ML20002A768

From kanterella
Jump to navigation Jump to search
LER 80-036/03L-0:on 801003,valve RW-AO-95 Would Not Close within Time Limit.Caused by Miller-64A One Piston Air Operator,Which Is Valve Operator on Discharge Valve,Not Closing.Valve Tested Satisfactorily for Last Four Wks
ML20002A768
Person / Time
Site: Cooper Entergy icon.png
Issue date: 10/31/1980
From: Scheer J
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20002A767 List:
References
LER-80-036-03L, LER-80-36-3L, NUDOCS 8011210499
Download: ML20002A768 (1)


Text

,

. ~

>"'3 *F O R M'366 U. S. NUCLE A17.EGULATOIY COMMISSION I h V LICENSEE EVENT REPORT CONTROL BLOCK' l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIREo (NFORMATIONI ITTT] l Nl LaCENSEE El ClCODE Pl RI 1l@l 01 d -l 0LacENSE 14 15 l 0 l NUMBER 0l Ol -l 0l Ol Ol@l 25 26 4 lLICENSE 1 l 1lTYPE Il J0 ll@l57 LATl 58 l@

7 8 9 CON'T IOI11 $$ "CE l Lj@l0 l 5 l 0 l 0 l 0 l 2j_9l 8l@l il 01 Ol 18 l 074l@l75 11 REPORT Ol 3lDATE11 8l Ol@80 7 6 60 61 DOCK ET NUuS ER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 [During normal operation whP e performing S.P. 6.3.1.4, RW-AO-95 would not close l I O l a i Iwithin T.S. time limit. RW-AO-95 is recuired to close in _< 15 seconds per RTS I o 4 13.7.D.1, Table 3.7.1. The valve was closed manually and no significant occurrence i IoIs1 Itook place. RW-AO-94 was tagged closed per Tech. Spec. 3.7.D.2. There were no ad- I 1016 I lverse nffects to nublic han11-h pnd unf 7, l

l l0 l 7 l l I

LO I R ] l "

7 8 9 OE COOE Susc E CovPONENT CODE Susc DE SL E Ld2]8 l M l A l@ [X,l@ IJ

[Zj@IJ- l Vl Al Ll Vl 0l Pl@ J@ ] @ its l9 10 7 9 to is SE QUE N TI AL OCCUR R E NCE R EFOR T REVISION tgR Ro EVENTYEAR REPORT NO. COOE TYPE NO.

@ tgg .,21 18101 22 l-l 23 1013 l 61 24 26 1/l 27 10131 23 29 i Ll 30 l-l 31 1 01 J2 i KEN A TO ON PLANT 4ET O HOURS S8 IT FOR S. SUPPLt %IANUF CTURER lC l@lJ4 Zl@ [ Z_j@ [Z_j@

36 l 0l Ol 0l 0l 31 40

[Nj@

41 l

l@ l43Z l@ lZ 1919 l947l@

44 JJ JS 42 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

l i l o I lA M111er-64A one piston air operator which is the valve operator on a discharge I i i Ivalve from drvwell ecuinment hn "C" would not close. The vMve han been tested I i 2 tweekly for the last four weeks and has operated properly. To prevent further occur- 1 y jrences, the valve cycle fTequency has been increased from quarterly to monthly. I I

mi 5 9 7 80 ST s  % POWER OTHERSTATUS SCO Y DISCOVERY DESCRIPTION W (JJ@

l0 'l 9 l 5 l@!o 32 NA 44 I I4sBl@las operator Observation 80 l

A!Tivity CC4 TENT -

RELE ASED OF RELE ASE AMOUNT OF ACTIVITV LOCATION OF RELEASE l

Ii IeI8 9W @ W@l 7 10 11 NA 44 l

45 NA 80 l

PER$0NNEL f APOSURES NuY8 t R TYPE DESCRIPTION 1 Til 101010 l@lz_j@l u l

' ' ' ' '2 "

n RSONNE L ,~20R'iES NUMME R DESCRIPTION EC I n l n i n l@l M 9 11 IJ u

80 I

L uss OF Ott DAMAGE TO F ACILITV Q TYPE DESCHiPf 80N v 8 L7J@l i n 'l to NA I 80 e

I E C641Pf 40N

.' o Nh,u@l NA l 1111till11i!l}

f M ') 10 ti8 69 80 5 Jerry L. Scheer 402-825-3811 NAVE OF PREPARER PHONE: {

sol un o V99

'