05000333/LER-1981-062-04, /04T-0:on 810804,isolation Adjustment Potentiometer Malfunctioned,Possibly Allowing Isolation Setpoint & Actual Setpoint to Differ.Caused by Loose Set Screw Due to Wear & Tear.Set Screw Tightened

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/04T-0:on 810804,isolation Adjustment Potentiometer Malfunctioned,Possibly Allowing Isolation Setpoint & Actual Setpoint to Differ.Caused by Loose Set Screw Due to Wear & Tear.Set Screw Tightened
ML20010F792
Person / Time
Site: FitzPatrick 
Issue date: 09/02/1981
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010F786 List:
References
LER-81-062-04T, LER-81-62-4T, NUDOCS 8109110339
Download: ML20010F792 (1)


LER-1981-062, /04T-0:on 810804,isolation Adjustment Potentiometer Malfunctioned,Possibly Allowing Isolation Setpoint & Actual Setpoint to Differ.Caused by Loose Set Screw Due to Wear & Tear.Set Screw Tightened
Event date:
Report date:
3331981062R04 - NRC Website

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NPC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION I

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LICENSEE EVENT REPORT L

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60 61 COCKET NLV8ER 66 69 EVENT DATg 74 75 REPORT DATE 60 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012l l During normal operation, personnel noted that the isolation adlustment potentiometeli j

[o ial I for the radwaste effluent monitor was malfunctioning in su:h a manner that the 1

t o l4 i I indicated isolation set point and actual set point could differ.

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