05000321/LER-1981-027-03, /03L-0:on 810406,feedwater Valve B21-F032A Was Determined Not to Pressurize.Caused by Excessive Leakage. Investigation Underway.Valve Will Be Repaired

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/03L-0:on 810406,feedwater Valve B21-F032A Was Determined Not to Pressurize.Caused by Excessive Leakage. Investigation Underway.Valve Will Be Repaired
ML20003G472
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 04/23/1981
From:
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20003G471 List:
References
LER-81-027-03L, LER-81-27-3L, NUDOCS 8104290575
Download: ML20003G472 (2)


LER-1981-027, /03L-0:on 810406,feedwater Valve B21-F032A Was Determined Not to Pressurize.Caused by Excessive Leakage. Investigation Underway.Valve Will Be Repaired
Event date:
Report date:
3211981027R03 - NRC Website

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EVENT DESCRIPTloN AND PROBABLE CONSEQUENCES h o 12110n 3-30-81, with Unit I shutdown for a refuelina/ torus modification out-1 On 4-6-81, 1

o lai Lage LLRT of the feedwater valv_e B21-F032A was performed.

I Io 14J [the LLRT coordinator reviewed the data sheets, and it was determined This would t f a lsi lthat the valve would not pressurize due to excessive leakage.

O 6 Icause the.60 La limit of Tech Snecs 4.7.A.2.G to be exceeded.

This is 1 1017] la repetitive occurrence - refer to LER 50-321/1981-024.

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I' 1018] leffects on public health or safety due to this event.

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33 34 Jb 36 37 43 di 42 43 44 47 CAUSE DESCRIPTloN AND CORRECTIVE ACTIONS 27 lilolIThe cause of the valve leaking is unknown at the present time; an inves-1 itigation is underway.

The valve will be repaired and successfully re-I i i An update report will be j gi121 l tested prior to startup following the outage.

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50-321/1981-027 Licensce:

Georgia Power Company Facility Name:

Edwin I. Hatch Docket #:

50-321

Narrative

Report for LER 50-321/1981-027 On 3-30-81, with Unit 1 shutdown for a refueling / torus modif-ication outage local leakage rate tests of the feedwater check valve B21-F032 was performed per HNP-1-3952 (Primary Contain-ment Periodic Type B and Type C Leakage Tests).

On 4-06-81, the LLRT coordinator reviewed the data

sheet, and it was determined that the valve (B21-F032) was leaking'such that the test volume could not be pressurized.

This would cause the

.60 La overall allowable Icakage limit of Tech Specs 4.7.A.2.G to be exceeded.

This is a repetitive occurrence refer to LER 50-321/ 1981-024.

There were no effects on public health or safety.

\\c' The cause of the valves leaking is unknown at the present time; an investigation is underway.

The valve will be repaired and successfully retested prior to startup following the outage.

Im update report will be submitted.

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