05000333/LER-1981-015-03, /03L-0:on 810129,primary Containment Isolation Valve 10-MOV-39B Motor Contactor Tripped Due to Water Entering Motor Control Ctr from Electrical Conduit Outside Bldg.Caused by Const Deficiency.Motor Contactor Dried Out

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/03L-0:on 810129,primary Containment Isolation Valve 10-MOV-39B Motor Contactor Tripped Due to Water Entering Motor Control Ctr from Electrical Conduit Outside Bldg.Caused by Const Deficiency.Motor Contactor Dried Out
ML20003C124
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 02/23/1981
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003C121 List:
References
LER-81-015-03L, LER-81-15-3L, NUDOCS 8102260667
Download: ML20003C124 (1)


LER-1981-015, /03L-0:on 810129,primary Containment Isolation Valve 10-MOV-39B Motor Contactor Tripped Due to Water Entering Motor Control Ctr from Electrical Conduit Outside Bldg.Caused by Const Deficiency.Motor Contactor Dried Out
Event date:
Report date:
3331981015R03 - NRC Website

text

NRC FORM 263 U. S. NUCLEAR R EGULATORY COMMISSION 17 77)

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