ML19344E086

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LER 80-021/03L-0:on 800622,while Performing Routine Surveillance Test procedure,6.3.9.4,MSIV-86A Was Found to Have Closing Time Faster than Tech Spec Allowance.Caused by Setting MSIV-86A Too Close to Fast Limit During Shutdown
ML19344E086
Person / Time
Site: Cooper Entergy icon.png
Issue date: 07/22/1980
From: Mayer D
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E079 List:
References
LER-80-021-03L, LER-80-21-3L, NUDOCS 8008260602
Download: ML19344E086 (1)


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OATE 80 7 8 60 61 DOCK ET NUMB ER EVENT OATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h F6T21 [Ihe reactor was operating at 48% rated thermal power. While performing routine sur- l 10 l a l Iveillance test procedure 6.3.9.4, MSIV-86A was found to have a closing time faster l lo l4 l Ithan allowed by T.S. 3.7.D. Seven of the eight MSIV's were within the Tech. Spec. I i o I ., I ilimits so this occurrence presented no adverse consequences from the standpoint of l l o is 1 !public health and safety. l 101711 I I

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43 44 47 CAUSE DESCRIPTION AND CCRRECTIVE ACTIONS l i 1 o i lhormal steam flow and pressure aid in closing the MSIV's. MSIV-86A was set too closel m lto fast limit during shutdown. Immediate corrective action was to adjust closing i g l time for MSIV-86A. Other corrective action was to add closing limit to S.P. 6.3.9.4 l l,i3i lfor shutdown condition. The valve is an air operated Rockwell Edwards 24" angle  ;

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  1. 4 'J 10 Dennis Mayer 402-825-3811 o NAME F PREPARER PHONE: ,

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