05000348/LER-1981-012-03, /03L-0:on 810402,during Testing of Containment 1A Spray Pump,Containment Spray Sys Snubber CS2-Rl31 Declared Inoperable Upon Discovery of Hydraulic Fluid Leakage.Caused by Cracked Reservoir.Reservoir Replaced

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/03L-0:on 810402,during Testing of Containment 1A Spray Pump,Containment Spray Sys Snubber CS2-Rl31 Declared Inoperable Upon Discovery of Hydraulic Fluid Leakage.Caused by Cracked Reservoir.Reservoir Replaced
ML20003H973
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 05/04/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20003H971 List:
References
LER-81-012-03L, LER-81-12-3L, NUDOCS 8105080256
Download: ML20003H973 (1)


LER-1981-012, /03L-0:on 810402,during Testing of Containment 1A Spray Pump,Containment Spray Sys Snubber CS2-Rl31 Declared Inoperable Upon Discovery of Hydraulic Fluid Leakage.Caused by Cracked Reservoir.Reservoir Replaced
Event date:
Report date:
3481981012R03 - NRC Website

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COCKET NUM8ER 6d 69 EVENT DATE 74 75 REPORT DATE 63 EVENT DESCRIPTION AND PRC9ABLE CONSEQUENCES h IC i2l l At 0900 on 4/2/81, during testing of 1A containment stiray mro, contairrent spray l

systcm snubber CS2 - R131 was declared inoperable sten it was noted that all of the i

1a ia # l Io # 4 i i hydraulic fluid had leaked frcm the snubber. Tech. Spec. 3.7.9.1, in part, requires CS2 - R131 to be operable. Tech. Spec. 3.7.9.1 action statecent requirenents were i o,3, i

io,,,i met. Health / safety of the public was not affected by this occurrence.

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