05000298/LER-1980-044-01, /01T-0:on 801115,reactor Scram Occurred & Normal Cooldown Rate Exceeded.Caused by Failed Card (Westinghouse- Hagan 398522) in Computer Controlled Turbine Control Sys Forcing Main Steam Bypass Valves to Remain Open

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/01T-0:on 801115,reactor Scram Occurred & Normal Cooldown Rate Exceeded.Caused by Failed Card (Westinghouse- Hagan 398522) in Computer Controlled Turbine Control Sys Forcing Main Steam Bypass Valves to Remain Open
ML20002B939
Person / Time
Site: Cooper Entergy icon.png
Issue date: 11/25/1980
From: Borer P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20002B938 List:
References
LER-80-044-01T, LER-80-44-1T, NUDOCS 8101070357
Download: ML20002B939 (1)


LER-1980-044, /01T-0:on 801115,reactor Scram Occurred & Normal Cooldown Rate Exceeded.Caused by Failed Card (Westinghouse- Hagan 398522) in Computer Controlled Turbine Control Sys Forcing Main Steam Bypass Valves to Remain Open
Event date:
Report date:
2981980044R01 - NRC Website

text

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RE POR T D ATE e,0 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l o 12 l l During APRM surveillance testing (S.P. 6.1.29), a reactor scram occurred.

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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i j o l l A failed card (Westinghouse-Hagan #398522) in the ecmouter controlled turbine con- !

en,rene I Ii ii l l trol svstem caused the main steam bvoass valves to rem in open f ol i n u f n c.

scram. The failed component was replaced and tested during the outage subsequent i i,,,,l to the scram.

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