ML20023D930

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IE Insp Repts 50-245/83-06 & 50-336/83-08 on 830227-0416. Noncompliance Noted:Failure to Maintain Reactor Power Below 89% While Monitoring Core Linear Heat Rate w/ex-core Detector Monitoring Sys
ML20023D930
Person / Time
Site: Millstone  
Issue date: 05/21/1983
From: Elsasser T, Lipinski D, Shedlosky J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20023D921 List:
References
50-245-83-06, 50-245-83-6, 50-336-83-08, 50-336-83-8, NUDOCS 8306060171
Download: ML20023D930 (19)


See also: IR 05000245/1983006

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U. S. NUCLEAR REGULATORY COMMISSION

Region I

t

50-245/83-06

Report No.

50-336/83-08

50-245

Docket No.

50-336

DPR-21

License No. DPR-65

Priority

Category

C


Licensee:

Northeast Nuclear Energy Company

P. O. Box 270

Hartford, Connecticut 06101

Facility Name: Millstone Nuclear Power Station, Units 1 & 2

Inspection at:

Waterford, Connecticut 06385

Inspection conducted:

February 27, 1983, thru April 16, 1983

Inspectors:

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J. T. Shedlosky, Sr. Resident Insp~ector

date signed

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D. R. Lipinski, Resident Inspector

date signed

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Approved by: -4

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T. C. EPrfsser, Chief

dat$tigh'ed

Reactor Projects Section 18,

Division of Project & Resident Programs

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Inspection Summary:

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Unit 1:

Routine facility safety inspections, February 27, 1983, thru April 16, 1983.

(Report Number 50-245/83-06) including:

evaluations of plant operations, equipment

alignments and readiness, radiation protection, physical security, fire protection,

plant operating records, maintenance and modification, surveillance testing and

calibrations, and reporting to the NRC. The inspection involved 146 hours0.00169 days <br />0.0406 hours <br />2.414021e-4 weeks <br />5.5553e-5 months <br /> of

onsite, regular, and backshift inspection effort by two resident inspectors.

Results: No' violations . identi fied.

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8306060171 830523

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PDR ADOCK 05000245

C

PDR

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Unit 2:

Routine facility safety inspections, February 27, 1983, thru April 16, 1983

(Report Number 50-336/83-08) including: evaluations of plant operations, equipment

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alignments and readiness, radiation protection, physical security, fire protection,

plant operating records, maintenance and modifications, surveillance testing and

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calibrations, ard reporting to the NRC. The inspection involved 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> of

onsite, regular, and backshift effort by two resident inspectors.

Results: One violation was identified - Failure to maintain reactor power below

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89% while monitoring in core linear heat rate with the Excore Detector Monitoring

System.

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DCS Identification Numbers

Inspection Report

50-245/83-06

50-336/83-08

DCS Number

Report Paragraph

50336-830301

3j

50245-830324

31

50245-830324

3m

50245-830331

3n

50245-830203

6

50245-830207

6

50245-830207

6

50245-830125

6

50245-830216

6

50245-830215'

6

50336-830302

6

50336-830127

6

50336-830219

6

50336-830218

6

50336-830219

6

50336-830318

6

50336-830319

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DETAILS

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1.

Persons Contacted

The below listed technical and supervisory level personnel were among those

contacted:

R. Asafaylo, Training Supervisor

J. Crockett, Unit 3 Superintendent

F. Dacimo, Quality Services Supervisor

J. Etheridge, Radioactive Materials Handling Supervisor

B. Granados, Health Physics Supervisor

D. Kross, Unit 2 Instrumentation and Control Supervisor

R. J. Herbert, Unit 1 Superintendent

J. Kangley, Radiological Services Supervisor

J. Keenan, Unit 2 Maintenance Supervisor

J. J. Kelley, Unit 2 Superintendent

E. J. Mroczka, Station Superintendent

V. Papadopoli, Quality Assurance Supervisor

R. Place, Unit 2 Engineering Supervisor

R. Palmieri, Unit 1 Engineering Supervisor

W. Romberg, Unit 1 Operations Supervisor

S. Scace, Unit 2 Operations Supervisor

F. Teeple, Unit 1 Instrumentation and Control Supervisor

W. Varney, Unit 1 Maintenance Supervisor

P. Weekley, Security Supervisor

2.

Status of Open Items

New Items:

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Unit 1

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None

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Unit 2

50-336/83-08-01

Violation: Failure to maintain reactor power below 89% as

required when monitoring fuel linear heat rate with the

Excore Detector Monitoring System.

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50-336/83-08-02

Open Item: Followup results of licensee study of poential

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methods of more positively identifying and alarming process

computer failures.

Old Items:

None reviewed.

3.

Review of Plant Operation - Plant Inspection (Units 1 and 2)

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The inspectors reviewed plant operations through direct inspection and obser-

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vation of Units 1 and 2 throughout the reporting period. Unit 1 operated at

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full power through the inspection period with the exception of a forced out-

age March 24 through 31 to correct high reactor coolant system leakage (in-

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cluding reactor trips on March 24 and 31). Unit 2 operated a full power

throughout the inspection period with the exception of a forced outage March

1 through 17 to correct high reactor coolant system leakage.

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a.

Instrumentation

Control room process instruments were observed for correlation between

channels and for confomance with Technical Specification requirements.

No unacceptable conditions were identified.

b.

Annunciators

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The inspector observed various alarm conditions which had been received

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and acknowledged. These conditions were discussed with shift personnel

who were knowledgeable of the alams and actions required.

During plant

inspections, the inspector observed the condition of equipment associated

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with various alanns.

No unacceptable conditions were identified.

c.

Shift Manning

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The operating shifts were observed to be staffed to meet the operating

requirements of Technical Specifications, Section 6, both to the number

and type of licenses.

Control room and shift manning was observed to

be in conformance with Technical Specifications and site administrative

procedures.

d.

Radiation Protection Controls

Radiation protection control areas were inspected. Radiation Work Permits

in use were reviewed and compliance with those documents as to protective

clothing and required monitoring instruments was inspected.

Proper posting

of radiation and high radiation areas was reviewed in addition to verifying

requirements for wearing of appropriate personal monitoring devices.

There were no unacceptable conditions identified.

e.

Plant Housekeeping Controls

Storage of material and components was observed with respect to

prevention of fire and safety hazards.

Plant housekeeping was evaluated

with respect to controlling the spread of surface and airborne contamina-

tion. There were no unacceptable conditions identified,

f.

Fire Protection / Prevention

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The inspector examined the condition of selected pieces of fire

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fighting equipment.

Combustible materials were being controlled and

were not found near vital areas.

Selected cable penetrations were

examined and fire barriers were found intact.

Cable trays were clear

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of debris. There were no unacceptable conditions identified.

g.

Control of Equipment

During plant inspection, selected equipment under safety tag control

was examined.

Equipment conditions were consistent with information

in plant control logs.

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Instrument Channels

Instrument channel checks recorded on routine logs were reviewed. An

independent comparison was made of selected instruments.

No unacceptable

conditions were identified.

1.

Equipment Lineups

The inspector examined the breaker position on switchgear and motor

control centers in accessible portions of the plant. Equipment

conditions, including valve lineups, were reviewed for conformance

with Technical Specifications and operating requirements. No unacceptable

conditions were identified.

J.

Forced Outage - March 1 Through 17 (Unit 2)

During the period of March 1 through 17, Unit 2 was in a forced

maintenance outage to correct Reactor Coolant System (RCS) leakage.

Total RCS leakage had risen irregularly during the operating cycle.

On March 1, 1983, the licensee determined that unidentified RCS

leakage exceeded Technical Specification 3.4.6.2 limit of 1.0 gallon

per minute (GPM).

The inspectors reviewed the licensee's actions and plar.t conditions

prior to, during and after the outage. This review focused in three

areas:

the measurement of total RCS leakage; the training and

control of workers in preparation for steam generator inspection and

maintenance, and the steam generator tube inspections.

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(1) Measurement of RCS Leakage

Technical Specification 3.4.6.2 establishes limits for RCS leakage

for 1.0 GPM unidentified leakage and 0.5 GPM primary-to-secondary

leakage through either steam generator. The Safety Analysis Bases

for these limits is to provide early detection of additional leakage,

which may be pressure boundary leakage, and to ensure that the dosage

contribution from tube leakage is limited to a small fraction of Part

100 limits in the event of a tube rupture or a steam line break.

Total RCS leak rate is calculated by an inventory mass balance in the

RCS, the Chemical Volume Control System and associated make-up and

waste tanks. This is normally calculated by the process computer

which, as part of the calculation, subtracts leakage collected by

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closed systems, such as the reactor coolant pump (RCP) controlled

seal flow subsystem. Technical Specification 1.14 allows for correcting

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for leakage into closed systems and leakage into the containment

atmosphere. That leakage must be from sources which are specifically

located; do not interfere with RCS leakage detection systems; are not

pressure boundary leakage and do not exceed 10.0 GPM. A quality

verification of the process computer calculations is performed using

a special engineering test procedure, T83-5, Revision 0, dated

February 4, 1983. During this test, potential leakage from the

Chemical Volume Control System is removed as is the uncertainty

associated with RCP seal flow.

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The inspectors have reviewed both methods of leak rate calculation.

There were no unacceptable conditions identified.

(a) RCS Leakage Prior to Shutdown

Prior to the plant shutdown on March 1,1983, leakage totaling

0.12 GPM had been identified from valve 2-SI-247, a safety

injection check valve, and from valve 2-RC-405, a power operated

relief valve blocking valve.

This leakage, into the containment

atmosphere, was first observed on March 9, 1982; had been

measured weekly by the licensee during the operating cycle and

was used to correct the total RCS leakage to determine the

unidentified RCS leakage.

A primary-to-secondary leak in the No. 1 Steam Generator, first

detected on March 10, 1982, was calculated at 0.29 GPM prior to

shutdown on March 1, 1983. This leakage was calculated using

radio-isotopic concentrations in the reactor coolant and steam

generator secondary water.

A reactor shutdown was begun at 1730, March 1, 1983 when total

and unidentified RCS leak rates were determined to be 1.77 GPM

and 1.34 GPM, respectively.

Because no other sources of leakage

were known, Operating License Amendment No. 82 was issued to

allow an additional 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> before the reactor was required to

be in Cold Shutduwn, Mode 5.

This allowed additional time for

inspection at operating temperature and pressure.

Inspections were conducted on March 2.

No additional sources of

RCS leakage were found; a plant cooldown was commenced at 1427,

March 2.

The reactor was placed in cold shutdown at 0908, March

3.

(b) Primary-to-Secondary Leakage No.1 Steam Generator

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An effort was made to corroborate the calculated primary-to-

secondary leak rate of the No. 1 Steam Generator.

During an

inspection, leakage from one tube was measured at 800 cc per

minute. Plant conditions established for this test were to fill

and presse<!ze the steam generator secondary to 200 psia and to

drain and vent the steam generator primary channel head.

This leakage collected corresponds to a primary-to-secondary

leak rate at operating conditions of between 0.39 and 0.68

GPM.

These valves are within the range of calculated leak

rates occuring when various assumptions are made for defect

size, shape and stability with pressure and temperature changes.

Primary-to-secondary leakage, therefore, exceeded the 0.5 GPM

limit of Technical Specification 3.4.6.2.c.

Because of this test and the inconsistency between the leak

rate calculated during operations (0.29 GPM) and that calculated

as the result of inspections (0.39 to 0.68 GPM) the NRC included

a more restrictive specification for primary-to-secondary

leakage in Operating License Amendment 83. The previous limit

of 0.5 GPM has been changed to 0.35 GPM through the end of the

present operating cycle.

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During this period the inspectors observed the licensee's

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testing program and performed independent calculations.

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Following repairs, total RCS leak rates have remained below

0.2 GPM and primary-to-secondary leakage has remained below

0.1 GPM. The licensee is investigating the inconsistency in

leak rate calculations. Although these calculations were

qualified by several outside organizations, there is no allowance

for interference caused by the sludge pile. Since the defect

location is at the top of the steam generator tube sheet, a form

of " hide-out" may occur as fission products migrate through the

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sludge pile, which is nine inches thick.

There were no additional unacceptable conditions identified.

The issue of leak rate calculations is being addressed with

the licensee by the NRC Division of Licensing.

(2) Worker Training and Radiological Controls

The inspectors observed the training conducted on March 6.

The

training was conducted prior to entry into the steam generator

primary channel heads to install reactor coolant piping nozzle covers

and CCTV cameras. The training was found to simulate actual conditions

in and around the steam generators and used full-scale mock-ups.

After indoctrination discussions, the workers were trained in teams

needed to perform the required tasks.

They were outfitted in the

same type of protective clothing used for steam generator entry and

repeated the exercise until the results and stay times were acceptable.

To further evaluate the training, an inspector participated in

mock-up training being conducted for inspection personnel on March 7.

During periods of steam generator entry for inspection or repair,

observations of the implemented radiological controls were made.

The inspectors reviewed radiological survey data taken prior to

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worker entry into the steam generators.

Using this data the stay-times

established by the licensee were verified as being conservative.

There were no unacceptable conditions identified.

(3) Steam Generator Tube Inspections

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As described in paragraph (1)(b) above, a steam generator tube

leakage test was conducted. One tube, No. 120-94 in the No. 1 Steam

Generator Hot Leg side, was found leaking. That tube is adjacent to

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a Tie Rod, which is a structural support for the steam generator tube

support plate.

Eddy Current Testing (ECT), a non-destructive examination, was

conducted of the defective tube, the five others surrounding the

tie rod and the three remaining tubes surrounding the defective

tube. Additionally six other tubes adjacent to a second tie rod

in the No. 1 Steam Generator Hot Leg side were tested.

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One other tube was found with a recordable defect of 34 percent

wall thickness. That tube, No. 121-93, is adjacent to the defective

tube and the tie rod. Both tubes were removed from service by

plugging.

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Technical Specification 4.4.5.1.3.c.1 requires additional, unscheduled

inservice inspections of steam generator tubes in the event primary-to-

secondary leakage exceeds 0.5 GPM in either steam generator.

Because

there was evidence that leakage exceeds 0.5 GPM additional inservice

inspection was required; however, since the licensee was planning a

large scale inservice inspection program for the refueling outage

scheduled to start on May 28, 1983, the NRC provided a one time

exemption from additional inservice inspection requirements. Operating

License Amendment 83 deferred the inspection requirements of Technical Specification 4.4.5.1.3.c, Table 4.4-6, Category C-1 because of

the events associated with the March 1, 1983 outage.

(4) Results of Previous Steam Generator Tube Inspections

The defective tube (120-94) had been ECT examined during the 1982

outage. The tube had not been rejected during that program and no

defects were recorded for it in the final program report.

Because this tube was now leaking, the licensee located the magnetic

tapes which contain the 1982 ECT data for this tube; then, reviewed

and re-analyzed the data. The licensee has concluded that a defect

in excess of the 40 percent plugging limit did exist, but, was

overlooked in 1982. The depth of the defect was quantified to be 83

percent of tube wall thickness when the 1982 data was re-analyzed in

March, 1983. The licensee has attributed this lack of performance in

ECT due to the location of the defect which is at the elevation that

the tube penetrates the top of the steam generator tube sheet. The

transition through the tube sheet along with an apparent dent in

the tube wall at the same height creates interferences with the

analysis of the ECT signal.

The licensee has reviewed the ECT data for other tubes in the No. 1

Steam Generator for which a dent signal was recorded at the top of

the tubesheet elevation during 1982 inspections.

From this review,

no additional defects were identified.

This data was presented to

the NRC as the bases for Operating License Amendment 83.

There were no additional unacceptable items identified.

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Implementation of NRC Balletin 82-02 During Maintenance (Unit 2)

NRC Bulletin 82-02, " Degradation of Threaded Fasteners in the Reactor

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Coolant Pressure Boundary of PWR Plants", includes inspection requirements

for cracking and corrosion when components are opened for maintenance.

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During the March I through 17 outage, valve 2-SI-247 was opened for

maintenance. This valve is a 12-inch swing check valve located in a

0.35 Roentgen per hour radiation field and had levels of 2.0 Roentgen

per hour on contact.

Bulletin 82-02 provides for relief from certain requirements when

components are located in high radiation fields.

This is due to

worker exposure considerations. Based on previous experience, there

was a possibility for galling the A453 Grade 660 stainless steel

studs when being removed from the A351 Grade CF-8M cast stainless

steel valve body. As there were 16 studs in all, representatives of

the Office of Inspection and Enforcement granted relief from the full

inspection requirement during a conference call with the licensee on

March 10. Two stainless steel studs were to be fully examined using

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surface non-cRstructibletest methods; a carbon steel stud was to be

examined and then replaced with a stainless steed stud. All studs

were to be visually examined for evidence of boric acid cyrstals,

pitting, and cracking. Of particular importance was the transition

of chrome plated surfaces at the threads. Unacceptable conditions

would include gross pitting of pin-head size in the threads.

Stud

deformation was to be monitored during reassembly.

No evidence of closure stud degradation was observed during this

inspection. No unacceptable conditions or practices were identified.

1.

Forced Outage - March 24 through 29 (Unit 1)

During March 24 through 29, Unit 1 conducted a forced maintenance

outage to correct high unidentified RCS leakage.

During the preceding weeks, calculations of unidentified RCS leak

rates displayed an upward trend. On March 24 the leak rate exceeded

the Technical Specification limit of 2.5 GPM.

This leak rate is calculated

by integrating the flow from the drywell floor drain sump over a

period of time. A reactor shutdown was conducted on March 24.

Inspection revealed packing leakage from valve 1-IC-1, the Isolation

Condenser steam supply line inboard isolation valve, and a body-to bonnet

leak from a mechanical seal in valve 1-FW-118, a feedwater supply

line manual isolation valve.

Following repairs, the reactor was made

critical on March 27. A final inspection during heatup identified

additional packing leakage and mechanical connection leakage from

valve 1-MS-3A, a Target Rock Safety / Relief Valve. The reactor was

returned to cold shutdown and repairs completed. The reactor was

again made critical on March 29.

Since then, RCS unidentified

leakage has remained below 0.4 GPM.

No unacceptable conditions were identified,

m.

Reactor Trip - March 24 (Unit 1)

During the shutdown on March 24, a reactor trip occurred from low

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power level (Intermediate Range Monitor (IRM) range No. 8) at 2205.

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Reactor water level was in manual control using the feedwater regulating

valve (FRV) bypass valve. When additional water was needed, the

blocking valve for one of the two FRV's was opened.

In this case the

operator mistakenly opened the blocking valve associated with the FRV

which was selected for use with the Feed Water Coolant Injection

(FWCI) subsystem.

Since reactor water level was below the setpoint

level, the FWCI selected FRV was open. The resulting inrush of

cooler water caused power level to rise to the IRM upscale high

reactor trip level.

This transient was investigated because the running Condensate

Booster Pump and Feedwater Pump tripped due to insufficient net

positive suction head when feedwater flow rapidly increased. The

concern was that the FWCI subsystem would cause the same sequence of

events, resulting in tripping of running pumps.

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The licensee completed an engineering analysis which resulted in

changing setpoints for the feed water pump flow limiter. This

subsystem, part of the reactor water level control system, acts to

close the FRV and limit flow to 105 percent of rated. Administrative

controls have been established to require that the feed water pump

minimum flow valve be operated in automatic and that a minimum of two

condensate pumps and three condensate demineralizers be in service

during startup and shutdowns to provide adequate FWCI response in

high flow demand conditions originating from low reactor power.

Subsequent testing has confirmed acceptable FWCI performance.

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Reactor Trip - March 31 (Unit 1)

On March 31, 1983 at 1502, Millstone Unit 1 experienced a reactor

trip from 87% of full power.

The reactor trip resulted from a turbine trip caused by a false high

level sensed in the turbine moisture separator. The moisture separator

drain tank level control valve air operator diaphram had previously

been replaced and the valve cycled for testing. The valve subsequently

failed in the full open position due to a defective positioner. As

the drain tank emptied, staam flow through the moisture separator

resulted in vibration which spuriously tripped the mercury float-type

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level switch. All other equipment functioned properly during the

transient. The reactor was again made critical at 2241 on March 31

and reached full power on April 2.

No unacceptable conditions were observed.

4.

Review of Plant Operations - Logs and Records (Units 1 and 2)

During the inspection period, the inspector reviewed operating logs and

records covering the inspection time period against Technical Specifications

and Administrative Procedures requirements.

Included in the review were:

Shift Supervisor's Log

-daily during control room surveillance

Plant Incident Reports

-2/27/83 through 4/16/83

Jumper and Lifted Leads Log

-all active entries

Maintenance Requests & Job Orders -all active entries

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Construction Work Permits

- all active entries

Safety Tag Log

- all active entries

Plant Recorder Traces

- daily during control room surveillance

Plant Process Computer Printed Output - daily during control room surveillance

Night Orders

- daily during control room surveillance

The logs and records were reviewed to verify that entries are properly made;

entries involving abnormal conditions provide sufficient detail to communi-

cate equipment status, deficiencies, corrective action, restoration and test-

ing; records being reviewed by management; operating orders do not conflict

with the Technical Specifications; logs and incident reports detail no viola-

tions of Technical Specification or reporting requirements; and logs and re-

cords are maintained in accordance with Technical Specification and Administra-

tive Control Procedure requirements.

There were no unacceptable conditions identified.

5.

Review of Periodic and Special Reports

Upon receipt, periodic and special reports submitted by the licensee pursuant

to Technical Specification 6.9.1 and 6.9.2 and Environmental Technical Speci-

fication 5.6.a were reviewed by the inspector. This review included the fol-

lowing considerations: the report included the information required to be re-

ported by NRC requirements; test results and/or supporting information are

consistent with design predictions and performance specifications; planned

corrective action is adequate for resolution of identified problems; determin-

ation of whether any information in the report should be classified as an ab-

normal occurrence; and the validity of reported information. Within the scope

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of the above, the following periodic reports were reviewed by the inspector:

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Monthly Operating Report, Units 1 and 2, February, 1982

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Annual Report 1982, Units 1 and 2*

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  • Includes report of safety / relief valve challenges made in accordance with

NUREG-0737, Item II.K.3.3.

6.

Licensee Event Reports (LERs)

The inspector reviewed the following LERs to verify that the details of the

event were clearly reported including the accuracy of the description of cause

and adequacy of corrective action. The inspector detennined whether further

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information was required, and whether generic implications were involved. The

inspector also verified that the reporting requirements of Technical Specifi-

cations and Station Administrative and Operating Procedures had been met, that

appropriate corrective action had been taken, that the event was reviewed by

the Plant Operations Review Committee, and that the continued operation of the

facility was conducted within the Technical Specification limits.

Unit 1

83-03

Setpoint drift,1 of 4 High Reactor Pressure pressure switches. LER

82-25 reported setpoint drift of a pressure switch used in this appli-

cation; however, a different switch was involved.

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83-04

Diesel Generation inoperable.' The resident inspector observed

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subsequent corrective maintenance and retesting as described

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in Inspection Report 50-245/83-05.

83-05

Setpoint drift,1 of 4 Main Steam Line Low Pressure, pressure '

switches.

LER 83-01 reported setpoint drift of a pressure

switch used in this application; however, a different switch

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was involved.

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83-06

Setpoint drift,1 of 16 Steam Tunnel High Temperature thermal

switches.

LER 82-26 reported similar drift.

83-07

Setpoint drift,1 of 8 Main Steam Line Isolation Valve limiti

switches. LER 82-15 reported setpoint drift in a limit switch

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used in this application; however, a different switch was

involved.

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83-08

Setpoint drift,1 of 2 Isolation Condenser Isolation differ-

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ential pressure switches.

LER 82-07 also reported drift in

this switch.

83-09

Setpoint drift,1 of 4 Reactor water level switches which

actuate ECCS systems.

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A liquid radioactive release was made without continuously

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83-01

recording the associated radiation monitor output.

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charge limits were exceeded. Alarm functions were unimpaired.

83-02

Failure to conduct operability test on "C" Charging Pump due

to personnel error.

83-03

High reactor coolant system iodine concentration following

the reactor trip of February 19.

Peak activity reached 1.32

microcuries per gram dose equivalent iodine 131.

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83-04

Dropped Control Element Assembly.

Inspection Report 50-336/

83-06 addresses this event

83-06

Voluntary entry into an action statement involving credit for

a repaired but yet untested High Pressure Safety Injection Pump.

83-07

An error was discovered in the reactor safety transient

analysis involving a postulated steam generator tube rupture.

The steam generator pressure which had been " assumed" to be

conservative was shown to be non-conservative.

Recalculation

of the consequences of a steam generator tube rupture event

indicates continued compliance with 10 CFR 100 (Paragraph 10).

83-08

A reactor mode change inadvertently occurred due to a feedwater

system transient. A hydraulic pipe snubber required to be

operable in the new mode was undergoing repair. Within 2

minutes, power was reduced. Snubber repairs were completed

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prior to return to power operation.

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83-09

Operation of the reactor at a power level exceeding Technical Speci-

fication limits for existing plant conditions during a period of over

5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> on March 26, 1983.

At 1546 on March 25, Millstone Unit 2 experienced a failure of its pro-

cess computer which caused computer output screens to fail to update,

and to continue to display the last values of parameters computed.

Digital clocks on both video monitors on main control board C04 and

the video monitor on the reactor operator's desk were frozen at

15:46:43. This failure went unnoticed by plant operators through a

shift change and was not identified until 2100 on March 26.

Indica-

tions of this failure available in the control room included lack of

updates of data on the three video monitors described above, particu-

larly clock updates; lack of updates of the Balance of Plant Log; and

lack of updates on the Alarm Typer.

At Millstone Unit 2, the process computer plays important roles in mon-

itoring Control Element Assembly (CEA) position and fuel linear heat

rate. Technical Specification 3.2.1 requires that fuel linear heat

rate be limited to 15.8 kilowatts per foot (KW/ft). The accompanying

surveillance requirements permit monitoring linear heat rate usirig

either incore neutron detectors or excore neutron detectors.

Incore

detector monitoring requires use of the process computer.

Excore de-

tector monitoring is independent of the process computer; but, due to

greater measurement uncertainties, reactor power is limited to a maxi-

mum of 89% of full power when relying upon excore detectors.

From the time of the failure, reactor power remained at 100% until the

operators discovered the failure and took action to reduce power.

Reac-

tor power reached 86% of rated power at 2148 on March 26. Troubleshoot-

ing revealed a fault in a circuit card (IBM Part Number 5800199). The

computer was returned to service at 0259 on March 27.

During this event, the reactor was operated at full power, above that

permitted by Technical Specifications with the process computer and in-

core neutron detectors inoperable for a period of over 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Num-

erous symptoms of the process computer failure were available in the

control room during that time.

Failure to maintain reactor power be-

low 89% while monitoring linear heat rate with the Excore Detector

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Monitoring System is a violation (50-336/83-08-01).

Followup analysis by the licensee of plant conditions prior to, during

and following the event indicate that it is not likely that the fuel

linear heat rate limit of 15.8 KW/ft was exceeded. The licensee has

reinstructed plant operators on the necessity of monitoring the pro-

cess computer. The engineering department has undertaken a study of

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possible modifications to the process computer system to more posi-

tively identify and alarm computer failures. The inspectors will

follow this effort under open item 50-336/83-08-02.

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83-10

Usage factor applied to pressurizer spray line because .of high

differential temperature during plant cooldown.

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7.

Plant Maintenance and Modifications

During the inspection period, the inspector frequently observed various

maintenance and problem investigation activities. The inspector reviewed

these activities to verify:

compliance with regulatory requirements,

including those stated in the Technical Specifications; compliance with

the administrative and maintenance procedures; compliance with applicable

codes' and standards; required QA/QC involvement; proper use of safety

tags; proper equipment alignment and use of jumpers; personnel qualifica-

tions; radiological controls for worker protection; fire protection;

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retest requirements; and, reportability as required by Technical Specifi-

cations.

In a similar manner the implementation of design changes and

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modifications were reviewed.

In addition to those items addressed above,

the licensee's safety evaluation was reviewed.

Compliance with require-

ments to update procedures and drawings were verified and post modifica-

tion acceptance testing was evaluated. The following activities were

included in this review:

Unit 1

Hanger / Seismic Support modifications to the Core Spray System

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suction ring header.

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Hanger / Seismic Support modifications to the Torus -Drywell

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Vacuum Breakers.

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Drywell Nitrogen Compressor mounting modifications.

Corrective maintenance to Feedwater Manual Stop Valve,

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1-FW-118.

Corrective maintenance on Drywell Air Coolers HVH-18 and

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HVH-22.

Unit 2

Inspection and corrective maintenance on No. 2 Steam

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Generator.

Corrective maintenance on Safety Injection Check Valve,

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2-SI-247.

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8.

Inspector Witnessing of Surveillance Tests

The inspector witnessed the performance of surveillance testing of

selected components to verify that:

the surveillance test procedure was

properly approved and in use; test instrumentation required by the procedure

was calibrated and in use; technical specifications were satisfied prior

to renoval of the system from service; the test was performed by qualified

personnel; the procedure was adequately detailed to assure performance of

a satisfactory surveillance; and test results satisfied the procedural

acceptance criteria or were properly dispositioned. The inspector witnessed

the performance of:

Unit 1

" Reactor Coolant Chemistry at Stea;ning Rates of 100,000

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Pounds per Hour or Greater" per SP-840, Revision 0 on

March 14.

" Analysis of Reactor Coolant for Radioactivity" per SP-838,

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Revision 1, on March 14.

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" Conductivity Bridge - L&N" per CP-801J, Revision 1, on

March 14*.

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" Chloride Analysis by Spectro Photometry Method" per

CP-808L, Revision 0, on March 14**.

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" Stack Gas Monitor System Functional Test" per CP-836,

Revision 2, Change 1, on March 15.

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" Main Steam Line Radiation Monitor Functional Test" per

SP-406B, Revision 1, on March 15.

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" Turbine Stop Valve Closure Functional Test" per SP-408F,

Revision 4, on March 15.

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" Main Steam Safety / Relief Valve Discharge Vacuum Breaker

Valves ISI Readiness Test" per SP-1093, Revision 0, on March 15.

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" Inspection of Hydraulic Snubbers" per SP-673.2, Revision 4,

on March 25.

(Inspection of recirculation system snubbers

located inside primary containment)

Unit 2

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" Aerated Liquid Rad Waste Process Radiation Monitor Functional

Test RM-9116" per SP-2404A, Revision 1, Change 3, on March 18.

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" Calibration of Excore Nuclear Instrument (NI's) to Incores"

per SP-2401E, Revision 6, on March 22.

  • This chemical analysis procedure is consistant with American Society

for Testing and Materials (ASTM), Part 23, Standard D-1125.

    • This chemical analysis procedure is consistent with ASTM, Part 23,

Standard D-512-67.

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" Power Range Safety Channel and Delta T Power Channel Calibra-

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tion" per SP-26010, Revision 3, on March 22.

9.

Bulletin Follow-Ups-(Unit 2)

Bulletin 83-04 -

" Failure of the Undervoltage Trip Function of

Reactor Trip Breakers"

The inspector observed the licensee actions taken in response to Bulletin 83-04. The Reactor Protective System (RPS) at Millstone Unit 2 uses

General Electric Type AK-2 circuit breakers.

Both undervoltage and shunt

trip coils are actuated by the RPS.

Reactor Protective System integrated

response time testing is presently incorporated in the planned surveil-

lance system.

On March 14, the licensee tested'the breaker-trip mechanism for each

RPS Trip Breaker by separately de-energizing the undervoltage coil or

energizing the shunt trip coil.

Each t,'ip coil in each breaker was

tested at least once.

The inspector observed a portion of the testing;

the results were acceptable.

On March 17, the definition of " failure" in context of the subject Bulletin

was provided by the NRC OIE Events Analysis Branch as...

" ... failure to trip is considered to be either complete failure

to open, or " sluggish" action in excess of the overall system

response time (400 milliseconds for CE plants) assumed by plant

safety analyses."

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Surveillance testing of the breaker undervoltage trip devices only was

conducted on March 17 and witnessed by the inspector. All breaker under-

voltage trip devices actuated ana caused the respective breakers to open

within 0.050 seconds of voltage removal.

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The plant maintenance program addresses these breakers and includes re-

furbishment, alignment, and testing each cycle.

An independent review

is being conducted of these procedures prior to use in the May 1983

refueling outage.

A written account of the Salem fail-to-trip event has been circulated

among licensed operators reporting for shift duty. The resident inspector

reviewed routing sheets bearing operator initials documenting operator

review of the event.

No unacceptable conditions were observed.

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10.

Error in Steam Generator Tube Rupture Accident Analysis -(Unit 2)

On March 18.. the licensee determined that an ' error had been made by the

NSSS, Combustion Engineering, in the assumed initial plant conditions

for the analysis 'of a Steam Generator Tube Rupture. The current analysis

incorrectly assumed t5at the Main Steam System Atmospheric Steam Dump

Valves were operated in the manual mode and that the Steam Generator

secondary pressure was 860 psia. Lower than normal pressure was selected

to maximize the primary to secondary flow through the~ break.

A re-analysis made by the licensee established initial conditions of

Atmospheric Steam Dump Valves operating in automatic and Steam Generator ,

secondary pressure at 933 psia. The higher initial pressure resulted in-

operation of both the Atmospheric Steam Dump Valves and Steam Generator

Safety Valves, these being the release point to the environment.

In

contrast, the current analysis resulted in a release from the Unit 2

vent stack through the condenser and air ejector system.

The re-analysis resulted in a calculated thyroid dose of 250 mrem at

the site boundary. The less conservative analysis had calculated

6 mrem. This is contained in Section 14.14 of the Millstone Unit 2

FSAR, dated June 10, 1982.

This error is potentially generic because it.had been made by the NSSS supplier.

The licensee has provided the NRC with information in an LER No.50-336/83-07.

11. Design Deficiency in Emergency Diesel Generator Control Circuit - (Unit 1)

A design deficiency was determined to exist in the Millstone Unit 1 Emer-

gency Diesel Generator Control Circuit. This deficiency would prevent

successful re-start of the diesel engine during accident conditions

following re-set of the generator lock-out relay.

The diesel generator is a Colt Industries, Fairbanks-Morse Model 3800

TD8-1/8. The control circuit is a combination of designs made by Colt

Industries, Euclid Equipment and Ebasco Services.

However, other units

with a timed diesel fuel shutoff may have a similar design deficiency.

The time delay ensures that the diesel has come to a complete stop prior

to a re-start attempt, and is implemented with a 34 second time delay

relay which energizes the governor shut-down solenoid.

The problem exists during accident conditions when the Emergency Safety

Systems actuation logic provides a continuous start signal to the

diesel generator control circuit.

If the diesel is shutdown, as could

occur through operation of the generator lock-out relay, manual emer-

gency stop or local stop switches or start failure circuit, the diesel

cannot be restarted. Unless the time delay fuel shut-off relay inter-

rupts the start signal along with the diesel fuel supply, the machine

will attempt to start without fuel and will either deplete its air

start reservoir or shutdown after an unsuccessful attempt to start.

This problem may be generic to other emergency power sources having a

timed diesel fuel shutdown circuit.

It was discovered at Millstone

while following-up INPO Significant Event Report 62-82 which described

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a loss of Emergency Bus event at North Anna 2 on March 8,1982 (LER 50-

339/82-13). Details concerning this finding were provided to the

NRC OIE which subsequently issued Information Notice 83-17; " Electrical

Control Logic Problem Resulting in Inoperable Auto-Start of Emergency

Diesel Generator Units".

The licensee is preparing a modification which, using an additional relay,

will interrupt the air start signal when the fuel cut-off solenoid is

energized.

It is expected to be implemented on April 18.

12. Emergency Planning Exercise

The inspectors observed a functional test of the Emergency Plan on March 2.

The test included a radiological assessment exercise which was implemented

through a team of drill controllers using a radiological survey scenario.

A recently developed system for transmission of control room data was used.

There were no unacceptable conditions identified.

13. . Review of Radioactive Material Shipments - (Unit 1)

The inspector reviewed the activities concerning the shipment

of a'" limited quantity" shipment of contaminated tools from

Millstone Unit 1 to Vermont Yankee Atomic Power Station. The

inspector observed package preparation, radiological surveys,

and documentation. An " Exclusive use" vehicle was used. The

inspector conducted independent radiological surveys to confirm

licensee results.

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No unacceptable conditions were identified

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' 14.

Exit Interview

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At periodic intervals during the course of the inspection, meetings were

held with senior facility management to discuss the inspection scope and

findings.

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