05000298/LER-1980-025-04, /04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased

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/04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased
ML19344E100
Person / Time
Site: Cooper Entergy icon.png
Issue date: 07/25/1980
From: Borer P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E097 List:
References
LER-80-025-04T, LER-80-25-4T, NUDOCS 8008260629
Download: ML19344E100 (1)


LER-1980-025, /04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased
Event date:
Report date:
2981980025R04 - NRC Website

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