05000333/LER-1981-037-03, /03L-0:on 810427,average Planar Linear Heat Generation Rate Surveillance Found Not Performed on 810420, 21 & 23 Per Tech Spec 4.5.H.Caused by Personnel Error. Personnel Will Review Event Rept to Prevent Recurrence

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/03L-0:on 810427,average Planar Linear Heat Generation Rate Surveillance Found Not Performed on 810420, 21 & 23 Per Tech Spec 4.5.H.Caused by Personnel Error. Personnel Will Review Event Rept to Prevent Recurrence
ML20004B155
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 05/21/1981
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004B154 List:
References
LER-81-037-03L, LER-81-37-3L, NUDOCS 8105270306
Download: ML20004B155 (1)


LER-1981-037, /03L-0:on 810427,average Planar Linear Heat Generation Rate Surveillance Found Not Performed on 810420, 21 & 23 Per Tech Spec 4.5.H.Caused by Personnel Error. Personnel Will Review Event Rept to Prevent Recurrence
Event date:
Report date:
3331981037R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSloll (7 77)

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8 60 61 DOCKET NUYBER 68 63 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PRCS ABLE CoNSECUENCES 10 !:l l During normal operation, as a result of management review, it was discovered that I g o ;3, ; part of the Average Planar Linear Heat Generation Rate (APLHGR) surveillance 1

lo ja; j required by TS 4.5.H was not performed on 4/20/81, 4/21/81 and 4/23/81.

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