05000335/LER-1982-067-03, /03L-0:on 821225,redundant 120-volt Ac Instrument Power Bus Lost When Output Breaker of Static Inverter 1A Opened,Causing Loss of Reactor Protection & ESF Channel. Caused by Defective Output Frequency Module.Module Adjusted

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/03L-0:on 821225,redundant 120-volt Ac Instrument Power Bus Lost When Output Breaker of Static Inverter 1A Opened,Causing Loss of Reactor Protection & ESF Channel. Caused by Defective Output Frequency Module.Module Adjusted
ML20028E129
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 01/12/1983
From: Rotella T
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028E128 List:
References
LER-82-067-03L, LER-82-67-3L, NUDOCS 8301210012
Download: ML20028E129 (1)


LER-1982-067, /03L-0:on 821225,redundant 120-volt Ac Instrument Power Bus Lost When Output Breaker of Static Inverter 1A Opened,Causing Loss of Reactor Protection & ESF Channel. Caused by Defective Output Frequency Module.Module Adjusted
Event date:
Report date:
3351982067R03 - NRC Website

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