05000219/LER-1981-046-03, /03L-0:on 810920,three Hydraulic Snubbers in Shutdown Cooling Sys Could Not Obtain Drag Load within Acceptable Limits.Caused by Dirty Oil,Cracked Brass Head Ring,Faulty O-ring & Seals.Snubbers Replaced

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/03L-0:on 810920,three Hydraulic Snubbers in Shutdown Cooling Sys Could Not Obtain Drag Load within Acceptable Limits.Caused by Dirty Oil,Cracked Brass Head Ring,Faulty O-ring & Seals.Snubbers Replaced
ML20011A896
Person / Time
Site: Oyster Creek
Issue date: 10/21/1981
From: Fitzgerald M
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20011A895 List:
References
LER-81-046-03L, LER-81-46-3L, NUDOCS 8111030330
Download: ML20011A896 (1)


LER-1981-046, /03L-0:on 810920,three Hydraulic Snubbers in Shutdown Cooling Sys Could Not Obtain Drag Load within Acceptable Limits.Caused by Dirty Oil,Cracked Brass Head Ring,Faulty O-ring & Seals.Snubbers Replaced
Event date:
Report date:
2191981046R03 - NRC Website

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% l Three hydraulic snubbers located in tne Shutdown Cooling SystcIn could This candition is per-l d inot obtnin drag load within acceptable limits.

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42 43 44 4y CAUSE DESCRIPTICN AND CORRECTIVE ACTIONS 27 The causes were attributed to various prob 1 cans with each snubber, inclu-g iiO 1 j ding dirty oil, a cracked brass head ring, a faulty 0-ring $53 faulty i ii1 !

- I2j i seals. The 3 were replaced with operable spares and will lator bc i I a1 l repaired. A program on rebuilding and testing hydraulic snubbers will i;. II be conducted through the manufacturer in the near future.

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