ML20039D101

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IE Insp Rept 50-302/81-15 on 810721-0825.Noncompliance Noted:Emergency Feedwater Pump Turbine Bearing Oil Sightglasses Not Adjusted Per Mod Approval Records 78-1-1 & 78-1-1A on 810813
ML20039D101
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 09/24/1981
From: Brownlee V, Orlenjak R, Beverly Smith, Stetka T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20039D085 List:
References
TASK-1.A.2.1, TASK-2.B.4, TASK-2.F.1, TASK-TM 50-302-81-15, IEB-80-03, IEB-80-09, IEB-80-18, IEB-80-24, IEB-80-3, IEB-80-9, IEB-81-12, IEC-79-13, IEC-79-20, IEC-79-22, IEC-79-23, IEC-79-4, IEC-80-04, IEC-80-14, IEC-80-4, NUDOCS 8112310317
Download: ML20039D101 (22)


See also: IR 05000302/1981015

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION il

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101 MARIETTA ST

N.W.. SUITE 3100

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ATLANTA, GEORGIA 30303

Report No. 50-302/81-15

Licensee:

Florida Power Corporation

3201 34th Street, South

St. Petersburg, FL 33733

Facility Name: Crystal River 3 fluclear Generating Plant

Docket No. 50-302

License No. DPR-72

Inspection at Crystal River site near Crystal River, Florida

C!2N[8-/

Inspectors: l >LNA.t

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T. F. Shef.ka, Senior Residdnt Inspector

Date ' Signed

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D . Srfith, R sident Inspdctor

Da'te Sitjned

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R. V.

lenja , Reactor Insp#ctor

Date Sfsned

Approved by:

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V. L. Bfownlee, Acting Chief, Reactor Projects

Da~te Signed

Section 2B, Division of Resident and

Reactor Project Inspection

SU!!!t\\RY

Inspection on July 21 through August 25, 1981

Areas Inspected

Routine inspection by the resident inspectors of plant operations, security

radiological controls, procurement, Licensee Event Reports (LERs) and Non-

conforming Operations Reports (NCOR's), non-routine events, licensee action on IE

Bulletins and Circulars, reactor coolant system leak rate verification,

Inplementation of T111 Action Plan Items, and licensee action on previous

inspection items. Numerous facility tours were conducted and facility operations

observed.

Some of these tours and observations were conducted on back shifts.

The inspection involved 284.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> on site by two resident inspectors and one

regional inspector.

Results

Two violations were identified (Failure to perform plant modifications in

accordance with procedures as required by 10 CFR 50, Appendix B, Criterion V,

paragraph 5.B.(11)b; Failure to perform safety evaluations for plant modifi-

cations as required by 10 CFR. 50.59 paragraph 9.b.

8112310317 811223

PDRADOCK05000g

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DETAILS

1.

Persons Contacted

Licensee Employees

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P. Baynard, Manager, Nuclear Support Services

    • G. Boldt, Technical Services Superintendent
      • C. Brown, Nuclear Compliance Supervisor

J. Buchner, Security Officer

      • J. Bufe, Compliance Auditor

M. Collins, Reactor Specialist

      • J.

Cooper, QA/QC Compliance !!anager

B. Crane, Planning Engineer

    • W. Herbert, Technical Specification Coordinator

V. Hernandez, Compliance Auditor

S. Johnson, itaintenance Staff Engineer

W. Kemper, Plant Training Manager

      • K. Lancaster, Quality Assurance Auditor

T. Lutkehaus, Technical Assistant to the Nuclear Plant Manager

    • P. McKee, Operations Superintendent

G. Perkins, Health Physics Supervisor

  • D. Poole, Nuclear Plant Manager

R. Rogers, Nuclear Stores Supervisor

    • G. Ruszala, Chemistry / Radiation Protection Manager

J. Smith, Senior Quality Programs Auditor

D. Smith, Technical Services Superintendent

D. Todd, Materials QC Inspector

    • J. Lander, Maintenance Superintendent

G. Williams, QA/QC Supervisor

K. Wilson, Licensing Specialist

Other personnel contacted included office, operations, engineering,

maintenance, chem / rad, and corporate personnel.

  • Present at the Exit Interview conducted on August 19.
    • Present at the Exit Interview conducted on August 25.
      • Present at both Interviews.

2.

Exit Interview

The inspectors met with licensee representatives (denoted in paragraph 1) on

numerous occasions during and at the conclusion of the inspection on

August 25, 1981.

During this meeting, the inspector surmiarized the scope

and findings of the inspection as they are detailed in this report.

During

this meeting, the violations, an unresolved item, and inspector followup

items were discussed.

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3.

Licensee Action on Previous Inspection Findings

(0 pen) Unresolved Item (302/81-02-06): The licensee has begun developing

new vz ve lineup proced"res that will include instrument valves and is

completing revisions to system flow diagrams. The licensee will complete

drawing revisions and implement the new valve lineup procedures prior to

returning the plant to operation from the refuel outage scheduled to begin

on September 27.

(0 pen) Inspector Followup Item (302/81-05-12): The licensee was notified by

the Clark Relay Company that a relay rebuild kit is now available that will

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replace the relay shafts with a new design. The licensee has purchased

these rebuild kits and will replace the relay shafts on all safety-related

Clark relays during the upcoming refuel outage scheduled to begin

September 27.

The replacement will be performed in accordance with flAR

81-5-20 and Work Request 24403.

(0 pen) Inspector Followup Item (302/80-42-12):

The licensee has added signs

on all equipment in the fossil plants (CR-1 & 2) that effect operation of

the nuclear plant (CR-3) to warn fossil plant personnel to notify CR-3

personnel prior to removing said equipment from service.

In addition a

revision to Administrative Instruction (AI)-1300, Crystal River

Units 1 and 2 Interface with Crystal River Unit 3, is being written to list

this equipment. This revision will be issued by September 30, 1981. This

item remains open pending revision of AI-1300.

(Closed) Violation (302/81-05-02):

The licensee revised procedure RP-101,

Radiation Protection 11anual, as Revision 14 on July 29, 1981, to include an

enforcement policy for Radiation Work Permit violators. The licensee's

actions on this item are complete.

(Closed) Unresolved Item (302/81-02-15): The licensee has revised flodifi-

cation Approval Record (itAR) 80-11-74 on June 10 to provide for partial

replacement of solid state triac relays in the ES system.

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(Closed) Inspector Followup Item (302/81-07-11): The licensee revised

procedures CP-115, In-Plant Clearance and Switching Orders, as Revision 35

on liay 28, 1981 to include a listing of safety-related equipment.

(Closed) Inspector Followup Item (102/81-11-09):

The licensee has revised

procedures QC-200, Training and Qualification of Nuclear Quality

Assurance / Quality Control Inspection Personnel, and QC-201, Training of

Nuclear Compliance Personnel to specify that training will be completed

within two years.

(Closed) Unresolved Item (302/81-05-06): Work instruction cards utilized by

the Chem / Rad Technicians as a guide for performing their duties were revised

to alert the technician that if a Standing Radiation Work Permit (SRWP) is

going to expire prior to the next update, the technician should notify a

Chem / Rad Supervisor so that a determination of renewing or cancelling the

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SRWP can be made.

The inspectors' review of the outstanding SRWP's

indicates that the revised system is working.

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(Closed) Unresolved Item (302/81-11-06): The licensee performed a second

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level supervisory review of the completed data from procedure SP-417 on

June 30, 1981 and determined that the results were satisfactory. Trainir

sessions were conducted during the period of August 3-7, 1981 and on

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August 13, 1981, for all plant staff personnel except the operations staff

to re-enforce the supervisory revits requirements of AI-400. The operations

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staff personnel will receive their training during requalification training.

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The licensee's action on this item is considered to be canplete.

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(Closed) Inspector Followup Item (302/81-07-03): The licensee has revised

preventative maintenance procedure PM-119, Inspection and Cleaning of 480

Volt Motor Control Centers, to include a requirement to check the cabinet

filters and to clean or replace them as necessary.

(Closed) Inspector Followup Item (302/81-01-02):

Reviews of the Clearance

Order Book indicates thu'. the required clearance audits are being performed.

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(Closed) Inspector Followup Itan (302/81-02-19): The licensee's requalif-

ication training syllabus now includes the interrelationship between the

waste disposal system and the reactar coolant system.

(Closed) Violation (302/81-07-12): The inspector reviewed the licensee's

response to this violation and verified training completion and procedural

revisions to SP-187 and HP-106.

The licensee's actions on this item are

considered complete.

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4.

Unresolved Items

Unresolved items are matters which more infonnation is required to determine

whether they are acceptable or may result in violations. A new unresolved

item identified during this inspection is discussed in paragraph 5.B(12).

5.

Review of Plant Operations

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The plant continued with Mode 1 power operations until July 31 at which time

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a reactor trip occurred due to personnel error. The plant returned to

Mode 1 power operations on July 31 and continued in this mode for the

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duration of the inspection period.

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a.

Shift Logs and Facility Records

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The inspectors rev,ewed the records listed below and discussed various

entries with operations personnel to verify compliance with T.S. and

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the licensee's administrative procedures.

-Shift Supervisor's Log;

-Operator's Logs:

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- Equi pmen t-ou t-o f-Service-Log ;

-Shif t Relief Checklist;

-Control Center Status Board;

-Short Term Instructions;

-Auxiliary Building Operators' Log; and

-0perating Daily Surveillance Log.

In addition to these record reviews, the inspector independently

verified selected clearance order tagouts.

b.

Facility Tours and Observations

Througout the inspection period, facility tours were conducted to

observe operations and maintenance activities in progress. Some

operations and maintenance activity observations were conducted during

back shifts. Also during this inspection period, numerous licensee

neetings were attended by the inspectors to observe planning and

management activities.

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The facility tours and observations encompassed the following areas:

-Security Perimeter Fence;

-Turbine Building;

-Meteorological Tower;

-Control Room;

-Emergency Diesel Generator Rooms;

-Auxiliary Building;

-Intermediate Building;

-Battery Rooms; and,

-Electrical Switchgear Rooms.

During these tours, the following observations were made:

(1) Monitoring instrumentaticn - The following instrumentation was

observed to verify that indicated parameters were in accordance

with the Technical Specifications for the current operational

mode:

-Equipment operating status;

-Area, atmospheric and liquid radition monitors;

-Electrical system lineut;

-Reactor operating parameters; and

-Auxiliary equipment operating parameters.

(2)

Safety Systems Walkdowns

The inspectors conducted walkdowns of the following safety systems

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to verify lineups were in accordance with license requirements for

system operability:

-Emergency Diesel Generator (EDG) Fuel Oil Transfer System;

-EDG Compressed Starting Air and Engine Exhaust System;

-fiuclear Services and Decay Heat Seawater System; and

-4160V and 480 Engineered Safeguard Busses

(3) Shift Staffing

The inspectors verified by numerous checks that operating shift

staffing was in accordance with Technical Specification require-

ments.

In addition, the inspectors observed shift turnovers on

different occasions to verify the continuity of plant status,

operational problems,and other pertinent plant information was

being accomplished.

(4) Plant Housekeeping Conditions

Storage of material and components and cleanliness conditions of

various areas throughout the facility were observed to determine

whether safety and/or fire hazards exist. The general house-

keeping conditions are acceptable.

(5) Radiation Areas

Radiation Control Areas (RCA's) were observed to verify proper

identification and implementation. These observations included

review of step-off pad conditions, disposal of contaminated

clothing, and area posting.

Area postings were verified for

accuracy through the use of the inspector's own radiation

monitoring instrument.

fio problems were identified in this area.

(6)

Fluid Leaks

Various plant systems were observed to detect the presence of

leaks.

fio problems were identified in this area.

(7) Piping Vibration

flo excessive piping vibrations were noted.

(8) Pipe Hangers / Seismic Restraints

Several pipe hangers and seismic restraints (snubbers) on

safety-related systems were observed.

fio problems were identified

in this area with the exception of the issue discussed in Section

6.B(2) of this report.

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(9) Security Controls

Security controls were observed to verify that security barriers

are intact, guard forces are on duty and access to the protected

area is controlled in accordance with the facility security plan,

fio problems were identified in this area.

(10) Operating Procedures - Operating Procedures were observed to

verify that:

-approved procedures were being used;

-qualified personnel were perfoming the operations; and

-Technical Specification requirements were being followed.

The following Operating Procedures were observed:

-0P-407, Liquid Waste Disposal System, and associated liquid

release permit for the release of "A" Evaporator Condensate

Storage Tank water.

-0P-210, Reactor Startup, and OP-203, Plant Startup, fcr plant

restart following the reactor trip on July 31, 1981.

(11) Tour of Auxiliary and Intermediate Buildings

a.

During a tour of the Auxiliary Building the inspector sted

that the handwheel of pneumatically operated itakeup Valve

(HUV)-253, outside reactor building isolation from reactor

coolant pump controlled bleed-off, was removed from the valve

stem and secured to the piping below the valve.

It appeared

that a pipe hanger located near the valve stem would

interfere with the installation of the valve handwheel. The

inspector discussed this issue with the licensee and was told

that the necessary actions would be taken to reinstall the

!!UV-253 handwheel .

Inspector Followup Item (302/81-15-01): Review the

licensee's actions to reinstall MUV-253 handwheel.

b.

During a tour of the Intermediate Building on August 13, the

inspector noted that the position of the bearing oil level

sight glasses on the turbine driven emergency feedwater pump

(EFP)-2 appeared to be different than that described in

Modification Approval Records (MAR) 78-1-1 and 78-1-1A.

The

inspector obtained copies of the MARS and verified that the

installed sight glass positions on EFP-2 were not as

indicated in the f1ARs. This finding was presented to licensee

representatives and the licensee conducted an investigation.

The original modification was perfomed in accordance with

itAR 78-1-1 and the work request (W/R) for performanc of the

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f1AR was signed off as complete on September 28, 1978.

Apparently during some subsequent routine maintenance, the

sight glasses were returned to their original configuration.

(The licensee does not have documentation to reflect this

change.) During the period of February 12-16, 1979, NRC

Inspection 50-302/79-04 was conducted and the repositioned

sight glasses were identified by the inspectors following a

review of MAR 78-1-1.

At this time the licensee was issued

an item of noncompliance. The licensee responsed to this

item and stated that the sight glasses were returned to the

configuration required in MAR 78-1-1.

This re-modification

was accomplished by issuing a new 14AR 78-1-1A and the W/R for

this modification indicates this work was completed on

!! arch 22, 1979.

MAR 78-1-1A was then sent to the licensee's engineering

department as required by the licensee's procedures.

The

engineering department approved the itAR on January 25, 1980,

but did not close out the package.

The engineering depart-

ment also added a requirement in the MAR to scribe low oil

level lines on the turbine casing to allow sighting from each

sight glass and to remove all high/ low level marks from the

sight glasses proper.

This additional modification was not

perfomed.

Sometime between the completion of MAR 78-1-1A and August 13,

apparently tne EFP-2 sight glass configuration was again

changed as identified by the inspector. The licensee is

unable to produce documentation to reflect this change.

Failure to accomplish plant modifications in accordance with

procedures, instructions, and drawings is contrary to the

requirements of 10 CFR 50 Appendix B, Criterion V governing

activities affecting quality and the requirements of

procedure CP-114, Procedure for Preparation of Permanent and

Temporary Modifications, with regard to verifying that a MAR

is properly completed, is considered to be a violation.

Violation (302/81-15-02):

Failure to perfom plant modi-

fications as required by 10 CFR 50 Appendix B Criterion V,

FSAR section 1.7.6.7.1, and CP-114.

The additional violations against 10 CFR 50 Appendix B

Criterion V identified in paragraphs 8(a) and 9.a following

are considered to be further examples of the licensee's

failure to adhere to procedures for the control of plant

modifications.

Similar violations of 10 CFR 50, Appendix B, Criterion V with

respect to plant modifications were identified during the

inspection period of February 12-16,1979 (NRC Report

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50-302/79-04) and therefore this violation is considered to

be recurrent and uncorrected.

(12) Surveillane Testing - Surveillance testing was observed to

verify that:

-approved procedures were being used;

-qualified personnel were conducting the tests;

-testing was adequate to verify equipment operability;

-calibrated equipment, as required, were utilized; and

-Technical Specification requirements were being

followed.

The following tests were observed:

-SP-110, Reactor Protective System Functional Testing

(Channel "A" and "B");

-SP-140, IN-Core Neutron Detector System Calibration (Data

review only);

-SP-317, Reactor Coolant System Water Inventory B:ilance;

-SP-334, Spent Fuel Pool Pump Operability;

-SP-335, Radiation Monitoring Instrumentation Functional Test

(Section 6.3); and,

-SP-340, ECCS Pump Operability (Return to operability of "A"

Decay Heat ump and "A" Building Spray Pump following

maintenance .

During observation of SP-110, Reactor Protective System (RPS)

Functional Testing, the inspector noted that the method used

for functionally testing RPS analog channel bistables did not

include verification of bistable trip point by vcitage

measurement at the bistable input. The present method uses

an indicator for verification of bistable trip setpoint

(example: RCS low pressure bistable trip point is verified by

the RCS pressure indicator in the RPS cabinet).

In addition,

the acceptance tolerances for the bistable trip setpoints in

the procedure allow values to be accepted that could

potentially be beyond that allowed in Technical Specifi-

cations for (TS) "!!aximum allowable trip setpoints."

The inspector also noted that this same concern (bistable

setpont verification) exists similarly in Procedur SP-130

Engineering Safeguards fionthly Functional Test. This issue

was discussed with the licensee and the inspector's concerns

were acknowledged.

The inspector stated that adherence to

Technical Specification requirements for functionally testing

analog channel bistable trip functions thould include

verification of bistable setpoints by voltage measurement

with suitable acceptance tolerances to ensure bistable trip

setpoints do not exceed Technical Specification maximum

allowable trip setpoints. The licensee will revise

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functional testing procedures, where required, to ensure

analog channel bistable setpoints are verified.by voltage

measurements at the histable input and that suitable

acceptance criteria are provided.

Unresolved Item (302/81-15-03):

Revise functional test

procedures to ensure analog channel bistable trip setpoints

do not exceed TS required limits.

(13) Maintenance Activities - The inspector observed maintenance

activities to verify that:

-Correct equipment clearances were in effect;

-Work Requests (W/R's), Radiation Work Permits (RWP's),

and Fire Prevention Work Pemit, as required, were

issued and being followed;

-Quality Control personnel were available to inspection

' activities as required; and,.

-Technical Specification requirements were being

followed.

The following maintenance activities were observed:

Preventive Maintenance Procedure (Pli)-133, Equipment Lubri-

cation (Decay Heat Pump (DHV)-1A and Building Spray Pump

(BS)-1A oil replacement).

Maintenance Procedure (MP)-131, Disassembly and. reassembly of

DHP-1A (Replacment of DHP-1A pump due to bearing failure).

Troubleshooting activities on Auxiliary Building Air handling

fans to correct damper problem.

Maintenance Procedure (MP)-149, Check Valve Cap Removal and

Reinstallation (Repair of Nuclear Services Closed Cycle : Check

Valve (SWV-101).

Troubleshooting meteorological tower 175' and 33' temperature

indication.

No problems were identified in this area.

(14) Prerefueling Acitivities

The inspectors witnessed the unloading and transfer to the

new fuel storage area of several burnable poison rods (BPR's)

in accordance with refueling procedure (FP)-303, New Control

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Component Receipt, Inspection, Storage and Container

Reclosing.

In addition, the inspectors witnessed Quality

Control inspection of several BPR's.

No problems were identified in this area.

6.

Review of Licensee Event Reports and Nonconfonning Operations Reports

(NCORs)

a.

The inspector reviewed Licensee Event Report (LER's) to verify that:

-The reports accurately described the events;

-The safety significance is as reported;

-The report satisfies requirements with respect to information provided

and timing of submittal;

-Corrective action is appropriate; and

-Action has been taken.

LER's 80-43, 80-47, 81-33, 81-37, 81-38, 81-39, 81-41, 81-42, 81-43,

81-44, 81-45, 81-47, 81-48, 81-49, and 81-51 were reviewed. As a

result of this review the following items were identified:

1.

LER 81-36 stated as a part of the corrective actions that an

evaluation would be performed to determine if failed fuel was

present. A test was run during the period of July 29, 1981

through July 31, 1981 of approximately 43.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> duration with

the reactor at steady state full power and the purification system

isolated.

During this time period, samples were taken at

approximately four hour intervals and were analyzed for dose

equivalent iodine 131. An excessive increase in Iodine 131 would

be indicative of fuel degradation.

The results of this testing were reviewed by the licensee's

corporate engineering group and the reactor vendor (Babcock and

Wilcox) and it was determined that no abnormal criteria were

observed. The inspector discussed this determination with

licensee representatives and reviewed some data results. The

inspectors have no further questions on this item at this time.

2.

LER 81-38 reported an increase in the Strontium 90 (Sr-90) levels

in green leafy vegetable samples analyzed at station C48. This

increase exceeded ten times the control station value. This

increase in Sr-90 could not be explained and the licensee has

conducted a resample to confirm the initial findings.

The results

of this resample were examined on August 25, 1981 and since both

the control station and critical station exhibited a Sr-90

increase of similar magnitude, the licensee attributes the higher

Sr-90 level to nuclear weapons testing conducted by the Peoples'

Republic of China in December,1980.

As of August 25, the

licensee has determined that the increase in Sr-90 at the critical

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station was less than 10 times the control station (actual

magnitude about 3.5 times) and therefore the LER was not required.

The licensee is considering withdrawing this LER. The inspectors

have no further questions on this item at this time.

3.

LER 91-51 was issued as a followup to a prompt report of August 14

which reported an inadequacy of the design of the Cable Spreading

room floor. The licensess's Architech-Engineer (AE), Gilbert

Associates Incorpoated (GAI), determined, during an engineering

nyestigation for a fire protection modification, that concrete

embedments in the wall supporting the cable spreading room floor

were not adequate to sustain dead load, live load,and seismic

requirements.

These embedments were detemined to be adequate as

long as the live loading was restricted.

The licensee took immediate action to restrict live loads by

securing the room with lock and key.

Key control is via the Shift

Supervisor who has explicit instructions on the amount of

permissible live loading. The licensee is developing a modif-

ication (tiAR 81-8-15) that will be installed to utilize the walls

beneath the ficor for added support.

Until this modification is

completed, live loading in the cable spreading room will be

restricted.

The inspectors examined and are satisfied with the licensee's

actions.

Inspector Followup Item (302/81-15-04):

Review the licensee's

progress in modifying the cable spreading roon floor to increase

floor loading capacity.

b.

The inspector reviewed NCOR's to verify the following:

-Compliance with the Technical Specifications;

-Corrective actions as identified in the reports or during subsequent

reviews have been accomplished or are being pursued for completion;

-Generic items are identified and reported as required by 10 CFR Part 21; and,

-Items tre reported as required by the Technical Specifications.

The following NCOR's were reviewed:

81-43

81-259

81-272

81-300

81-117

81-262

81-276

81-301

81-148

81-263

81-278

81-302

81-150

81-264

81-279

81-303

81-153

81-265

81-282

81-304

81-250

81-266

81-284

81-305

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81-251

81-267

81-287

81-306

81-252

81-268

81-280

81-252

81-269

81-291

81-288

81-289

81-254

81-270

81-292

81-290

81-257

81-299

81-288

81-295

81-297

Based on this review, the following items were identified:

(1.) NCOR 81-0265 reported the failure of decay heat system valve

DHV-41 to open in 120 seconds during performance of Surveillance

Procedure SP-370, Quarterly Cycling of Valve.

Review of this

event indicates that SP-370 was developed to satisfy the quarterly

valve cycling requirement of ASME Section 11 Inservice Inspection

(ISI) and the isolation requirement of Technical Specification (TS) 3.6.3.1.

The Licensee has detennined that DHV-4: does not

receive an engineered safeguards (ES) closure signal, the valve

is normally closed in operational Modes 1, 2 and 3, and is only

used during normal decay heat removal operations. Therefore the

isolation time specified in TS 3.6.3.1 is not applicable and the

TS appears to be incorrect. The licensee has also determined that

the following valves are also apparently incorrectly specified in

TS 3.6.3.1.

-BSV-3 and BSV-4, only get an open signal at 4 psi Reactor

Building Pressure;

-DHV-42 and 43, does not receive an ES closure signal and are

maintained closed during Itodes 1, 2, and 3;

-DHV-4, does not receive an ES closure signal and is maintained

closed during Modes 1, 2, and 3, and only has an interlock to open

at 284 psi for decay heat operation; and,

-DHV-5 and 6, receives an ES signal to open for low pressure

injection when RCS pressure is less than 500 psig.

The licensea is presently stroking these valves either open or

closed to verify TS stroking times and to meet AMSE ISI require-

ments.

The licensee also determined that auxiliary spray isolation valve

DHV-91 was not being tested for closure time by SP-370 or SP-435,

Valve Testing During Cold Shutdown. The licensee verified that

this valve was tested for closure time during post-maintenance

testing. The inspector reviewed the data from this valve testing

,

and verified the stroke time was in accordance with TS require-

men ts .

_

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.

13

The licensee will submit a TS change request to revise section

3.6.3.1 to be consistent with actual plant operation.

The

licensee will also revise procedures SP-370 and SP-435 to provide

for monitoring the closure time for DHV-91 and to insure closure

times on the previously listed valves are monitored until a TS

change is approved.

Inspector Followup Item (302/81-15-05):

Review licensee action to

resolve inaccuracies in TS 3.6.3.1 and procedures SP-370 and

SP-435.

(2.) NCOR 81-279 reported a potential generic problem with aluminum

adapter bushings installed in hydraulic snubbers manufactured by

Power Piping Co..

Since July 1979, eleven aluminum adapter

bushings have been found cracked during surveillance testing of

safety-related snubbers. Subsequent testing of the affected

snubbers showed that six of the snubbers passed and five failed

the operability criteria. All of the cracked aluminum adapter

,

bushings were replaced with stainless steel bushings.

In

addition, the licensee has been replacing the aluminum adapter

bushings with stainless steel bushings on any snubbus removed for

other reasons (testing, bent piston rods, etc). At this time

approximately 8% of the safety-related snubbers have stainless

steel bushings. The inspectors discussed the extent of the

cracking problem and what actions were being taken to correct the

problem with licensee representatives. The licensee stated they

were unable at this time to classify the cracked aluminum bushings

as a generic problem based on the failure rate being less than 1%

for the total number of visual examinaticns performed on the

aluminum bushings.

In addition, an ongoing failure analysis study

of the cracked bushings indicated the failures do not appear to be

thermal or fatigue induced or a casting problem. The licensee is

presently conducting a special surveillance inspection of all

accessible snubbers outside of the reactor building that will

include vibration measurements as a possible aid in the failure

analysis study.

If this inspection does not indicate exceptional

cracking problems then the licensee will continue with their

original plans for replacing approximately 25% of the snubbers in

the reactor building during the refueling outage, scheduled to

begin September 27, 1981, with snubbers having stainless steel

bu shings.

If exceptional cracking is evident the replacement

amounts will be re-evaluated. The inspectors are closely

monitoring this issue and concur with the licensee's action at

this time.

Inspector Followup Item (302/81-15-06):

Review licensee's action

regarding cracked aluminum adapter bushing on hydraulic snubbers.

_

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14

(3.) NCOR 81-299 reported that core quadrant power tilt exceeded the

Technical Specification (TS) steady-state value for the Incore

Instrumentation following a power reduction.

The out of core

instrumentation did not indicate evidence of an incore tilt.

The

inspector's investigation of this event revealed that the licensee

had just completed the incore instrumentation check portion of

surveillance procedure SP-140, In-core Neutron Detector System

Calibration, but that the procedure did not direct the instrument

technicians to substitute a zero value into the plant computer for

any failed detectors. As a result the computer utilized the

failed detector values in the incore tilt calculation, thus giving

an erroneous incore tilt. When zeros were substituted for the

failed detectors, the incore tilt returned to a value consistent

with the out of core detectors. The inspector verified that the

number of failed detectors did not exceed TS required number for

operability. The licensee will revise SP-140 to direct instrument

technicians to substitute a zero in the plant computer for each

failed detector.

Inspector Followup Item (302/81-15-07): Verify revision to SP-140

to require substitution of zeros into the plant computer for

failed incore detectors.

(4.) NCOR 81-300 reported that a procedure was not available to reduce

the Reactor Protection System (RPS) nuclear overpower trip

setpoints that are based on reactor coolant system flow and axial

power imbalance. The licensee is revising calibration procedure

SP-113 Power Range Nuclear Instrumentation calibration, to provide

for these setpoint reductions.

Inspector Followup Item (302/81-15-08):

Review the revision to

SP-113 that will include a setpoint reduction procedure for

nuclear overpower trip.

7.

Review of IE Bulletins and Circulars

The following IE Bulletins (IEB) and Circulars (IEC) were reviewed to verify

adequacy of the licensee's actions:

a.

IEB 80-03

Loss of Charcoal from Standard Type II, 2 Inch Tray

Absorber Cells

b.

IEB 80-09

Hydramotor Actuator Deficiencies

c.

IEB 81-12

Decay Heat Removal System Operability

d.

IEB 80-18

Maintenance of Adequate Minimum Flow Thru Centrifugal

Charging Pumps Following Secondary Side High Energy Line

Rupture

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_ _ _ _

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15

e.

IEB 80-24

Prevention of Damage Due to Water Leakage Inside

Containment (October 17, 1980 Indian Point 2 Event)

f.

IEC 79-13

Replacement of Diesel Fire Pump Starting Contactors

g.

IEC 79-20

Failure of GTE Sylvania Relay, Type PM Bulletin 7305,

Catalog 3U12-11-AC with a 120V AC Coil

The GTE Relays identified in this Circular are similar

to the Clark P!1 Relays utilized at this facility (Clark

relays are now manufactured by Sylvania).

The licensee

has identified a " burring" problem on the shaft of

these relays that was reported to the NRC in Licensee

Event Report (LER) 81-14, that interferes with relay

operation. The licensee's actions in this regard are

being tracked in accordance with Inspector Followup

Item (302/81-05-12) (See paragraph 2 of this report).

h.

IEC 79-22

Stroke Times for Power Operated Relief Valves

i.

IEC 79-23

Motor Starters and Contactors Failed to Operate

j.

IEC 80-04

Securing of Threaded Lockfsg Devices on Safety-Related

Equipment

The inspectors review of the licensee's action ca this

circular indicates that the licensee intends to add

caution statements into various Preventive thintenance

Procedures (PM's) and flaintenance Procedures (MP's).

These additinns will be made, as applicable, when the

procedures come up for periodic review.

Since this

periodic review cycle occurs over a two year period, it

is conceivable that these procedure changes would not be

completed until 1983.

The inspector discussed this issue with licensee

representatives and stated that the two year cycle

appeared inadequate to assure that such events do not

l

occur at this facility especially since the facility is

about to enter an extensive refuel outage on

September 27.

Licensee representatives acknowledged the

inspectors' remarks and are reviewing the status of this

review.

This circular remains open.

k.

IEC 80-14

Radioactive Contamination of Plant Demineralized Water

Systen and Resultant Internal Contamination of Personnel

With the exception of IEC 80-04, which remains, open, no additional

inadequacies were identified and the licensee's actions on these Bulletins

and Circulars are considered to be complete.

. . . . .

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8.

Implementation of Three Mile Island (TMI) Action Plan Items

,

The NRC is requiring licensees to implement certain items tqa L were-

determined to improve plant safety as a result of the lessen learned from

the TMI accident that occurred on thrch 28, 1479.

These Task AcEion Plib '

(TAP) items were delineated in NUREG 0585, 0660, and 0137.1 in,variods

~"

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,

correspondence between Nuclear Reactor Regulation (HRR) and tne licensees,

'

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and in various Inspection and Enforcement (IE) 3uiletins and Circulars.

'

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/

The following TAP's were reviewed:

<-

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a.

II.F.1. (1A) Accident Monitoring

.

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NRC Inspection Report 50-302/80-25, paragraphs 12c, d, and 3 discusses

'

a status of review of NUREG 0578 pa, agrap),2.1.8. items.

At the time

'

r

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of the report (June,1980), the inspectors noted in paragraph 12c that

,

the licensee was in process of. installins 3 main steam line (MSL)

~

radiation monitoring system and that the Mystem would be canpleted by

4

the licensee's cannitment date of January 1,1981.

In addition, in a

Florida Power Corporation (FPC) letter to Mr. Rober W. Reid of Nuclear

.

)

Reactor Regulation (NRR) dated April 20, 1980, the licensae stated that

1

MSL monitors would be installed to monitor each of the two steam

genera tors .

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.

The inspector reviewed Modification Approval Records (HAL)~30-5-78,A,

s

B, and C that were developed to install (MAR 80-5-78 A.and B) and cest

~

(MAR 80-5-78c) the MSL monitors.

In addition, the inspeciars have _,

,,

examined the installed monitors to verify installation und operability.

'

_

Two MSL Monitors have bain installed and they monitor t00' of the four

MSLs. The installation is arranged juch that monitorirs or each steam

s

generator is provided.

The licensee will install two atsef MSL

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monitors on the remaining MSLs during the upcaning refuel catage

'

scheduled to begin September 27.

,

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During the inspectors review of MAR' 80-5-78c that provided a functional

,-

,

test of the MSL monitors, it was noted that a temporary change was made

to the test procedure and that the data sheet was incorrectly

-

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comple ted.

The inspector questioned licensee representa6ives about

,

these discrepancies and also questioned, based upon review of this test

procedure, whether the MSL monitors were operational.

s

Licensee representatives investigated these descrepancies and

determined that an apparent unauthorized change was made t'o :he ucta

j

sheet and concurred with the inspector's findtog that the test'was

performed incorrectly. The licensee provideJ additional documentation

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to the inspector to demonstrate that-the instrumentation had beek

properly tested and therefore was considered to be operational. Th'e

inspector reviewed this additional. data and concurred with the

licensee's conclusions.

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Ba cd on"theke reviews, it appears the licensee has met their

5.nnitment with respect to the installation and operability of the itSL

menitors. The' licensee has not, however, complied with the require-

"

ments' of their own procedure CP-114, Procedure for Preparation of

Pemonedt and Temporary liodifications, with regard to making !!AR

_

chsges in the field and to verify the fiAR is properly accomplished.

The .br ukdown in the MAR system is considered to be a violation. This

violation >is another example of the tiAR system violation that is

discussed in paragraph 5.b(11)6 of this report.

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b.

I. A.2.1(4) Irme(iath Upgrading of Reactor Operator and Senior Reactor

Operator Training and Qualifications

,,_

Reactot Operato'- (RO) and Senior Reactor Operator (SRO) training

^

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rograir.s and qualification requirements have been upgraded to meet the

aew req;irements of TAP 1. A.2.1, Enclosures 1 and 2 as presently

-

,.

implemen ted. To verify this upgrading the inspector discussed program

and qu6lification upgrading with licensee representatives and reviewed

~ the following documentation:

,

,

-Resumes and qualification records of three licensed reactor operators

. that are in training for upgrading to senior reactor operator

,

,

Sicenses;

,

-Attendade sheets for the requalification program to verify attendance

by-training instructors; and,

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-Syllabuses for the SR0 training program and licensed operator

requalification program to verify that the program included training

in heat transfer, fluid flow, and thermodynamics.

,

Based upon thir review, the licensee's program appears to be consistent

with their short range commitments to the flRC. The inspectors have

,

,

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no further questions on this item at this time.

c.

II.B.(2A Training for Mitigating Core Damage

"

g

The, licensee 4eveloped a training program for mitigating core damage on

j.

January 1,1931 and comnenced the training program in April,1981.

Tnese dates are consistent with the commitments made to fiuclear Reactor

.

.

Regulation (NRR) on December 15, 1980. As of August 12, 1981, the

'

licensee has completed training 23 of the 37 licensed operators and all

_

of the hot licensed training class. The licensee has not yet commenced

training of managers and technicians in the Instrumentation and Control

_

and Chem / Rad departments. All this training is expected to be

completed by October 1,1981.

~

The inspector reviewed the syllabus in use by the licensee to

(

_ accomplish this training.

The syllabus was developed for the licensee

"

by the reactor Nen%r (Babcock and Wilcox) and includes all the

requirements ouilned in TAP 1.A.2.1, Enclosure 3.

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_ - - _ _ _ _ _ _ _ _

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Based upon this review, the licensee's progress is consistent with the

n-

commitments to the NRC. Completion of this training- remains to be

. verified and is considered to be an inspector followup item.

. Inspector Followup Item (302/81-15-09): Verify completion of training

for citigating core damage to licensed' operators and nonlicensed

nanagers and technicians.

9.

Plant Modification Review

The insheter reviewed two potential enforcement findings that were

l.

identified during the Management Appraisal inspection conducted in February,

'

1981 thatjconcerned modification 'and design changes.

_

a.

Modtf'ication Approval Record (MAR) 80-02-72B required pipe support

EFH-64 to be modified in accordance with GAI drawing 32064. This

x

' drawing' required the installation of a 12"' square baseplate

perpendicular to the pipe run and a 12" x 19" baseplate in line with-

the pipe.

Drawing 32064 required bolt to bolt spacing of 8" for

baseplate "D".

It also required installation of grout under the

!~

basepla tes.

Installation. records for pipe support EFH-64 showed that the baseplates

3"

were reversed. The records also showed that minimum bolt spacing for

~

baseplate "D" was 7 3/8 inches. The baseplates were grouted without a

"

,

j

written procedure for grouting.- There was no record of an engineering

evaluation and' acceptance of these conditions.

'

'

Failure to accomplish plant modifications in accordance to procedures,

instructions, and drawings is' contrary to the requirements of 10 CFR

'

.50, Appendix B, Criterion V and the requirements-of procedure CP-114,

Procedure for Preparation of Permanent and Temporary Modifications, and

is considered to be a violation.

This violation is another example of the MAR system violation that is

discussed =in paragraph 5.b.11.b of this report.

b.

' MARS 79-5-62 and 79-5-62A contained a modification safety evaluation

"

that was prepared by the Nuclear Operations Engineering Department

"

(N0E) Jnd approved by the Nuclear Technical Specification Coordinator.

%

The modification involved removal and plugging of one or seven

Emergency Feedwater (EF) system pipe runs between each EF system and

O

each Steam Generator. The modification safety evaluation indicated

that Babcock and Wilcox (B&W) had advised N0E that " sufficient EF can

i

be" injected through 6 nozzles (rather than old 7)."

No written

confirmation from B&W was available. No documented N0E verification of

+

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.

this was available.

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19

In addition, MAR 79-5-62 shows that the EF system piping to both steam

generators was modified on' July 15, 1980, but a safety evaluation of

the effect of this system configuration change on the seismic analysis

of the system had not been done.

10 CFR 50.59 requires that the holder of a license authorizing

operation of a production or utilization facility may make changes in

the facility as described in the safety analysis report without prior

comission approval unless the proposed change involves an unreviewed

safety question. FSAR Figure 4-5 shows seven auxiliary feedwater lines

to each steam generator.

FSAR paragraph 10.2.1.2 describes the

emergency feedwater head requirements.

FSAR paragraph 10.2.1.2 also

indicates that emergency feedwater piping is designated to seismic

category 1.

Failure to perform safety evaluations of facility changes is contrary

to the requirements of 10 CFR ~50.59 and is considered to be a

violation.

Violation (302/81-15-10): Failure to comply with the requirements of

10 CFR 50.59 safety evaluations for plant modifications.

A similar violation of 10 CFR 50.59 with respect to, safety evaluation

of plant modifications was identified during the inspection period of

February 12-16,1979 (NRC Report 50-302/79-04) and therefore, this

violation is considered to be recurrent and' uncorrected.

10.

Reactor Coolant System Leakrate Verification

The NRC has recently developed a computer program which is used with the

Hewlett Packard (HP) 41C system for verification of Reactor' Coolant System

(RCS) leakrates calculated by licensees. The program has been developed to

perfonn leakrate calculations .for the three general types of pressurized

water reactors.

Before the program can be used at a specific facility the

inspector must prepare a set of magnetic data cards containing the " plant

specific" data for the facility. Using these cards, along with the general-

program, the inspector now has a " custom" program 'for the facility, in this

case Crystal River Unit 3.

The inspector can now verify RCS leakrates

accurately in a matter of minutes.

On August 12, 1981, the licensee performed a RCS leakrate calculation in

accordance with Surveillance Procedure, (SP)-317, RCS Water inventory

balance. The procedure was comenced at 0900 and was completed at 1300 (4

hrs.). The inspector observed the plant instrumentation and independently

verified the final results using the NRC calculator, and compared these

results with the licensee's final data computed in accordance with SP-317.

The licensee's final results were withir plus or minus .2 gpm of the NRC

calcu'lator results.

.

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20

Test Results

SP-317

NRCCalculator

Gross (gpa)

.706

.70

Identified (gpm)

.527

.53

Unidentified (gpm)

.178

.18

Based on .these results, it appears that the licensee's leakrate calculation

procedure, SP-317 is providing adequate results. The inspectors have no

further questions on this item at this time.

11.

Procurement

The inspector reviewed the licensee's procedures for procurement, storage,

and handling of Quality Materials.

Areas examined included:

(1) Qualified

personnel receiving safety-related items, (2) storage and packaging

requirements, (3) preventive maintenance, and (4) identification (trace-

ability).

The inspector witnessed a stores receipt examination of Quality Materials

performed by the licensee. The licensee conducted the examination in

accordance with their Quality Operating ilanual Proceudres. The licensee's

" hold compound" was also toured by the inspector and found to be satis-

factory.

Parts and materials were appropriately identified with release,

hold and discrepancy tags.

Records for two safety-related items (Quality 11aterial) were chosed at

random by the inspector to verify traceability.

Records inspected included:

(1) Purchase Order, (2) Receipt Record,

(3) Issue Record, and (4)

Certification Record. The locations of the items in storage were also

verified.

During this review the inspector noted a problem with a Production Quality

itaterial Issue document (QCI 21867) for material purchased under Purchase

Order No F10515Q.

On flay 8,1981, the QCI was signed for issuance, however it was not signed

for receipt (i.e., the material picked up by a mechanic for use in the

field) until June 1,1981. Therefore, the time difference between the issue

signature and receipt signature was almost three weeks.

During this three

week period, on May 12, a Quality Programs Department (QPD) audit was

conducted.

The audit selected P0 tio. F10515Q for review and detemined that

there was a discrepancy in the certification records supplied by the

material's vendor. The item was immediately removed from stores and the

certification proMem was corrected. The item was then received by the

Field on June 1.

The issued QCI 21867 did not reflect the removal and

replacement of the material from stores for the certification problem.

. _ _ _ - _ _ _ _ _ _ _ .

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21

The record keeping involved with this event gave the impression that

uncertified material was released to the field.

Though this did not happen,

the possibility of this occurring is enhanced by allowing an exceptional

time delay between signing a QCI for issuance and signing the QCI for

receipt. The inspector reviewed approximately fifty additional QCI's and

noted that the maximum time period between issuance and receiving of

material was approximately one day.

The licensee will revise Quality Control llanual procedure QOP 7.0, Issue and

Return of Quality Material, to specify that QCI's will not be signed for

issuance until they are ready for receipt.

Inspector Followup Item (302/81-15-11):

Revu the licensee's actions to

revise Q0P 7.0 to specify a time limit between issuance and receipt of a

QCI.

12.

Nonroutine Event

At 0730 on July 31, the reactor tripped from full power due to high reactor

coolant system (RCS) pressure.

The high RCS pressure was caused by an

increase in RCS temperature which resulted when the "B" liain Feedwater (MFW)

Pump tripped. Upon loss of B !!FM pump, the Intergrated Control System (ICS)

began a plant runback, however the runback was not fast enough to prevent

the reactor trip.

Preliminary investigation of this trip indicated that the B fiFW pump tripped

when it lost its pump control speed signal.

The signal was lost when an

instrument technician inadvertently opened a circuit breaker supplying speed

signal power. The technician had intended to open an adjacent circuit

breaker, however due to the close proximity of the two breakers, the speed

signal breaker was opened instead.

A normal plant shutdown to Mode 3 (Hot Standby) occurred. by 1040 the

reactor was again made critical and by 1321 the plant returned to 11 ode 1

(Power Operation).

The resident inspector arrived in the control room soon after the plant trip

and observed the plant shutdown.

The inspector reviewed this event and

noted that the circuit breakers involved were clearly marked.

Thus it

appears that the event was strictly the result of operator error. The

inspectors have no further question on this event at this time an will

review the licensee's post trip report.

Inspector Followup Item (302/81-15-12):

Review the lessons' learned post

trip report for the July 31 reactor trip.

. . . _ .