05000219/LER-1981-021-03, /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage

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/03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage
ML20009A549
Person / Time
Site: Oyster Creek
Issue date: 07/01/1981
From: Riggle E
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009A541 List:
References
LER-81-021-03L, LER-81-21-3L, NUDOCS 8107130301
Download: ML20009A549 (1)


LER-1981-021, /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage
Event date:
Report date:
2191981021R03 - NRC Website

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