05000333/LER-1981-048-03, /03L-0:on 810604,during Normal Operation,Drywell Equipment Drain Sump Pump B Lost Suction.Cause & Corrective Action Will Be Determined at Future Plant Outage

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/03L-0:on 810604,during Normal Operation,Drywell Equipment Drain Sump Pump B Lost Suction.Cause & Corrective Action Will Be Determined at Future Plant Outage
ML20009A658
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 07/02/1981
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009A655 List:
References
LER-81-048-03L, LER-81-48-3L, NUDOCS 8107130446
Download: ML20009A658 (1)


LER-1981-048, /03L-0:on 810604,during Normal Operation,Drywell Equipment Drain Sump Pump B Lost Suction.Cause & Corrective Action Will Be Determined at Future Plant Outage
Event date:
Report date:
3331981048R03 - NRC Website

text

NRC FOR1Wl *J54 U, S. NUCLEAR RE:ULATORY COMMISSloN 0 771 ~

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63 61 DOCK E T NUMBER 68 63 EVENT OATE 14 iS REPORT DATE EO EVENT DESCntPTION AND PROB ABLE CONSEQUENCES h I'O TTI I INTERIM REPORT:

Durina normal operation. drywell eaulement drain sumo pumo 'B' l

10131 l lost suction and could nCt effect sump pump out.

Pump

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0 4 l the leakage monitoring system, which provides sump level, pumpout flow rate and I

O s I flow jntegration used to neet TS 4.6.D, were fully operable.

TS 3.6 3.2 was not i

ITITI I clear with respect to pumci operabili ty recuirements however, the abilitv to 1

0 7 I monitor and determing leal <aae was not imoaired.

No slanificant hazard existed.

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i i i plant outage.

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LER 81-021 is a related event.

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