  • Attended exit interview.

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

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Acronyms and initialisms used in this report are listed in the last

paragraph.

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During the month of June 1993, several management changes were announced

for Sequoyah.

These changes were:

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R. Shell replaced M. Cooper as the Site Licensing Manager

effective June 10, 1993.

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T. Flippo replaced P. Wallace as Acting Site Support Manager

effective July 1,1993.

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K. Powers replaced R. Beecken as the Sequoyah Plant Manager

effective July 5,1993.

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On June 22, 1993 the NRC Restart Panel was on site to discuss restart

activities with licensee management.

The licensee presented an update

on implementation of their restart action plan.

NRC management in

attendance included:

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S. Ebneter, Region II Administrator

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E. Merschoff, Director, DRP, Region II

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A. Gibson, Director, DRS, Region II (NRC Restart Panel Chairman)

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F. Hebdon, Project Director, NRR (NRC Restart Panel Member)

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R. Crlenjak, Chief, DRP Branch 4, RII (NRC Restart Panel Member)

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D. LaBarge, Senior Project Manager, NRR (NRC Restart Panel Member)

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P. Kellogg, Section Chief, DRP, Branch 4, RII

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2.

Plant Status

Unit 1 began the inspection period in day 60 of the Cycle 6 refueling

outage (vessel defueled). The licensee commenced refueling of the

reactor (MODE 6 entry) on June 18. On June 19, refueling operations

were suspended due to the toppling of a fuel assembly in the reactor

pressure vessel. This event and recovery of the assembly is further

discussed in paragraph 3.a (1). After recovery of the fuel assembly,

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the licensee completed inspections of the toppled assembly and lower

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core support areas and discovered that foreign material had caused the

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fuel assembly to fall.

On July 6, subsequent core inspections

identified two additional pieces of foreign material.

On July 7, the

licensee decided to unload the 37 assemblies in the core to facilitate

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further inspections for foreign materials. On July 8, the licensee

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recommenced refueling (MODE 6 entry). At the end of the inspection

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period the licensee was continuing with fuel onload (approximately 60%

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of the core had been reloaded).

Unit 2 began the inspection period in MODE 5 (Day 97 of a forced

outage).

During the period activities continued with regard to piping

replacement in the secondary plant due to erosion.

In addition, other

items identified as required for restart of the unit were also worked.

At the end of the period, Unit 2 remained in MODE 5 with work ongoing in

accordance with the licensee's forced outage schedule.

3.

Operational Safety Verification

(717'J7)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, TS, and LCOs; examination of

panels containing instrumentation and other reactor protection

system elements to determine that required channels are operable;

and review of control room operator logs, operating orders, plant

deviation reports, tagout logs, temporary modification logs, and

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tags on components to verify compliance with approved procedures.

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The inspectors also routinely accompanied plant management on

plant tours and observed the effectiveness of management's

influence on activities being performed by plant personrel.

(1)

During a routine tour of the Auxiliary Building on June 8,

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two NRC inspectors identified an AU0 that appeared to be

less than fully alert while on duty.

The individual was in

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the auxiliary building AVO station on elevation 669. After

observing the individual for several minutes, the inspectors

entered the station to ensure that the individual was not

physically ill.

The AUD became alert when the inspectors

approached.

The inspectors informed Operations Management of the

incident. After reviewing the problem, licensee management

informed the inspectors that the subject AU0 was not

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performing duties at the time of the observation, as he was

waiting to be called for portions of leak rate testing that

had not yet begun. The AVO was disciplined for being less

than attentive while on duty. The inspectors considered the

licensee's actions appropriate.

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After the event, the inspectors were informed that this

individual had been observed less than attentive by peers,

prior to the inspectors identification.

The inspectors

consider that operator peer identification of the problem,

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without taking action prior to the inspectors

identification, was a weakness in the way operators

performed their jobs (acceptance of peer inattentiveness as

acceptable performance). The fact that operators recognized

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their weakness after the problem, and were willing to share

the observations with management was an indicator to the

inspectors that they are recognizing that past performance

has been lacking, and that they are willing to improve in

the way they will perform their jobs in the future.

(2)

On June 19, 1993, the resident inspectors were notified by

the licensee that fuel movement on Unit I was halted due to

fuel assembly H64 (in core location G-7) tilting out of

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position during core reload evolutions. This event is

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discussed further in paragraph 3.f (4).

The fuel assembly which tilted had been used during one

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previous cycle.

It also was the 44th assembly being loaded.

The core holds 193 assemblies when fully loaded.

Operators had completed landing the assembly into position,

unlatched the assembly from the fuel handling manipulator

crane, and were raising the manipulator into the mast.

Operators looked into the vessel from the bridge and noticed

the assembly tilting over. The top of the assembly came to

rest on the core baffle plate approximately at location A7,

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with the assembly about 21 degrees from a vertical position.

Operators immediately stopped fuel handling evolutions.

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Operators also entered A0I-29, DROPPED OR DAMAGED FUEL

ASSEMBLY OR LOSS OF REACTOR CAVITY WATER LEVEL, and

performed applicable steps.

On June 21, 1993, the licensee commenced reco.ery operations

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in accordance with Fuel Handling Instruction FHI-3A,

RECOVERY OF LEANING FUEL ASSEMBLY H64. The NRC granted

discretionary enforcement of TS 3.9.6, which requires fuel

assemblies to be moved with the manipulator crane, to allow

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for recovery of the fuel assembly with the manipulator crane

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auxiliary hoist.

The auxiliary hoist was used to raise the

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assembly to a vertical position and secure it so that it

could be latched by the manipulator crane.

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C" ring the recovery operati:n. the maximum allowable weight

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of the recovery Ligging and assembly (1750 pounds) for the

auxiliary hoist wat exceeded.

The weight limit was

specified in the p.ocedure and had been briefed prior to

commencing recovery operations. Manaaement had to hhit the

evolution due to command and communication problems between

the control room and the containment.

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NRC personnel observed portions of the these initial

recovery efforts from several locations.

One inspector was

in the control room monitoring the licensee evolutions.

Another inspector was in the containment during portions of

the recovery.

Also, an NRC senior project manager was

observing recovery evolutions on a closed circuit tel

sion

in one of the licensee's conference rooms.

All of the NRC

personnel noted poor command and control during this part of

the recovery evolution, in that the refueling crew appeared

to be more concerned with getting the job done than focusing

on safety.

The inspectors reviewed Site standard practice SSP-12.1,

CONDUCT OF OPERATIONS, Revision 5. Paragraph 3.1.2 discusses

the responsibilities of the Operations department positions.

Step 3.1.2.M.8 of SSP-12.1 requires that the fuel handling

supervisor (a licensed SRO) ensure that all work is

performed in a safe manner by the appropriate procedure.

The inspectors concluded that the fuel handling supervisor

did not perform the evolutions of FHI-3A in accordance with

the requirements of SSP-12.1.

Failure to ensure that all

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fuel handling was performed in accordance with SSP-12.1 is

identified as a Violation (327/93-23-01).

The inspectors were also concerned that management in the

control room was having a difficult time communicating with

the refueling crew in containment.

The inspectors consider

that the command and control of the fuel recovery evolution

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could have been better managed and that senior plant

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management's decision to stop the fuel handling recovery

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effort was appropriate.

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To preclude further command and control problems, plant

management established a special recovery team in

containment to control the evolutions.

The team included a

test director (505/SR0) to direct all operations and

communicate with the CIPTE manager in the control room. The

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refueling SRO in containment took his orders directly from

the test director in containment, although he maintained his

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function as specified in TS.

The inspectors monitored licensee recovery operations during

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selected portions of the remainder of the recovery

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operation, and found the new recovery organization to be

more responsive to safe and controlled recovery of the fuel

assembly.

Pretest briefings stressed a conservative,

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cautious approach.

Requirements and expectations were

effectively conveyed regarding chain of command,

communications, procedural compliance, step by step

signoffs, and maintenance of chronological test logs. The

avoidance of becoming frustrated and impatient was strongly

stressed.

Personnel being briefed displayed a good

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questioning attitude, and there was good QA involvement

throughout the process.

Inspectors observed subsequent evolutions in progress from

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the control room, inside Unit I containment, and from other

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locations which had closed circuit TV monitoring of the

evolutions. The activities were professionally conducted,

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and demonstrated good command and control. Order was well

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maintained despite the presence of a large number of people

in the containment.

The test director was effective in

communicating information from the containment to the

control room clearly and completely.

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On June 25, 1993, the licensee recommenced recovery

operations for fuel assembly H64 in core location G-7. The

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fuel assembly was being held in place with J-hooks and

associated rigging attached to the auxiliary hoist, and

rested approximately three quarters of an inch above the

lower core plate. Revision 1 of FHI-3A included steps for

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transferring the assembly from the auxiliary hoist to the

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manipulator gripper so that the manipulator gripper could be

used to move the assembly to the upender.

To secure and

stabilize the assembly during and after disconnecting the J-

hooks in preparation for latching by the manipulator

gripper, a stainless steel wedge and/or hydraulic duckbill

jack would be installed under the FA bottom nozzle.

Further

stabilization would be provided by looping a wire rope under

the top nozzle of H64 in G-7, and by a wire rope hooked to

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the assembly in location J-7.

These wires were to be

secured to the cavity wall.

If necessary, the duckbill jack

could provide supplemental lifting force to free the

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assembly without exceeding TS limits on the hoist.

During performance of step 5.1B [1] of FHI-3A, the operators

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were unable to hook the cable on the upper nozzle plate for

the assembly in core location J-7.

The procedure was halted

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for equipment modification. Also during this evolution, QA

identified that the J-hooks used in the rigging were carbon

steel, rather than stainless steel as specified in the

safety evaluation.

A corrective action document was

initiated to address this discrepancy.

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On June 26, 1993, the licensee recommenced recovery

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operations of fuel assembly H64. Operators were able to

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connect the hook to the fuel assembly upper nozzle in core

location J-7 and secured the cable on the refueling cavity

wall.

However, during performance of step 5.lB [4] of FHI-

3A, the operators were unable to loop the wire rope under

the bottom of the top nozzle of assembly H64. The evolution

was again halted for equipment modification and procedure

revisions.

On June 27, 1993, the licensee recommenced recovery

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operations of fuel assembly H64.

Procedure FHI-3A had been

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revised to allow for positioning of a wedge and a jack under

assembly H64 ahead of looping the wire rope as described

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above.

Installation of the wedge was accomplished; however,

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the wedge did not contact the fuel assembly lower nozzle

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foot as required by step 5.1B [6] of the procedure. Also

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during placement of the duckbill jack in accordance with

step 5.1B [7], the jack would not stay in position. The

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procedure was again halted to address these additional

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problems.

A new bracket was designed, constructed, and tested to allow

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for accomplishment of step 5.1B [4] of the revised

procedure. The operators effectively positioned the bracket

with wire ropes attached on the top nozzle of assembly H64.

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The wire ropes were then tied off at appropriate locations

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on the North and East sides of the refuel floor. After

completion of this evolution, all recovery evolutions were

halted pending resolution of the wedge and jack problems.

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At this point, the licensee had Westinghouse engineer better

recovery equipment and demonstrate that the equipment was

effective at its Waltz Mill facility.

The licensee's

reactor engineering manager participated in the testing of

the redesigned jack, which utilized a parallel jaw lifting

mechanism to better fit the assembly foot. In addition, the

jack was designed to be secured in position through

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alignment on one of the flow holes. A training film was

provided by Westinghouse to aid in briefing the recovery

crew on use of the new equipment.

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On July 1,1993, the licensee recommenced recovery

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operations of fuel assembly H64. However, during attempts

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to install the new jack assembly, an interference was

encountered with an incore thimble guide nut located at an

adjacent location on the core basket. This guide nut had

not been considered in the equipment design and the mockup

testing at Waltz Mill. The evolution was again halted for

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equipment modifications and procedure revisions.

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On July 2,1993, the licensee recommenced recovery

operations of fuel assembly H64.

Video recordings from the

previous day had shown a dark line on the lower core plate

near location G-7 which might have represented a defect or

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foreign object. The licensee conducted further observations

of the core plate with the underwater camera and confirmed

that the dark line was a scratch rather than a crack or

foreign object.

The modified jack was installed and 200 pounds of pressure

was applied to assembly H64's lower nozzle plate foot, then

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the auxiliary hoist load was reduced to remove the J-hooks

that had been used to upright the assembly.

After the J-

hooks and auxiliary hoist rigging were moved out of the way,

the licensee latched assembly H64 with the manipulator

crane. The assembly was successfully pulled up by the

manipulator crane using a force less than limits prescribed

by procedure. The jack was not needed to further assist in

freeing the assembly.

The bracket and rigging on assembly H64 was removed and the

assembly was transported to the refueling transfer canal.

The assembly lower nozzle plate was inspected at this

location and no significant damage was observed.

The assembly was then lowered into the transfer cart

upender. However, the assembly would not fully insert into

the upender. Operators decided to remove the assembly from

the cart and transfer it back to the reactor vessel.

The

assembly was transferred back to location A-5 in the reactor

vessel. The assembly was left in this location, latched to

the manipulator crane, two inches off index in both

directions.

Recovery evolutions were secured for the day.

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Following removal of assembly H64 from location G-7, the

licensee noticed a foreign object located on the lower core

internals at location G-7 adjacent to assembly location H-7.

The licensee determined that the foreign object was

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approxim: tely 3/4 inch high and was cylindrical in

configuration.

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On July 3,1993 the licensee recommenced recovery operations

on fuel assembly H64. The assembly was returned to the

transfer cart upender; however, additional attempts to

insert the assembly into the upender were unsuccessful.

Operators then placed assembly H64 in the RCC change fixture

location in the transfer canal and _ inspected the upender

with the underwater camera.

No problems with the upender

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were identified.

Fuel assembly H64 was then transferred

from the RCC change fixture location back to location A-5 in

the reactor vessel. The assembly was left in this location,

latched to the manipulator crane, and recovery evolutions

were secured for the day.

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On July 4, 1993 the licensee recommenced recovery operations

of assembly H64. The licensee established two refueling

crews for recovery operations from this point forward and

continued with recovery evolutions on a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> basis. The

SOS /SR0 test director position was secured and normal

refueling staffing resumed.

The licensee moved assembly H64 back to the RCC change

fixture while a manipulator crane load functional test was

performed. The wedge and jack used for stabilizing H64 was

removed from the vessel, and the hook released from the

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assembly in core location J-7.

Blanking plates were

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installed in the flow holes in core locations G-7, G-8, and

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H-8 in the lower core internals of the reactor vessel.

Operators then removed the fuel assembly from location H-7

and returned the assembly to the spent fuel pool where it

would be inspected for damage.

Flow holes at location H-7

were then blanked and the foreign object was retrieved.

The

licensee determined that the foreign object had been in the

RCS for a reasonably long period of time based on radiation

levels of the object after retrieval. The flow nozzle

blanking plates were then removed, and a lower internals

video inspection performed.

The licensee then commenced removal of fuel assemblies at

locatio,s G-6 and H-6 to the spent fuel pit to be inspected

for possible damage.

The assemblies in locations J-7, J-9,

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and G-9, which are symmetric to location G-7, were removed

for replacement with new fuel assemblies. Calculations were

performed to support the core design change.

On July 5, 1993 the licensee had revised the procedure to

allow for loading of assembly H64 into the upender in a

manner that would accommodate additional bowing of the

assembly. The assembly was successfully loaded and

transferred to the spent fuel pool.

After assembly H64 had

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been transferred to the spent fuel pool, the licensee exited

the NOUE at 11:35 pm on July 5, 1993.

Overall, the inspectors consider that the licensee recovered

the tilted fuel assembly in a generally safe manner.

Although the recovery evolutions on June 21, 1993, were not

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accomplished in accordance with procedure and resulted in a

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violation described earlier in this paragraph, subsequent

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evolutions were well controlled.

However, greater

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thoroughness in the licensee's planning efforts for the

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recovery could have prevented delays for modification of

equipment and/or procedural changes.

The inspectors review of activities related to the removal

of the cylindrical object from the Unit 1 core which caused

the assembly to topple and other foreign objects found in

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the core is discussed in paragraph 4.b.

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b.

Weekly Inspections

The inspectors conducted weekly inspections in the following

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areas:

operability verification of selected ESF systems by valve

alignment, breaker positions, condition of equipment or component,

and operability of instrumentation and support items essential to

system actuation or performance.

Plant tours were conducted which

included observation of general plant / equipment conditions, fire

protection and preventative measures, control of activities in

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progress, radiation protection controls, missile hazards, and

plant housekeeping conditions / cleanliness.

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The inspectors noted that on June 8, 1993 an unannounced

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fire drill was performed to satisfy the requirements of an

annual QA fire protection audit.

Neither of the two AU0s

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assigned to the fire brigade responded within the required

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time limit. One individual said he was delayed in exiting

the auxiliary building. The other said that he was unable

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to find gear in the equipment cage which fit him. This

second individual had notified his supervisor two weeks

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previously that he did not have proper gear, but did not

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mention the lack of equipment again when subsequently

assigned to the fire brigade.

The fire drill was successfully repeated the folicwing day.

This second drill was also unannounced. The first of the

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AU0s from the previous day's drill participated and reached

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the designated area in a timely manner.

The second AU0 from

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the previous day's drill was made ineligible for the fire

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brigade until he obtained proper gear.

Three additional

drills were subsequently conducted, and all were

successfully completed.

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Operations management issued Operations Policy statement 93-

037 to clarify AVO fire brigade responsibilities, pending

revision of the appropriate plant procedures. The AU0s

assigned to the fire brigade are responsible for physically

verifying that their gear is in the storage cage and in good

shape, and they are required to notify their supervision if

assigned to a c-zone or other duties which could interfere

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with their timely response to a fire.

Personnel have been

trained on these responsibilities.

(2)

On June 16, 1993, the inspector noted a half-filled bucket

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of waste oil next to control air system air compressor A.

A

Transient Fire Load

aching permit (#93-0119, dated March

24,1993) was hung tearby.

The inspector noted that this

breaching permit expired the previous day, June 15.

This

condition was identified to the licensee and the bucket of

oil and the permit were promptly removed.

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(3)

During tours of the turbine building, inspectors noted

improperly secured high pressure gas bottles.

The

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inspectors brought this issue to the attention of the

licensee. The licensee conducted a walkdown of the plant to

correct the deficiencies.

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The inspectors consider the above practices to be examples of poor

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attention to detail and a lack of sensitivity by operators in

assuring that issues are promptly identified and corrected,

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c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following

areas:

verification review and walkdown of safety-related tagouts

in effect; review of the sampling program (e.g., primary and

secondary coolant samples, boric acid tank samples, plant liquid

and gaseous samples); observation of control room shift turnover;

review of implementation and use of the plant corrective action

program; verification of selected portions of containment

isolation lineups; and verification that notices to workers are

posted as required by 10 CFR 19.

d.

Other Inspection Activities

Inspection areas included the turbine building, diesel generator

building, ERCW pumphouse, protected area yard, control room, Unit

I containment, vital 6.9 KV shutdown board rooms, 480 V breaker

and battery rooms, and auxiliary building areas including all

accessible safety-related pump and heat exchanger _ rooms.

RCS leak

rates were reviewed to ensure that detected or suspected leakage

from the system was recorded, investigated, and evaluated; and

that appropriate actions were taken, if required.

RWPs were

reviewed, and specific work activities were monitored to assure

they were being accomplished per the RWPs.

Selected radiation

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protection instruments were periodically checked, and equipment

operability and calibration frequencies were verified.

On July 1,1993, the inspector toured the lower compartment of

Unit 2 containmmt.

The inspector noted that containment was

generally clean, but did observe some items in containment (e.g.

gloves, a rag, a tape measure).

The inspector observed two items

that needed to be assessed or repaired. These were:

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Oil underneath the Number 1 RCP.

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A torn electrical conduit into the valve actuator for the

accumulator Number 1 outlet block valve.

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The licensee verified the inspector's observations and brought

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these concerns to outage management to resolve prior to restart.

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The licensee initiated WR C173654 to fix the accumulator block

valve.

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e.

Physical Security Program Inspections

In the course of the monthly activities, the inspectors included a

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review of the licensee's physical security program. The licensee

performance of various shifts of the security force was observed

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in the conduct of daily activities to include: protected and vital

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area access controls; searching of personnel and packages;

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escorting of visitors; badge issuance and retrieval; and patrols

and compensatory posts.

In addition, the inspectors observed

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protected area lighting, and protected and vital areas *.,arrier

integrity.

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f.

Licensee NRC Notifications

(1)

On June 11, 1993 the licensee made a four hour notification

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to the NRC as required by 10 CFR 50.72. They reported

discovery of inadequate ventilation design which may have

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resulted in both trains of both units' vital power supplies

being inoperable. The licensee determined that the design

was inadequate in the area of ventilation cooling for the

480 volt board room power supplies. The licensee identified

that one train of ventilation supplied redundant trains of

safety-related components.

A failure of this train could

have led to exceeding temperature limitations for the vital

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power supply areas.

The licensee will implement corrective

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actions to provide appropriate train cooling for vital power

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supplies prior to either unit entering MODE 4.

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(2)

On June 14, 1993 the licensee made a four hour notification

to the NRC as required by 10 CFR 50.72 due to an ESF

actuation.

Unit 1 MCR operators were attempting to start

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the #1 RCP motor, which was uncoupled to the pump. The

uncoupled run was requested due to a motor change out during

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the refueling outage. The motor was started and the 1A

start bus tripped on overcurrent, which deenergized the 1A

and 1C 6.9 KV Unit boards. The 1C Unit board was supplying

the IB shutdown board (SDB), and thus caused an undervoltage

condition on the IB SDB. Undervoltage on the IB SDB

completed the logic to start all four EDGs.

All four EDGs

started as designed, and the IB SDB completed its load shed

and subsequently was carried by the IB EDG.

The load shed

and load sequencing of the IB SDB occurred as designed with

no problems. At the time of the event, Unit I was defueled.

One of the two spent fuel pool cooling pumps tripped off

during this event, and thus no spent fuel pool cooling was

lost.

The MCR appropriately implemented AOI 35 for blachut

operation, and all systems responded normally.

(3)

On June 15, 1993 the licensee made a four hour notification

to the NRC as requirea by 10 CFR 50.72 regarding a degraded

conditior, while shut hwn. As discussed above, on June 14,

1993, the licensee made a four hour notification as a result

of an ESF actuation (EDG start) due to loss of an offsite

start bus breaker. The licensee's investigation determined

the root cause to be an overcurrent current transformer that

was installed out of phase since November 1991. This

condition would allow the breaker to trip under nominal load

which is outside design basis.

(4)

On June 19, 1993 the licensee made a call to the NRC as

required by 10 CFR 50.72 due to a Notification of Unusual

Event. On June 19, 1993, at approximately 10:55 A.M., fuel

movement on Unit I was halted due to a fuel assembly (H64)

tilting out of position during core reloading evolutions.

The assembly had been used during one previous cycle.

It

also was the 44th assembly being reloaded. The core holds

193 assemblies when fully loaded.

Operators had completed landing the assembly in position,

unlatched the assembly from the fuel handling manipulator

crane, and were raising the manipulator into the mast.

Operators looked into the vessel from the bridge and noticed

the assembly tilting over. The top of the assembly came to

rest on the core baffle plate approximately 1ocation A7.

After movement stopped, the assembly appeared to be

approximately 21 degrees from a vertical position.

Operators immediately stopped fuel handling evolutions.

Operators also entered A01-29, DR0pPED OR DAMAGED FUEL

ASSEMBLY OR LOSS OF REACTOR CAVITY WATER LEVEL and performed

applicable steps.

After discussions between operations and management, a

decision was made to enter the site emergency plan.

At 1149

A.M., The licensee declared a notification of unusual event

based on conditions that warrant increased awareness.

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Initial assessments indicated that radiation levels had not

changed and that the assembly was not damaged (no indication

of increased activity due to possible fuel pin failure).

The licensee immediately convened an incident investigation

team to review the event. Plans were formulated to recover

the fuel assembly. This effort is further discussed in

paragraph 3.a (2) of this report.

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The NRC senior resident inspector responded to the site to

review the event and evaluate licensee actions.

The

inspectors monitored licensee recovery actions until the

assembly was recovered and returned to the spent fuel pit.

The licensee exited the notification of unusual event at

11:35 pm on July 5, 1993.

(5)

On June 25, 1993 the licensee made a notification to the NRC

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as required by TS 3.7.11.1 due to inoperability of the plant

fire suppression system.

Portions of the system became

inoperable when the licensee closed valve 0-26-696 to

isolate a leak in one suppression header which was being

aligned for maintenance. The licensee complied with all

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required ACTION statements of TS 3.7.11.1.

(6)

On July 2,1993 the licensee made a notification to the NRC

as required by TS LC0 3.7.11.1 ACTION b.2.a which requires

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> notification. However, the entry was accomplished

on June 21, 1993 in accordance with approved procedure. The

licensee failed to notify the NRC within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> as

required by TS LC0 3.7.11.1 ACTION b.2.a.

All other LC0

ACTION requirements were accomplished with the exception of

the notification. The licensee instituted an incident

investigation to determine why proper notifications were not

made.

Failure to notify the NRC as required by TS LC0

3.7.11.1 ACTION b.2.a is identified as a non-cited violation

(327,328/93-23-02). This violation will not be subject to

enforcement action because the licensee's efforts in

identifying and correcting the violation meet the criteria

specified in Section VII.B of the Enforcement Policy.

(7)

On July 4,1993 the licensee made a four hour notification

to the NRC as required by 10 CFR 50.72 concerning an

inadvertent ESF actuation.

At approximately 2:55 pm, three

of the four emergency diesel generators received an

automatic start signal due to the IB-B, 6.9 KV shutdown

board isolating from its normal power supply.

The IB-B

emergency diesel did not start due to it being out of

service in accordance with approved maintenance procedures.

Some minor loads powered from the IB-B, 6.9 KV shutdown

board were deenergized until the board was restored with

normal power.

The other three diesels did not connect to

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their respective shutdown boards due to normal power being

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available. All safety systems performed as designed.

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The initial evaluation of the cause of the ESF signal was

determined to be an inadequate procedure. . The licensee

commenced an incident investigation to evaluate the cause of

the ESF actuation and propose corrective actions. An LER

will be written for this event.

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g.

Outage Functional Area Reviews

During this period, the inspectors focused on review of licensee

performance at the end of the Unit 1 Cycle 6 refueling outage, as

well as the Unit 2 forced outage in several functional areas.

The

following conclusions were reached during this period:

Operations - Operator performance during this period was

considered to be mixed. Most evolutions, including system

restorations, processing of clearances, and monitoring of plant

status were accomplished in accordance with requirements.

However, initial recovery evolutions of the tilted fuel assembly

H64 were not accomplished as required by procedures.

In addition,

the inattentive AUD issue was considered to be an operational

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weakness. These conduct of operations issues resulted in

identification of a violation of regulatory requirements and an

operational weakness (see paragraph 3.a).

Radiological Controls - Performance in this area was considered to

be very good.

Person-rem expenditure and personnel contaminations

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continued to be well below projected levels even though RWP work

growth continued. The inspectors consider that the sustained good

performance in this area is a strength.

Maintenance - Performance in this area for the inspection period

was considered mixed. Most maintenance activities reviewed were

accomplished in accordance with requirements. However, activities

associated with foreign material exclusion, indicate that

additional management attention is needed in this area.

Engineering / Technical Support - Performance in this area was

considered to be generally good.

Reviews of system backlogs

determined that system engineers were knowledgeable on their

systems and the status of backlogs.

However, some system

engineers were not aware of current status of system corrective

action implementation.

Safety Assessment / Quality Verification - Performance in this area

was considered to be mixed. The licensee had conducted good

assessments of several areas and were benefiting from results of

the assessments in continuing with corrective actions for problem

areas identified at the plant. However, regulatory issues

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identified in paragraphs 4.b and 7.b of this report indicated that

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corrective actions for past problems had not always been

effective.

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Within the areas inspected, one violation and one non-cited violation

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were identified.

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4.

Maintenance Inspections

(62703 & 42700)

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During the reporting period, the inspectors reviewed maintenance

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activities to assure compliance with the appropriate procedures and

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requirements.

Inspection areas included the following:

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a.

ARROWHART CONTRACTOR INSPECTIONS

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On June 7, 1993, PER 930208 was written identifying a problem with

the subject contractors. The PER described a condition where

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interlock contacts on the Arrowhart contractor for 1-FCV-67-124

were found gummed up to the point it caused the valve to

malfunction. The PER also determined that the problem could

potentially affect operability on both units. At the time of

identification of the problem, Unit I was defueled and Unit 2 was

in MODE 5.

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The licensee evaluated the PER and commenced an inspection effort

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of breakers with Arrowhart contractors on June 9, 1993. The

licensee initially believed that the problem was limited to the

Unit I contractors due to recent PMs being performed on Unit 1.

During the rest of the inspection period, the inspectors monitored

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licensee activities associated with the Arrowhart contractor

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issue.

The inspectors met with system engineers on several

occasions to obtain an update on the findings. When the

inspection period ended, the licensee had identified a total of 58

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failures (17 safety-related/41 non safety related) on motor

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starters with Arrowhart contractors. The procedural criterion for

identification of failure was auxiliary contacts sticking or

sluggish when tested.

In addition, another 139 contractors were

cleaned during the inspections. The total number of motor

starters inspected was approximately 609.

The inspectors reviewed work order 93-03411-00 associated with

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operational checks of identified contacts associated with 18

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starters for A and B train components, work order 93-03350-00

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associated with inspections of starter contractors located on

Reactor MOV boards IB1-B and 282-B in the auxiliary building, and

work order 93-03351-00 associated with inspections of starter-

contractors for 21 components on Unit 1 Reactor and MOV boards.

The inspectors concluded that the inspections were conducted in

accordance with procedural requirements.

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The inspectors concluded that the licensee had identified a

significant problem associated with Arrowhart contractors on motor

starters located throughout the plant.

However, no failures

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occurred on the units during this period which caused safety-

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related components required for MODE 5 or MODE 6 operation to

become inoperable. The inspectors also considered the actions

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taken by the licensee to be necessary in order to assure

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reliability of the starters. This issue was further reviewed by a

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region based inspector and discussed in inspection report 327,

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328/93-31.

b.

FOREIGN MATERIAL INSPECTIONS

During the inspection period the inspectors reviewed licensee

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activities associated with the recovery of the foreign objects

from the Unit I reactor core.

An event occurred on June 19, as

described in paragraph 3.a.2, which involved the tipping of a fuel

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assembly due to a foreign object on the lower core support plate

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when the assembly was being placed in the core.

Two additional

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small foreign objects were also discovered in similar locations in

the Unit I reactor core.

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The inspectors monitored the foreign object removal process at

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numerous instances and verified the activities were in accordance

with WR C128210 and MI-1.1.5, GENERAL FOREIGN OBJECTS RETRIEVAL

PROCEDURE - UNITS 1 AND 2, Revision 1.

Observations of activities

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in-process concluded that the individuals involved in the

activities performed the recovery evolutions in a safe manner.

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All of the objects identified were recovered.

Blanking plates

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were properly installed in the flow holes at appropriate locations

,

to prevent movement of the object further into the core. The

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inspectors concluded that the retrieval activities were performed

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in accordance with requirements.

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The inspectors reviewed the objects recovered from the Unit 1

)

reactor core. The object related to the fuel assembly tipping

event was identified as an expander device for a Westinghouse

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steam generator tube plug approximately 0.75 inch in height and

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0.5 inch in diameter. The additional two objects consisted of a

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paint chip approximately 1.0 inch square and a metallic item

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approximately 1 x 0.25 x 0.0625 inches (possibly a section of

gasket material). At the end of the inspection period, the

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licensee had not completed the root cause investigation for entry

of the foreign material into the Unit I vessel.

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In addition to the above, the inspectors specifically reviewed the

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opportunities that the licensee had to identify the expander plug

which caused the fuel assembly to tilt.

Discussions with reactor

engineering personnel indicated that two inspections of the lower

support plate were performed to identify foreign material.

The

first was performed on June 12 by TVA personnel and the second by

Westinghouse personnel on June 17.

Both inspections were

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performed utilizing a camera attached to a pole and lowered into

the reactor core.

The Unit I core onload was begun on June 18.

The inspectors noted that water clarity and lighting appeared

[

adequate for performing the lower core inspections.

On July 8, 1993 the inspectors attended a PORC meeting, which

presented Incident Investigation II-S-93041, Tilted Fuel Assembly

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During Unit 1 Core load. At this meeting, the inspectors learned

that a video recording and additional verification of the lower

core inspection was not performed for the current UIC6 reload.

The inspectors recalled that during independent review of a video

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recording made during the VICS outage, the licensee identified

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foreign material on the lower support plate. The identification

of the foreign material was made after the commencement of core

reload activities; however, was in time to allow the licensee to

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remove the foreign material (part of an upper grid assembly) prior-

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to placing an assembly in the subject area.

This possibly

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prevented a previous tilted fuel assembly problem.

The inspectors discussed with the licensee why a video review,

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which had appeared to have been proved prudent in previous core

reloads, was not performed for the UIC6 core load. The licensee

indicated that they did not feel that the video taping and

additional review was necessary. The licensee stated that they

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primarily relied the personnel performing the inspections "on

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line" to properly identify any foreign objects. Additionally, the

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video was previously performed because it was convenient to

complete coincident with other required inservice inspection

procedures.

Corrective actions for 11-S-91-118, which were

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initiated as a result of the foreign material found during the

UICS outage, included procedure revisions to N-VT-8, VISUAL

EXAMINATION OF PWR REACTOR VESSEL INTERIORS AND INTERNALS. The

revisions were made to ensure that timely review of the video was

performed prior to fuel reload. However, prior to the VIC6

4

reload, responsibility for foreign material inspections was

transferred to the reactor engineering group.

Video taping and

additional reviews were not included in the reactor engineering

procedural requirements.

Based on the above information and discus.; ions with the licensee,

the inspectors concluded that, review of a video inspection of the

core support would not have ensured the identification of the

foreign object.

However, the video review would have provided an

additional opportunity for identification, as was established

during the Unit 1 Cycle 5 outage.

The inspectors reviewed the licensee's performance regarding

foreign material exclusion / detection during the Unit 1 Cycle 6

refueling outage from a regulatory point of view. During the Unit

1 Cycle 5 refueling outage, the licensee discovered a foreign

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object in the reactor vessel during fuel reload.

The licensee was

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able to recover the object prior to placing any fuel assembly in

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the location of the foreign object. An incident investigation of

that event was conducted and the licensee implemented corrective

actions to prevent recurrence. However, those corrective actions

were not effective in preventing a foreign object from causing a

fuel assembly to tilt out of position during the Unit 1 Cycle 6

refueling outage.

10 CFR 50, Appendix B, Criterion XVI requires, in part, that

measures shall be established to assure that conditions adverse to

quality such as.nonconformances are promptly identified and

corrected.

In the case of significant conditions adverse to

quality, the measures shall assure that the cause of the condition

is determined and corrective action taken to preclude repetition.

Failure to adequately implement corrective action for

identification and removal of foreign material in the reactor

vessel prior to the Unit 1 Cycle 6 core reload is identified as a

violation of 10 CFR 50, Appendix B, Criterion XVI (327, 93-23-04).

Within the areas inspected, one violation was identified.

5.

Surveillance Inspections

(61726 & 42700)

During the reporting period, the inspectors reviewed various

surveillance activities to assure compliance with the appropriate

procedures and requirements. The inspection included a review of the

following procedures and observation of surveillances:

H

a.

On July 10, 1993, the inspectors reviewed activities associated

with 2-SI-0PS-026-180.A, FIRE PUMP 2A-A START TEST, Revision 2.

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The SI partially fulfills Surveillance Requirement 4.7.ll.1.a by

providing steps to verify the operability of- the 2A-A fire pump

via a start and 15 minute run. The inspectors reviewed the-

documentation in the SI package and verified the as-left condition

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of components utilized during the testing activities.

No

discrepancies were noted.

b.

Late in the inspection period, the inspectors reviewed

approximately 35 records contained in 0-SI-0SL-000-011.0,

CONTAINMENT ACCESS, Revision 3.

The records reviewed were for

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Unit 2 containment access authorizations for July 9,1993. The-

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inspectors noted that all records appeared to be accurate,

detailed, and complete.

Sign-off's for end of work cleanliness

and foreign material accountability were completed as required.

These reviews were accomplished, in part, due to recent licensee

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identified problems associated with foreign material exclusion

issues.

The inspectors will continue to closely monitor this

area.

Within the areas inspected, no violations were identified,

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6.

Evaluation of Licensee Self-Assessment Capability (40500)

During this inspection period, selected reviews were conducted of the

licensee's ongoing self-assessment programs in order to evaluate the

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effectiveness of these programs.

,

a.

On June 11, 1993 the inspectors attended the exit meeting for a

Senior Management Oversight Group (SM0G) which had been

established for the purpose of providing senior TVA nuclear

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management with independent assessments of the Sequoyah Restart

Program, its implementation, and an operational readiness review

prior to restart. The principal function of the group was to

provide advice and assistance to TVA management on the

programmatic issues related to the restart of Sequoyah Nuclear

Pl ant.

The SM0G had concluded at this point in their review that the

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current Sequoyah Restart Plan is adequate, and if executed as

planned would provide for return of Sequoyah to safe operation.

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The SM0G considered that the restart schedule was aggressive and

that a continuation of observed performance errors raised a

concern of the effectiveness of ongoing corrective actions.

The inspectors consider that the SMOG exit provided licensee

,

senior management with a frank and honest perception of where

Sequoyah was regarding restart readiness.

The inspectors will

continue to monitor the results of the licensee's independent

assessments.

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b.

During this inspection period, the inspectors have been provided

with weekly updates on the licensee's Nuclear Assurance Restart

Readiness Reviews.

The Nuclear Assurance department has been

conducting reviews in several areas in order to evaluate Sequoyah

readiness for restart. These areas include (1) Balance of Plant,

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(2) Operations department, (3) Programs, (4) Backlogs / Work

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Prioritization, (5) Personnel, Organization, and Culture, and

Corporate / Site Interface.

Reviews through July 1, 1993 indicate that improvement is needed

in all areas reviewed except for Corporate / Site Interface. The

inspectors will continue to monitor the licensee's effort in this

area. However, the inspectors are also continuing with

independent assessments of the licensee's restart plan.

The inspectors consider that the Nuclear Assurance effort is

providing positive feedback to plant management.

The effort is

identifying several areas which need continuing management

attention.

c.

On July 2, 1993 the inspectors attended the exit meeting for the

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Sequoyah Nuclear Plant Restart Readiness Team (RRT) review of

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Operations. The RRT was a team lead by a TVA senior manager and

staffed by experienced contractors. The RRT conducted reviews of

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the Operations Department in the middle of May 1993, and returned

on June 21, 1993 for an additional 2 weeks of assessment.

The team noted several positive observations during the exit

meeting on July 2.

They were: (1) Communications between the

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Operations department management and the Operations staff

continued to improve; (2) 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shift rotation implementation

with five discrete groups was considered a significant

accomplishment which would strongly support a team approach to

plant operation; (3) General operator attitudes continued to

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improve; (4) Some progress had been made in upgrading procedures;

and (5) Operations ownership of plant conditions was improving.

Several other observations were made concerning site management

following through with what they started, other departments

support of the Operations initiatives, and Operations management

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emphasis of SOS /ASOS tours of the plant / procedural compliance

across the board / consistent self checking practices.

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The RRT concluded that the Operations department would be ready

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for the planned restart of Unit 2 provided that consistent

application of standards by management continues, and provided

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more proactive, effective support is undertaken by other

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organizations.

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The inspectors consider that the RRT provided a reasonable

assessment of their observations of the Operations department.

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The inspectors will continue with their independent assessment of

the performance of the Operations department.

Inspector

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observations for this period are discussed in paragraphs 3 and 9

of this report.

The inspectors considered that the licensee's ongoing self assessments

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are providing meaningful input to site and corporate management

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regarding restart plan acceptability and implementation.

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Within the areas inspected, no violations were identified.

7.

Licensee Event Report Review (92700)

The inspectors reviewed the LERs listed below to ascertain whether NRC

reporting requirements were being met and to evaluate initial adequacy

of the corrective actions.

The inspector's review also included

followup on implementation of corrective action and/or review of

licensee documentation that all required corrective action (s) were

either complete or identified in the licensee's program for tracking of

outstanding actions.

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a.

(Closed) LER 327/92-19, Technical Specification Radiation Monitor

Setpoints Nanconservative. The licensee issued this LER when

certain TS radiation monitors setpoints were found calculated

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nonconservatively. The subject monitor setpoints.did not account

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for the system design, which has the gas sample chamber upstream

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of the sample pump. This arrangement creates a partial vacuum

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near the detector when sampling, which reduces the air (and

potential radionuclide) density. To account for actual

radionuclide concentration, a correction factor is made to the

radiation monitor setpoint. The licensee had revised affected

l

procedures by December 31, 1992 to account for their design.

To verify that they did not exceed an actuation setpoint on this

monitor during previous operations, the licensee reviewed previous

!

plant data sheets. The licensee's review showed that they did not

exceed an actual actuation setpoint during previous plant

i

operations.

The licensee attributed the root cause for this event as a

miscommunication within TVA. The radiation monitor vendor

informed the licensee about the basis for the detector

t

calibration, but the plant did not receive this information.

The

licensee noted that their current controls of vendor information

l

'

should prevent a similar problem.

i

b.

(Closed) LER 327/92-21, Failure to Verify Valve Positions for

Verification of Containment Integrity.

The issue involved failure

i

to perform verification of containment integrity for ten manual

drain and test connection valves in each unit. The su. 1illance

instruction steps were waived by the performers when the units

'

were at power because of potential industrial safety concerns.

_

The inspectors reviewed the licensee's corrective actions and

i

verified that SSP-2.51, RULES FOR PROCEDURE USE, Revision 0 was

!

issued to clarify requirements for procedure step waiver.

!

)

However, the licensee also stated in their LER response that 7.n

earlier LER 327/92-03 identified an event where fire protection

i

valves inside containment were waived for inspection. The

'

inspectors concluded that the corrective actions for LER 327/92-03

should have identified the problem discussed in this LER.

10 CFR Appendix B, Criterion 16 requires, in part, that conditions

adverse to quality are promptly identified and corrected.

Failure

j

to promptly identify the procedure problem associated with this

,

LER during corrective action for LER 327/92-03 is identified as a

]

,

violation (327, 328/93-23-03).

,

c.

(Closed) LER 327/92-22, Control Room Emergency Ventilation System

Inoperable Because of Closure of Tornado Dampers.

The issue

involved entry into LCOs 3.0.3 and 3.7.7 when both trains of the

control room emergency ventilation system (CREVS) were declared

..

.

,

I

j

22

inoperable following clesure of the tornado dampers that isolate

the fresh air intake to the CREVS. Operations personnel closed

the tornado dampers in accordance with abnormal operating

instruction (A01). After the downgrading of the torndo warning

i

to a tornado watch, the CREVS was returned to operable status, and

the LCOs were exited.

The inspector reviewed A01-8, Tornado

Watch / Warning, and concluded that the correct actions,

i.e.,

'

closing the tornado dampers, were implemented in response to the

tornado warning.

d.

(Closed) LER 327/93-01, Ice Bed Monitoring Surveillance

i

Requirement Time Interval Exceeded Because of Poor Communications.

l

The issue involved inadequate communication between operators and

i

others regarding conditional surveillance requirements when the

equipment normally used to monitor a TS required parameter becomes

i

inoperable.

Licensee corrective actions included additional

!

training and review of this event with operations crews.

In

'

addition, a more formal method of initiating conditional sis was

developed and implemented.

e.

(Closed) LER 327/93-02, Manual Reactor Trip as a Result of a Lock-

!

up of the Rod Control System. The issue involved operator

initiation of a manual trip due to experiencing an urgent failure

'

condition in the rod control system during a controlled shutdown.

i

The operators manually tripped the reactor from low power due to

'l

Xenon increasing and possibly shutting down the reactor while

troubleshooting was being planned for the rod control system. The

!

cause of the rod control problem was subsequently determined to be

i

a problem in the timing circuitry of the rod control system. The

inspectors reviewed the licensee actions at the time of the

'

problem and the LER. All actions were considered to be correct

2

based on conditions.

t

f.

(Closed) LER 327/93-03, Reactor Trip as a Result of an Inadvertent

,

Trip of the Exciter Field Breaker. The issue involved an

automatic reactor trip of Unit I from approximately 100 percent

power due to personnel error. The event was discussed in

inspection report 327, 328/93-05.

Licensee corrective actions

included appropriate action against the person making the mistake.

'

In addition, a plant policy on activities associated with

sensitive equipment was established. This policy was established

.

'

with a new procedure (SSP-12.63, SENSITIVE EQUIPMENT CONTROL,

Revision 0). The inspectors reviewed the LER and the licensee's

corrective action.

g.

(Closed) LER 327/93-04, Containment Personnel Airlock Blind Flange

Leakage Causes Airlock Inoperability. The issue involved licensee

identification of a potential containment leakage path which was

i

greater than TS bypass leakage limits. This issue was discussed

!

in inspection report 327, 328/93-05. A violation of regulatory

requirements was issued for this event.

The inspectors reviewed

___

_

,

.

.

,

.

23

the LER and will review other licensee corrective actions during

closecut of the violation.

,

h.

(Closed) LER 327/93-05, Inadvertent Actuation of a Containment

Isolation Valve During Response-Time Testing Performance as a

Result of Personnel Error. The issue involved instrument

'

maintenance personnel shorting a circuit during performance of a

,

maintenance activity. The shorted circuit resulted in a blown

fuse and a containment isolation valve closing. After the event,

1

the fuse was replaced and the valve reopened. Part of the event

was attributed to limited access for installation of test

l

equipment.

Corrective actions included instructing maintenance

personnel to be more careful when working in limited access areas.

The inspectors reviewed the LER and licensee actions.

,

i

i.

(Closed) LER 327/93-07, Inadvertent Actuation of a Containment

!

^

Isolation Valve as a result of Removal of Fuses from the Wrong

Circuit. This issue involved the actuation of a containment

isolation valve when its control power fuses were mistakenly

removed. The subject valve is a containment radiation monitor

isolation valve. The mistake was immediately identified by the

AU0 performing the fuse removal. The licensee attributed the

event to personnel error as a result of inadequate self-checking

'

and a failure to follow applicable procedures during the

installation of clearance tags.

In addition, equipment label

l

deficiencies were considered contributing factors.

The inspectors reviewed the specific errors made during the fuse

3

pulling process. According to the licensee's report, two

personnel were performing the evolution utilizing independent

,

verification techniques, rather than second-party verification

,

techniques. The individual incorrectly assumed that the

'

independent verification was of a higher quality than the second

party process. However, in the situation of pulling fuses, this

assumption allowed an error to occur, which resulted in the

inadvertent actuation.

'

The licensee has had previous problems with regard to independent

and second party verifications.

Like this event, the majority of

them issues were the result of the wrong type of verification

beix .ssigned to the activity. However, the inspectors

,

'

considered that the previous activities resulted in the wrong type

of verification being assigned due to the existence of an

i

inadequate PMT with the activity.

Regardless, the inspectors were

'

concerned that corrective actions taken for the previous events,

,

which included increased verification training, did not preclude

this event.

The inspectors reviewed the corrective actions for this event.

,

Immediate actions included the restoration of the affected

i

equipment to service. Other actions included the installation of

fuse column identification nameplates for the identified areas,

j

.

".

,

.

.

l

24

'

In addititn, retraining was provided to personnel that perform

clearance process tagouts with regard to the proper verification

methods.

The licensee is also continuing to emphasize

expectatiors relative to personnel errors, failure to follow

procedures, and work verification requirements via long term

corrective attions for these type of events.

Based on the

inspectors re/iew, corrective actions for this event are

)

considered adequate.

,

!

j.

(Closed) LER 328/92-14, Limiting Condition for Operation Entered

i

Because of Hydrogen Analyzer Inoperability.

The issue involved

the entry into TS 3.6.4.1 and 3.0.5 because the A-train hydrogen

analyzer was inoperable, and the emergency power to the B-train

hydrogen analyzer was out of service for routine maintenance. The

A-train hydrogen analyzer wn inoperable because of a leaking

t

pressure-relief, pop-off valv2 on the reagent gas supply header.

The pop-off valve had allowed the reagent gas bottles to slowly

I

leak down such that insufficient gas was available for the

hydrogen analyzer to perform its intended function. The root

cause of the event was the unexpected failure of the pop-off

i

valve.

The inspector reviewed the licensee's documentation of the

corrective actions taken which involved replacing a seal ring in

the valve. The work was performed per Work request C133967 and

completed, final review, on November 13, 1992.

k.

(Closed) LER 328/93-02, Containment Boundary Isolation Valves

,

Discovered Misconfigured for an Indeterminate Reason. The event

occurred on March 21, 1993 on Unit 2 while in Mode 5, and involved

an unplanned clo.sure of Engineered Safety Feature valve 2-FCV-77-

10.

It resulted from a high spike on radiation monitor, 2-RM-90-

278, Reactor Coolant Drain Tank Discharge and resulted in the

initiation of Incident Investigation, II-S-93013, which revealed

that the RM had been spiking and closing the valve since November

13, 1992. However, this was not considered to be reportable since

the radiation monitor does not initiate an ESF signal and was not

an instrument required by the Technical Specifications.

The inspectors reviewed the incident investigation and learned

that the corrective actions taken by the licensee were to upgrade

the work priority for Work Request, WR C174065, that had been

initiated on November 13, 1992 to correct the condition. The WR

had not been given sufficient priority based on an evaluation that

the instrument was not a Technical Specification requirement and

replacement of the monitor was not completed until April 4,1993.

Although the event first occurred in November 13, 1993, the

licensee determined it not to be reportable and therefore no

report was issued.

The event occurred several more times and not

reported until the occurrence on March 21, 1993. The earlier

determinations that the event was not reportable was based on the

-

-

.

.

.,

.

25

philosophy that component level actuations were generally not

reportable. This philosophy was later discussed on May 6,1993 in

an NRC sponsored workshop on Draft Revision 1 to NUREG-1022,

'

" Event Reporting Systems - 10 CFR 50.72 and 10 CFR: 50.73:

Clarification of NRC Systems and Cuidelines for Reporting." It

appears that the philosophy used which resulted in the licensee

not reporting the earlier events meets the criteria for non-

reportability as outlined in the workshop discussions. The

inspectors determined the licensee's corrective actions were

acceptable.

1.

(Closed) LER 328/93-03, Inadvertent Actuation of Engineered Safety

Feature Component as a Result of Equipment Failure. The issue

involved continued spiking of a radiation monitor causing a

containment isolation valve to close. After increased sensitivity

by operators determined that the valve closure was reportable,

prioritization of maintenance was increased and the radiation

monitor was determined to have a failed detector. The failed

detector was replaced to resolve the problem in March 1993.

The inspectors reviewed the event and corrective actions. The

inspectors also noted that management has reenforced expectations

to operations personnel with emphasis on escalation and resolution

of repeat alarms from plant equipment. The inspectors have noted

this type of increased operator sensitivity during the recent

past.

m.

(Closed) LER 328/93-04, failure to Perform a Technical

Specification Surveillance Instruction for Verification of Ice

Condenser Chemistry Within the Required TS Timeframe.

The issue

involved the licensee's failure to perform a TS required

surveillance of the boron concentration of the ice in the Unit 2

ice condenser within 12 months. This issue was reviewed in

-

inspection report 327, 328/93-09.

In that report a review of the

issue and licensee corrective actions resulted in identification

of a non-cited violation. The inspector reviewed other corrective

actions identified in the LER and determined that they were

accomplished.

Within the areas inspected, one violation was identified.

8.

Action on Previous Inspection Findings

(92701,92702)

a.

(Closed) VIO 328/92-11-02, Failure to Follow and/or Inadequate

Procedures Resulting in a Loss of Configuration Control of the

Spent Fuel Pit Cooling System. The issue involved improper

operational control of the spent fuel pit cooling system due to

inadequate procedures.

In addition, configuration control

administrative processes were either not required for this

condition or applied in an inconsistent manner.

. _ _ -

_

_

_

._

-

,

.

.

.

26

!

The licensee responded to the violation in a letter dated June 12,

,

1992. Corrective actions for the violation included revision of

the applicable operational procedures to provide valve checklists

for different conditions.

In addition, the administrative-

,

controls for configuration of systems was enhanced.

Also,

.

operations personnel performance meetings were conducted to

j

emphasize rigorous and consistent application of basic operational

tools in everyday performance of work to prevent mistakes.

-

The inspectors reviewed the licensee's implementation of

corrective actions for configuration control problems and consider

that actions are complete for this violation.

.

b.

(Closed) VIO 327/92-29-01, failure to Maintain Operable B Train

i

Safety Injection Pump From July 31 to August 10, 1992. The issue

!

'

involved a misaligned (stuck) pump breaker trip button which

rendered the subject pump inoperable for the period stated.

,

t

'

The licensee responded to the violation in a letter dated October

29, 1992.

Corrective actions included design and installation of

new, longer pump trip buttons on all safety-related 6.9 KV

breakers.

In addition, the licensee instituted extensive

corrective measures to enhance the verification and post-

maintenance testing processes and practices.

The inspectors reviewed the licensee's implementation of

corrective actions for this violation.

The inspectors have

verified that all safety-related 6.9 KV pump breakers have been

modified with longer trip buttons.

In addition, the inspectors

are reviewing ongoing corrective actions for verification of

,

system configuration control and post-maintenance testing. The

inspectors consider that corrective actions have progressed to a

point where this violation can be closed.

c.

(Closed) VIO 327, 328/92-36-03, Failure to follow and/or

inadequate procedures for configuration control of RWST heaters

I

and EDG fuel oil pump transfer switch positions. The issue

involved misposition of the IB1-B and the IB2-B day tank supply

pump handswitch to the off position instead of the auto position.

The normal position of the switch is the auto position, reference

i

501-82.2 Diesel Generator IB-B, Revision 39, Section 82.2G, V.B.2.

The licensee responded to the above violation by letter to the

NRC, dated February 16, 1993. The inspector verified that the

licensee completed actions as stated in the above letter.

i

d.

(Closed) URI 327, 328/88-37-01, Concerns Regarding High Impedance

Faults and the Requirements of 10 CFR 50, Appendix R.

The issue

involved the requirements of 10 CFR 50, Appendix R, Section

III.G.2 with regard to maintaining one train of hot standby

systems free of fire damage.

Concerns were identified in IR 327,

328/88-37, that high impedance faults were not addressed in the

.-

.

$

27'

i

Associated Circuits Analysis which would affect the licensee's

i

ability to meet the requirements of 10 CFR 50, Appendix R.

.

To address the concern, the licensee prepared Calculation No. SQN-

APS-015, dated April 9, 1990. The calculation concluded that

there was margin available in all of the normal upstream feeder

i

breaker trip settings for each distribution board such that, a

breaker trip, as a result of high impedance fault currents during

.

an Appendix R event, was not a concern and that no modifications

!

were reeded. Subsequent review by the NRC staff concluded that

'

the licensee's calculation was acceptable. The review determined

i

that the calculation was acceptable. The review also recognized

1

that the calculation addressed certain recommendations for other

'

possible improvements; however, NRC review concluded that there

was sufficient margin in the main feeder breakers' long-time trip

settings such that no plant modifications were warranted.

,

On September 1,1992, the licensee revised Calculation SQN-APS-015

,

to remove the recommendations to de-energize the load breakers for

the non-1E power outlets and resetting the long-time setting for

!

the 480 volt C & A vent board 2Al-A. These revisions were made

based on the adequate margins to sustain high impedance faults on

the Appendix R distribution boards as detailed in the calculation.

Based on review of the licensee's calculation SQN-APS-015, the

'

inspectors consider the URI closed.

!

e.

(Closed) IFI 327, 328/88-37-02, Concerns Regarding Separation of

Cables and the Requirements of 10 CFR 50, Appendix R.

The issue

involved the requirements of 10 CFR 50, Appendix R, Section '

III.G.2 with regard to maintaining one train of hot standby

systems free of fire damage. Concerns were identified in IR 327,

i

328/88-37 with respect to separation of cables associated with the

VCT and Charging Pump B such that the licensee could not meet the

i

requirements of 10 CFR 50, Appendix R and would not be met until

completion of certain modifications.

The issue was originally identified as part of a 1984 10 CFR 50,

Appendix R, reevaluation.

The concern was identified as

Interaction 120 in IR 88-37.

Interaction 120 identified cables

that could interact with the control cables for the VCT outlet

j

valves (FCV-62-132, 133) at multiple locations within the plant.

Because these valves are connected in series, spurious actuation

(caused by fire) of either valve could cause a loss of suction to

both of the charging pumps. The licensee took immediate

compensatory actions via placing the area under a roving fire

watch round while the issue was being resolved.

The licensee's original disposition of the issue consisted of

j

operator action to remove power from the valves and to switch over

to the RWST for CCP suction if fire was confirmed in various areas

of the auxiliary building. NRC IR 88-24 concluded that this

disposition was unacceptable. This was based on inadequate

.

-

.

.

28

assurance that, if the valves closed and the non-operating CCP was

also damaged by fire, the operating CCP could be shut off before

sustaining damage.

The licensee's final resolution of Interaction 120 was to add

ste -mounted limit switches on the VCT outlet valves designed to

open the redundant train RWST outlet valve. The modification

ensures that adequate suction is maintained on the operating CCP

in the event of the postulated fire. The inspectors verified

completion of the above modifications via the work documentation

package. The work was performed during each Unit's respective

cycle 4 refueling outage.

Based on a review of the above modification, the NRC staff

considered that Appendix R requirements for Interaction 120 were

being met.

Within the areas inspected, no violations were identified.

9.

RESTART REVIEW ACTIVITIES

During this period, inspection activities continued regarding review of

the licensee's restart plan. These inspections included verifications

that the licensee was following their plan in the backlog and operations

areas.

Initial inspections of the licensee's restart plan were

addressed in inspection report 327, 328/93-16.

a.

Review of Backlog Evaluation Process (71707)

During this inspection period, the inspectors reviewed the

licensee's backlog evaluation process. The inspectors verified

,

that open items which were evaluated by the licensee as restart

1

items met the criteria established.

Items which were not restart

items were verified by the inspectors to have an acceptable

justification to defer until post restart. The inspectors

reviewed the system backlog notebooks which the licensee developed

to document these evaluations. The system notebooks contained

!

maintenance work request listings, CAQ corrective actions, DCNs,

Major Issues List items, obsolete equipment items, and other open

i

issues. The inspectors verified that items recommended.by the BRC

,

as restart items were listed on the most current Restart Evalu-

l

ation For Sequoyah Nuclear Plant printout or were scheduled to be

presented to the MRRC.

Items identified as non restart items were

j

reviewed and discussed as necessary with the accountable system

,

engineer to ensure that adequate justification existed to defer

until post restart.

The inspectors reviewed system notebooks for the following sys-

tems:

System 01

-

Main Steam

-

. . -

-

-

'

>

.

. .

..

i

.

I

I

29

i

System 03

-

Auxiliary Feedwater

)

'

l-

System 15

-

' Steam Generator Blowdown

System 18

-

Fuel Oil

l

,

System 26

-

High Pressure Fire Protection

System 30

-

Ventilation

.

System 56

-

Temperature Monitoring.

l

System 62

-

Chemical and Volume Control

System 63

-

Safety Injection

,

System 65

-

Emergency Gas Treatment

System 67

-

Essential Raw Cooling Water

System 70

-

Component Cooling Water

System 72

-

Containment Spray

System 74

-

Residual Heat Removal

e

System 78

-

Spent Fuel Pit Cooling

System 82

-

Standby Diesel Generators

I

!

System 83

-

Hydrogen Recombination

System 86

-

D/G Starting Air

1

1

System 88

-

Containment Isolation

j

System 90

-

Radiation Monitors

Reactor Protection

.

System 99

-

System 249 -

Standby Diesel Batteries

System 268 -

Hydrogen Mitigation

The inspectors identified that the work request listings were

difficult to audit because each system engineer did not annotate

restart items consistently.

The inspectors required system engi-

neers assistance to interpret the notations in the backlog

notebooks in order to evaluate the disposition of work requests.

In addition, the inspectors identified several cases where

department manager signatures or system engineer concurrences were

not signed off on the Backlog Review For Restart forms. The

.e

l

.

,

,

.

'

30

inspector considers this a lack of attention to detail in

i

documenting the backlog reviews.

The incomplete sign-offs were

corrected when the inspector informed the licensee.

The inspector

considered system engineer knowledge good and did not identify any

instances where backlog items were deferred without proper

justification.

During reviews of the RHR, Containment Spray, and Containment

f

Isolation systems, the inspectors considered the system engineer

'

knowledge and understanding of the overall system condition to be

good. The inspectors identified several items that were

identified as non restart that did not contain sufficient detail

in the system notebooks to determine the extent and scope of the

activity to be accomplished and did not contain adequate

documentation to justify the non restart determination. These

.i

items were discussed with the system engineer and determined to be

l

non restart items; however, in several instances the system

engineer was not completely cognizant of the activity identified

,

as non restart and had to research the item prior to providing the

justification for the item being identified as non restart.

,

During reviews of the CVCS, SI, and Radiation Monitoring system

notebooks, the inspectors noted inconsistencies in methodologies

'

used by each system engineer to keep the notebooks current which

made the books difficult to understand and audit.

System

engineers were generally very knowledgeable of their systems and

'

the application of the restart criteria to the identified backlog

,

items, however; they were not aware'of the status of work

completion on their systems.

During inspections of backlog for the ERCW and FP systems, the

t

inspectors concluded that backlog reduction decisions were made on

i

number rather than criteria.

For the ERCW systems some of these

,

types of calls were made for the backlog of open WRs (180) to be

i

reduced by 60%. One exception was the replacement of the

traveling screens wire mesh. The mesh has a large number of holes

and the WR will install stainless steel mesh.

This was not made a

restart item even though the system engineer stated that the

traveling screens were one of the top three system problems.

,

,

Of the 99 open WRs in the Fire Protection System, only 25% will be

closed prior to restart. The inspectors questioned some of the

items in this system that will not be worked for restart.

They

>

were:

,

-

Reachrod inoperable for hose station isolation valve

-

Sticking handswitch for strainer backflush

-

Slow response time for annunciator and pump start signal

due to pressure switch not actuating properly

.

. _ _

_

-

_

_

_

__

__

_-

.

.

.

'

.

31

-

Isolation valve difficult to operate (two men could not

operate)

-

Need to replace leaking valve which allows ERCW pump house

1

hose station to pressurize and makes it difficult to use

j

During reviews of the backlog status for the Fuel Oil and Spent

I

Fuel Pit Cooling systems with cognizant system engineers, the

j

inspectors concluded that the system engineers were significantly

.

involved in the initial backlog review, for items prior to May 1,

1993, and the restart criteria had been implemented correctly in

l

each of the backlog dispositions for these systems.

Both system

l

engineers indicated that they were satisfied with the backlog

'

dispositions for all open work.

The inspectors noted that backlog reviews were not included in the

i

notebooks for items identified after May 1, 1993.

In addition,

i

the inspectors discussed Operations review of WR/W0s with the SRO

l

assigned to review them for. the Work Control section. This SR0

-

'

stated that backlog evaluation sheets were not filled out for new

WR/W0s; the backlog determination were made by the work control

SR0 and documented on the WR card. Any item required to be

completed prior to restart would then be placed on the restart

i

list. The remainder of the items will be part of the backlog.

!

The licensee's restart plan for backlog includes programmatic

reviews for several types of programs. The inspectors discussed

!

the licensee's method.for conducting the programmatic reviews and

i

!

identified no concerns. The inspector reviewed the backlog status-

for TACFs and discussed the justification for the restart

'

dispositions with the cognizant engineer.

From this_ review, the

'

inspector concluded that the restart criteria were satisfactorily

i

implemented for TACFs.

l

During reviews of the Hydrogen Mitigation, and Hydrogen

!

Recombiners systems, the inspectors noted only one work request

per system was identified as backlog. The inspectors determined

i

that both had been properly evaluated by the licensee for restart.

During reviews of the Component Cooling System, the inspectors

,

noted 100 open work orders that were not identified in the outage

schedule.

Fifty-seven of these items were designated as required

i

for restart.

Five DCNs were identified and 4 of those were

,

designated as required for plant restart.

The inspectors agreed

with the licensee's evaluation of the work items based on the

restart criteria. However, the inspectors consider that post

i

restart items which do not jeopardize the function of the system

i

such as missing needles on local indicators should receive high

!

priority for post restart corrective action.

l

!

The inspectors performed a walkdown of Reactor MOV Boards to

[

evaluate the adequacy of the drawings to the configuration for the

<

i

!

t

!

. , _

_

r

...

.

.

.

.

32

Component Cooling System.

The following drawings were reviewed as

l

part of this inspection for the electrical breakers. These were

i

as follows:

-

CCD 1,2-45N751-8, R-II, Wiring Diagrams 480V Reactor MOV BD

182-B Single Line SH-2

,

-

CCD 1,2-45N751-4, R-9, Wiring Diagrams 480V Reactor M0V BD

1A2-A SINGLE LINE SH-2

-

CCD 1,2-45W751-3, R-10, Wiring Diagrams 480V Reactor MOV BD

1A2-A Single Line Sheet-1 One discrepancy was identified on

this drawing. The hand switch for FCV-70-139 was identified

as FCV-70-130 handswitch. The licensee initiated action to

correct the deficiency.

Preventative Maintenance

The preventative maintenance for the following electrical breakers

was reviewed during the inspection period to determine the

>

adequacy of the preventative maintenance program. The results of

this review are as follows:

Date of Reg'd

Board

Compartment

Equipment

Last PM Frequency

SD 181-B

3C

CCS PMP 1B-B

4/90

3rd Refuel

SD 1A2-A

4C

CCS PMP C-S

4/90

3rd Refuel

SD 1Al-A

4B

CCS PMP 1A-A

4/90

3rd Refuel

'

MOV IB2-B

13B

FCV-70-26

NONE

MOV 1B2-B

11A

FCV-70-3

NONE

MOV IB2-B

14B

FCV-70-75

NONE

MOV IB2-B

20A

FCV-70-207

NONE

MOV IB1-B

SE

T.B. PUMP IB-B

7/93

4th Refuel

MOV 1A2-A

19E

FCV-70-197

NONE

'

MOV 1A2-A

13A

FCV-70-10

NONE

j

VENT 2Al-A

SC

H2 INVERT 0R

NONE

VENT 281-B

7B

H2 INVERT 0R

NONE

,

The General Electric Vendor Manual, SQN-VTM-Gn30-0010, recommended

i

two tests be performed on the subject breakers which consisted of:

(a) Routing Field Testing and (b) Verification Field Testing.

However, the vendor specified that the frequency of testing should

include allowances for environmental conditions at the breaker

locations, such as dust, temperature, frequency of operation, and

etc.

However, EPRI did issue a recommended test periodicity for

molded case circuit breakers. This was published in EPRI NP-7410s

Vol. 3, October 15, 1991.

The licensee has indicated that the current program does not

provide for testing of molded case circuit breakers that are not

included in the Technical Specifications.

Some plans have been

.

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33

,

!

initiated to start testing the safety-related breakers which are

not designated as required by the Technical Specifications to

verify operability. However, the test program for testing

-

breakers not specified in the Technical Specifications has not

'

been formalized. This will be identified as an Inspector Follow-

up Item, 327, 328/93-23-05, Review of Licensee Program to Test Non

T.S. Molded Case Circuit Breakers.

,

,

During the last week of the inspection period, the inspectors

reviewed the restart determinations for backlog and emergent work

items for system 99, Reactor Protection System, and portions of

the ventilation system designated as system 30. The inspection

t

consisted of system notebook reviews, discussions with system

engineers, comparisons of information in the system notebooks with

the work scope defined in the outage work list and that contained

in the work request / order data base, and review of the outage

scope addition and deletion process.

For system 99, no items were identified which should have been

i

designated restart per the Restart Plan criteria that were not

identified as such.

However, Unit I restart item number 103 was

,

consider closed, as indicated by completion of a closeout form by

the Technical Support ICE supervisor on July 1,1993, with only

part of the work performed. The system engineer indicated that

the intent of the item had been met and the form contained

adequate justification that replacement of only three of the four

specified Solid State Protection System power supplies were

necessary prior to restart. At the time restart item numSer 103

was reviewed by MRRC, MRRC was informed that the vendor had five

power supplies available and work request C128741 and C128742 were

designed to be performed prior to restart. These work request

were written to either replace or refurbish the powers supplies on

unit 1 SSPS trains A and B.

Subsequently, the vendor was able to

only provide three new power supplies. Thus, the closeout

involved a reduction in scope and was authorized at a level of

management below the level of management that had required it to

be performed.

This inappropriate practice was discussed with

plant management. Work request C007360 was subsequently issued on

July 8 to replace the fourth power supply.

In addition, at the

end of the report period, guidance was being prepared to inform

plant personnel of management's expectations involving processing

closure of items involving scope reductions.

During discussions concerning the appropriateness of the closure

of restart item number 103, the licensee identified to the

'

inspectors that the closure form had been signed at a level of

management below that anticipated. The management expectation was

that closure forms would be signed by a department manager or

higher level of management, i.e., was not to be delegated down the

management chain. At the end of the report period, actions were

being taken to ensure that appropriate personnel were aware of

this management expectation.

>

.

.

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34

The inspection of the system 30 items was not completed in that it

was not possible to determine why certain items did not meet the

restart criteria.

The lead system engineer for the system was not

available during the inspection and the other system engineer that

was assigned portions of this system was unable to explain, from

the existing documentation, why some items were included or

excluded from the restart work scope.

This was especially evident

in discussions associated with ventilation components for the

turbine building.

For the safety-related components, it was

1

apparent that the criteria for designating items as work prior to

restart had been conservatively implemented.

During the inspection, it was determined that inconsistencies

,

existed among system engineers' understanding of the priority

codes 'as they related to restart.

Engineering supervision

.'

indicated that actions would be taken to ensure engineering

'

personnel understand the use of priority codes.

In addition, the

inspectors determined that there were significant inconsistencies

among system engineer's understanding involving management's

implementation expectations for restart criteria 5 and 6

associated with B0P equipment availability and plant reliability.

At the time of the inspection, this appears not to be a problem

'

due to the amount of special management oversight and the

conservatism used to date in categorizing items. However, during

future outages, when the special review processes of the present

outages are no longer in place, it will be important that system

engineers clearly understand managements' expectations in this

'

area.

During a briefing on July 9,1993, the Site Vice-President

indicated that this observation involving the system engineers'

restart criteria understanding independently confirmed information

that he had received from his staff.

He indicated that additional

training would be provided to the system engineers, possibly

including meetings between the system engineers and the MRRC.

As part of the inspection associated with emergent items, the

inspectors reviewed the use of the addition / deletion form, Att.

3.2 to the Restart Plan. The inspectors determined that there had

existed a misunderstanding concerning when deletion of items from

the outage required use of Att. 3.2 with its additional management

reviews, as well as, Site Standard Practice form 7.2, the usual

mechanism for removing items from the outage. When this was

discussed with plant management, the inspector was informed that

this problem had previously been identified and actions had been

taken to identify and correct this deficiency for unit 2 items and

similar actions had been initiated for unit 1 items.

In addition,

the inspectors noted that, on occasion, Att. 3.2 forms would

indicate that an item was to be deleted from the outage due to

lack of materials but would not address why it was acceptable per

the restart criteria to delete it as a restart item.

In each

instance, the form had been returned or in the process of being

returned to the system engineer for additional deletion

justification. This was discussed with the cognizant Technical

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35

Support supervisor who indicated that he would review the

situation and take actions, if necessary, to address this

-

observation.

The inspectors noted examples in which communication problems had

occurred between various management organizations.

In addition to

the closure form signature authorization misunderstanding

discussed above, the following examples were noted. The BRC

members had_ indicated to the inspectors that for emergent items

identified between May 1 and July 1,1993, the BRC had been tasked

by the MRRC to verify by sampling that the items had been properly

classified as restart or non-restart. However, the Site Vice-

P.'esident informed the inspector that each and every one of the

emergent items issued during this period would be reviewed by the

,

BRC.

In another instance, the MRRC delegated the approval of the

deletion of MRRC approved restart items to the BRC.

It was the

+

MRRC's understanding than the BRC would periodically review this

process with the MRRC including examples of items being removed.

However, when this deletion approval authority had been described

to the inspectors by the BRC, the report back to MRRC was not

described. This discrepancy was subsequently discussed with

management and the only BRC member that could be reached indicated

that he was unaware of this expectation.

Furthermore, although

the BRC had been granted deletion authorization for approximately

one week and had begun implementing this responsibility, the

individual responsible for revisions to the Restart Plan was

unaware of this change.

The inspectors reviewed proposed changes to the Restart Plan.

The

significant process changes were typically enhancements to the

Restart Plan involving additional management or independent

reviews to provide assurance that the intent of the Restart Plan

was and would be successfully implemented.

This was censidered

noteworthy and reflected a commitment by management to effect

positive change at the site.

j

The inspectors performed partial system walkdowns of the following

i

systems:

System 01

-

Main Steam

System 03

-

Auxiliary Feedwater

System 18

-

Fuel Oil

System 30

-

Ventilation

System 62

-

Chemical and Volume Control

System 63

-

Safety Injection

System 65

-

Emergency Gas Treatment

.. ~

.

-

-

'

-

.

.,

.

.

i

36

,

System 67

-

Essential Raw Cooling Water

i

System 72

-

Containment Spray

System 74

-

Residual Heat Removal

,

System 82

-

Standby Diesel Generators

,

System 249 -

Diesel Standby Batteries

,

Several minor discrepancies were identified including: pressure

transmitter housing cover was loose for 1-PT-3-132C; control air

was heard to be leaking in the Unit I steam generator level

control valve mezzanine, and a level control valve had evidence of

a significant packing leak.

The licensee was informed of these

items and the inspector noted that the packing leak was previously

identified by the licensee under WR C126530 and was determined to

be a restart item during the backlog evaluations.

The overall

material condition of most of the systems was good.

The inspector performed a limited walkdown of portions of the Unit

l

2 CVCS system, SI system, RHR A and B systems. There were

'

numerous temporary component identification tags (" green tags"),

some dating back a few years.

Some seal leakage was observed on

i

RHR 2A-A pump as evidenced by a large accumulation of crystallized

.

'

boric acid. There were several very loosely secured argon bottles

in the 2A-A centrifugal charging pump room and 2B-B safety

injection pump room which presented a potential personnel safety

and missile hazard.

In addition, an industrial cleaner (Dyna-

Clean Foam) was found by the inspector in a painters bucket in the

'

2A-A centrifugal charging pump room. This cleaner was

_

specifically marked as "not approved for use with materials that

come in contact with the RCS".

Discussions with responsible

chemistry department personnel revealed that this cleaning agent

"

was not authorized for use in those areas.

Inspectors from Region

II, Division of Radiation Safety and Safeguards were informed and

will follow this issue.

During a walkdown of selected portion of the ERCW system, the

inspectors noted the overall housekeeping condition of the plant

was fair to good. However,the ERCW pump house was an exception.

The pump house was dirty with trash not having been picked up.

There were several spared junction boxes that were left in place

when some heat tracing was abandoned.

Also, two examples of inattention to detail by maintenance

personnel were noted. The first one dealt with parts taken off

the AFW pump turbine being placed in the corner of the room and

!

not being bagged nor tagged.

Some the items were bolts which

could be confused for other applications.

The second item dealt

with the motor driven AFW pump constant level oilers being loose.

There are set screws or thumb screws for tightening the oilers but

!

i

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.

.

.

,

.

!

>

37

about half of the oilers were loose. Also the instructions in the

.

PM procedure for changing out the oil only addresses one type of

!

I

oiler. The inspector talked with system engineer about the need

to included all relevant information.

A walkdown of various system 30 components in the auxiliary and

,

diesel generator buildings was performed.

Excluding identified

deficiencies, the material condition of equipment was generally

,

'

good. The inspectors observed three conditions which required

further evaluation. These were: 1) two of the four Auxiliary

Building Gas Treatment System fan A-A mounting bolts appeared to

have the nuts improperly installed; 2) cooling air flow could not

,

be detected through the diesel generator 2A-B control board; and

!

3) the diesel generator IA room exhaust fan damper was not full

open.

In addition, the system engineer, who accompanied the

inspectors, identified that the exhaust fan for the diesel

generator 2A-A electric board room was operating; however, its

discharge damper was closed.

Engineering personnel indicated that

i

work request would be issued to correct these conditions as

required.

Review of Design Changes

The inspectors reviewed the following design change notices (DCNs)

.

on system 82.

DCN M6604 - This design change was initiated due to a 10CFR part

21 notice from Morrison Knudsen on SQN EDG's not having an

independent pneumatic starting air system, but it also corrected

several undesirable wiring situations existing for some time.

Additional problems were identified.

DCN M6604 was revised to

correct them and achieved the following:

.

-

Rewired the air start motor engaged contacts so that a EDG

starting air system could be taken out of service without

affecting the EDG's ability to start.

-

Rewired the EDG's idle start circuitry to prevent the

initial speed surge to greater than 550 RPM on starting,

from releasing the Idle circuit seal in.

-

Replaced the indicating lamps on the EDG engine control

panel. The original lamp sockets were susceptible to

i

shorting out while installing a bulb which blew a fuse that

'

disabled the Diesel Generator.

-

The Manual and Auto voltage M0P controllers panel wiring was

changed to allow the vendor current controller to be a

direct replacement part. Controller are only available

direct acting and were being rewired prior to being

installed as reverse acting controller.

-

_

_

.

-

.

I

38

l

-

Rewired the air valve solenoid to prevent disabling the

diesel on an air valve solenoid fuse blowing.

-

An FDCN is planned to be submitted to address the speed M0P

in a similar manner as item above.

.

DCN M9096 - This design change was to eliminate an EMF noise being

introduced in to the Woodward Governor panel of EDG 2B-B and

causing it to swing its load. This DCN installed an interposing

,

relay in the engine control panel to isolate the Woodward Governor

l

panel from EMF noise.

i

!

There are currently 24 design change issues which are directly

associated with the main steam system. Six of these are considered

restart required items. These are:

-

Issue #93106 Main Steam Dump Drain Tank level switch (Unit

2)

-

Issue #93107 Main Steam Dump Drain Tank level switch (Unit

.

!

1)

.

-

-

Issue #93142 Hanger Modification

-

Issue #93183 Replace 1-FCV-1-17 (Terry Turbine)

-

Issue #93057 Unit 1 Foxboro controller relay replacement

'

for steam dumps and PORV's

-

-

Issue #92257 Unit 1 Valve vault overpressurization

.

An additional two modifications will be implemented prior to

restart.

i

-

Issue #93148 U1 pressure seal valve

-

Issue #93149 U2 pressure seal valve

The inspectors noted that the remaining modifications are

tentatively scheduled to complete by the conclusion of the cycle

10 refueling outages. The inspectors concluded that the licensee

has addressed all necessary modifications for system 01 for

restart.

Several post-modification tests and ongoing maintenance were also

observed from start to finish including discussions with foremen

and supervisors.

The inspections, to date, indicate that the licensee is addressing

,

backlog issues in the manner described in the Sequoyah Restart

Pl an .

However, several restart plan inconsistencies were noted by

the inspectors during this period. They were:

.

.

.

.

= = . -

.-

.

+

3

.

1

!

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!

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39

l

1

-

Need for clarification on how emergent issues (issues after

May 1, 1993) were being reviewed.

l

-

Need for clarification of how post restart issues would be

,

prioritized.

(The process for this item had not been

!

presented to the inspectors when the inspection period

ended.)

.

-

Need for senior plant management to better communicate

expectations to BRC, lower levels of management, and system

engineers regarding execution of the restart plan (uniform

clarification of restart criteria to all). This observation

!

was considered to take on added importance later in the

inspection period based on the inspectors comments during

the last week of this period.

,

Several plan enhancements or corrections were accomplished during

this inspection period. The inspectors consider that the licensee

i

needs to formally incorporate these enhancements or corrections

,

into the plan and formally communicate this information to the

NRC.

i

b.

Plant Operations (71707)

(1)

One June 9, 1993, the inspector attended an all-day

Operations Standdown meeting, during which various licensee

managers addressed Operations, Work Control, and Fire

Operations personnel. The meeting included both short and

long term performance goals, and emphasized management

expectations for Operations as the " responsible owner" of

Sequoyah.

Findings of a recent assessment of operator

performance by the Restart Readiness Team were discussed,

and the need for improvement in the identified areas was

strongly stressed.

,

Recent operational weaknesses were discussed. On June 8,

1993, NRC inspectors had discovered an AUD who was

inattentive to his duties.

On June 8, 1993, two AV0s failed

to respond to a fire drill within the required time limits.

These occurrences are discussed in more detail in paragraphs

3.a (1) and 3.b (1), respectively.

Licensee management made it quite clear that these and other

recent performance problems could not continue without

serious consequences.

Good performers were urged to take

personal responsibility to improve poorer performers, for

'

the mutual success of the itam.

Significant time was devoted at the standdown to

configuration control, and to the procedures, policies, and

expectations for independent verification. A number of

example situations were discussed. The amount of dialogue

l

4

.

.

.

.

l

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40

which ensued indicated that this clarification by management

was beneficial.

In the future, independent verification

will be used for configuration control, and concurrent

independent verification will be used for procedure steps

i

which present immediate plant safety or personnel hazards if

improperly performed. With the exception of certain system

i

alignment checklists, required independent verifications are

to be performed before performing the next step in the

procedure, unless proper approval is granted. Persons

performing independent verification may travel together as

long as the work is actually independent.

The quality and use of procedures was stressed by management

as an area in particular need of improvement. Operators

were reminded to apply a common sense approach to

implementing procedures, not to live with problems with

equipment and procedures, and to be proactive rather than

i

reactive. Policies on procedure notes vs. formal changes,

j

and for marking steps as NA, were clarified.

Procedure

adherence was reinforced by a training film provided by Duke

Power.

A highly experienced ex-navy individual had been hired by

the licensee to act as an AUD evaluator, coach and mentor.

He discussed his activities to improve the level of

performance of AVO rounds and related activities and to

foster communication and teamwork.

The Operations Superintendent addressed the usage of E0Ps

and A01s. He discussed an operational event where

performance of an A01 interfered with the performance of an

E0P, and described instances during simulator training where

operators had consciously and unnecessarily delayed obvious

and prudent actions until they reached these steps in the

procedure.

He stated that if plant conditions warrant the

performance of an A0I during an E0P, then the required A01

should be performed concurrently (on a not-to-interfere

basis) with the E0P. Also, independent actions to mitigate

the effects of an adverse condition may be taken which are

not addressed by procedure or may be taken earlier than the

sequence specified in the procedure. SRO concurrence is

required before performance of such actions. A01s and

independent actions will not be performed while performing

time-critical evolutions or immediate action steps. When

the A01 for a loss of offsite power is run concurrently with

an E0P, the ASOS/SR0 will assign an operator responsibility

for the A0I if an ASOS is not available.

Other areas reviewed and discussed during the standdown

included shift staffing, operator aids, disablement of

nuisance alarms, compensatory measures, operator tours and

roundsheets, logkeeping, sensitive equipment control,

_ _

_

_ _

.

-

.

.

41

surveillance instruction coversheets, procedure change

processes, the TSCCR process, and general conduct of

operations.

In general, the presentations were clear and

thorough. The Operations Superintendent explained the

rationale behind many of the procedure steps and changes,

,

which was a positive feature of the briefings.

>

Operations personnel appeared receptive to the policies and

expectations conveyed by licensee management. Throughout the

standdown, the inspectors noted that operations personnel

did not hesitate to ask probing questions, offer their

I

suggestions to management, and express perspectives and

i

opinions even when these differed from those of management.

.l

The inspectors concluded that the operations standdown

i

meeting adequately presented the performance expectations of

i

management, particularly with respect to an attitude of

ownership and personal responsibility for quality.

(2)

During this assessment period, inspectors from other plants

,

and Region II reviewed operations performance in the areas

i

of control room conduct, operator logs, control room draw-

ings and shift turnovers.

Senior operator and operator

!

knowledge of system status and plant conditions was accept-

'

able, and accurately reflected in control room logs. Con-

>

duct and turnovers was also adequate.

During a review of

control room drawings, the inspectors noted the AFW system

flow diagram was cluttered and difficult to interpret, since

it depicted all three trains of AFW for both units on a

l

single drawing.

The inspectors also noted that the electri-

cal drawings were not clearly indexed and it was difficult

.'

to move from larger one-line drawings to component level

elementary diagrams.

One inspector attended the operations shift turnover

!

conducted at 7:00 am on June, 18, 1993.

The inspector

4

-

considered that the turnover was well conducted with a good

i

exchange of information from the SOS to the crew.

.

Discussion of issues and activities was encouraged and

carried out during the turnover.

In addition, the crew was

addressed by the Site Vice President and Plant Manager about

expectations and the upcoming " quiet time" for Unit 1.

Expectations for operator attention to detail was addressed

by the Operations Superintendent. The inspector considered

the turnover and status handout provided to the crew was

good.

It contained sufficient detail on ongoing activities

and problems, and was written in an easy-to-read format.

The defense in depth status sheets were considered to be

beneficial.

(3)

On June 28, 1993 the operations department commenced 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

shift operation.

Shift turnover times were established at

._.

.

_

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. - .

l

.

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42

I

7:00 am and 7:00 pm.

This change resulted in SRO, R0, and

ADO turnover times being the same.

Previous shift coverage

had SR0s on 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts, and R0s and AU0s on 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

shifts. The inspectors monitored shift turnover activities

to evaluate implementation of the new shift hours. They

';

noted that turnovers with full crew complements allowed for

better communication of turnover issues to the operations

oncoming crew. However, during one of the morning shift

,

turnovers, the inspectors noted excessive noise level in the

cafeteria area.

The inspectors concluded, based on licensee assessments, review of

,

operations standdown meetings, and general observations during the

period that general operator performance regarding attention to

,

detail and sensitivity to not living with past problems is

'

improving.

No Violations or Deviations were identified.

10.

Review of Licensee Previous Commitments

(92701, 92702)

>

The inspectors reviewed the licensee's corporate commitment tracking

system (CCTS), and performed independent verification of selected items

to determine if the licensee had satisfied commitments that were open

when Units 1 and 2 restart in 1988. The purpose of this review was to

determine if the licensee's CCTS was adequately identifying and tracking

NRC commitments. The review identified that all commitments that were

open at the time of the 1988 Sequoyah Units 1 and 2 restart have been

i

closed, with the following exceptions:

-

Commitment items associated with control room design review (CRDR)

remain open. These items consist of Category 3 Human Engineered

Deficiencies (HEDs) (non safety significance), to be completed

,

during each unit's cycle 6 refueling outage. Unit 1 is currently

in the cycle 6 refueling outage, with Unit 2 scheduled to begin

cycle 6 refueling in January 1994. The licensee plans to

implement 14 items during these refueling outages. The schedule

for these remaining open items was provided to the NRC in a letter

dated February 4, 1993. This submittal also indicated that 107

nonsafety significant HEDs would not be pursued because resolution

is no longer cost effective. All Category 1 and 2 HEDs (safety

,

significant) have been completed.

-

-

Civil issues identified in Inspection Report 50-327,328/88-12

remain open. The licensee has submitted additional information

for all remaining issues, which is currently under review by NRR.

-

The licensee has yet to complete modifications to resolve the

problem of Unit Board breaker capability.

Several letters have

,

'

been docketed informing the NRC of changes in the licensee's

approach to resolution of the issue, and schedule changes. The

.

--

l

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.

43

licensee stated in a March 24, 1993 letter, that the completion of

l

modifications for this issue would be accomplished by the end of

the Unit 2 cycle 6 refueling outage. This outage is currently

i

scheduled for January 1994.

The licensee identifies this issue as

not a nuclear safety concern.

'

The inspectors conducted an independent review of selected items and

commitments that were open at the time of the Units 1 and 2 restart in

1988.

The following items were reviewed by the inspectors, with status

as noted:

'

a.

EDG voltage transient response and EDG performance evaluations.

This issue is associated with the licensee's commitment to improve

EDG voltage trar.sient response performance.

By letter dated March

!

3,1988, the licensee informed the NRC of the actions taken to

evaluate improvements and recommended in the Sequoyah Nuclear

.

Plant Diesel Generator Evaluation Report (DGER). This report

documented that the 1987 EDG test results were bounded by TVA's

i

EDG analysis and that the safety related systems and components

will perform their intended safety function when powered by the

EDGs with acceptable margin to insure their operability.

Additionally, the DGER contained actions that could be taken to

improve EDG performance.

By letter dated July 8, 1988, the licensee identified to the NRC

various commitments as a result of their review of the DGER.

These commitments included:

.i

(1)

Modifications to enhance the EDG transient voltage response

'

for one EDG, which included (1) resetting the exciter-

current transformer taps to achieve flat compounding, and

(2) rep?acement of the existing pneumatic load sequence

timers with more accurate electric timers.

1

(2)

Upon completion of item (1), the licensee will perform a PMT

to determine if improvement in the EDG transient voltage

response is acceptable.

'

(3)

If the evaluation from (2) is unacceptable, the licensee

will install a voltage overshoot reduction device (V0RD) on

the above EDG.

.

(4)

The licensee will perform a PMT on the above EDG to

determine the acceptability of the VORD.

(S)

The licensee will implement the modifications that provide

an acceptable improvement in the transient voltage response

on the three remaining EDGs.

(6)

PMTs on the remaining EDGs will then be performed.

j

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44

(7)

The licensee will provide the NRC with the evaluation and

i

test results of the PMTs which provide acceptable

l

improvement in the four EDG transient voltage responses.

The inspector reviewed the following documentation:

'

,

t

-

Diesel Generator Voltage Response Improvement Report.

-

PMTs associated with the above EDG testing.

I

,

!

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DCN M007398, Reset exciter control current transformer taps

on EDG 1B-B.

This DCN satisfies commitment (1) (1) above.

!

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ECN L7286B, Replacement of EDG load sequence electro-

mechanical timing relays with electronic relays. This ECN

satisfies commitment (1) (2) above.

!

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DCN M01367A, Installation of a VORD, and reset exciter

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control current transformer taps (Unit 1). This DCN

,

satisfies commitment (3) above.

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DCN M013678, Installation of a VORD, and reset exciter

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control current transformer taps (Unit 2).

This DCi1

satisfies commitment (5) above.

,

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By letter dated May 18, 1990, the licensee provided the NRC

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with the evaluation and test results of the PMTs which

provide acceptable improvement in the four EDG transient

!

voltage responses.

This letter satisfies commitment (7)

,

above.

,

Based on a review of the above documentation and discussions with

i

the EDG system engineer, the inspector concluded that the licensee

has satisfied the above commitment associated with investigating

i

and implementing modifications to improve EDG voltage transient

response.

b.

Issues related to cable installation and test program,

qualification of cables for expected life of the plant before

return from refueling outage, including silicone cables. The

inspector reviewed related correspondence associated with the

'

silicone rubber-insulated cable 40 year qualification test report.

This correspondence included a test report conducted by Wyle

Laboratories, entitled " Qualification Test Program for Silicone

Rubber Insulated Cables for Use in Tennessee Valley Authority's

Sequoyah and Watts Bar Nuclear Plants", which was performed in

December 1988. This test report concluded that the test

specimens, subjected to normal radiation exposure, thermal aging,

and accident radiation exposure, demonstrated the capability to

,

maintain specified voltage and current during the specified Design

Basis Event (LOCA Simulation).

The licensee docketed the findings

,

.

of this test report in a letter to the NRC dated March 13, 1989,

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45

,

and concluded that the samples have successfully demonstrated that

the silicone rubber insulated cables installed at the plant are

capable of performing their intended function inside containment

for the life of the plant plus LOCA conditions, and that the

remaining concerns have been resolved regarding cable installation

practices at the plant. The inspector concluded this issue to be

'

closed.

c.

From the Supplement 1 NUREG 1232, TVA committed to submit the

accelerated field weld program for Unit I within six months after

the restart of Unit

1..

TVA satisfied this commitment with a

submittal to the NRC dated May 5,1989.

'

d.

TVA to resolve the problem of Unit Board breaker capability.

The

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inspector reviewed the licensee's internal correspondence and

_i

discussed planned modifications with the system engineer.

In a

TVA letter to the NRC dated August 4, 1989, TVA committed to

provide a detailed description and the implementation schedule for

the resolution of Sequoyah's fdult current problem for the 6.9 KV

unit board breakers by October 20, 1989. The letter indicated

!

that 6.9 KV unit boards are equipped with ITE Imperial Corporation

7.5HK500 breakers that have a one time interrupting capability of

550 megavoltamperes (43,829 amperes at a maximum system voltage of

1

7.245 KV. The maximum calculated fault current for these boards

is 49,455 amps at 7.245 KV. To correct the problem, TVA committed

to installation of instantaneous overcurrent relays on the

'

incoming breakers from the unit station service transformers so

that a high level fault on the load feeder would be interrupted by

the incoming breaker. The licensee satisfied this commitment by

letter dated October 19, 1989, which provided a detailed

description and implementation schedule. TVA committed to

implement the required modifications before startup after the Unit

>

2 Cycle 5 refueling outage. TVA stated that this issue was not a

nuclear safety concern.

By letter dated November 29, 1991, the licensee informed the NRC

that a reevaluation of the planned resolution determined that it

was not required, for the following reasons.

lhe licensee is

installing new common station service transformers (CSSTs) with

automatic load tap chargers. When installation is complete, the

CSSTs will be able to provide the units with a better voltage-

regulated power supply.

For this reason, the licensee will be

using the CSSTs instead of the unit station service transformers

(USSTs) as the normal power supply for the unit boards. The USSTs

will only be used to supply power to the unit boards while at

power for maintenance purposes. The licensee committed to the

completion of the above modifications before the end of the Unit I

cycle 6 refueling outage.

The NRC's Electrical Distribution System Functional Inspection

(50-327,328/91-02) reviewed the licensee's planned modifications

to the CSSTs and concluded that it would provide a permanent

,

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46

)

solution to the bus transfer scheme problem.

The Inspection

Report also stated that the control circuitry should be carefully

{

evaluated and the question of reliability should be addressed.

'

By letter dated March 24, 1993, the licensee informed the NRC of

.

an extension of commitments associated with this issue. Due to

!

procurement problems associated with load cabling for the CSSTs,

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the licensee stated that the completion of modifications for this

issue would be accomplished by the end of the Unit 2 cycle 6

refueling outage.

This outage is currently scheduled for January

j

1994.

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Although the licensee satisfied the original docketed commitment

)

by letter dated October 19, 1989, the inspector concluded that the

!

licensee has yet to install hardware to resolve this issue.

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However, the inspector also concluded that the licensee has

docketed several letters that inform the NRC of changes in their

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approach to resolution of the issue, and schedule changes.

?

The licensee's CCTS identified the original items related to this

,

issue as closed.

However, new items were opened (and remain open)

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with appropriate references to the original issue.

.

e.

From Supplement 1 NUREG 1232, URI 50-327,328/88-37-01, and IFI 50-

-

327,328/88-37-02. Both of these items were associated with Fire

!

Protection. The licensee had provided information related to

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these issues to the NRC for review.

Subsequent review by the NRC

i

staff indicated that the licensee had adequately resolved both of

the issues.

Closure of these items was discussed in paragraph 8.

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of this inspection report.

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f.

TVA to revise the HVAC instrumentation accuracy calculation and

address the seismic threshold limits, specify the HVAC equipment

to be inspected after a seismic event, provide an inspection

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procedure, and clarify the calculation. The NRC considered

resolution of this issue could be implemented after restart. The

i

inspector reviewed documentation associated with this issue, which

included CAQR SQP880101. The issue was specifically related to

the licensee's failure to consider the effect on plant environment

i

and equipment qualification of a main steam line break in the

.

vicinity of the auxiliary building air intake canopy. Temperature

+

switches 1-TS-30-103, 1-TS-30-103A, 2-TS-30-104, and 2-TS-30-104A

were added to the HVAC room on each respective unit to detect a

main steam or feedwater line break in the vicinity of the

~

auxiliary building air intake canopy. The switches were installed

i

with appropriate logic to initiate an auxiliary building isolation

!

to preclude the HVAC system from spreading steam throughout the

!

auxiliary building general spaces. These switches however, were

!

added prior to implementation of equipment qualification

guidelines. The HVAC equipment room had always been thought to be

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a mild environment. During analysis it was shown that the

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postulated main steam /feedwater line break could result in a harsh

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environment.

Part of the corrective actions for this CAQR was to

,

relocate, replace, or qualify existing equipment. Accordingly,-

.

the above temperature switches were to be replaced with switches

I

which were qualified for the harsh environment.

Other equipment

in the room was also to be evaluated for environmental effects on

operability.

As part of the CAQR, the licensee had established

.

'

compensatory measure 880101 prior to completion of the above

i'

activities.

The inspector reviewed documentation associated with the above

issue. This documentation included:

-

DCN M-00263B, Unit 1 DCN provided for the replacement of

original Unit I temperature switches, and relocation-of

electronics for other equipment. The safety evaluation

>

associated with this DCN also evaluated other equipment and

reviewed accuracy calculations associated with the

temperature switches. This DCN was completed and closed

November 11, 1991.

-

DCN X00155B, Unit 2 DCN provided for the replacement of the

original Unit 2 temperature switches, and safety evaluation

for other equipment. The safety evaluation associated with

this DCN also evaluated other equipment and reviewed

accuracy calculations associated with the temperature

switches. This DCN was completed and closed ' August 14,

1992.

Based on a review of the above documentation, the inspector

concluded that the licensee has satisfied the commitment

associated with the above issue.

g.

Corporate guidance to be developed on use of teflon tape and a

single defined tape replacement plan. The inspector reviewed

documentation associated with this issue, which included CAQR CHS

870003. This issue was also discussed in Inspection Report 50-

327,328/87-37. The CAQR discussed discrepancies between a

corporate specification and a Sequoyah site specification

document. The inspector reviewed G-29 Volume IV Materials

Handling and Process Specifications for Material Fabrication and

Handling Requirements for Austenitic Stainless Steel, Process

Specification 4.M.I.1, Revision 14, Section 3.10.1.

This

specification delineates the temperature and radiation level usage

requirements of TFE type thread sealant materials, the pipe thread

position to start the tape, and acceptable vendor brand numbers.

The site specific procedure has been revised to delete reference

to the use of teflon tape. As such, the use of teflon tape is now

controlled via the corporate procedure G-29. -The inspector

concluded the licensee has satisfied the above commitment.

h.

Resolution of Safety Systems Outage Modification Inspection

(SSOMI) Issues from IR 50-327,328/86-68 (See IR 90-06). Inspection

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48

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Report 90-06 addressed issues in which most were closed. Other

i

issues were translated into IFI 90-06-05, which were closed in IR

i

90-28.

i.

Replace bismuth solder FLAS-5 fuses from lots 2 and 3 with cadmium

!

solder fuses before Mode 4.

This issue was identified in LER

,

327/87-30 regarding a blown fuse in emergency start circuits

l

resulting in spurious emergency diesel generator starts on two

i

i

occasions. This LER was reviewed and closed in NRC Inspection

Report 50-327,328/88-19, with the licensee replacing the fuses

,

with fuses of the proper lot number.

j

The inspectors concluded from the review of the commitments that the

t

licensee has implemented a comprehensive and effective program to track

and respond to commitments.

11.

Exit Interview

The inspection scope and results were summarized on July 13, 1993 with

those individuals identified by an asterisk in paragraph I aLsve. The

inepectors described the areas inspected and discussed in detail the

is lection findings listed below.

Proprietary information is not

,

contained in this report.

Dissenting comments were not received from

-

the licensee.

Item Number

Descriotion and Reference

VIO 327/93-23-01

Failure to ensure that all fuel

handling was performed in accordance

with SSP-12.1.

NCV 327, 328/93-23-02

Failure to notify the NRC as

required by TS LC0 3.7.11.1 ACTION

b.2.a.

VIO 327/93-23-03

Failure to adequately implement

corrective action for identification

and removal of foreign material in

the reactor vessel prior to the Unit

1 Cycle 6 core reload.

VIO 327, 328/93-23-04

Failure to promptly identify the

procedure problem associated with

LER 327/92-21 during corrective

action for LER 327/92-03.

IFf 327, 328/93-23-05

Review of Licensee Program to Test

Non T.S. Molded Case Circuit

Breakers.

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49

Strengths and weaknesses summarized in the results paragraph were

i

discussed in detail.

.

Licensee management was informed of the items closed in paragraphs 7

and 8.

,

12.

List of Acronyms and Initialisms

AFW

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Auxiliary Feedwater

A0I

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Abnormal Operating Instruction

AS05 -

Assistant Shift Operations Supervisor

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AVO

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Assistant Unit Operator

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Backlog Review Committee

BRC

--

CAQ

-

Condition Adverse to Quality

' ,i

CCD

-

Configurated Control Drawing

<

CCS

-

Component Cooling Water System

CFR

-

Code of Federal Regulations

'

CIPTE -

Complex or Infrequently Performed Test or Evolution

CR

-

Control Room

-

CREVS -

Control Room Emergency Ventilation System

CVCS -

Chemical Volume and Control System

+

CVI

-

Containment Ventilation Isolation

DCN

-

Design Change Notice

+

DRP

-

Division of Reactor Projects

-

EDG

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Emergency Diesel Generator

.

E0P

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Emergency Operating Procedure

l

EPRI -

Electric Power Research Institute

ERCW -

Essential Raw Cooling Water

ESF

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Engineered Safety Feature

,

FCV

-

Flow Control Valve

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FP

-

Fire Protection

FSAR -

Final Safety Analysis Report

HX

-

Heat Exchanger

IDP

-

Individual Data Package

IFI

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Inspector Followup Item

IR

-

Inspection Report

KV

-

Kilovolt

LCO

-

Limiting Condition for Operation

LCV

-

Level Control Valve

LER

-

Licensee Event Report

LOCA -

Loss of Coolant Accident

!

MCR

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Main Control Room

MOV

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Motor Operated Valve

MRRC -

Management Restart Review Committee

NCV

-

Non-cited Violation

NRC

-

Nuclear Regulatory Commission

NRR

-

Nuclear Reactor Regulation

OCC

-

Operational Control Center

PCV

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Pressure Control Valve

PERP -

Plant Evaluation Review Panel

PM

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Preventative Maintenance

PMT

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Post-maintenance Test

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PORC -

Plant Operations Review Committee

PORV -

Power Operated Relief Valve

PPM

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Parts per Million

PWR

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Pressurized Water Reactor

QA

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Quality Assurance

i

RCC

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Rod Centrol Cluster

RCDT -

Reactor Coolant Drain Tank

RCS

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Reactor Coolant System

,

RHR

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Residual Heat Removal

RII

-

NRC Region II

'

RM

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Radiation Monitor

R0

-

Reactor Operator

RRT

-

Restart Readiness Team

.

RWP

-

Radiation Work Permit

RWST -

Refueling Water Storage Tank

SDB

-

Shutdown Board

SI

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Surveillance Instruction

S0

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System Operations

S01

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System Operating Instruction

SOS

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Shift Operating Supervisor

i

SRO

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Senior Reactor Operator

i

SSP

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Site Standard Practice

i

SSPS -

Solid State Protection System

.

TACF -

Temporary Alteration Control Form

.

TS

-

Technical Specifications

,.

TSCCR -

Technical Specification Component Condition Record

'

URI

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Unresolved Item

i

VCT

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Volume Control Tank

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VIO

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Violation

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WO

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Work Order

WR

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Work Request

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