LER-1981-050, /03L-0:on 810731,primary Coolant Dose Equivalent I-131 Discovered Exceeding Tech Spec Limit.Caused by Leaking Fuel or Tramp U & Dose Equivalent Iodine Transient Following RCS Transient.Rcs Purification Flow Increased |
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(7 171 LICENSEE EVENT REPORT CONTROL BLOCN l )
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e 60 61 DOCir ET NUMBE R 68 69 EVENT DATE 74 75 REPORT DATE B0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Oto y t 0945 on 7/31/81 during Reactor Coolant sampling, it was discovered that prir'ary I
A coolant Dose Equivalent I-131 exceeded the linit of T.S.
3.4.8.
Redundancy NA.
There l
was no effect upon the health or safety of the general public. This is the twenty-l
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g fourth event reporte. under this Specification, g
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CAUSE
CAUSE COMP.
VALVE CODE CODE SU8 CODE COVPONENT CODE SUBCOOE SUBCODE l0l9l l Z l Z lh lZ lZ lh lZ lZ lZ lZ lZ lZ l l Z lh [Z] @
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9 TO 11 12 13 18 19 20 SEOUE NTI AL OCCtJR RE NCE REPORT REVISION
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33 34 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i l 0 l l The cause of the event is attributed to leaking fuel or " tramp uraniun" (i. e., uraniur,l
,,,,; [n the cladding within one recoil radius of the surface) and an anticir>ated Dom ran i m -l fentIodinetransientfollowingaLeactorCoolantSystentransient. RCS purification l
l1 l3i flwwasincreased; Doce Equivalent I-131 was less than 1.0 raicrocuries per gran at l
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8 9 STA S
% POWE R OTHER STATUS ISCO RY D:SCOVERY DESCRIPTION NA l
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8 9 to 11 PERSONNEL E xFOSLRES NUVBE R TYPE
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8 9 11 12 LOSS OF OR Dr.'/ AGE TO F ACILITY TYPE
DESCRIPTION
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NRC USE ONLY 8109080269 810827
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NA*.tE OF PREPARER OMTMfqHED SUPPLDIENTARY CNFORMATION SHEET)
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REACTOR POWER HISTORY OF PRIOR FORTY-EIGHT HOURS ITIN I LVINT DATE:
July 31, 1981
SUPPIDENTARY INFORMATION Repe-t#50-302/81-050/03I,-0 Facility: Crystal River Unit 3 Report Dat August 27, 1981 Occurrence Date:
July 31,1981 Identification of Occurrence:
Primary Coolant Dose Equivalent I-131 was greater than 1.0 microcuries per gram contrary to Technical Specificatien i
3 4.8.
i Conditions Prior to Occurrence:
Mode 3 - (Hot Shutdown 04)
Description of Occurrence:
At 0945 on July 31, 1981 after a Reactor trip, li; was disyvered that Dose Equivalent I-1 31 exceeded 1.0 mic. euries per gram.
Designation of Apparent Cause:
The cause of this event is attributed to leaking fuel or
" tramp uranium" (i.e., uranium in the cladding within one recoil radius of the surface) and an anticipated Dose Equivalent Iodine transient following a Reactor Coolant System transient.
Analysis of Occurrence:
There was no effect upon the health of safety of the general public.
Corrective Action
The Reactor Coolant System flowrate through the Makeup and Purification System 'tas increased.
Dose Equivalent I-131 i
was determined to be less than 1.0 microcuries per gram a' 0100 on August 1, 1981.
FPC Nuclear Support Servicee is also conducting an evaluation to determine if failed 1% 1 is present.
Failure Ihta:
This is the twenty-fourth event reported under this Specification.
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h2 DATE 7r29r81 k. Ll m
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( % HOUR GMWE TURB G MWTH NI RATIO RATIO u,. g,J^+,"u f
(E710)
(T856)
(P753)
(P723)
NI/MT ME/MT m'
~,
=/aFP BTU /KWH aJaFP n/aFP
- - AFP a/*FP
( %'
1 96.71 105tti 99.51 99.80 1.003
-.972
.r*
3 2'
96.70 10545 99.51 99.90 1.004
.972.
T- ' 'D L2E-3 96,65 10552 99,55 - -99,90 1,004 w971 Mi E ( h22' e
Lt 96.73 10569 99.51 99.90
- 1. 0 0 tt
.972 a
'i M
5 96.91 10529 99.31 99.70
- 1. 0 0 Lt
.976
~
4 6
97-. f4 4 10L&88
- 99. 8tt ---10 0 10 1, S t)3
.976
.h;p;%
l k. f 7
97.33 110391 99.88 100.20 1.003
.975
.. JJ B
97.844 10238 99.92 100,10 1.002
.975 3
I,-
! (
9 97.45 - - 10247 100.04 - 100,10 1,-001
.974
~
,5
.l] E {' d 10 97.32 1026tt 100.0tt 109.10 1.001
.973 4
11 97.11 10271 99.88 100.20 1.003
.972
!34 12 9.7.1.1 10266 99,8tt 1.00.20 1.0 0l+.
.973
(' [
3 13 97.09 10273
. 99.88 100.20 1.003
.972
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14 97.09 10255 100.00 100.20 1.002
.971 33
- - 15 97,15 10237 - 99.92 100r10 1-i O O 2
.972 T[. s 16 97.10 102f47 99.92 100.10 1.002
.972
,..gI 17 97.11 10239 99.92 100.20 1.003
.972
'4 '
18 96.12 10249 98.98 99.30 1-003
.971 19
- - 9 6.169
- - 10252 99.39 99.70 1.003-
.971 b,37}
13 8 I 20-96.71
~10277 99.59 100.00 1.004
.971
~
N 21 96,82-10261 99,71 100.00.003 - _.971 d
22 96.94 10368 99.67 99.90 1.002
.973 b
23
- 96. 9 tt 105tt5 99.67 99.90 1.002
.973 d21 94 9L 87 10536 99 63 99 80 1.009
.979
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(~ d AVERAGE DAILY GENERATOR GROSS 829.11 MWH(E)
Ld7j AVERAGE DAILY THERMAL POWER 24t+LF. 96 MWH( T)
~44>se
- VERAGE DAILY _ TURBINE _ GROSS _ HEAT _ RATE 10360_ BTU /KWH
'4? AVERAGE DAILY MWTH POWER 99.713 */aFP C 5 AVERAGE DAILY NUCLEAR INST. POWER 99.983 a/*FP
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i RAT IO OF NI TO MWTH = 1. 0 02
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NI RATIO RATIO 4!
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(T856)
(P753)
(P723)
NI/MT ME/MT 6['
a/aFP BTU /KWH
1 96,_77 10450 9L59 99 a0 1A03
.9.72 W
2 96.84 10053 99.59 99.80 1.002
.972 6 ' 5j 3
.96.90-10050 99.63 99.80 1.002
.973
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96.82,.
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.96.91 10048 99.67 100.20 1.005
.972 6y 6
96.02 10056 99.63 100,10 1.005'
.972 7
9L 30 10.025 9 1 8.0 100J0 1 003
.915 [13j 8
97.36-10028 99.88 100.20 1.003
.975 63 9
97.44 10027 100.00 100.40 1.004'
.974 i' 5' - 1 0____.S.L J+ 2 10031 100.04 100.8+0 1.0_0 l+
974 v..gw.2 Ufj 11 97.37 10036 100.08 100.60 1.005
.973
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6 M' 12 97.47 10025 100.00 100.60 1.006
.975 JS 13 9.L.33__10 0 34 99_.S2 100.10 1.S05
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14 97.29 10033 99. 81+
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AVERAGE DAILY THERMAL POWER l35. AVERAGE DAILY TURBINE GROSS HEAT RATE 10041 BTU /KWH
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hVERAGE_ DAILY _MWTH_E0WER 91B62_.a/ EP 2
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NI/NT ME/MT l%
1 97.23 10018 99.63._._100.10_ _ 1.005
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- - 2 97.29 10011 99.63 99.90
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97.22 10021 99.67 99.80 1.001
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97.26 10022 99.84 100.10 1.003
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97.24 10027 994.88 100.10 1.002 9.74 4
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?h 1-6 0.00 0
8.69 0.-00
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9.54 0.00 0.000 0.000 [N- [kh 18 1.46 30723 11.13 15.70 1.410
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19 25.57 1-2836 31.r24 39r00 1r248
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'22 67.53 10258 70..11 76 90 14097 i963 I
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23 71.01 10557 76.10 81.00 1.064
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.968 JL
.rs
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l. 2 f._ AVER AGE _ DA ILY.ISENE R ATO R_ G ROSS - 377 86 MWH(E) 9 AVERAGE DAILY THERMAL POWER 117tt.96 MWH(T) b !35l AVERAGE DAILY TURBINE GROSS HEAT RATE 6954 BTU /KWH kAVERAGE_ DAILY-MWTH_ POWER
4.7.918 a/>EP b7: AVERAGE DAILY NUCLEAR INST. POWER 48.225 a/*FP
( n wm-n.,:
. !+$ RATIO OF NI TO MWTH = 1.006
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FUEL BURNUP BY CORE REGION ITB4 2 EVHiT DATE:
July 31,1981
ITH4 2 THE BUMP WAS CAICUIATED AT 265 9 EPPD FOR THE TIEEE (3) HEICIMNT REGIONS.
BATCH NUMBER OF FA BURNUP (MWD /MTU)
B 9
25,552 C
60 23,589 D
52 13,745 E
56 6,891 AV.15,514 MWD /MTU
CLEANUP FLOW HISTORY ITH4 3 EVHTT DATE:
July 31, 1981
ITIM 3 CLEANUP FLOW HISTORY FORTY-EIGHT (48) HOUBS PRIOR TO THE FIRST SAMPLE IN WHICH THE LIMIT WAS ET.CEEDED INDICATED A LETDOWN FIOWRATE OF R)R1T-FIVE (45) GPM.
NEITHER MEGJP AND PURIFICATIN DIMINERALIZER WAS IN SIRVICE DUE TO A IOSS'0F ACCURATE PRIMARY SYSTIM ph C0h'IROL.
9L DIMIN FIOWRATE 7/29/81 "A"
47 7/30/81 0
DEAS OPERATION ITH4 4 EVBIT DATE:
July 31,1981
i ITD4 4 DEASSING OPH1ATIONS PRIOR TO EXCEDING LIMIT (7/29/81 at 1115 through 7/31/81 at 1115) 7/30 0255 Started pressurizer spray 0618 Stopped pressurizer spray 7/31 0435 started pressurizer spray 0630 Stopped pressurizer spray
z a
TIME DURATION WHEN DEI-131 EXCEEDED 1.0 u Ci/ gram and I-131 ANALYSIS RIEULTS ITD4 5 EHNT DATE:
July 31, 1981 l
l
a ITm 5 AS PER TECHNICAL SPECIFICATION 3 4.8, the FOUR (4) HOUR SAMPLING FRMUINCY AS DEPICTED m THE TABLE BELCV WAS INITIATED AT 0945 AND THE DOBE MUIVALINT I-131 WAS 138 MICR0CDRIIB PIR GRAM.
THE FOUR HOUR SAMPLING FREUINCY WAS TIEMINATED AT 8 /1 /81 0100 hrs.
WHEN THE DEI-131 WAS DETERMINED TO BE 0.648 MICROCURIIB PIR GRAM.
THE TIME DURATIN WHIN THE SPECIFIC ACTIVITY OF PRIMARY COOLANT EKCEEDED 1.0 MICROCURIIB PIR GRAM DTE MUIVAINT IS:
15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />, 15 minutes DATE TIME DEI-131 (uCi GRAM) 7 1
0945 1 38 7
1 1300 1 54 7
1 1700 1 59 7
1 2105 1.19 8
81 0100 6.48E-1 l
l
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| 05000302/LER-1981-001-01, /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | | | 05000302/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000302/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000302/LER-1981-002-03, /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | | | 05000302/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000302/LER-1981-003-01, /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | | | 05000302/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000302/LER-1981-004-03, /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | | | 05000302/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000302/LER-1981-005-03, /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | | | 05000302/LER-1981-006-03, /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | | | 05000302/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000302/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000302/LER-1981-007-03, /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | | | 05000302/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000302/LER-1981-008-03, /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | | | 05000302/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000302/LER-1981-009-03, /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | | | 05000302/LER-1981-010-03, /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | | | 05000302/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000302/LER-1981-011, Forwards LER 81-011/01T-1 | Forwards LER 81-011/01T-1 | | | 05000302/LER-1981-011-01, /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | | | 05000302/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000302/LER-1981-012-03, /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | | | 05000302/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000302/LER-1981-013-03, /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | | | 05000302/LER-1981-014-03, /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | | | 05000302/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000302/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000302/LER-1981-015-03, /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | | | 05000302/LER-1981-016-03, /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | | | 05000302/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000302/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000302/LER-1981-017-03, /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | | | 05000302/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000302/LER-1981-018-03, /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | | | 05000302/LER-1981-019-03, /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | | | 05000302/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000302/LER-1981-020-03, /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | | | 05000302/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000302/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000302/LER-1981-021-03, /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | | | 05000302/LER-1981-022-03, /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | | | 05000302/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000302/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000302/LER-1981-023-03, /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | | | 05000302/LER-1981-024-03, /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | | | 05000302/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000302/LER-1981-025-03, /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | | | 05000302/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | |
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