LER-1982-033, /03L-0:on 821005,1A2 Battery Cell 12 Dropped Below Tech Spec Limits,Resulting in Battery a Failure to Pass Discharge Test.Caused by Battery Age & Repetitive Discharge Testing.New 24/48-volt Dc Battery Will Be Installed |
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NAC FORM 384
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U. S. NUCLE A0 REIULATCCY COMMISSION 87 77)
LICENSEE EVENT REPORT CONTROL BLOCK:
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8 60 61 OOCKETNUM8ER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES O'O 10121 l On October 5, 1982, the Unit One 24/48 VDC "A" Battery Test Discharge, QTS 120-2, wasl gl pe r fo rmed. The I A2 battery cell number 12 dropped to.13 VDC(1.75 VDC required l
o 4 l minimum) between six and seven hours into the eight hour test.
This dropped the "A" l
IO isi l ' battery voltage below the required 21 volts at 10 emps and therefore, the "A"
l battery failed to pass the discharge test as required by Technical Specification l 016 i I 4.9.B.3.
The "A" battery could have provided eiriht hours of power at actual load I
conditions (5.5 amps),
in addition, the "lB" 24/48 volt battery was found l0l7ll operable and would have provided power for the other redundant half of the l
24/4G VDC instrumentation.
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' OCCURRENCE REPORT REVISION LE R, RO EVENT YEAR REPORT NO.
CODE TYPE No.
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33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1 10ll The pross failure of cell 12 of the IA2 24/48 VDC volt battery caused the "A"
1 L.'_L'_J l battery to fail its discharae test.
This failure has been attributed to batterv I
, 2 I age and repetitive discharge testing.
A new "A" 24/48 VDC will be Installed prior l
l i 3 5-l l to Unit One startup.
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% POWER OTHER STATUS DISS O RY DISCOVERY DESCRIPTION y l Hl@ l 0 l 0 l 0 l@l NA l
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A TIVITY CO TENT
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KELEASED OF RELEASE AMOUNT OF ACTivlTY LOCATION OF RELEASE
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DESCRIPTION
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7 8 9 11 12 80 LOSS OF OR DAVAGE TO FACILITY TYPE
DESCRIPTION
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PuBLETY 8211080172 821027 iSSuEo@OESCRiPTiON h NRC USE ONLY PDR ADOCK 05000254 j
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PDR 2 O 68 69 30 5 eM lB NAME OF PREPARER PHONE:
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LER NUMBER: LER/R0 82-33/03L-0 11.
LICENSEE NAME: Commonwealth Edison Company.
Quad-Cities Nuclear Power Station Ill.
FACILITY NAME:
Unit One IV.
DOCKET NUMBER: 050-254.
V.
EVENT DESCRIPTION
On October 5,1982, QTS 120-2, Quad-Cities ' unit one 24/48 VDC "A" Battery Test Discharge was being performed.
Technical Specification j
4.B.3 requires that the 24 VDC battery be discharged at ~ a manufacturer's amp-hour rated capacity of ten amperes for eight hours (80 amp hours).
This test criteria is specified in IEEE Standard 450-1975 At some interval between the sixth and seventh hour of the discharge test, the Unit One IA2-24 VDC battery terminal voltage dropped below the minimum-specified battery voltage of 21 volts, as per IEEE 450-1975 Cell 12 voltage of the IA2 battery fell below the minimum specified cell voltage (1.75 VDC) to 0 31 VDC, which indicated cell replacement was necessary. The estimated minimum capacity of the I A2-24 VDC battery
~
at a 10 ampere discharge. rate was 75 percent of the manufacturer's specification.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
Load trend -review on the I A2-24 VDC -battery indicates that operating load on the battery would be approximately 5 5 amperes.
Had the need arisen, the IA2 battery would have performed its function as required, and, maintained operation for the minimum of eight hours required.
In addition, the "1B" 24/48 VDC battery was found to be completely operable and would have provided power for the other half of the
- - requi red 24/48 VDC instrumentation.
Unit One was in the REFUEL mode and in Cold Shutdown.
The fuel had been completely removed from the vessel, therefore, the battery was
[
not require'd to be operable at the time of the test.
Vll.
CAUSE
j The direct cause of this event is gross failure of cell 12.in the IA2-24 VDC battery.
The other 11 cells were still well above the 1.75 VDC minimum cell voltage.
Failure of the cell has been attributed to the near end-of service life of the 24/48 VDC battery and repetitive dis-charge testing of-the battery.
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CORRECYlVE ACTION:
Due to the failure of the 2A2-24 VDC battery (DR 4-2-81-53) in. January, 1981, the 24/48 VDC batteries were evaluated.
It was decided to replace all of the 24/48 VDC batteries. The lA and IB 24/48 VDC batteries are scheduled to be replaced before the end of this refueling outage.
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| 05000254/LER-1982-001-03, /03L-0:on 820113,during Routine Calibr of ECCS Level Switches,Switch LIS-1-263-72A Was Damaged.Caused by Instrument Personnel Not Being Familiar W/Tech Spec Requirements for Switches.Switch Repaired | /03L-0:on 820113,during Routine Calibr of ECCS Level Switches,Switch LIS-1-263-72A Was Damaged.Caused by Instrument Personnel Not Being Familiar W/Tech Spec Requirements for Switches.Switch Repaired | | | 05000254/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000265/LER-1982-001, Forwards LER 82-001/01T-0 | Forwards LER 82-001/01T-0 | | | 05000265/LER-1982-001-01, /01T-0:on 820115,during Drywell Entry,Small Leak Discovered on Reactor Water Cleanup Sys Suction Line Between Inboard Isolation Valve & Drywell Penetration.Stress Corrosion Cracking Postulated as Cause | /01T-0:on 820115,during Drywell Entry,Small Leak Discovered on Reactor Water Cleanup Sys Suction Line Between Inboard Isolation Valve & Drywell Penetration.Stress Corrosion Cracking Postulated as Cause | | | 05000254/LER-1982-002-03, /03L-0:on 820202,after Completion of 1/2 Emergency Diesel Generator Monthly Preventive maint,failure-to-start Alarm Sounded When Diesel Was Started.Caused by Bent Insulator Card Next to Engine Starting & Control Relay | /03L-0:on 820202,after Completion of 1/2 Emergency Diesel Generator Monthly Preventive maint,failure-to-start Alarm Sounded When Diesel Was Started.Caused by Bent Insulator Card Next to Engine Starting & Control Relay | | | 05000254/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000265/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000265/LER-1982-002-03, /03L-0:on 820126,main Steam Line Low Pressure Switch PS-2-261-30D Found to Trip at 794 Psig.Caused by Instrument Drift.Switch Recalibr | /03L-0:on 820126,main Steam Line Low Pressure Switch PS-2-261-30D Found to Trip at 794 Psig.Caused by Instrument Drift.Switch Recalibr | | | 05000265/LER-1982-003-03, /03L-0:on 820224,differential Pressure Switch DPIS 2-1360-1B+ Failed to Operate.Caused by Instrument Drift.Switch Recalibr & Tested Satisfactorily | /03L-0:on 820224,differential Pressure Switch DPIS 2-1360-1B+ Failed to Operate.Caused by Instrument Drift.Switch Recalibr & Tested Satisfactorily | | | 05000265/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000265/LER-1982-003-01, /01T-0:on 820223,while Performing Reactor Vessel Hydrostatic Pressure Test,Leak Found in Control Rod Drive. Cause Undetermined.Fillet Weld Made Around Withdrawal Line at Point of Entry to Flange & CRD Returned to Svc | /01T-0:on 820223,while Performing Reactor Vessel Hydrostatic Pressure Test,Leak Found in Control Rod Drive. Cause Undetermined.Fillet Weld Made Around Withdrawal Line at Point of Entry to Flange & CRD Returned to Svc | | | 05000254/LER-1982-003-03, /03L-0:on 820205,comparison of Control Room & Local Sightglass Indications of Suppression Pool Level Disparity of 0.5 Inch.Actual Level as Indicated by Sightglass Was Below Tech Specs | /03L-0:on 820205,comparison of Control Room & Local Sightglass Indications of Suppression Pool Level Disparity of 0.5 Inch.Actual Level as Indicated by Sightglass Was Below Tech Specs | | | 05000254/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000254/LER-1982-004-03, /03L-0:on 820307,reactor Core Isolation Cooling Steam Line Was Isolated When High Steam Line Differential Pressure Alarm Received.Caused by Instrument Drift of Pressure Switch DPIS-1-1360-1A.Switch Recalibr | /03L-0:on 820307,reactor Core Isolation Cooling Steam Line Was Isolated When High Steam Line Differential Pressure Alarm Received.Caused by Instrument Drift of Pressure Switch DPIS-1-1360-1A.Switch Recalibr | | | 05000265/LER-1982-004, Forwards LER 82-004/03L-0.Detailed Event Analysis Encl | Forwards LER 82-004/03L-0.Detailed Event Analysis Encl | | | 05000254/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | | 05000265/LER-1982-004-03, /03L-0:on 820224,while Performing Quarterly Reactor Core Isolation Cooling Steam Line High Flow Calibr & Functional Test,Differential Pressure Switch Qis 18,DPIS 2-1360-1B+ Failed to Operate.Caused by Instrument Drift | /03L-0:on 820224,while Performing Quarterly Reactor Core Isolation Cooling Steam Line High Flow Calibr & Functional Test,Differential Pressure Switch Qis 18,DPIS 2-1360-1B+ Failed to Operate.Caused by Instrument Drift | | | 05000265/LER-1982-005-03, /03L-0:on 820420,while Performing QIS-6,pressure Switch PS-2-1001-88D Found to Trip Above Tech Spec Limit. Caused by Instrument Setpoint Drift.Pressure Switch Recalibr & Functionally Tested | /03L-0:on 820420,while Performing QIS-6,pressure Switch PS-2-1001-88D Found to Trip Above Tech Spec Limit. Caused by Instrument Setpoint Drift.Pressure Switch Recalibr & Functionally Tested | | | 05000265/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000254/LER-1982-005-03, /03L-0:on 820325,reactor Core Isolation Cooling Sys Failed to Operate During Monthly Test Qos 1300-2.Caused by Ground in Logic Circuit Initiating Low Voltage at Electrical Overspeed Trip Sensor | /03L-0:on 820325,reactor Core Isolation Cooling Sys Failed to Operate During Monthly Test Qos 1300-2.Caused by Ground in Logic Circuit Initiating Low Voltage at Electrical Overspeed Trip Sensor | | | 05000254/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000265/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000254/LER-1982-006-03, /03L-0:on 820412,pressure Switch PS-1-1001-89B Found Inoperable.Caused by Instrument Setpoint Drift of O Ring PS-1-1001-89B.Pressure Switch Recalibr & Functionally Tested | /03L-0:on 820412,pressure Switch PS-1-1001-89B Found Inoperable.Caused by Instrument Setpoint Drift of O Ring PS-1-1001-89B.Pressure Switch Recalibr & Functionally Tested | | | 05000254/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000265/LER-1982-006-03, /03L-0:on 820514,during Monthly Testing of Suppression Chamber to Drywell Vacuum Breakers,Valve AO-2-1601-32C Opened But Failed to Close.Caused by Improperly Positioned Counterweight | /03L-0:on 820514,during Monthly Testing of Suppression Chamber to Drywell Vacuum Breakers,Valve AO-2-1601-32C Opened But Failed to Close.Caused by Improperly Positioned Counterweight | | | 05000254/LER-1982-007-03, /03L-0:on 820415,during Surveillance Test Qos 1000-2,D Residual Heat Removal Svc Water Booster Pump Outboard Bearing Failed & Pump Declared Inoperable.Caused by Leakage from Adjacent Packing.Bearing & Packing Replaced | /03L-0:on 820415,during Surveillance Test Qos 1000-2,D Residual Heat Removal Svc Water Booster Pump Outboard Bearing Failed & Pump Declared Inoperable.Caused by Leakage from Adjacent Packing.Bearing & Packing Replaced | | | 05000254/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000265/LER-1982-008, Forwards LER 82-008/03L-0 | Forwards LER 82-008/03L-0 | | | 05000254/LER-1982-008, Forwards LER 82-008/03L-0 | Forwards LER 82-008/03L-0 | | | 05000254/LER-1982-008-03, /03L-0:on 820420,negative Flow Switch DPIS-1-1360-1A Failed.Caused by Damage During Reassembly by Mechanic to Positive Switch Indicating Needle,Thus Preventing Mechanical Trip of Negative Switch | /03L-0:on 820420,negative Flow Switch DPIS-1-1360-1A Failed.Caused by Damage During Reassembly by Mechanic to Positive Switch Indicating Needle,Thus Preventing Mechanical Trip of Negative Switch | | | 05000265/LER-1982-008-03, /03L-0:on 820515,during Maint Outage,Acoustic Monitors for Electromatic Relief Valves 2-203-3A,3B & 3C Failed to Give Open Indication When Valves Were Opened & Thermocouple Type Position Sensor 2-203-3B Was Out of Svc | /03L-0:on 820515,during Maint Outage,Acoustic Monitors for Electromatic Relief Valves 2-203-3A,3B & 3C Failed to Give Open Indication When Valves Were Opened & Thermocouple Type Position Sensor 2-203-3B Was Out of Svc | | | 05000254/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000254/LER-1982-009-03, /03L-0:on 820430,significant Amount of Water Found in Bearing Oil Reservoir of 1-1001-65C RHR Sys Svc Water Pump.Caused by Leaking Seal Packing,Due to Normal Packing Wear.Reservoir Changed & Seals Repacked | /03L-0:on 820430,significant Amount of Water Found in Bearing Oil Reservoir of 1-1001-65C RHR Sys Svc Water Pump.Caused by Leaking Seal Packing,Due to Normal Packing Wear.Reservoir Changed & Seals Repacked | | | 05000265/LER-1982-010-03, /03L-0:on 820624,motor Operated Valve MO-2301-8 Would Not Open When Given Open Signal During HPCI Sys Valve Inoperability Surveillance,Qos 2300-3,rendering HPCI Inoperable.Caused by Broken Arm in Open Torque Switch | /03L-0:on 820624,motor Operated Valve MO-2301-8 Would Not Open When Given Open Signal During HPCI Sys Valve Inoperability Surveillance,Qos 2300-3,rendering HPCI Inoperable.Caused by Broken Arm in Open Torque Switch | | | 05000265/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000254/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000254/LER-1982-010-03, /03L-0:on 820519,while Performing Cooling Water Pump Flow Rate Test Quarterly Surveillance Emergency Diesel Generator Cooling Water Pump 1/2 Overheated.Caused by Failed Motor Bearing,Due to Improper Oil Level | /03L-0:on 820519,while Performing Cooling Water Pump Flow Rate Test Quarterly Surveillance Emergency Diesel Generator Cooling Water Pump 1/2 Overheated.Caused by Failed Motor Bearing,Due to Improper Oil Level | | | 05000265/LER-1982-011-01, /01T-0:on 820715,LPCI Inboard Injection Valve MO-2-1001-29B Failed to Open.Caused by Detached Electrical Lead on Torque Switch of Valve Motor Operator.Inboard Valve Manually Opened & Torque Switch Replaced | /01T-0:on 820715,LPCI Inboard Injection Valve MO-2-1001-29B Failed to Open.Caused by Detached Electrical Lead on Torque Switch of Valve Motor Operator.Inboard Valve Manually Opened & Torque Switch Replaced | | | 05000265/LER-1982-011, Forwards LER 82-011/01T-0 | Forwards LER 82-011/01T-0 | | | 05000254/LER-1982-012-01, /01T-0:on 820622,following Scram on Unit 2,1/2 Diesel Generator Tripped When a RHR Svc Water Pump Started. Caused by Underexcitation of Diesel Relays.Relays Removed Pending Design Change | /01T-0:on 820622,following Scram on Unit 2,1/2 Diesel Generator Tripped When a RHR Svc Water Pump Started. Caused by Underexcitation of Diesel Relays.Relays Removed Pending Design Change | | | 05000254/LER-1982-012, Forwards LER 82-012/01T-0 | Forwards LER 82-012/01T-0 | | | 05000265/LER-1982-012-03, /03L-0:on 820714,controllers for Valves 2-203-3A, 3B,3C & 3E Found to Trip at Pressures in Excess of Specified Tech Spec Limits.Caused by Improper Calibr of Pressure Switches | /03L-0:on 820714,controllers for Valves 2-203-3A, 3B,3C & 3E Found to Trip at Pressures in Excess of Specified Tech Spec Limits.Caused by Improper Calibr of Pressure Switches | | | 05000265/LER-1982-012, Forwards LER 82-012/03L-0 | Forwards LER 82-012/03L-0 | | | 05000254/LER-1982-013-03, /03L-0:on 820621,while Diesel Generator Cooling Water Pump Was Being Run in Conjunction W/Hpci Monthly Operability Surveillance,Qoc 2300-2 Pump Observed to Have No Flow by Local Indications.Caused by Pump Being Air Bound | /03L-0:on 820621,while Diesel Generator Cooling Water Pump Was Being Run in Conjunction W/Hpci Monthly Operability Surveillance,Qoc 2300-2 Pump Observed to Have No Flow by Local Indications.Caused by Pump Being Air Bound | | | 05000254/LER-1982-013, Forwards LER 82-013/03L-0 | Forwards LER 82-013/03L-0 | | | 05000265/LER-1982-014-03, /03L-0:on 820802,outboard Gland & Packing Nut Found Off & Lantern Ring & Packing Found Partially Out of 2-1001-65C RHR Sys Svc Water Main Pump.Cause Under Investigation.Pump Repacked on 820802 | /03L-0:on 820802,outboard Gland & Packing Nut Found Off & Lantern Ring & Packing Found Partially Out of 2-1001-65C RHR Sys Svc Water Main Pump.Cause Under Investigation.Pump Repacked on 820802 | | | 05000265/LER-1982-014, Forwards LER 82-014/03L-0 | Forwards LER 82-014/03L-0 | | | 05000254/LER-1982-014-03, /03L-0:on 820708,discharge Damper on Standby Gas Treatment Train B Failed to Open When Train auto-started. Caused by Failure of Auxiliary Contact on Motor Starter. Contact Replaced | /03L-0:on 820708,discharge Damper on Standby Gas Treatment Train B Failed to Open When Train auto-started. Caused by Failure of Auxiliary Contact on Motor Starter. Contact Replaced | | | 05000254/LER-1982-014, Forwards LER 82-014/03L-0 | Forwards LER 82-014/03L-0 | | | 05000265/LER-1982-015-03, /03L-0:on 820804,during Monthly Preventive Maint on Emergency Diesel Generator,Small Leak Found in Flexible Hose to Fuel Line Pressure Gauge.Caused by Crack in Hose. Hose Removed.Connection Sealed W/Threaded Plug | /03L-0:on 820804,during Monthly Preventive Maint on Emergency Diesel Generator,Small Leak Found in Flexible Hose to Fuel Line Pressure Gauge.Caused by Crack in Hose. Hose Removed.Connection Sealed W/Threaded Plug | |
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