LER-1980-025, /01T-0:on 800913,ultrasonic Insp Revealed Crack Indications in Three Welds on Core Spray Loop a & Two Welds on Core Spray Loop B.Caused by Probable Metallurgical Failure.Elbows & Short Sections of Pipe Will Be Replaced |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2541980025R01 - NRC Website |
|
text
,,
LICENSEE EVENT REPORT O
- - - i i
i i + i ie 4.--n - E m Eoe--
e Llo lil I il LI Qi A l 0 l 1 l@l 0 l0 l0 l-l0 l0 l0 l - l 0 l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l l
l@
7 8 9 LICENSEE COOE 14 iS LICENSE NUMSER 25 26 LICENSE TYPE Jo 5 7 GAT 58 CON'T.
IoI1l
'"ERS l L l@l 0 l 5 l 0 l 0 l0 l2 l 5 l4-l@l 0 l 9 l 1 l 3 l 8 l 0 ]@l 0 l 9 l 2 l 3 l 8 l o l@
5 7
9 60 61 OOCKET NUMBER 6d 69 EVENT OATE 74 75 REPORT DATE do EVENT DESCRIPTION AND PROB A8LE CONSEQUENCES h 10121 l Ultrasonic inspections revealed crack indications in three welds on the "A" core spray l g o,3, I loop and two welds on the "B" core spray loop. All indications were located in the l
g l welds and heat affected of pipe-to-elbow and elbow-to-elbow section between the l
jo;,j l reactor vessel penetration and the first manual isolation valve. Three of the crack l
IO lo i l indications had propagated through the pipe wall. However, a significant leak would jol,; ; have been detected during operation, therefore, the probable consequences are minimal.
l 101811 I
'COI'E [O$E sis 8C$0E COMPONENT CODE SusC O'E 5
OE lO191 l SlFl @ { @ lL l@ l P ll l P lE lX lX l@ {@ ]@
7 A
9 to 11 12 13 18 19 20 SEQUENTIAL CCCURRENCE REPORT REVISION LER eRo EVENT YE AR REPORT NO.
COOE TYPE NO.
O aE y l218 l0 l l-l l O l 215J l/l lo 11 l [T_j
[-j l 0l sy 22 2J 24 26 27 28 23 30 31 32 7
N A ON C P NT TET WOURS 22 S8 ITT POR B.
SUPPLIE MAN FACTUREA l A lgl34Fl@
l Z lg lZ-l@
l0l0l0l0l lYl g lY [g
{ g lT l0 13 l5 l@
33 05
.6.
37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilOi ] The~ crack indications are attributed to probable metallurgical failure caused by l
1i li l l Intergrannular stress corrosion. The elbows and short sections of pipe will be l
g.l replaced with, carbon steel rather than the' original. stainless steel prior to unit
[
ii l3 l startup.'
l U,L,j l l
7 3 9 80 ST S
- &*CWER OTHER STATUS IS O RY OISCOVERY CESCRIPTION li 15 I l Z l@ - l 0 l 0 l0 lgl NA l
lC[gl Special Inspection l
COSTENT ACTivcv 11 13 ] l Zl g lZ lgl AuOusT OP ACriviTv @ l LOCATicN OP RELEASE @
RELE ASEC OP RELE ASE HA l
NA l
7 4 3 to 11 44 45 PERSONNEL EXPOSURES 40 NUP.'B E R TYPE @l DESCRI' TION
~ l i l 71 1 O! 01 O l@l e
l I
' ' PERSONNEL ~uLS DESCRIPTION @
Nu.mER y l0l0l0l@l NA l
7 1 ?
11 17 80 LOSS 08 OR OAMACE TO PACILITv I
p g
hPE DESCRl8 TION -
)
j l ' l 3 l l Z lgl NA ~
.i g
U l
i 4,
m m
30
.S$
E3CmPTION i: soil _f81 NA lllllllli; ;,jj 7
$ 3
?C 63' 69
.C.:
. AVE CF #REPAbit Daryl G Clark 309-654-2241. ext. 170 80 3
?HC*:E:
1.
LER NUMBER: 80-25/01T-0 11.
LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station Ill.
FACILITY NAME: Unit One IV.
DOCKET NUMBER: 050-254 V.
EVENT DESCRIPTION
On August 31, 1980, Unit One was shutdown for the end of cycle five refueling outage. As was comnitted to the NRC in LER/R0 80-06/01T-0, 100 percent of the core spray piping located inside the primary con-tainment was ultrasonic tested. The ultrasonic inspection disclosed several linear indications in three welds of "A" core spray loop and two welds of "B" core spray loop. The indications were located in the pipe-to-elbow and elbow-to-elbow welds between the reactor vessel penetration and the first manual isolation valve in both loops in the drywell. The inspection was performed by a contracted inspection firm under the direct supervision of the Commonwealth Edison Company SNT-TC-1A Level 111 Examiner.
VI.
P,ROBABLE CONSEQUENCES OF THE OCCURRENCE:
Although three of the crack indications had propagated through the pipe wall, a leak o' significant size during reactor operation would have been detected by the routine monitoring of the containment sump levels and by the routine containment atmospheric monitoring program. The core spray piping which is included in the primary coolant system boundary is inspected as part of the station inservice inspection program.
Several special inspections have also been performed, consisting of the inspec-tions required in R0 Bulletin 75-01, and an augmented inspection recom-l mended in General Electric Service Information Letter #117 The results
}
of the inservice inspection and the special inspections had been j
satisfactory.
Vll. CAUSE:
The cause of the occurrence has been attributed to a probable metallur-gical failure.
Results of laboratory analysis of core spray piping that was removed f rom Quad-Cities Unit Two in the si ring of 1980 indicated that intergrannular stress corrosion crat. ng was evident, and was found to be the cause of the cracking indications.
It is reasonable to ascertain that stress corrosion cracking is the failure mode in the Unit One core spray piping also. All of the linear indications were located in the welds and heat-affected zone of the elbows. The section of piping where the indications were found is a normally stagnant line which is exposed to reactor operating pressure and elevated coolant temperatures.
The core spray oiping is type A-312, grade TP 304,10 inch, schedule 80 seamless stainless steel pipe.
The elbows are type A403, grade WP 403, 10 inch, schedule 80, seamless stainless steel elbows.
o Vllt. CORRECTIVE ACTION:
The 105 elbows will be cut out of both core spray loops as well as a short section of pipe on each end of the elbows. The elbows will be stored at the station pending future investigations. The elbows and short sections of pipe will be replaced with carbon steel piping.
Replacing the stainless steel with carbon steel piping should eliminate the probability of stress corrosion cracking in this section of the piping.
The replacement carbon steel pipe is Type SA-333, grade 6, schedule 80 seamless pipe. The fittings are Type SA-420, grade WPL-6, schedule 80 seamless elbows. The repair work will be performed under the requi re-ments of ASME Boller and Pressure Vessel Code Section XI.
The repair parts have been procured in accordance with ASME Boiler and Pressure
. Vessel Code, Section ill, Class 1.
Non-destructive testing following the repair will include 100 percent examination by radiography, magnetic partici?. or dye penetrant test of all areas adjacent to the repair welds, and 100 percent examination of the repair weld with ultra-sonics to be used as a baseline for future inspections.
Prior to reactor startup, the core spray lines will be pressure tested during the reactor vessel pressure test.
A re-inspection of the welds for both core spray loops in the drywell will be performed during the next Unit One Refueling Outage.
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000265/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001-03, /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | | | 05000254/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000254/LER-1980-002-03, /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | | | 05000265/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000265/LER-1980-002-03, /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | | | 05000265/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000265/LER-1980-003-03, /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | | | 05000254/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000254/LER-1980-003-03, /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | | | 05000254/LER-1980-004-03, /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | | | 05000254/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004-03, /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | | | 05000265/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000265/LER-1980-005-03, /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | | | 05000254/LER-1980-005-03, /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | | | 05000254/LER-1980-006-03, /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | | | 05000254/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000265/LER-1980-006-01, /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | | | 05000265/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000254/LER-1980-007-03, /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | | | 05000254/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000265/LER-1980-007-03, /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | | | 05000265/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000254/LER-1980-008-03, /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | | | 05000265/LER-1980-008-03, /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | | | 05000265/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000254/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000265/LER-1980-009-03, /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | | | 05000265/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-009-03, /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | | | 05000254/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-010-03, /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | | | 05000254/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-010-03, /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | | | 05000265/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-011-03, /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | | | 05000265/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-011-03, /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | | | 05000254/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000265/LER-1980-012-03, /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | | | 05000254/LER-1980-012-03, /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | | | 05000265/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000254/LER-1980-013-03, /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | | | 05000265/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000254/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000265/LER-1980-013-03, /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | |
|