LER-1981-022, /01T-0:on 810520,secondary Containment Integrity Not Maintained Due to Personnel Access Airlock Doors Ajar. Caused by Personnel Error & Loosened Striker Plate on Inside Door.Outside Door Closed & Striker Plate Repaired |
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8 9 to 68 66 go.; i Michael J. Fitzgerald (609) 693-6038 o-NAME OF PRE 8ARER PHCNE:
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OYSTER CREEK NIX 1 EAR GENERATING STATICN Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/81-22/01T Report Date June 3, 1981 Occurrence Date i
May 20, 1981 l
Identification of Occurrence A violation of Technical Specifications, paragraph 3.5.B.1 occurral when secondary contaht integrity was not maintainal at all times. Both personnel access airlock doors en the Northwest side of the Peactor 9141 ding were found ajar.
'Ihis event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.a.6.
conditions Prior to Occurrence The plant was shutdown in the REEUEL Itode with reactor tatperature less than 2120F.
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yescription of Occurrence At approximately 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on May 20, the offgoing drywell Security Guard discovered both the inside and outside (NW corner, 23' elevation) Reactor Building personnel access airlock doors ajar. In this configuration the door interlock systen prevents either door frcm closing. The Group Shift Supervisor was imadintely notified and the problem was corrected by bypassing the inter-lock systen and closing the doors. The doors had been checked earlier on the 4-12 shift and were found closed. It is postulated that when the inside door failed to close due to a loosened striker plate, the outside door was opened using the installed interlock bypass systen by persons unknown. Once both doors were open the interlock prevented them frcxn closing.
Apparent cause of Occurrence The cause of the occurrence was attributed to personnel error. Although the 3
inside door failed to close due to a' loosened striker plate, the interlock protecting the 'seccnd door frcm opening had to be deliberately bypassed.
Analysis of Occurrence Secondary containment is designed to minurize any ground release of radioactive materials which might result frcxn a serious accident. 'Ihe Beactor Building provides secondary containment during reactor operation when the drywell is sealed and in service and provides prirrary containment when the reactor is shutdown and the drywell is open.
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Reportable Occurrence Page 2 Report No. 50-219/81-22/0lT Mien this event occurred, all of the requiremnts of the Technical Specifications
. paragrapt 3.5.B.1, except for the reactor mode switch position, were met for conditions which do not require secondary containment integrity. 'Ihe reactor mode switch was in "REEUEL", whereas the Technical Specifications required "SifrIDCm" if secondary containment integrity is not maintained. In strmary, the major functional requirenents were met for conditions not requiring secondary containment integrity.
Corrective Action
The offgoing Security Guard inmiiately notified the Group Shift Supervisor, who closed the outside door by manually overriding the interlock mechanism. Within several minutes Mechanical Maintenance personnel repaired the loosened striker plate on tra inner door and the doors were returned to service. Currently, as
~ part of the General Enployee Training, the proper operation of personnel airlock doors is addressed. The secondary containment airlock doors and interlock mechanism will be added to the P.M. schedule to reduce the possibility of door malfunctions which may result in individuals bypassing the interlock.
Failure Data Not Applicable.
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| 05000219/LER-1981-001-03, /03L-0:on 810102,containment Spray Sys High Drywell Pressure Indicating Switch IP-15C Tripped Above Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset & Study Examining Causes of Repeatability Undertaken | /03L-0:on 810102,containment Spray Sys High Drywell Pressure Indicating Switch IP-15C Tripped Above Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset & Study Examining Causes of Repeatability Undertaken | | | 05000219/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000219/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000219/LER-1981-002-03, /03L-0:on 810102,gaseous Releases to Stack Found Not Continuously Monitored as Required by Tech Spec.Caused by Tripping of Stack Gas Sample Pump Due to Normal Wear.Pump Replaced W/Spare | /03L-0:on 810102,gaseous Releases to Stack Found Not Continuously Monitored as Required by Tech Spec.Caused by Tripping of Stack Gas Sample Pump Due to Normal Wear.Pump Replaced W/Spare | | | 05000219/LER-1981-003-03, /03L-0:on 810112,during Visual Insp of Fire Hydrants,Hydrant 2 Found to Contain Frozen Water in Barrel, Rendering Hydrant Inoperable.Caused by Water Leaking from Hydrant Valve & Freezing in Barrel.Hydrant Thawed | /03L-0:on 810112,during Visual Insp of Fire Hydrants,Hydrant 2 Found to Contain Frozen Water in Barrel, Rendering Hydrant Inoperable.Caused by Water Leaking from Hydrant Valve & Freezing in Barrel.Hydrant Thawed | | | 05000219/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000219/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000219/LER-1981-004-01, /01T-0:on 810116,studies Indicated That Emergency Diesel Generators May Exceed Load Rating During Accident Conditions.Caused by Using Different & More Conservative Methods to Calculate Load.Actions to Reduce Load Underway | /01T-0:on 810116,studies Indicated That Emergency Diesel Generators May Exceed Load Rating During Accident Conditions.Caused by Using Different & More Conservative Methods to Calculate Load.Actions to Reduce Load Underway | | | 05000219/LER-1981-005-03, /03L-0:on 810106,emergency Svc Water Pump 52B Current & Discharge Pressure Found Outside Tech Spec. Probably Caused by Clogged Pump Suction Strainer.Strainer Cleared | /03L-0:on 810106,emergency Svc Water Pump 52B Current & Discharge Pressure Found Outside Tech Spec. Probably Caused by Clogged Pump Suction Strainer.Strainer Cleared | | | 05000219/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000219/LER-1981-006-03, /03L-0:on 810115,during Surveillance Testing, Reactor Triple Low Water Level Indicator Switch RE-18B Tripped at Monometer Reading Higher than Allowed by Tech Spec Table 3.1.1.Caused by Instrument Drift.Switch Reset | /03L-0:on 810115,during Surveillance Testing, Reactor Triple Low Water Level Indicator Switch RE-18B Tripped at Monometer Reading Higher than Allowed by Tech Spec Table 3.1.1.Caused by Instrument Drift.Switch Reset | | | 05000219/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000219/LER-1981-007-03, /03L-0:on 810202,water-tight Door to Containment Spray Sys I Compartment Not Closed & Verification of Closed Door Not Performed.Caused by Personnel Error & Lack of Controls to Ensure Doors Are Closed After Passage | /03L-0:on 810202,water-tight Door to Containment Spray Sys I Compartment Not Closed & Verification of Closed Door Not Performed.Caused by Personnel Error & Lack of Controls to Ensure Doors Are Closed After Passage | | | 05000219/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000219/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000219/LER-1981-008-03, /03L-0:on 810210,water Seepage Observed Along West Wall of Nrw Bldg.Direct Survey Showed Detectable Ground Contamination Only within 6 Inches of Wall.Caused by High Levels in Tank Vaults.Herculite Secured & Sealed to Wall | /03L-0:on 810210,water Seepage Observed Along West Wall of Nrw Bldg.Direct Survey Showed Detectable Ground Contamination Only within 6 Inches of Wall.Caused by High Levels in Tank Vaults.Herculite Secured & Sealed to Wall | | | 05000219/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000219/LER-1981-009-03, /03L-0:on 810213,snubber 23/3 Found W/Very Low Oil Level & Oil Discovered on Floor at Base Connection During NRC walk-around Insp.Caused by Failure of Inner Shaft Seal Due to Deterioration.Snubber Replaced W/Operable Spare | /03L-0:on 810213,snubber 23/3 Found W/Very Low Oil Level & Oil Discovered on Floor at Base Connection During NRC walk-around Insp.Caused by Failure of Inner Shaft Seal Due to Deterioration.Snubber Replaced W/Operable Spare | | | 05000219/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000219/LER-1981-010-03, /03L-0:on 810202,during Routine Surveillance Testing,Main Steamline High Radiation Monitor RN-06B Tripped at Value Higher That Tech Spec Limits.Caused by Failure to Revise Trip Settings.Trip Settings Lowered | /03L-0:on 810202,during Routine Surveillance Testing,Main Steamline High Radiation Monitor RN-06B Tripped at Value Higher That Tech Spec Limits.Caused by Failure to Revise Trip Settings.Trip Settings Lowered | | | 05000219/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Encl | Forwards LER 81-011/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-011-03, /03L-0:on 810309,isolation Condenser Condensate Return Line Pipe Break Sensor IB11B2 Found to Trip at Value Greater than That Specified in Tech Specs.Caused by Instrument Repeatability.Replacement Recommended | /03L-0:on 810309,isolation Condenser Condensate Return Line Pipe Break Sensor IB11B2 Found to Trip at Value Greater than That Specified in Tech Specs.Caused by Instrument Repeatability.Replacement Recommended | | | 05000219/LER-1981-012-03, /03L-0:on 810313,electromatic Relief Valve High Pressure Actuation Switches 1A83C & 1A83E Tripped Higher than Limit Specified in Tech Spec.Caused by Instrument Repeatability.Pressure Sensors Reset to Trip within Limits | /03L-0:on 810313,electromatic Relief Valve High Pressure Actuation Switches 1A83C & 1A83E Tripped Higher than Limit Specified in Tech Spec.Caused by Instrument Repeatability.Pressure Sensors Reset to Trip within Limits | | | 05000219/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-013-03, /03L-0:on 810319,core Spray Hi Drywell Pressure Switch RV46B Tripped in Excess of 2 Psi Tech Spec.Caused by Sensor Repeatability.Sensor Recalibr.Replacement of Sensors Recommended by PORC | /03L-0:on 810319,core Spray Hi Drywell Pressure Switch RV46B Tripped in Excess of 2 Psi Tech Spec.Caused by Sensor Repeatability.Sensor Recalibr.Replacement of Sensors Recommended by PORC | | | 05000219/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-014, Forwards LER 81-014/01T-0.Detailed Event Analysis Encl | Forwards LER 81-014/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-014-01, /01T-0:on 810401,containment Oxygen Concentration Was Not Reduced to Less than 5% within 24-h After Placing Reactor Mode Switch in Run.Caused by Inerting at Significantly Reduced Rates | /01T-0:on 810401,containment Oxygen Concentration Was Not Reduced to Less than 5% within 24-h After Placing Reactor Mode Switch in Run.Caused by Inerting at Significantly Reduced Rates | | | 05000219/LER-1981-015-03, /03L-0:on 810324,main Steam Line High Flow Sensors Tripped at Values Greater than Tech Specs Limit.Caused by Instrument Repeatability.Both Sensors Reset | /03L-0:on 810324,main Steam Line High Flow Sensors Tripped at Values Greater than Tech Specs Limit.Caused by Instrument Repeatability.Both Sensors Reset | | | 05000219/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-016-03, /03L-0:on 810421,approx 10,000 Gallons of Leakage from Condensate Transfer Pump Bldg Was Discovered on North & South Sides of Bldg.Caused by Loss of Valve Packing on V-2-88.Leakage Was Diked & Valve Repacked | /03L-0:on 810421,approx 10,000 Gallons of Leakage from Condensate Transfer Pump Bldg Was Discovered on North & South Sides of Bldg.Caused by Loss of Valve Packing on V-2-88.Leakage Was Diked & Valve Repacked | | | 05000219/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000219/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-017-03, /03L-0:on 810415,one Containment Spray Sys Loop Considered Inoperable During Normal Operation.Caused by Large Amount of Sea Lettuce in Intake Canal,Overwhelming Trash Removal Sys.Circulating Water Pump Stopped | /03L-0:on 810415,one Containment Spray Sys Loop Considered Inoperable During Normal Operation.Caused by Large Amount of Sea Lettuce in Intake Canal,Overwhelming Trash Removal Sys.Circulating Water Pump Stopped | | | 05000219/LER-1981-018, Forwards LER 81-018/01T-0.Detailed Event Analysis Encl | Forwards LER 81-018/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-018-01, /01T-0:on 810417,equipment Operator Found Valves Were Blocked from Fully Opening by Scaffolding Placed by Contractor Personnel.Caused by Personnel Error.Scaffolding Repositioned | /01T-0:on 810417,equipment Operator Found Valves Were Blocked from Fully Opening by Scaffolding Placed by Contractor Personnel.Caused by Personnel Error.Scaffolding Repositioned | | | 05000219/LER-1981-019-03, /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised | /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised | | | 05000219/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000219/LER-1981-020-03, /03L-0:on 810501,isolation Condenser Shell Level Instrument IGO6B Found Reading High During Annual Calibr. Caused by Evaporation of Instrument Ref Column.Column Backfilled W/Water to Normal Operating Level | /03L-0:on 810501,isolation Condenser Shell Level Instrument IGO6B Found Reading High During Annual Calibr. Caused by Evaporation of Instrument Ref Column.Column Backfilled W/Water to Normal Operating Level | | | 05000219/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-021-03, /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage | /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage | | | 05000219/LER-1981-022-01, /01T-0:on 810520,secondary Containment Integrity Not Maintained Due to Personnel Access Airlock Doors Ajar. Caused by Personnel Error & Loosened Striker Plate on Inside Door.Outside Door Closed & Striker Plate Repaired | /01T-0:on 810520,secondary Containment Integrity Not Maintained Due to Personnel Access Airlock Doors Ajar. Caused by Personnel Error & Loosened Striker Plate on Inside Door.Outside Door Closed & Striker Plate Repaired | | | 05000219/LER-1981-022, Forwards LER 81-022/01T-0 | Forwards LER 81-022/01T-0 | | | 05000219/LER-1981-023-03, /03L-0:on 810603,drywell Vented to Reduce Drywell Torus Differential Pressure.Caused by Moisture Buildup in Sensing Line Resulting in Erroneous Indication of Increased Oxygen Concentration.Procedures Will Be Reviewed | /03L-0:on 810603,drywell Vented to Reduce Drywell Torus Differential Pressure.Caused by Moisture Buildup in Sensing Line Resulting in Erroneous Indication of Increased Oxygen Concentration.Procedures Will Be Reviewed | | | 05000219/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-024-03, /03L-0:on 810608,while Operating in Degraded Mode, Two Emergency Water Pumps Found Inoperable.Caused by Faulty Ammeter,Clogged Pump Suction Bells & Inadequate Administrative Controls.Ammeter Replaced & Bells Cleaned | /03L-0:on 810608,while Operating in Degraded Mode, Two Emergency Water Pumps Found Inoperable.Caused by Faulty Ammeter,Clogged Pump Suction Bells & Inadequate Administrative Controls.Ammeter Replaced & Bells Cleaned | | | 05000219/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-025-01, /01T-0:on 810617,secondary Containment Was Broken When Both Reactor Bldg Railroad Airlock Doors Were Opened Together.Caused by Failure of Top Inner Door Latch & Operator Error.Operators Will Be Reinstructed | /01T-0:on 810617,secondary Containment Was Broken When Both Reactor Bldg Railroad Airlock Doors Were Opened Together.Caused by Failure of Top Inner Door Latch & Operator Error.Operators Will Be Reinstructed | | | 05000219/LER-1981-025, Forwards LER 81-025/01T-0.Detailed Event Analysis Encl | Forwards LER 81-025/01T-0.Detailed Event Analysis Encl | |
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