ML19344E101

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LER 80-023/04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades
ML19344E101
Person / Time
Site: Cooper Entergy icon.png
Issue date: 07/22/1980
From: Borer P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E093 List:
References
LER-80-023-04T, LER-80-23-4T, NUDOCS 8008260630
Download: ML19344E101 (1)


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