05000298/LER-1980-019-01, /01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction

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/01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction
ML19344E065
Person / Time
Site: Cooper 
Issue date: 07/17/1980
From: Borer P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E061 List:
References
LER-80-019-01T, LER-80-19-1T, NUDOCS 8008260575
Download: ML19344E065 (1)


LER-1980-019, /01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction
Event date:
Report date:
2981980019R01 - NRC Website

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