LER-1980-016, /03L-0:on 801217,during Testing,Emergency Diesel Generator 4D Failed to Close in on Bus.Caused by Slippage of Flexible Shaft Coupling on Speed Sensing Frequency Generator Drive Shaft.Coupling Secured |
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| 2661980016R03 - NRC Website |
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60 68 OOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT OATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES h 1 o l a l l At 1210 hours0.014 days <br />0.336 hours <br />0.002 weeks <br />4.60405e-4 months <br />, 12-17-80, during testing the 4D emergency Diesel gener-I m l ator (common to Units 1 and 2) failed to close in on the bus.
The 3D 1
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.s ATTACHMENT TO LICENSEE EVENT ' REPORT NO. 80-016/03L Wisconsin Electric Power Company Point Beach Nuclear Plant, Unit 1 Docket No. 50-266 During an. Operations refueling test, Safety Injection with Loss of Engineered Safeguards AC - Unit 1, at 1210 hours0.014 days <br />0.336 hours <br />0.002 weeks <br />4.60405e-4 months <br /> December-17, 1980, the 4D emergency diesel generator, common to Units 1 and 2, failed to close in on the Unit 1 bus automatically.
The 3D emergency diesel generator was started and load tested at 1243 hours0.0144 days <br />0.345 hours <br />0.00206 weeks <br />4.729615e-4 months <br /> to verify its operability.
The 4D emcrgency diesel generator was returned-to-service at 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> after completion of initial repairs and testing.
Unit I was in the refueling cond1 tion.
Unit 2 was operating at full power.
4 The event led to a degraded mode of operation permitted by the Technical Specifications.
The redundant emergency diesel generator was operable and the public health and safety was not affected.
It should be noted that the 4D emergency diesel generator tested satisfactorily at 0536 hours0.0062 days <br />0.149 hours <br />8.862434e-4 weeks <br />2.03948e-4 months <br /> the same day, December 17, 1980, prior to performance of the Operations refueling test.
The event was due to a failure in the 4D emergency diesel generator speed sensing equipment.
Initially it was thought that the high speed relay setpoints (in the General Motors, Electromotive Division, Model EMD 8409614, speed sensine panel' assembly) had drifted preventing an indication of adequate engine speed to the bus breaker closing logic.
The setpoints were reset and the 4D emergency diesel generator was tested and returned-to-service that same day.
At 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br /> on December 30, 1980, the 4D emergency diesel generator was taken out-of-service for additional maintenance investigations regarding the' speed sensing panel relay setpoint drift.
At this time it was discovered that the basic cause for the event was not relay setpoint drift.
The event was caused by loosening of the setscrew that secures the flexible shaft coupling (General Motors, Electromotive Division, Part Number 8276102) to the frequency generator drive shaft.
This resulted in inadequate signal generation from the speed sensing frequency generator due to insufficient rotational energy transmission from the camshaft adapter to the frequency generator drive shaft.
The setscrew that locks the coupling to the shaft and the jam setscrew had both backed out of the coupling probably due to vibration.
As.a precautionary measure, both of the setscrews were replaced, lectighted, and staked.
The shaft coupling was secured and the 4D emergency diesel generator was tested and returned-to-service at 1312 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.99216e-4 months <br /> the same day.
Based upon four satisfactorv tests (December-17, 25. and two tests on the 27th), it was determined that the'4D emergency diesel cenerator would have nerformed its recuired safety function with the-initial setcoint adiustment.
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| 05000266/LER-1980-001-01, /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | | | 05000266/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-001-01, /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | | | 05000301/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-002-01, /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | | | 05000266/LER-1980-002, Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welde | Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welded | | | 05000266/LER-1980-002-01, /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | | | 05000301/LER-1980-002, Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | | | 05000266/LER-1980-003, Forwards LER 80-003/03T-0 | Forwards LER 80-003/03T-0 | | | 05000301/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000266/LER-1980-003-03, /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | | | 05000301/LER-1980-003-01, /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | | | 05000266/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000301/LER-1980-004-03, /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | | | 05000301/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000266/LER-1980-004-03, /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | | | 05000266/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-005-03, /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | | | 05000301/LER-1980-005-03, /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | | | 05000301/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-006-03, /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | | | 05000301/LER-1980-006-01, /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | | | 05000301/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000266/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000301/LER-1980-007-01, /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | | | 05000266/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-007-01, /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | | | 05000301/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000266/LER-1980-008-03, /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | | | 05000301/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000301/LER-1980-008-01, /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | | | 05000301/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000301/LER-1980-009-03, /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | | | 05000266/LER-1980-009, Forwards LER 80-009/01T-0 | Forwards LER 80-009/01T-0 | | | 05000266/LER-1980-009-01, /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | | | 05000266/LER-1980-010-03, /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | | | 05000266/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010-03, /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | | | 05000301/LER-1980-011-03, /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | | | 05000301/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011-03, /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | | | 05000266/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000266/LER-1980-012-03, /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | | | 05000301/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000301/LER-1980-012-03, /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | | | 05000266/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000266/LER-1980-013-01, /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | |
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