05000321/LER-1981-056-03, /03L-0:on 810610,during Startup,Offgas Hydrogen Analyzer 1N62-N009A Was Reported Inoperative.Caused by Personnel Error.Root Valve N62-F064 a Was Found Closed. Valve Opened

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/03L-0:on 810610,during Startup,Offgas Hydrogen Analyzer 1N62-N009A Was Reported Inoperative.Caused by Personnel Error.Root Valve N62-F064 a Was Found Closed. Valve Opened
ML20009F573
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/02/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F572 List:
References
LER-81-056-03L, LER-81-56-3L, NUDOCS 8107310318
Download: ML20009F573 (2)


LER-1981-056, /03L-0:on 810610,during Startup,Offgas Hydrogen Analyzer 1N62-N009A Was Reported Inoperative.Caused by Personnel Error.Root Valve N62-F064 a Was Found Closed. Valve Opened
Event date:
Report date:
3211981056R03 - NRC Website

text

U. S. NUCLEAR REGULATCRY COMMISSION l

NRC FORM 366 (7 77)

LICENSEE EVENT REPORT CONVROL BLOCX: l

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l While the olant was in start-uo.1N62-N009A. Off-nan H3 Analyzer was I

lo l3 l l found to be inoperative.

The event date is unknown, but reported in-I l o 14 l l operative on June 10, 1981.

Tech Specs Table 2.1.3.h reouires one coer-l loIsl l able channel.

Redundant Hp Analyzer, IN62-N009B, was operable. P1 ant I

l o 16 I l operation nor the health and safety of the oublic was not affected by I

lol7ll this event.

This is a repetitive event as last reported on Reportable I

ioisi l Occurrenca Report No. 50-321/1980-094.

I C DE CODE SUBCO E COYPONENT CODE SLBC DE SU ODE lo19l lM lB l@ lA l@ l X l@ l V l A l L l V i E l X l@ J@ l Nl@

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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECT lVE ACTIONS h liloll The cause of this event has been attributed to oersonnel error.

Root I

li li I l Valve N62-F064A was found to be closed.

Valve N62-F064A was ooened I

ii i7i I and N62-N009A was returned to service.

The unit is now in full I

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compl iance.

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LER No.: 50-321/1981-056 Licensee: Georgia Power Company Facility:

Edwin I. Hatch Docket No. : 50-321

Narrative

Report for LER 50-321/1981-056 While the plant was in start-up, IN62-N009A, Off-gas H2 Analyzer, was found to be inoperative. The event date is unknown, but was reported inoperative on June 10, 1981. Tech Specs Table 2.1.3.h, page 2-7, requires one operable channel.

Redundant H2 Analyzer, IN62-N009B, was operable.

The health Plant operation was not affected as a result of this event.

and safety of the public was not affected.

This is a repetitive event as last reported on Reportable Occurrence Report 50-321/1980-094.

The cause of this event has been attributed to personnel error.

Root Valve, N62-F064A, was found to be closed. Valve N62-F064A was opened and N62-N009A returned to service.

The unit is now in full compliance with the requirements and no further reporting is required.

A generic review revealed no inherent problems.

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Georg a Power Company Post Ott,ce Box e42 Bauley. Georgta 31513 op}.1CIAL Cf ti>1' r 'eonone912 367 778, e

912 537-9444 m

Edwin 1. Hatch Nuclear Plani i. :l COrgia POWCT ttne sourtnwn eucre sywn July 2, 1981 PM-81-575

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PLANT E. I. HATCH Docket No. 50-321

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Licensee Event Report g

T3 United States Nuclear Regulatory Commission 6

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Office of Inspection and Enforcement

%E Region II Suite 3100 101 Marietta Street

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g Atlanta, Georgia 30303 T /I ATTENTION:

Mr. James P. 0'Reilij Pursuant to Section 6.9.1.9.c of Hatch Unit I Technical Specifications, please find attached Reportable Occurrence Report No.50-321/1981-056.

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Plant Manager MM/RTN/mla xc:

J. H. Miller, Jr.

R. J. Kelly W. A. Widner J. T. Beckham, Jr.

C. L. Coggin R. D. Baker Control R00m ff File [4

U. S. NUCLEAR REGULATORY COMMISSION NRC FOFIM 366 17 77)

LICENSEE EVENT REPORT CONTROL BLOCK: l l

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60 61 OOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l While the clart was in start-uo.1N62-N009A. O'f-nas H3 Analyzer was l

[ol3} l found to be inoperative.

The event date is unknown, but reported in-I lo l4 l l operative on June 10, 1981.

Tech Specs Table 2.1.3.h reou f res one ooer-I lo Is! l able channel.

Redundant H2 Analyzer., IN62-N0098, was operable. Plant I

lo is ] l operation nor the health and safety of the oublic was not affected by 1

l0l7ll this event.

This is a repetitive event is last reported on Reportable l

loisl l Occurrence Report No. 50-321/1980-094.

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40 41 42 43 44 47 CAUSE DESCRIPTIO:'i AND CORRECTIVE ACTIONS h lilo1l The cause of this event has been attributed to oersonnel error.

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li liI i Valve N62-F064A was found to be closed.

Valve N62-F064A was oopned I

t iii2i l and J62-N009A was returned to service.

The unit is now in full I

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LER No. :

50-321/1981-056 Licensee: Georgia Power Company Facility:

Edwin I. Hatch Pocket No.:

50-321 Narrative Report for LER 50-321/1981-056 While the plant was in start-up, IN62-N009A, Off-gas H2 Analyzer, was found to be inoperative. The event date is unknown, but was reported inoperative on June 10, 1981.

Tech Specs Table 2.1.3.h, page 2-7, requires one operable channel.

Redundant H2 Analyzer, IN62-N0098, was operable.

Plant operation was not affected as a result of this event.

The health and safety of the public was not affected.

This is a repetitive event as last reported on Reportable Occurrence Report 50-321/1980-094.

The cause of this eveng has been attributed to personnel error.

Root Valve, N62-F064A, wbs Qfbund to be closed.

Valve N62-F064A was opened and N62-N009A returned to service.

The unit is now in full compliance with the requirements and no further reporting is required.

A generic review revealed no inherent problems.

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