ML20045D175

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Insp Rept 50-458/93-10 on 930314-0424.Violations Noted But Not Cited.Major Areas Inspected:Plant Status,Onsite Response to Events,Operational Safety Verification,Maintenance & Surveillance Observation
ML20045D175
Person / Time
Site: River Bend Entergy icon.png
Issue date: 06/01/1993
From: Gagliardo J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20045D171 List:
References
50-458-93-10, NUDOCS 9306280057
Download: ML20045D175 (18)


See also: IR 05000458/1993010

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APPENDIX

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-458/93-10

Operating Li anse: NPF-47

Licensee:

Gulf States Utilities

P.O. Box 220

St. Francisville, Louisiana 70775-0220

Facility Name:

River Bend Station

Inspection At:

St. Francisville, Louisiana

Inspection Conducted: March 14 through April 24, 1993

Inspectors:

W. F. Smith, Senior Resident Inspector

D. P. Loveless, Resident Inspector

R. H. Bernhard, Senior Resident Inspector,

Grand Gulf Nuclear Station

Approved:

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J.E.~GagBardo7ChTef,PyectSectionC

Date

Inspection Summary

Areas Inspected:

Routine, unannounced inspection of plant status, onsite

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response to events, operational safety verification, maintenance and

surveillance observations, and an engineered safety feature walkdown.

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Results:

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The licensee's actions in the early plant staff recognition and

identification and the reactor engineering analyses, planning, and

implementation of testing to locate and suppress further degradation of

the reactor fuel leak were' excellent, with one exception, as described

below (Section 2.1).

The operators departed from the licensee's self-checking process when

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they scrammed the wrong control rod during reactor flux tilting tests.

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A noncited violation was identified in' view of the minimal safety

significance of the event and corrective actions taken (Section 2.1).

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The licensee's corrective actions in conducting detailed reviews and

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identifying and correcting overlap discrepancies in logic system

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functional test surveillance procedures continued to demonstrate good

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performance. - However, the number of discrepancies confirmed the need to

perform the detailed reviews (Section 2.2).

Finding a test fixture installed in Source Range Monitor (SRM) A after

completion of the functional test and documentation of its removal was-

identified as a potential violation pending further review to determine

the cause. An unresolved item was opened (Section 2.3).

The licensee's response to insure that an occurrence similar to the

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Perry Nuclear Plant emergency core cooling system (ECCS) suction

strainer clogging event should not occur at River Bend Station was

thorough and timely (Section 2.4).

Control room operator performance and professionalism was found to be

improving, based on routine daily observations and observation of the

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shutdown that was implemented on April 17 and 18, 1993 (Section 3.1).

The performance of maintenance observed during this inspection period

was good.

Procedures provided by the maintenance work orders (MW0s)

appeared to be appropriate in each case.

Summar_y of Inspection Findings:

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A noncited violation was identified (Section 2.1).

Unresolved item 458/93010-1 was opened (Section 2.3).

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Inspection Followup Item 458/93010-2 was opened (Section 5.1)-,

Attachment:

Attachment - Persons Contacted and Exit Meeting

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DETAILS

1 PLANT STATUS

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At the beginning of this inspection period, the plant was operating at

100 percent power.

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On March 26, 1993, the licensee reduced reactor power to 65 percent, in order

to perform flux tilt testing.

This testing is further described in

Section 2.1 of this report.

The reactor was returned to 100 percent power on

April 1.

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On April 2, a problem with the turbine moisture separator reheaters resulted

in a power reduction to 92 percent, until April 5 when power was restored to

100 percent after repairs.

Power remained at 100 percent until April 17, when the plant was shut down and

cooled to ambient temperature and pressure to replace reactor recirculation

pump seals.

The outage was originally scheduled to end on April 28.

However,

because a main steam isolation valve failed to close, the outage was extended

to identify the root cause(s) and to implement corrective actions.

Details of

the main steam isolation valve problems were documented in special NRC

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Inspection Report 50-458/93-18.

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At the end of this inspection period, the plant remained shut down at; ambient

conditions.

2 ONSITE RESPONSE TO EVENTS (93702,61726)

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2.1 Reactor Fuel Integrity Failure

As documented in NRC Inspection Report 50-458/9:-05, on February 25, 1993, the

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licensee identified a fuel cladding failure as ividenced by a significant

increase in the offgas pretreatment release rate.

On March 23, the licensee

requested relief from the required actions of Technical Specification 3.1.4.2,

" Rod Pattern Control System," to allow for continuous rod withdrawal of an

individual rod to its original notch position after the rod was fully inserted

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by a manual scram from a partially inserted position.

The purpose of the

relief request was to allow performance of testing to help. locate the leaking

fuel rod.

On March 26, the NRC granted the relief in a Notice of Enforcement Discretion,

which concluded that plant safety would not be unduly compromised and that

such action was in the best interest of public health and safety.

The relief

was granted for a period of 7 consecutive days, beginning from the first use

of the relief from the Technical- Specification requirements.

Later.that day, the licensee reduced reactor power to 65 percent and began

testing. The inspectors observed portions of the testing as it was conducted

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in accordance with Test Procedure TP-93-0006, Revision 0, " Flux Tilting." The

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inspectors reviewed the procedure.to ensure it reflected the relief as

described in the Notice of Enforcement Discretion and that it was otherwise

consistent with the facility license. 'The procedure was.well structured for.

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an orderly progression of the' test and had appropriate' prerequisites,

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precautions, limitations, and independent verifications.

However, General

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Guidelines Step 6.4, and Procedure Step 9.1.7 provided-direction to

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continuously insert, rat M r than scram, control rods-that were not fully

withdrawn.

The inspectors noted that the Notice of Enfurcement Discretion was

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issued with the understanding that the relief from Technical Specification

requirements was necessary to allow scramming of control rods that were not

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fully withdrawn and to allow continuous withdrawal of the control rod to

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return it to its pretest condition.

Upon discussing the natter with cognizant _

NRC staff, the inspectors confirmed this understanding.

The licensee was requested to supplement their request for relief prior to

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proceeding in a manner that was contrary to the methods described in the

Notice of Enforcement: Discretion. 'On March 29, the licensee' submitted a

letter providing appropriate technical and safety ' justification. On March 30,

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the NRC staff gave the licensee verbal concurrence to proceed with testing

partially inserted control rods by inserting rather than scramming the rods.

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Even though the licensee failed to clearly communicate the methodology

intended for testing partially inserted con +rol rods to the NRC, the

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inspectors and the NRC staff considered the amecded method to be more

conservative, in that 'it reduced the severity of mechanical and hydraulic

stresses on the control rods and control rod drives.

The NRC staff followed

up with written amendment to the Notice of Enforcement Discretion on_

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April 8, 1993.

As specified in Procedure TP-93-0006, testing of the 120 fully withdrawn

control rods was accomplished by Surveillance Test Procedure STP-052-3701,

Revision 7, " Control Rod Scram Testing." This procedure had been used in the

past to conduct scram timing tests of 10 percent of the control rods once per

120 days of operation in o'rder to satisfy Technical Specification surveillance

requirements for operability. .This provided a well-established, contro11ed'

method of inserting and withdrawing individual rods for the : flux tilting test.

On March 29 an apparent breakdown in communications between two operators at

the hydraulic control units resulted in scramming the wrong control rod.

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procedure required Rod 20-25 to be scrammed, but the operator scrammed

Rod 20-45 instead. The licensee identified and documented the error on

Condition Report 93-0152.

Intended Rod 20-25 was in the fully withdrawn

position.

Rod 20-45 was in the. fully inserted position, so there was no rod-

movement and no unexpected flux changes. The hydraulic control unit for

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Rod 20-45 was restored to its proper lineup and testing was halted. After-

counseling the operators on proper communications.and self-checking, the shift

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supervisor directed that a copy of the control rod movement' sheet'from

Procedure TP-93-0006 be provided to the operators at the hydraulic control

units so that they could visually compare the rod to be tested, with the

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verbal test- direction coming from the control room. The remainder of. testing

was completed without any additional errors.

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The-licensee conducted an evaluation to determine the facts,. event chronology,

-and any existing conditions pertaining to the event in accordance with

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Procedure OSP-018, Revision 1, " Operations Accountability Review." The

results of that review revealed a change in the self-checking routine used by

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the same operators on all other rods. . In this instance, one operator relied

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on the other to select the next hydraulic control unit based on his

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overhearing a telecommunications repeat-back, and then the~first operator did

not visually verify, by the label plate, that he was scramming the correct

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rod.

The licensee also took personnel actions appropriate to the

circumstances.

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Failure to scram the correct control rod in the sequence established by

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Procedure TP-93-0006 was in violation of Technical Specification 6.8.1.d,

which requires test activitie.s of safety-related equipment to be implemented

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by written procedures.

However, since the' licensee's corrective actions were

appropriate, this licensee-identified violation is not being cited because the

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criteria specified in paragraph VII.B.2 of Appendix C to 10 CFR Part.2 of the

- NRC's " Rules of Practice" were satisfied.

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By March 31, the licensee had identified the approximate location of the fuel

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leak. When Rod 44-29 was inserted from 40 notches to 00 notches', there~was a.

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significantly greater change in radiation levels in-the offgas pretreatment-

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piping as read on a temporarily installed Eberline SRM 200 radiation monitor.

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In addition, as the operators attempted to withdraw the rod back to its

original position, radiation levels increased at such a rate that the reactor

engineer directed the rod to be reinserted, and left inserted, to. suppress

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neutron flux in that part of the core.

After retesting three rods in close proximity to Rod 44-29, the ;icensee

confirmed that dod 44-29 was closest to the fuel leak and concluded that

operation for the remainder of the fuel cycle would be with Rod 44-29 inserted

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to minimize the local power in the vicinity of the leak.

In that manner,

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degradation of the leak would probably be minimized while at power.

The flux tilting process used by the licensee appeared to be successful in

identifying the location of the fuel leak so that power and consequent

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degradation could be suppressed by leaving the appropriate rod' inserted.

Offgas, grab samples taken on April 6, after full- power operation was resumed

and stabilized, indicated approximately 8,000 microcuries per second.

Prior

to testing, offgas grab samples indicated approximately 12,000 microcuries per..

second.

Because the recoil levels before the leak was noted were about

4,000 microcuries per second, the release rate was cut approximately -in half.

Despite'the operator error in scramming the wrong rod and the poor

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communications between the NRC staff and the licensee over the testing ~ methods

to be used, the licensee's performance in the identification, reactor

engineering analyses, planning, and implementation of the testing to find and

suppress further degradation of the reactor fuel leak was nottworthy. The

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inspectors noted good support of the test by the radiation protection

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organization by providing a sensitive and responsive radiation monitor and

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recorder setup to detect changes in offgas radiation levels.

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significantly reduced exposures that would have been received through

otherwise frequent grab sampling.

2.2 Continued Discrepancies Found in Logic System Functional Tests (LSFTs)

In Section 2.1 of NRC Inspection Report 50-458/93-05, the inspector described

licensee-identified discrepancies found in certain LSFT surveillance test

procedures.

In each case, the problem was a failure to maintain testing

continuity or overlap on LSFTs to assure that all logic components, from the

sensor through the actuated device, were tested to verify operability.

The

licensee's initiative in finding the deficiencies and taking appropriate

immediate, as well as long-term corrective actions, was appropriate.

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addition, the components in question were found to be operable in each case.

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During this inspection period, as a result of long-term corrective action

accelerated because of the above findings, the licensee identified the

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following additional deficiencies in LSFTs:

On March 26, the licensee identified that a wire connecting the reactor

core isolation cooling (RCIC) low supply pressure contacts to the

remainder of the logic circuit was not being tested.

Also the wire

connecting the high main steam line temperature contacts to the

remainder of the RCIC logic was not being tested.

Vacuum breaker

isolation Valves E51-F077 and E51-F078 required an RCIC low supply

pressure signal, among others, to automatically isolate.

One of the

wires connecting the appropriate relay contacts was not tested by any

procedure.

Technical Specification 4.0.3 was implemented, and the

surveillance test procedures were changed and subsequently performed.

The circuits were all verified to be operable within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

This was

documented in Condition Report (CR) 93-0145.

On March 26, the licensee identified a condition in the safety relief

valve / automatic depressurization system LSFT where no check was made to

verify that the "LO-LO SET" setpoint remained in effect until the reset

pushbutton was pressed as required by Technical Specification 4.4.2.2.1.b.

Technical Specification 4.0.3 was

implemented, the test procedures were revised, and the circuits were

verified operable within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

This was documented in CR 93-0145.

On March 31, the licensee identified that there was no test in the

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Division I and Il electrical power systems LSFT to verify the function

of the contacts associated with the loss of coolant accident signal,

which was in series with the short time degraded voltage signal.

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contacts were tested and verified operable within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

This was

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documented in CR 93-0158.

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On April 5, the licensee found the contact used to trip Standby _ Service

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Water Pump ISL?*P2C on receipt of a sustained undervoltage signal' on the

Division 111 bus was not being tested.

The procedure was revised and

the contact was tested and found to be operable within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. .This

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was documented in CR 93-0168.

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On April 12, the licensee identified that the Division III electrical

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power system LSFT did not test to verify the function of the contacts

associated with the loss of coolant accident signal that was in series

with the short-time degraded voltage signal,

This condition was similar

to those of Divisions I and 11 discussed above found on March 31.

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procedure was corrected and the contact was tested and found to be

operable within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

This was dor umented in CR 93-0178.

On April 15, the licensee discovered that there was no monthly channel

functional test on two relays associated with the RCIC high; steam flow

timer.

Surveillance test procedures were revised and implemented within

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and the circuits were found to be operable. This was

documented in CR 93-0184.

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At the end of this inspection period, the licensee was approximately

35 percent complete on their detailed review of LSFTs.

On March 15, 1993, the

licensee documented these issues in Licensee Event Report (LER)93-002, with a

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commitment to update the report. On April 2, the license issued a supplement-

to the LER with a continuing commitment to update the LER incrementally as

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additional LSFT overlap problems were discovered as a result of their

corrective action.

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In all cases, the untested circuits were found to be operable. Additional

inspection will be conducted as followup to LER 93-002 to review the

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licensee's completed reviews.

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2.3 Test Fixture Found in SRM A

On April 17, 1993, while performing postshutdown source range nuclear

instrument functional surveillance testing on SRM A, a test fixture used to

hold down the inoperative inhibit pushbutton-was found installed.

The

technicians were performing Surveillance Test Procedure STP 503-4503,

Revision 6A, " Control Rod Block-Source Range Monitor A Weekly Channel

Functional (C51-K600A, C51-R601A, C51-R602A)." When the " operate" switch was

taken out of the " operate" position in accordance with Section 7.1.7 of the

procedure, the appropriate annunciators failed to alarm as expected. Upon

opening the instrument drawer, the technicians found the test fixture

installed. The licensee documented the. deficiency on CR 93-0196.

The inspector reviewed the completed surveillance test documentation from the

last time SRM A was tested, which was on December 7, 1992, during the previous

outage.

Section 7.2.2 of Procedure STP-503-4503 required removal of the

fixture, thus releasing the pushbutton.

This section was signed off as

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compl eted .

There was also a signed-off independent verification in

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Attachment 4, with Step 2 verifying restoration of the pushbutton_and removal

of the test fixture.

The licensee could not produce any subsequent

documentation showing that SRM A was tested or worked on since December.7,

1992, nor was it apparent to the inspector that anyone would have a need to

install the test fixture until April 17. As of the end of this_ inspection

period, the licensee did not have a cause identified to explain why the test

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fixture was installed.

The inspector questioned the proper implementation of

the licensee's independent verification program.

Previously, the inspector

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identified a possible weakness in this program in NRC Inspaction

Report 50-458/92-32, Section 5.1.

The licensee's investigation was not

completed and, therefore, appropriate corrective actions had not yet been

taken.

The safety significance of the test fixture being left installed was mitigated

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by the fact that, when the instrument was operating, the function switch had

contacts which were closed in parallel with the inoperative inhibit

pushbutton.

Therefore, the instrument was capable of performing its intended

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safety functions when it was required to be operable.

The inspector was

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concerned, however, that this event indicated a possible breath in the

integrity of the licensee's independent verification program or a failure to

control the installation of the test fixture, if it was reinstalled after

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December 7, 1992.

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Either scenario is a potential violation of NRC regulations, pending the

results of further review. This is an unresolved item (458/93010-1).

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2.4 Licensee Response to Perry Strainer Issue

On April 15, 1993, a potential common mode failure was identified at the Perry

Facility, a General Electric boiling water reactor (BWR-6) with a Mark III

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containment.

The suppression pool suction strainer for Residual Heat Removal

Pump B was observed to have accumulated substantial amounts of debris.

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February 1993, they cleaned the suppression pool and replaced the residual

heat removal suction strainers following identification of strainer fouling

and deformation.

NRC Region IV staff informed Gulf States Utilities of the

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event and expressed concern that similar circumstances might apply to

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River Bend Station, given that River Bend Station did not have an installed

suppression pool cleanup system.

The licensee responded by assembling an ECCS suction strainer task force

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comprised of a senior management sponsor, a team leader from system

engineering management, and representatives from system engineering, design

engineering, operations, and chemistry, with licensing and quality assurance

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oversight.

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The inspector monitored the licensee's. activities and reviewed the results of

actions taken. Activities included:

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A review of pump inservice data and trends.

An operational events search for similar events.

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A design review and comparison between River Bend Station and Perry

Station considering strainer construction and location of suction and

discharge points.

Suppression pool cleanliness and sampling plans.

(During the 1992

refueling outage, River Bend emptied and cleaned the suppression. pool.)

Divers to inspect strainers, suppression pool, and sample bottom of pool

for precipitates or sludge.

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Conduct of resin blockage tests on strainers with smaller holes.

In addition to the above tasks, before disturbing the installed ECCS strainers

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and' dispatching divers, the licensee conducted a 24-hour test run of the low

pressure core spray pump at full design flow, with return to the suppression

pool.

The suction strainer was not cleaned prior'to the test.

The test was

run in accordance with special Test Procedure TP-93-0009, Revision 0, "ECCS-

Suction Strainer Test Procedure." The inspector witnessed portions of the

test and reviewed the data. The test procedure implemented the normal pump

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inservice test surveillance procedure with an extended run to obtain data.

After 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, there was no degradation of suction pressure, as read on a

precision test gauge.

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The ECCS suction strainers at River Bend Station were found to be different

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from the perforated cone type sheet metal strainers at Perry Station. The

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River Bend Station strainers were made up of a series of perforated plates and

spacers bolted together.

It appeared that they would not collapse, even if

subjected to a full vacuum on the pump suction side.

However, the perforated

plates had 3/32-inch holes which could become clogged.

The strainers were

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manufactured by Zurn Industries and were designed to provide adequate flow

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with 50 percent clogging.

The licensee's ECCS Suction Strainer Task Force had not reached any final

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conclusions as of the end of this inspection period, but they informed the

inspector that the following items were under review, pending results of the

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above listed actions, to prevent an event similar to Perry Station's problem

from occurring at River Bend Station:

Chemistry sampling frequency

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Strainer inspection frequency

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Inservice test procedures

Specific trending for suction strainers

Tests and sampling after safety relief valve actuations

Overall, the inspectors concluded that the licensee's response to this

potentially significant issue was timely, thorough, and proactive.

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inspectors will continue to monitor the licensee's activities on this issue

through completion of final actions.

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2.5 Conclusions

The early plant staff recognition and identification and the reactor

engineering analyses, planning, and implementation of testing to locate and

suppress further degradation of the reactor fuel leak were excellent, with one

exception as described below.

A noncited violation was identified for operators departing from the

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licensee's self-checking process when they scrammed the wrong control rod

during reactor flux tilting tests.

The licensee's corrective actions in seeking out, identifying,.and correcting

overlap discrepancies in LSFT surveillance procedures continued to demonstrate

good performance. The number of discrepancies confirmed the need to perform

the detailed reviews.

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Finding a test fixture installed in SRM A after completion of' the functional

test was a potential violation pending further review to determine the cause.

An unresolved item was opened.

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The licensee's response to ensure that an occarrence similar to the Perry

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Station ECCS suction strainer clogging event should not occur at River Bend

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Station was thorough and timely.

3 OPERATIONAL SAFETY VERIFICATION (71707)

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The objectives of this inspection were to ensure that this facility was being

operated safely and in conformance with regulatory requirements and to ensure

that the licensee's management controls were effectively discharging the

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licensee's responsibilities for continued safe operation.

3.1 Control Room Observations

The inspectors observed operations in the control room on a daily basis when

on site.

Specific notice was taken of the licensee's work control process,

during the outage, to replace recirculation pump seals and other selected

work. The inspectors noted that implementation of a recent change to' isolate-

the work control station from the immediate area of the shift supervisor was

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working well_ and eliminated a significant amount of distraction from ~the. shift

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-supervisor and_the control operating foreman.

The licensee had placed- a

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senior reactor operator in charge of the work control. station who was? always

in close communication with the control room and was knowledgeable of the

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types of information the control room needed.

The inspectors noted that overall operator professionalism in the control room

during power operation and when shut down was good.

Shift turnover appeared

to be thorough and informative, and communications-observed between the

operators and control room supervisors was generally crisp and concise.

On April 17 and 18, 1993, the inspectors observed portions of the plant shut

down for Planned Outage 93-01.

The purpose of the outage was to replace

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degrading reactor recirculation pump mechanical seals.

The plant was reduced'

from full power at about 10 percent per hour.

Before the- planned scram from

about 30 percent power, the shift supervisor conducted a detailed briefing on-

what his expectations were from each operator.

The condensate storage tank.(CST) was essentially isolated because-of high-

total organic concentrations (discussed in NRC Inspection

Report 50-458/93-05). Therefore, the shift supervisor made sure that the

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operators were in a position to anticipate the effects of a different makeup:

water lineup.

Specifically, reference was made to the suction lineup for the

control rod drive hydraulic (CRD) pumps. The suction pressure regulator from

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the condensate header was. set abnormally low to minimize return flow to the

CST. Also, the CRD pump miniflow lines, which returned to the CST, were

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temporarily isolated. An operator was stationed'at the CRD pumps to restore

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suction and miniflow in the event of a pump trip when the control- rod -

hydraulic cylinders refill after the scram.

The scram was executed from 29 percent power at 3:19 p.m.

The operators were

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well coordinated and maintained reactor vessel level within the expected band.

The operating CRD Pump A tripped as anticipated on low suction pressure.

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operators experienced some difficulty in restoring CRD makeup flow, ostensibly

because of the slow response of the pressure regulator.

By 3:49 p.m. CRD pump

flow was restored. Overall, the shutdown to ambient conditions was safely

conducted.

3.2 Plant Tours

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On March 24, 1993, during a routine tour, the inspector observed that the

inner door of the 171-foot elevation containment personnel airlock was not

locked in a manner that would prevent the door from being opened.

As

described in NRC Inspection Report 50-458/93-11, the NRC has determined that

the airlock interlock mechanism was inoperable.

Technical Specification 3.6.1.4,-Action b, requires, with,the interlock mechanism

inoperable, that one airlock door be locked closed at all times.

During

personnel entry and exit through'the airlock, an individual must be dedicated

to assure that two doors are not opened simultaneously.

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Although the licensee considered the airlock to be operable at'the time, the

NRC staff disagreed.

This was established during a conference call between

Region IV personnel, NRR personnel, the resident inspectors, and licensee

personnel on March 11,-1993. The Plant Manager issued a directive to

implement the requirements of Technical Specification 3.6.1.4, Action

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Statement b, as a conservative action.

The inspector had noted.that this'

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action placed the plant in compliance with the Technical Specifications.

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However, during the March 24 tour, the inspector observed the firewatch' unlock

and open the outer door.

Following the outer door being chained, the

inspector observed a radiation protection technician.open the inner door and

enter containment without the benefit of the key. 'The technician stated'that

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he had obtained prior permission from the firewatch and that.the chain was not

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secured in a position that required. unlocking the chain to remove it.

He had,

therefore, simply slipped the chain from over the top of the handwheel' and

opened the door.

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The inspector discussed this incident with the shift supervisor, and he

documented the event in CR 93-0143.

The nuclear equipment operator identified

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a way of locking the airlock doors. in a secure manner, and the doors were

properly locked. The shift supervisor instructed the firewatch ' personnel on-

the proper way of locking the airlock:and had an operator aid posted to remind

personnel operating the airlock on the proper way to lock it.

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On March 31, during 'another tour, the inspector noted an instance where the

outer door of the 171-foot elevation containment persennel airlock was not

.being locked as required by the Plant Manager's dircctive.

In this instance,

the person responsible for locking the door was using the padlock but, again,

the chain was draped over the handwheel in such a manner that it could be

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easily removed without unlocking the padlock. Whcn cha'llenged by the

inspector, the person explained that the chain was too short. After the

inspector called his attention to other chains available to him in the

airlock, the individual-switched chains around, thereby solving the problem.

.The inspector informed the shift supervisor of the continuing problem with

people not complying with Technical Specification 3.6.1.4.b, as directed by

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the Plant Manager.

CR 93-0160 was issued to document the second problem.

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Actions were taken to ensure that individuals responsible for locking the

. airlock doors clearly understood the Plant Manager's directive, and double

padlocks were utilized to capture the handwheels.

These issues were addressed

during an enforcement conference conducted at Region IV Headquarters on

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April 21, 1993, and were reviewed in terms of immediate corrective actions

taken in response to' containment breaches and inoperability of airlock

interlocks discussed in NRC-Inspection Report 50-458/93-11.

Therefore,.no

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further action is necessary under this inspection report.

During an NRC management tour of the plant conducted on March 25, 1993,

several deficiencies were'noted. A ventilation discharge screen was covered

with what appeared to be dead insects.

The licensee stated that the

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ventilation was nonsafety-related and that the condition had been identified

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on plant management's housekeeping punchlist prior to the-tour. Additionally,

the inspectors ~ noted a foam-like substance floating on the surface of the

auxiliary building crescent area sump.

This sump was the suction point.of the

. safety related suppression pool pumpback system.

The licensee evaluated the

substance and convinced the inspector that it did not pose a safety concern

and did not affect the operability of the system.

Housekeeping had generally improved, but during a reactor building tour near

the end of the report period, the inspectors noted a number of flashlights,

poly bags, and small tools in the containment that had the potential for

falling into the suppression pool.

This was brought to the attention of

licensee management and was promptly corrected.

The inspectors have noted

fewer ladders improperly stored and less debris in the pl mt.

The inspectors noted continued improvements in plant preservation.

The

licensee had just completed painting of the 123 foot elevation

"T" tunnel.

This took extensive effort and made a large difference in the appearance of

the "T" tunnel, which was used as an entrance area for the turbine, radwaste,

and auxiliary buildings, as well as the auxiliary control room.

3.3 Conclusions

Control room operator performance and professionalism was found to be

improving, based on routine daily observations and by observation of the

shutdown that was implemented on April 17 and 18, 1993.

4 MONTHLY MAINTENANCE OBSERVATIONS (62703)

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The station maintenance activities addressed below were observed and

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documentation reviewed to ascertain that the activities were conducted in

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accordance with the licensee's approved maintenance programs, the Technical

Specifications, and NRC Regulations.

4.1

Division 11 Standby Diesel Generator (DG) Outage

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On April 14, 1993, the inspector observed maintenance activities associated

with a planned Division II Standby DG outage.

Three mechanical maintenance

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activities and part of one instrument and controls activity were observed.

The inspector reviewed the work packages and clearances.

The prejob briefing

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was attended and work followed to completion.

The tasks were MWO P564471,

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" Lubricate Diesel Keepwarm Oil Pump, lEGO*PIB"; MWO R170898, " Valve Leaks by

Seat-Repair, lEGA*V137"; MWO R170881, " Inspect Division II EDG Air Start

Distribution per CR 93-0035."

All the MW0s were under Clearance RB-1-93-6288.

The work packages were well

prepared with clear work instructions and clearly defined inspection hold

points.

During the valve repairs, care was taken to prevent foreign material

intrusion into the open pipe.

The inspection of the air start system involved

a custom test fixture to ensure an adequate vent path from the DG cylinders

after air pressurization during the start cycle. The system engineer was

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present during the work activities to explain the intent of. the work and

monitor progress. The inspector also observed the quality control inspections

during the valve repair. The quality control inspector verified the condition

of the parts upon disassembly, foreign material exclusion practices, condition

of materials upon reassembly, including seat contact area by confirming blue

checks, proper qualification of the gasket material, and final torque values

upon reassembly.

All work observed was performed in accordance with the work

instructions provided.

The inspector also observed portions of MWO P562478, a calibration of the.

alarm for the diesel Jacket outlet water temperature. One deficiency was

noted with the package. The inspector observed that the calibration directed

the technicians to perform calculations to compensate 'for the ambient

temperature due to the dissimilar metal junction introduced by the test leads

in the alarm cabinet, but did not provide space for the technicians to record

actual uncompensated values found, ambient temperature, and the corresponding

millivolt value to be subtracted, or the values resulting from the

calculation. This resulted in loss of actual values measured by the equipment

prior to the subtraction of the compensation. The foreman could not review

the calculations for accuracy prior to signing the package, because they were

not recorded. This observation, to enhance the maintenance calibration

process, was discussed with the licensee.

4.2 Rebuild of a Recirculation Pump Seal Package

On April 19, 1993, the inspector observed portions of the work performed under

MWO R175003. This MWO was written to rebuild the spare Seal

Package IB33*PC001B for installation on Reactor Recirculation Pump B.

The

inspector verified that the replacement parts to be used were acceptable for

installation in safety-related applications in accordance with the requisition

ticket.

Seal package body components, seals, and o-rings were verified by

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serial number to ascertain that the appropriate part was being utilized.

The inspector observed that the repairmen were utilizing the work package job

plan and Corrective Maintenance Procedure CMP-9020, "B33*C001 Reactor Water

Recirc. Pump Disassembly, Inspection, Rework and Reassembly." The individuals

were verified to be qualified for the work in accordance with the licensee's

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training procedures.

The individuals appeared to be knowledgeable of the job

and professed that they had performed the procedure in the past.

The

repairmen meticulously took measurements of parts to be reused as well as

those to be replaced.

The inspector noted that there was full time coverage of the job by a plant

quality control inspector. The inspection report indicated that all

observations were satisfactory.

Acceptable tolerances had been measured on

all parts. Hold points were met throughout the observation. Additionally,

the licensee had requested and procured the services of representatives from.

the pump manufacturer to assist as technical advisors in the rebuild effort.

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The inspector observed the radiation work practices used during the effort.

'The rebuild was performed within a contaminated zone in the hot machine shop.

At one point.the quality control inspector noted that the craftsmen did not

have enough room to pass one of the radiological boundaries without moving it

to one side.

The radiation protection technician was notified and the zone

was enlarged to provide adequate room as well as appropriate contamination

control.

4.3 C;nclusions

The performance of maintenance observed during this inspection period was

good.

Procedures provided by the MW0s appeared to be appropriate in each

case.

5 BIMONTHLY SURVEILLANCE OBSERVATIONS (61726)

The inspectors observed the surveillance testing of safety-related systems and-

components addressed below to verify that the activities were being performed

in accordance with the licensee's approved programs and the Technical

Specifications.

5.1 Retest of Replaced Potter & Brumfield MDR Relays

On April 23, 1993, the inspector observed portions of Surveillance Test

Procedure STP-511-4802, Revision 3, " Main Steam Line Isolation-Main Steam Line-

Radiation High, 18 Month Response Time Test, (D17-K610B,C) Channels B and C."

This test was designated in MWO 166031 as a retest following replacement of

Potter & Brumfield MDR-4171 Relay IC71A*K78.

The technicians followed the procedure in a step-by-step manner, demonstrated

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good communications with the operators, and followed the administrative

requirements for lifted leads.

A quality control inspector was present to

observe the test.

The technicians experienced problems with the frequency generator and noted

that voltage transients were causing partial trips.

Because they were unable

to resolve the problem by changing test equipment connecting wires, they

stopped the test and restored the system to normal. After. consulting with the

system engineer, the MWO was revised to require a much simpler test,

STP-511-4502, Revision 5, "RPS/ Isolation Actuation-MSLI-Main Steam Line

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Radiation-High Monthly Channel Functional (D17-K610B)."

Because of the difference in the two tests, the inspector questioned how the

simpler test could meet the retest requirements.

The foreman responded that

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they were able to take the bench test time response of the replacement relay

and add it conservatively to the previous system time response results from

the last refueling outage, leaving only the channel functional test to be

performed.

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In order to evaluate the adequacy of retesting specified for the replacement

.of MDR relays, the inspector requested the licensee to demonstrate in detail

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how the selected surveillance test procedures were verified to adequately

retest the new relays.

This was scheduled to occur on May 4, during the next

inspection period. The results will be documented in a future inspection

report under Inspection Followup Item 458/93010-2.

6 ENGINEERED SAFETY FEATURE WALKDOWN (71710)

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The objective of this inspection was to perform a detailed walkdown of a

representative sample of the accessible portions of the control room air

conditioning system to verify the system's capability to perform its intended

safety functions.

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6,1

System Status

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The control room air conditioning system, *;ith two independent air handling

unit / filter train subsystems were in an sperable status during power

operations and while shut down for Plan led Outage 93-01.

6.2 Procedure Reviews

The inspectors commenced a review of System Operating Procedure SOP-0058,

Revision 7, " Control Building HVAC System," for adequacy and technical

agreement with the system piping and instrument drawing.

The review was

incomplete as of the end of this inspection period and will continue into the

next inspection period and be documented in NRC Inspection

Report 50-458/93-19. No discrepancies were identified.

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ATTACHMENT

1 PERSONS CONTACTED

1.1 Licensee Personnel

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R. E. Barnes, Supervisor, Maintenace Engineering

  • J. B. Blakeley, Assistant Plant Manager, System Engineering
  • J. E. Booker, Manager, Nuclear Industry Relations
  • J. W. Cook, Senior Technical Specialist

D. R. Derbonne, Assistant Plant Manager. Operations, Radwaste & Chemistry

L. L. Dietrich, Supervisor, Nuclear Licensing

R. G. Easlick, Radwaste Supervisor

  • L. A. England, Director, Nucl.!ar Licensing
  • A. O. Fredieu, Supervisor, Maintenance Services

P. E. Freehill, Assistant riant Manager - Outage Management

  • K. D. Garner, Licensing Ergineer
  • K. J. Giadrosich, Supervisor, Quality Engineering

E. L. Glass, Supervisor, Instrument & Control

  • P. D. Graham, Vice President (RBNG)
  • J. R. Hamilton, Manager-Engineering
  • W. C. Hardy, Radiation Protection, Supervisor
  • G. R. Kimmell, General Maintenance Supervisor
  • G. D. Lipham, Chemistry Supervisor
  • D. N. Lorfing, Supervisor, Nuclear Licensing
  • l. M. Malik, Supervisor, Operations Quality Assurance

C. R. Maxson, Senior Compliance Analyst

J. Mead, Supervisor, Electrical and Special Projects

T. G. Murphy, Director, Management Systems

W. H. Odell, Director, Radiological Programs

R. L. Roberts, Electrical Maintenance Supervisor

  • J. P. Schippert, Plant Manager

B. R. Smith, Mechanical Maintenance Supervisor

  • M. A. Stein, Director, Design Engineering
  • K. E. Suhrke, General Manager, Engineering and Administration
  • W. J. Trudell, Assistant Operations Supervisor

R. J. Vachon, Senior Compliance Analyst

  • J. E. Venable, Operations Supervisor

C. W. Walker, Supervisor, Operations Quality Control

S. L. Woody, Director, Nuclear Station Security

  • Denotes personnel that attended the exit meeting.

In addition to the

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personnel listed above, the inspectors contacted other personnel during this

inspection period.

2 EXIT MEETING

An exit meeting was conducted on April 27, 1993.

During this meeting, the

inspectors reviewed the scope and findings of the report.

When the inspectors

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summarized the issue in Section 4.1 of the report, pertaining to a diesel

jacket outlet water temperature alarm calibration procedure not requiring the

technician to record actual uncompensated values found, the inspectors

emphasized the importance of recording raw data for future reference so that

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calculated values could-be verified.

Licensee management ackowledged the

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concern'and. stated that they would review the matter and advise the inspectors

of their. findings and corrective actions.

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The licensee did not_ identify as proprietary,.any information provided to, or.

reviewed by the inspectors.

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