05000364/LER-1981-006-03, /03L-0:on 810421 & 22,diesel Generator 2B Failed to Reach Rated Speed in Required Time.Cause Not Stated.Fuel Oil Day Tank Foot Valve Replaced & Fuel Line Check Valves Cleaned

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/03L-0:on 810421 & 22,diesel Generator 2B Failed to Reach Rated Speed in Required Time.Cause Not Stated.Fuel Oil Day Tank Foot Valve Replaced & Fuel Line Check Valves Cleaned
ML20004F640
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/12/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004F638 List:
References
LER-81-006-03L, LER-81-6-3L, NUDOCS 8106190322
Download: ML20004F640 (2)


LER-1981-006, /03L-0:on 810421 & 22,diesel Generator 2B Failed to Reach Rated Speed in Required Time.Cause Not Stated.Fuel Oil Day Tank Foot Valve Replaced & Fuel Line Check Valves Cleaned
Event date:
Report date:
3641981006R03 - NRC Website

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3 63 68 QC0KET %M3 ER 63 69 EVENT OATE 74 73 REPORT OATE EJ EVENT DESCRIPTION AND PROB AStE CC.NSECUENCES O'o lo 121 [ At 1826 on 4/21/81 and 1100 on 4/22/81, diesel generator 2B was declared ino'perable whan g 4 a ; 21 [it failed to reach rated speed in less than 10 seconds. Tech. Spec. 3.8.1.1, in part,

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'ilt i 123 was restarted, successfullv reached rated speed and voltace in less than 10 secends I

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