05000321/LER-1981-063-03, /03L-0:on 810630,high Pressure Core Injection Steamline Switch Found to Acutate High.Caused by Setpoint Drift.Switch Recalibr & Returned to Svc

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/03L-0:on 810630,high Pressure Core Injection Steamline Switch Found to Acutate High.Caused by Setpoint Drift.Switch Recalibr & Returned to Svc
ML20009E668
Person / Time
Site: Hatch 
Issue date: 07/17/1981
From:
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009E659 List:
References
LER-81-063-03L-01, LER-81-63-3L-1, NUDOCS 8107280348
Download: ML20009E668 (2)


LER-1981-063, /03L-0:on 810630,high Pressure Core Injection Steamline Switch Found to Acutate High.Caused by Setpoint Drift.Switch Recalibr & Returned to Svc
Event date:
Report date:
3211981063R03 - NRC Website

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60 61 DOCK ET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 CVENT DESCRIPTION AND PROBABLE CONSECUENCES h o ! fl l While the plant was in steady state coeration at 2376 Mit and cerforming i

o !3: I surveillance on HPCI Steam Line aP Instrumentation, 1E41-N005. HPCI l

ojal l Steamline AP Switch, was found to acutate at 243" H 0.

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3.2-2, Item 11, recuires actuation at 5+216" HoO - 37" H,o head correction.

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,oisl l repetitive event as last reported on Reportable occurrence 50-321/1979-102.

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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS jiioil The cause of this event was switch setDoint drift.

The Barton AP Switch i

1 li li i i was reca'ibrated and returned to service.

The unit is now in full com-1 l

i,,7i i pliance with the requiremer.ts.

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I LER No. :

50-321/1981-063 Licensee:

Georgia Power Company Facility:

P.lant Edwin I. Hatch Docket No. :

50-321

Narrative

Report for LER 50-321/1981-063 On June 30, 1981, while the plant was in steady state operation and performing surveillance on HPCI Steam Line Differential Pressure (flow)

Instrumentation,1E41-N005, HPCI Steam Line AP Switch, -was found to actuate at 243" H 0.

Tech Specs 3.2-2, Item 11, requires actuation at 5216" H 0 -

2 2

37" H O head correction.

This corresponds to 5300% of normal steam flow.

2 Redundant flow switch 1E41-N004 was operable.

Plant operation was not affected by this event. The health and safety of the public was not affected.

This is a repetitive event as last reported on Reportable Occurrence P.eport No. 50-321/1979-102.

T Ll'n The cause of this edent was switch setpoint drift.

The Barton AP Switch was recalibrated and returned to service.

The unit is now in full compliance with the requirements.

This type of Barton AP switch is used in the HPCI and RCIC systems on both units at Plant Hatch. Although several Reportable Occurrences have been written on these instruments, the problem is not believed to be generic in nature.

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