05000364/LER-1981-002-03, /03L-0:on 810525,during Testing,Steam Generator Code Safety Valve on Steam Line B Opened & Did Not Reseat. Cause Unknown.Valve Returned to Mfg for Investigation & Replaced

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/03L-0:on 810525,during Testing,Steam Generator Code Safety Valve on Steam Line B Opened & Did Not Reseat. Cause Unknown.Valve Returned to Mfg for Investigation & Replaced
ML20004F960
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/23/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004F954 List:
References
LER-81-002-03L, LER-81-2-3L, NUDOCS 8106260346
Download: ML20004F960 (1)


LER-1981-002, /03L-0:on 810525,during Testing,Steam Generator Code Safety Valve on Steam Line B Opened & Did Not Reseat. Cause Unknown.Valve Returned to Mfg for Investigation & Replaced
Event date:
Report date:
3641981002R03 - NRC Website

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'80 el OCCKET NUMBI A 64 69 EVENT OATE 74 75 AE7 CAT oATE 80 EVENT DESCRIPTION AND PROSAaLE CONSECUENCES h' o 121 l At 1540 on s/25/81, while performing Phase 3 test procedure 083-7-s27 (Dvnamic Automatic l 57T) l Stears Dump Operability Test), a steam generator code safety valve ofrthE "B" steam line l

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