ML19344E100

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LER 80-025/04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased
ML19344E100
Person / Time
Site: Cooper Entergy icon.png
Issue date: 07/25/1980
From: Borer P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E097 List:
References
LER-80-025-04T, LER-80-25-4T, NUDOCS 8008260629
Download: ML19344E100 (1)


Text

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LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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7 8 DATE EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h IO l2l During normal operation, condenser cooling water outlet temperature limit of l Io131 4030 F was exceeded. No effect on public health and safety. During the event an l l o 14 I bmergency need for power existed and the limit was exceeded in accordance with I l o 151 bur Technical Specifications. I I

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