LER-1980-030, /03L-0:on 801031,primary Containment Valve AO-2-1601-63 Required 30-s to Close.Caused by Malfunction of Pilot Solenoid SO-2-1601-71.Solenoid Replaced & Tested |
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U. E SaVCLEAR REGULATORY COMMIMtUN NCC FORM 366 I
(7 771 LICENSEE EVENT REPORT j
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60 6I COCKET NUVSE R 68 69 EVENT DATE 74 75 REPORT DATE 80 S
EVENT DESCRIPTION AND PROB ABLE CC,NSEQUENCES h After venting primary containment valve A0-2-1601-63, Standby Gas suction vent.
1 [3t:l l I: is, ;
required 30 seconds to respond to a closed sional.
Once the valve o m a ri to close I it closed in less than 10 seconds. The consequences were minimal because the slow l
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closure of A0-2-1601-63 would not have prevented the isolation of primary con-l
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- g # l tainment.
In addition, upstream isolation valves A0-2-1601-61, 62, and 23 were fully l l:);j l operable for primary containment isolation.
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VALVE SYSTEM
CAUSE
CAUSE
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42 4J 44 47 CAUSE DESCRIPTION AND CORRECT;VE ACTIONS h 6: t311 The cause of this occurrence is attributed to the malfunctionino of oilot solenoid l
J tt1l S0-2-1601-71 which had worn 0 rings. A0-2-1601-63 valve was left in the closed I
3.,.jj position. Solenoid 50-2-1601-71 was replaced and valve A0-2-1601-63 was stroked 1
) t.; j l three times satisfactorily on November 2, 1980.
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% POWER OTHER STATUS dis RY DISCOVERY DESCRIPTION NA l
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l !!llEl@ l0l9l8l@l A TivtTY CO TENT LOCATtON OP RELEASE 8tiLEASED OF RELEASE AVOUNT OF ACTivlTY NA l
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DESCRIP fiON 1
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i 9 to 309-654-2241, ext. ~ 172 i,
PHONE:
NAME OF PREP.ARER
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LER NUMBER: LER/R0 80-30/03L-0 i
11.
LICENSEE NAME: Commonwealth Edison Company a
quad-Cities Nuclear Power Station lll.
FACILITY NAME: Uni t Two IV.
D0,".KET NUMBER: 050-265 i
i V.
EVENT DESCRIPTION
1 On October 31, 1980, at 2:45 p.m., Unit Two was operating at 2464 MWt with a load of 812 MWe.
Primary Containment pressure reduction by vent.*ng to
- he Standby Gas Treatment System had Just been completed. The Standby Gas Treatment vent / suction valve A0-2-1601-63 required approximately 30 seconds i
to initially respond to.the signal to close from the Control Room. Once started, full closure of the valve was completed in less than 10 additional 4
seconds.
Technical Specification 3.7.D.I. requires that the A0-2-1601-63 valve operate within a maximum of 10 seconds. Work Request Q0878) was initiated to investigate and repair the valve malfunc :lon.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
The probable consequences o this occurrence were minimal. The slow 2
closure of the A0-2-1601-f3 valve would not have prevented the capability of the Primary Containme : System to isolate as designed. Valves A0 1601-60, A0-2-1601-61, oc "-1601-62 and A0-2-1601-23 which are located in-board toward the Primary ontainment, with respect to A0-2-1601-63, were fully operable. These valves could have properly isolated Primary Con-
)
tainment if a Group 11 PCI signal had occurred. This occurrence did not affect normal venting operations of the Primary Containment.
Radio-logical activity inside the drywell was low enough at the time to allow venting of Primary Containment through the Reactor Building ventilation exhaust system.
Vll.
CAUSE
[^
The cause of this occurrence was attributed to the malfunctioning of pilot i
solenoid valve 50-2-1601-71. The two-way solenoid-valve was discovered i'
to have worn 0-rings, which restricted free movement of the valve stem.
This 'resulted in 'the delayed response of A0-2-1601-63 The pilot tolenoid valve was manufactured by Versa Products, Model No. VSG-4322.
Vill. CORRECTIVE ACTION:
?
The corrective action tsken was to leave the A0-2-1601-63 valve in the closed position, thereby ensuring the capability of attaining Primary l
Containment until the precise cause of the malfunction could be identified and repaired. The pilot solenoid valve 50-2-1601-71 was replaced on November 2, 1980, and the valve was test' stroked three times satisfactorily.
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| 05000265/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001-03, /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | | | 05000254/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000254/LER-1980-002-03, /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | | | 05000265/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000265/LER-1980-002-03, /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | | | 05000265/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000265/LER-1980-003-03, /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | | | 05000254/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000254/LER-1980-003-03, /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | | | 05000254/LER-1980-004-03, /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | | | 05000254/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004-03, /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | | | 05000265/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000265/LER-1980-005-03, /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | | | 05000254/LER-1980-005-03, /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | | | 05000254/LER-1980-006-03, /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | | | 05000254/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000265/LER-1980-006-01, /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | | | 05000265/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000254/LER-1980-007-03, /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | | | 05000254/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000265/LER-1980-007-03, /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | | | 05000265/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000254/LER-1980-008-03, /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | | | 05000265/LER-1980-008-03, /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | | | 05000265/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000254/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000265/LER-1980-009-03, /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | | | 05000265/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-009-03, /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | | | 05000254/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-010-03, /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | | | 05000254/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-010-03, /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | | | 05000265/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-011-03, /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | | | 05000265/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-011-03, /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | | | 05000254/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000265/LER-1980-012-03, /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | | | 05000254/LER-1980-012-03, /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | | | 05000265/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000254/LER-1980-013-03, /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | | | 05000265/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000254/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000265/LER-1980-013-03, /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | |
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