05000321/LER-1981-072-03, /03L-0:on 810707,instrument Root Valve B21-F500 for Low Condenser Vacuum Switches Had Been Isolated Causing Instruments to Trip.Cause Unknown.Valve Returned to Correct Position.Root Valves Locked Open

From kanterella
(Redirected from ML20009F454)
Jump to navigation Jump to search
/03L-0:on 810707,instrument Root Valve B21-F500 for Low Condenser Vacuum Switches Had Been Isolated Causing Instruments to Trip.Cause Unknown.Valve Returned to Correct Position.Root Valves Locked Open
ML20009F454
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/21/1981
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F451 List:
References
LER-81-072-03L, LER-81-72-3L, NUDOCS 8107310170
Download: ML20009F454 (2)


LER-1981-072, /03L-0:on 810707,instrument Root Valve B21-F500 for Low Condenser Vacuum Switches Had Been Isolated Causing Instruments to Trip.Cause Unknown.Valve Returned to Correct Position.Root Valves Locked Open
Event date:
Report date:
3211981072R03 - NRC Website

text

l NRC FORM 366 U5 S. NUCLEAR REGULATORY COMMISSION

! (7 77)

LICENSEE EVENT REPORT e

CONTROL BLOCK: l l

l l

l l

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATioN) 1 6

lo lil lG l A lE II lH l1 l@l0 lo l_ lo l0 lo lo lo l_ lo lo l@l 4l 1l 1] 1] 1l@l l

l@

7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 L6 CENSE TYPE JO bl CAT 58 CON'T 10111 S[RC! l Ll@l0 15 10 10 l0 l3 12 l1 l@l 01 71 01 71 81 1 l@l 017 l 2l 1l8 l1 l@

7 8

60 61 OOCKiT NUMBER 68 69 EVENT DATE 14 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Ol2l lFollowing a reactor scram it was discovered that the instrument root j

[O i3 i l valve (B21-F500) for the low condenser vacuum switches (821-N056A,8) had i 10141 l bpon isolated. therphy. causing the instruments to be in the trin condi l lo151Itina.

Thorp were no effects uoon the oublic health and safety due to

_j nonrecetitive occurrence for the sub.iect valve andl 10161 I th i c nunnt This is a I

101) Ilswitches.

I 101811 oO E

CODE SU8CO E COMPONENT COOE SL8C DE SU E

lo191 i S lH l@ U@ l XI@ l V l A l L l V l E l X l@ l A l@ l Dl@

7 8

9 10 11 12 13 18 19 2u SEQUENTIAL OCCURRENCE REPORT REVISION

_ EVENT YE AR REPORT NO.

CODE TYPE NO.

b "LER ROl2181 Il l-l l 017121 l/l 1013 l lL l l-l l0 l Nug E

22 23 24 26 27 28 29 30 31 32 TAK N A T ON ON PL NT ME HCURS 22 S 8 IT FO b B.

SUPPLIE MANUFACTURER IX l@l Fl@

l Zl@

l Z l@

l010l0l0l l Y l@

lYl@

lAl@

lC161310l@

33 34 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilolIThe exact cause of valve misposition is not known.

Upon discovery, the l [i ti j l valve was returned to the correct position.

All low condenser vacuum I

ii#2i iroot valves have been locked open in a manner to prevent recurrence of I

tilai l inadvertent closing.

I I

l i i 41 I 80

/

8 9 STA S

% POWER OTHER STATUS IS O RY DISCOVERY DESCRIPTION Ii Is l l G l@ l 0l 0l Ol@l NA l

lAl@l Operator Observation l

ACTIVI TY CO TENT RELEAS5 AMOUNT OF ACTIVITY LOCATION OF RELEASE l i 16 I W @0 OF RELEASED @l NA l

L NA l

1 8 3 10 11 44 45 80 PERSONNEL EXPOSURES NUY8ER

DESCRIPTION

l i l 71 101 O l 0 hl TYPE @l Z

NA l

80 2

u PERSONNE t IN;u'R,,,

NUV8E R

DESCRIPTION

li lx l I o l o l 0 l@l NA l

go 7

8 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE

DESCRIPTION

"^

I U_12J LzJ@l 8107310170 810721 ao 7

8 9 10 PusuCiTY PDR ADOCK 05000321 NRC USE ONLY 4

PDR M [fj{Jhl ESCRIPTION ISSU E D D

g l

llllllllll lll{

NA 68 69 80 5 7

8 9 10 912-367-7851 2,

C. I rocain. Suot. Plt. Ena. Serv. psone:

MMF PREPARER

O LER #:

50-321/1981-072 Licensee:

Georgia Power Company Facility Name:

Edwin I. Hatch Docket #:

50-321

Narrative

Report for LER 50-321/1981-072 1

Following a Rx scram it was discovered that the instrument root valve (B21-F500) for the low condenser vacuum switches (B21-N056AGB) had been isolated, thereby, causing the instrum-ents to be in the trip condition.

This, in fa't, had caused a c

group 1

isolation and subsequently precipitated the reactor geram.

Redundant switches were available and operable.

The exact cause of the valve misposition is not known.

- In order to prevent recurrence the isolation valvesefor all low conden-ser vacuum switches on HNP-152 have been locked open in a

'aanner to prevent closing the valves without first removing the locking mechanism.

4 i

r,-

7