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Category:INTERNAL OR EXTERNAL MEMORANDUM
MONTHYEARML20217L7171999-10-22022 October 1999 Informs That Encl Questions Were Transmitted by Email to PT Vu of Duke Energy Corp,In Preparation for Upcoming Telcon Re 990624 Amend Request ML20216J2171999-09-30030 September 1999 Informs That Encl Questions Were Transmitted by Email on 990930 to M Purser of Duke Energy Corp for Preparation of Upcoming Telcon.Questions Pertain to 990624 Amend Request ML20210L6601999-08-0505 August 1999 Forwards single-page Document Given to G Belisle of Region II by T Clements of Nuclear Control Institute Re Mixed Oxide Fuel ML20196K6231999-07-0101 July 1999 Forwards Draft Safety Evaluation on TR DPC-NE-2009, Duke Power Co Westinghouse Fuel Transition Rept. Rept Was Transmitted to Warren in Order to Prepare for Conference Call ML20195J1181999-06-14014 June 1999 Forwards Documents That Were Transmitted by Fax on 990614 to a Jones-Young Re Issues to Be Discussed in Upcoming Telcon Re DPC Response to GL 98-04 ML20207G3661999-06-0909 June 1999 Reissued Notification with Date Change of 990618 Meeting with DPC in Rockville,Maryland to Discuss Compensatory Actions (Allowed Outage Time) for McGuire Nuclear Station ML20207E7741999-06-0202 June 1999 Notification of 990617 Meeting with Util in Rockville,Md to Discuss Compensatory Actions (AOT) for McGuire Nuclear Station ML20206U4231999-05-18018 May 1999 Notification of 990602 Meeting with Duke Energy Corp,Vepco & Others in Rockville,Md to Discuss Technical,Regulatory & Licensing Issues Related to Proposed Future Use of Mixed Oxide Fuel at Catawba,Mcguire & North Anna Nuclear Stations ML20205H9131999-03-24024 March 1999 Forwards NRC Operator Licensing Exam Repts 50-369/99-301 & 50-370/99-301 (Including Completed & Graded Tests) for Tests Administered on 990125-0205 ML20199B0491999-01-11011 January 1999 Notification of 990127 Meeting with Duke Energy Corp in Rockville,Md to Discuss License Amend for Taking Credit for Soluble Boron & Boraflex ML20195H0421998-11-17017 November 1998 Informs That Encl Questions Were Transmitted by e-mail to Warren of Duke Energy Corp in Preparation for Upcoming Telephone Call.Memo & Enclosure Do Not Convey Formal Request for Info or Represent NRC Staff Position ML20154L0811998-09-23023 September 1998 Notification of 981016 Meeting with Util in Rockville,Md to Discuss Recent Site Performance Major Plant Equipment Upgrades & Operational,Licensing & Regulatory Issues.Meeting Has Been Cancelled ML20153E0781998-09-23023 September 1998 Revised Notification of 981016 Duke Energy Corp in Rockville,Md to Discuss Recent Site Performance,Major Plant Equipment Upgrades & Operational,Licensing & Regulatory Issues.Meeting Revised to Change Date & Room Number ML20151X1931998-09-14014 September 1998 Notification of 981006 Meeting W/Duke Energy Corp in Rockville,Md to Discuss Recent Site Performance,Major Plant Equipment Upgrades & Operational,Licensing & Regulatory Issues ML20249C6451998-06-25025 June 1998 Notification of 980709-10 Meeting W/Duke Energy Corp in Rockville,Md to Discuss Technical Issues Re Proposed Improved TSs for Catawba & McGuire Nuclear Stations ML20249B6241998-06-19019 June 1998 Forwards Draft SE Re Relocation of Meteorological Tower for Plant ML20248F1061998-06-0202 June 1998 Notification of 980617 & 18 Meeting W/Util in Rockville,Md to Discuss Technical Issues Re Proposed Improved TSs for Catawba & McGuire Nuclear Stations ML20217Q6151998-05-0707 May 1998 Notification of 980518 & 19 Meeting W/Util in Rockville,Md to Discuss Technical Issues Re Proposed Improved TSs for Catawba & McGuire Nuclear Stations ML20217M1831998-05-0101 May 1998 Notification of 980514 Meeting W/Util in Rockville,Md to Discuss Plans for Changes to TS Re Following Ice Condenser Issues:Ice Weight Redistribution,Reduction & Block Ice Utilization ML20199A4781998-01-22022 January 1998 Notification of 980204 Meeting W/Util in Rockville,Md to Discuss Staff Recent RAI Re Snubbers ML20198M8931998-01-12012 January 1998 Notification of 980127 Meeting W/Util in Rockville,Md to Discuss Technical Issues Covered by DEC TR in Support of Future Transition from Framatome to Westinghouse Fuel ML20198S8131997-10-30030 October 1997 Notification of 971118 Meeting W/Util to Discuss Specific Aspects of Dual Unit Trip & Licensee Corrective Actions ML20198K1961997-10-16016 October 1997 Notification of 971030 Meeting W/Util in Rockville,Md to Discuss Matters Re Proposed Improved TSs for Catawba & McGuire ML20210M8231997-08-22022 August 1997 Forwards Signed Original of Subject Order Attached for Transmittal to Ofc of Fr for Publication.W/O Encl ML20141B3041997-06-20020 June 1997 Notification of 970709 Meeting W/Util in Huntersville,Nc to Discuss Licensee Revs to 1996 Plant UFSAR & How 1996 Rev Complies w/10CFR50.71 ML20206L5711997-01-16016 January 1997 Discusses Grinell Snubbers for Use in Steam Generator Replacement Project.Snubbers Did Not Meet Purchase Specifications for Environ Conditions ML20129H7401996-08-29029 August 1996 Ack Receipt of 960801 Memo Re Reactor Trip Breaker Problems at Plants.Recommended That AEOD or Appropriate Group within NRR Advise OE Whether Technical Staff Considers That Violations Occurred,Per 10CFR50.73 or 10CFR21 ML20128Q2431996-08-0101 August 1996 Discusses Concerns Raised During 960722 AEOD Program Review Re Reportability of Reactor Trip Breaker Problems at Plants NUREG-1299, Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl1994-06-29029 June 1994 Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl ML20059E0261994-01-0404 January 1994 Notification of 940105 Meeting W/Util in Rockville,Md to Conduct AIT Meeting & Discuss Results of Licensee Investigation of Recent Loss of off-site Power Event at McGuire Plant ML20058J5061993-11-29029 November 1993 Notification of Significant Licensee Meeting W/Util on 931203 to Discuss Licensee Intended EAL Changes for All Three Plants Relative to NUMARC Issues & Implementation of EPA-400 ML20058J4911993-11-24024 November 1993 Notification of Significant Licensee Meeting W/Util on 931206 to Discuss self-assessment of Plant Performance Since 930802-1130 ML20058C9631993-11-19019 November 1993 Notification of 931201 Meeting W/Util in Rockville,Md to Update NRC on Mcguire,Units 1 & 2 & Catawba,Unit 1 Steam Generator Replacement Project ML20057D1651993-09-27027 September 1993 Notification of 930929 Meeting W/B&W in Rockville,Md to Discuss Installation Process Used for B&W Kinetic Sleeves at McGuire Nuclear Station ML20057C5441993-09-23023 September 1993 Notification of 930929 Meeting W/Util in Rockville,Md to Discuss Results of Util Investigation of Unit 1 SG Tube Leaks & Util Actions as a Result of Findings from Investigation ML20056H3141993-08-24024 August 1993 Forwards Safety Evaluation Accepting Critical Aspects of Proposed TS Changes Involving Increasing Min Rswt Boron Concentrations from 2,000 Ppm to 2,275 Ppm & Increasing Min Cla Boron Concentration from 1,900 Ppm to 2,000 Ppm ML20134B2531993-02-11011 February 1993 Responds to 930113 Request for Exceptions to N+1 Policy for Listed Plants.Approved Exceptions W/Stated Conditions Effective for Period of 2 Yrs ML20128G8201993-02-0101 February 1993 Notification of Significant Licensee Meeting W/Util on 930211 to Discuss Enforcment Conference on Safeguards Issues ML20126F2821992-12-24024 December 1992 Forwards Description of Valves Affected by Stroke Testing & Effect of Valves Being Opened or Closed During Testing,W/ Respect to Encl LER 369/90-022-1 Re RHR Sys Being Inoperable ML20128A0361992-11-30030 November 1992 Notification of 921215 Meeting W/Util in Rockville,Md to Discuss Status of Licensees Plans to Implement Pilot Program for Use of Seismic Stops in Lieu of Snubbers at Plant ML20059H7861990-09-10010 September 1990 Forwards Revised Resolution of Plant-Specific Differing Prof Opinion (DPO) Issues Concerning McGuire Tech Specs, in Support of Completion of Dpos,Per Author 891229 Memo.Actions Re Tech Specs Listed ML20055D9791990-07-0505 July 1990 Notification of 900719 Meeting W/Util in Rockville,Md to Discuss Cause,Morphology & Future Plans Re Cracking Tubes at Expansion Transition Zone & at Tube Support Locations in Steam Generators.Agenda Encl ML20246P6001989-09-0505 September 1989 Notification of 890907 Site Visit & Meeting W/Util to Observe Existing Corrosion of Unit 1 Steel Containment Vessel & Discuss Adequacy of Remaining Wall Thickness for Units 1 & 2 ML20246B8381989-08-22022 August 1989 Notification of 890831 Meeting W/Util in Rockville,Md to Discuss Util Findings from Steam Generator Tubes & Plugs Inspected During Present Refueling Outage of Unit 2 from Earlier Related Metallurgical Analyses of Unit 1 Specimens ML20245K3261989-04-26026 April 1989 Notification of 890505 Meeting W/Util in Rockville,Md to Discuss Cause of Unit 890307-08 Tube Rupture,Corrective Actions & Plans for Restart ML20247B7351989-03-24024 March 1989 Notification of 890503 Meeting W/B&W,Inel & Util in Rockville,Md to Discuss Licensing Submittals for Plants ML20236E2931989-03-15015 March 1989 Discusses Closure of Outstanding Tech Spec Concerns Deriving from R Licciardo Differing Prof Opinion Review of Plant Tech Specs.Requests That Priority Be Given to Final Closure Including Completion of Remaining 45 Specific Items ML20236E2971989-03-15015 March 1989 Discusses Incorporation of Items Into Westinghouse STS Deriving from NRC Confirmation of Generic & multi-plant Action Concerns from R Licciardo Review of Plant Tech Specs ML20206E5691988-11-15015 November 1988 Summarizes 881109 Telcon W/Util Re Control Area Ventilation Sys Mod & Associated Tech Spec Change.Addl Info Requested Stated ML20058N6761988-10-18018 October 1988 Discusses Action Item 5 Assigned in 880406 Memo Related to Diagnostic Evaluation Team Report for Plant on Pump Damage Due to Low Flow Cavitation 1999-09-30
[Table view] Category:MEMORANDUMS-CORRESPONDENCE
MONTHYEARML20217L7171999-10-22022 October 1999 Informs That Encl Questions Were Transmitted by Email to PT Vu of Duke Energy Corp,In Preparation for Upcoming Telcon Re 990624 Amend Request ML20216J2171999-09-30030 September 1999 Informs That Encl Questions Were Transmitted by Email on 990930 to M Purser of Duke Energy Corp for Preparation of Upcoming Telcon.Questions Pertain to 990624 Amend Request ML20210L6601999-08-0505 August 1999 Forwards single-page Document Given to G Belisle of Region II by T Clements of Nuclear Control Institute Re Mixed Oxide Fuel ML20196K6231999-07-0101 July 1999 Forwards Draft Safety Evaluation on TR DPC-NE-2009, Duke Power Co Westinghouse Fuel Transition Rept. Rept Was Transmitted to Warren in Order to Prepare for Conference Call ML20195J1181999-06-14014 June 1999 Forwards Documents That Were Transmitted by Fax on 990614 to a Jones-Young Re Issues to Be Discussed in Upcoming Telcon Re DPC Response to GL 98-04 ML20207G3661999-06-0909 June 1999 Reissued Notification with Date Change of 990618 Meeting with DPC in Rockville,Maryland to Discuss Compensatory Actions (Allowed Outage Time) for McGuire Nuclear Station ML20207E7741999-06-0202 June 1999 Notification of 990617 Meeting with Util in Rockville,Md to Discuss Compensatory Actions (AOT) for McGuire Nuclear Station ML20206U4231999-05-18018 May 1999 Notification of 990602 Meeting with Duke Energy Corp,Vepco & Others in Rockville,Md to Discuss Technical,Regulatory & Licensing Issues Related to Proposed Future Use of Mixed Oxide Fuel at Catawba,Mcguire & North Anna Nuclear Stations ML20205H9131999-03-24024 March 1999 Forwards NRC Operator Licensing Exam Repts 50-369/99-301 & 50-370/99-301 (Including Completed & Graded Tests) for Tests Administered on 990125-0205 ML20199B0491999-01-11011 January 1999 Notification of 990127 Meeting with Duke Energy Corp in Rockville,Md to Discuss License Amend for Taking Credit for Soluble Boron & Boraflex ML20195H0421998-11-17017 November 1998 Informs That Encl Questions Were Transmitted by e-mail to Warren of Duke Energy Corp in Preparation for Upcoming Telephone Call.Memo & Enclosure Do Not Convey Formal Request for Info or Represent NRC Staff Position ML20154L0811998-09-23023 September 1998 Notification of 981016 Meeting with Util in Rockville,Md to Discuss Recent Site Performance Major Plant Equipment Upgrades & Operational,Licensing & Regulatory Issues.Meeting Has Been Cancelled ML20153E0781998-09-23023 September 1998 Revised Notification of 981016 Duke Energy Corp in Rockville,Md to Discuss Recent Site Performance,Major Plant Equipment Upgrades & Operational,Licensing & Regulatory Issues.Meeting Revised to Change Date & Room Number ML20151X1931998-09-14014 September 1998 Notification of 981006 Meeting W/Duke Energy Corp in Rockville,Md to Discuss Recent Site Performance,Major Plant Equipment Upgrades & Operational,Licensing & Regulatory Issues ML20249C6451998-06-25025 June 1998 Notification of 980709-10 Meeting W/Duke Energy Corp in Rockville,Md to Discuss Technical Issues Re Proposed Improved TSs for Catawba & McGuire Nuclear Stations ML20249B6241998-06-19019 June 1998 Forwards Draft SE Re Relocation of Meteorological Tower for Plant ML20248F1061998-06-0202 June 1998 Notification of 980617 & 18 Meeting W/Util in Rockville,Md to Discuss Technical Issues Re Proposed Improved TSs for Catawba & McGuire Nuclear Stations ML20217Q6151998-05-0707 May 1998 Notification of 980518 & 19 Meeting W/Util in Rockville,Md to Discuss Technical Issues Re Proposed Improved TSs for Catawba & McGuire Nuclear Stations ML20217M1831998-05-0101 May 1998 Notification of 980514 Meeting W/Util in Rockville,Md to Discuss Plans for Changes to TS Re Following Ice Condenser Issues:Ice Weight Redistribution,Reduction & Block Ice Utilization ML20199A4781998-01-22022 January 1998 Notification of 980204 Meeting W/Util in Rockville,Md to Discuss Staff Recent RAI Re Snubbers ML20198M8931998-01-12012 January 1998 Notification of 980127 Meeting W/Util in Rockville,Md to Discuss Technical Issues Covered by DEC TR in Support of Future Transition from Framatome to Westinghouse Fuel ML20198S8131997-10-30030 October 1997 Notification of 971118 Meeting W/Util to Discuss Specific Aspects of Dual Unit Trip & Licensee Corrective Actions ML20198K1961997-10-16016 October 1997 Notification of 971030 Meeting W/Util in Rockville,Md to Discuss Matters Re Proposed Improved TSs for Catawba & McGuire ML20210M8231997-08-22022 August 1997 Forwards Signed Original of Subject Order Attached for Transmittal to Ofc of Fr for Publication.W/O Encl ML20141B3041997-06-20020 June 1997 Notification of 970709 Meeting W/Util in Huntersville,Nc to Discuss Licensee Revs to 1996 Plant UFSAR & How 1996 Rev Complies w/10CFR50.71 ML20206L5711997-01-16016 January 1997 Discusses Grinell Snubbers for Use in Steam Generator Replacement Project.Snubbers Did Not Meet Purchase Specifications for Environ Conditions ML20129H7401996-08-29029 August 1996 Ack Receipt of 960801 Memo Re Reactor Trip Breaker Problems at Plants.Recommended That AEOD or Appropriate Group within NRR Advise OE Whether Technical Staff Considers That Violations Occurred,Per 10CFR50.73 or 10CFR21 ML20128Q2431996-08-0101 August 1996 Discusses Concerns Raised During 960722 AEOD Program Review Re Reportability of Reactor Trip Breaker Problems at Plants NUREG-1299, Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl1994-06-29029 June 1994 Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl ML20059E0261994-01-0404 January 1994 Notification of 940105 Meeting W/Util in Rockville,Md to Conduct AIT Meeting & Discuss Results of Licensee Investigation of Recent Loss of off-site Power Event at McGuire Plant ML20058J5061993-11-29029 November 1993 Notification of Significant Licensee Meeting W/Util on 931203 to Discuss Licensee Intended EAL Changes for All Three Plants Relative to NUMARC Issues & Implementation of EPA-400 ML20058J4911993-11-24024 November 1993 Notification of Significant Licensee Meeting W/Util on 931206 to Discuss self-assessment of Plant Performance Since 930802-1130 ML20058C9631993-11-19019 November 1993 Notification of 931201 Meeting W/Util in Rockville,Md to Update NRC on Mcguire,Units 1 & 2 & Catawba,Unit 1 Steam Generator Replacement Project ML20057D1651993-09-27027 September 1993 Notification of 930929 Meeting W/B&W in Rockville,Md to Discuss Installation Process Used for B&W Kinetic Sleeves at McGuire Nuclear Station ML20057C5441993-09-23023 September 1993 Notification of 930929 Meeting W/Util in Rockville,Md to Discuss Results of Util Investigation of Unit 1 SG Tube Leaks & Util Actions as a Result of Findings from Investigation ML20056H3141993-08-24024 August 1993 Forwards Safety Evaluation Accepting Critical Aspects of Proposed TS Changes Involving Increasing Min Rswt Boron Concentrations from 2,000 Ppm to 2,275 Ppm & Increasing Min Cla Boron Concentration from 1,900 Ppm to 2,000 Ppm ML20134B2531993-02-11011 February 1993 Responds to 930113 Request for Exceptions to N+1 Policy for Listed Plants.Approved Exceptions W/Stated Conditions Effective for Period of 2 Yrs ML20128G8201993-02-0101 February 1993 Notification of Significant Licensee Meeting W/Util on 930211 to Discuss Enforcment Conference on Safeguards Issues ML20126F2821992-12-24024 December 1992 Forwards Description of Valves Affected by Stroke Testing & Effect of Valves Being Opened or Closed During Testing,W/ Respect to Encl LER 369/90-022-1 Re RHR Sys Being Inoperable ML20128A0361992-11-30030 November 1992 Notification of 921215 Meeting W/Util in Rockville,Md to Discuss Status of Licensees Plans to Implement Pilot Program for Use of Seismic Stops in Lieu of Snubbers at Plant ML20059H7861990-09-10010 September 1990 Forwards Revised Resolution of Plant-Specific Differing Prof Opinion (DPO) Issues Concerning McGuire Tech Specs, in Support of Completion of Dpos,Per Author 891229 Memo.Actions Re Tech Specs Listed ML20055D9791990-07-0505 July 1990 Notification of 900719 Meeting W/Util in Rockville,Md to Discuss Cause,Morphology & Future Plans Re Cracking Tubes at Expansion Transition Zone & at Tube Support Locations in Steam Generators.Agenda Encl ML20246P6001989-09-0505 September 1989 Notification of 890907 Site Visit & Meeting W/Util to Observe Existing Corrosion of Unit 1 Steel Containment Vessel & Discuss Adequacy of Remaining Wall Thickness for Units 1 & 2 ML20246B8381989-08-22022 August 1989 Notification of 890831 Meeting W/Util in Rockville,Md to Discuss Util Findings from Steam Generator Tubes & Plugs Inspected During Present Refueling Outage of Unit 2 from Earlier Related Metallurgical Analyses of Unit 1 Specimens ML20245K3261989-04-26026 April 1989 Notification of 890505 Meeting W/Util in Rockville,Md to Discuss Cause of Unit 890307-08 Tube Rupture,Corrective Actions & Plans for Restart ML20247B7351989-03-24024 March 1989 Notification of 890503 Meeting W/B&W,Inel & Util in Rockville,Md to Discuss Licensing Submittals for Plants ML20236E2931989-03-15015 March 1989 Discusses Closure of Outstanding Tech Spec Concerns Deriving from R Licciardo Differing Prof Opinion Review of Plant Tech Specs.Requests That Priority Be Given to Final Closure Including Completion of Remaining 45 Specific Items ML20236E2971989-03-15015 March 1989 Discusses Incorporation of Items Into Westinghouse STS Deriving from NRC Confirmation of Generic & multi-plant Action Concerns from R Licciardo Review of Plant Tech Specs ML20206E5691988-11-15015 November 1988 Summarizes 881109 Telcon W/Util Re Control Area Ventilation Sys Mod & Associated Tech Spec Change.Addl Info Requested Stated ML20058N6761988-10-18018 October 1988 Discusses Action Item 5 Assigned in 880406 Memo Related to Diagnostic Evaluation Team Report for Plant on Pump Damage Due to Low Flow Cavitation 1999-09-30
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JUN 181982 Docket Nos: 50-369/370
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Elinor G. Adensan, Chief ##
MEMORAliDUH FOR:
Licensing Branch No. 4 N Division of Licensing G difyI EC~ D.D3 -
n B FRO?t: Ralph Dirkel, Project Manager g 7882A g-Licensing Branch No. 4 %
Division of Licensing '#$;
SUBJ ECT: MCGUIRE UllIT 1 OPERATING EXPERIENCE !M5('(&
Enclosed is the operating experience report for ItcGuire Unit I which covers the period of January 1,1981 to January 31, 1982. This report includes the information provided by Region II. AE00 could not assist usont51sreport.
f Ralph Birkel, Project Manager Licensing Branch Ho. 4 Division of Licensing
Enclosure:
As stated DISTRIBUTION Docket File (50-369/370)
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. I' MCGUIRE UNIT 1 OPERATING EXPERIENCE INTRODUCTION The McGuire Nuclear Station, Unit 1, is a PWR Westinghouse 4-loop reactor coolant system with a containment that employs a ice condenser pressure-suppression system.
The staff's review of the operating license application was issued in the SER, dated March 1978; however, following the TMI-2 accident the Commission " paused" in its licensing activities to assess the impact of TMI-2 accident.
The McGuire review resumed based on Commission guidance, the requirements derived from the NRC's Action Plant (NUREG-0660) and found in NUREG-0694, TMI-related Requirements for New Operating Licenses. ,
Supplement No. 4, dated January 1981 was issued in support of a Fuel Load and Zero Power License and Supplement No. 5, dated April,1981 was issued in support of a full power license for Unit 1. Unique;to this application was the need to install a hydrogen mitigation system since ice, condenser plants have relatively small containment volumes and a containment design pressure of 15 psig. A TMI-2 type of accident releases large volumes of hydrogen to containment; consequently some means is required to assu/e containment integrity. An interim distributive ignition system is used at McGuire. A permanent hydrogen mitigation system is still under review and McGuire Unit 1 was licensed on the basis that our near tem TMI requirements were satisfied and the longer tem TMI issues would be fulfilled as stipulated under the conditions of the license.
STARTUP AND OPERATING HISTORY Fuel Load and Zero Power License The license was issued on January 23, 1981 and fuel loading was completed on February 4,1981. For the next two months the licensee was engaged in filling and venting of the reactor coolant system and with cold precritical testing. Hot precritical testing was initiated in mid-April and not completed until mid-July due primarily to vario'us caponent leaks in the reactor coolant system. Numerous reactor coolant system check valves failed leakage test criteria. Leaks also developed on the residual heat removal pump flanges requiring disassembly and replac emnt. The abnomal number of leakage problems was attributed to the long lay-up following the TMI-2 accident.
Low Power License (5%)
Although the licensee was issued a 5% operating license on June 12, 1981, precritical testing was not completed until late July due, as mentioned previously, to a series of system problems which required draining, refilling and venting several tims to accommodate repairs. Approximately three months were devoted to these efforts. Initial criticality was reached on August 8,1981. By the end of August low power testing was successfully completed. All testing was completed to our satisf action wi thin the restricted power operation not to exceed 5% of rated core themal power.
), P .
o Full Power License (100%)
The full power license was issued on July 8,1981, which pennitted the licensee to proceed with the normal power ascension program that is described in the licensee's Final Safety Analysis Report. This is a test program of power level escalation in successive stages to closely examine, at each stage of power operation, both the reactor and unit operational characteristics.
There were several incidents which have delayed the McGuire power ascension program. Briefly these are:
a) September 14, 1981: Three day delay due to inability to completely transfer automatic control function of the auxiliary feedwater system to the local station during a loss of control room test. Correction involved circuit modi fications.
b) September 28, 1981: Seven days delay when a drain line on a turbine governor valve failed.
c) October 10, 1981: Ten days delay in repairing a body-to-bonnet leak on valve I
NDl, the first residual heat removal system isolation valve in series off the reactor coolant system.
d) November 15, 1981: Nine days delay perfonning eddy current testing of the tubes in steam generator "A". Inspection was performed as a precautionary measure because of recent findings of significant tube wastage in foreign reactors having steam generators similar to those at McGuire.
- e) Decenber 2,1981
- Thirty-one days lost due to an unplanned outage for repair of a damaged hydrogen cooler in the main generator. The hydrogen cooler was damaged by water hammer during restoration of secondary systems following an unsuccessful loss-of-offsite power test.
Incidents described i.n' a), b) and c) are not unusual for a new plant starting up. -
However, the additional eddy current testing (d)) and the damage to the hydrogen cooler (e)) are unusual incidents.
The additional eddy current testing resulted following recent tube failures of Westinghouse preheat type steam generators discussed below:
Ringhals Unit 3, a three-loop Westinghouse plant in Sweden, was shut down on October 21, 1981 because of a 2.6 gpm primary-to-secondary l eak . Before the leak, the unit had been operating at power levels l greater than 50% for approximately five months. The steam generators,
! W preheat type, are similar in design (Model D) to those at McGuire Unit 1, the only domestic operating plant with this type of steam l ge nerator.
T 9 .
The leaking tube was located within the preheater section on the cold leg side of the stean generator. The ECT results revealed -numerous tubes with ECT indications localized within the preheater section at baffle plate loca-tions. The tubes affected are in the peripheral rows (close to the steam generator shell) adjacent to the feedwater inlet. There are approximately 100 tubes with ECT indications for each steam generator. Approximately 45 of the tubes with ECT indications have wall reductions of greater than 50%.
The most recent eddy current testing of the steam generator tubes at Almaraz Unit 1 in Spain also revealed significant tube wall reduction at locations similar to those at Ringhals Unit 3. Almaraz Unit 1, with steam generators similar to those at Ringhals Unit 3 and McGuire Unit 1, had been operating at various power levels, including full power, for about four conths. ,
Westinghouse believes these ECT indications are attributable to excitation of the steam gendrator tubes from high fluid velocities and that the tube walls are being worn down from vibrational rubbing against baffle plates in the preheater sections of these steam generators.
Westinghouse further believes that a reduction of a flow velocity by controlling total feedwater flow should reduce the potential for vibration.
The licensee completed eddy current testing of approximately 170 tubes in steam generator A at McGuire Unit 1 on November 19, 1981 to determine if similar problems are being experienced in the McGuire steam generators. Pre-liminary findings show tube wall degradation no greater than 10%.
Due to potential wastage concerns with the McGuire steam generator tubes, the staff has limited power operation of the unit to no greater than 75% for limited time periods. Between January 3 and January 31, 1982, the unit operated at 50% power for most of the time in order to reduce any potential for flow induced vibration on the steam generator tubes by reducing feedwater inlet flow velocities. 'This was done as a precautionary measure to preclude problems experienced with foreign reactors. Power was escalated to 75% and 90% for a few
. days, and to 100% for one day.
Inspection and Enforcement History During the period of January 26 to August 8,1981, Region Il conducted 18 inspections at the site, including seven report periods for the resident inspector. Twenty-one violations were cited against the licensee, all of the Severity Levels V or VI categories. None of the violations were considered significant enough to warrant an enforcement meeting with the licensee or civil penal ty. Thirteen of the violations involved operational activities, including
?,
five related to health physics concerns, and eight were related to construction activities. Also, during this period 125 Licensee Event Reports were issued by Duke concerning McGuire 1. The reported events represented no threat to the public safety since the reactor had not yet been made critical.
From August 8 (initial criticality) to the end of 1981, 18 inspections were conducted by Region II. Six violations were identified, all in Severity Levels V or VI category. One violation involved security, two housekeeping,.and three opera tion s. The operational violations involved failure to make an adequate log book entry; and improper tripping of a particular safety circuit, and misinter-pretation of a test prerequisite. There were 15 unplanned reactor trips and three safety injections while the reactor was at some power level. One of the safety injections did not introduce water into the reactor coolant system. There were 134 Licensee Event Reports (LERs) issued during this period. Of the total of 259 issued in 1981, 194 were found, after evaluation, to have been reportable.
Many of the difficulties included above are not unusual and can be expected in starting up a new plant. The items of most concern were poor communication between operations and the support staff, failure to follow procedure, and in some instances, inadequate prodedures.
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