05000298/LER-1980-018-03, /03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error

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/03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error
ML19344B334
Person / Time
Site: Cooper Entergy icon.png
Issue date: 07/17/1980
From: Lawrence L
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344B332 List:
References
LER-80-018-03L, LER-80-18-3L, NUDOCS 8008260633
Download: ML19344B334 (1)


LER-1980-018, /03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error
Event date:
Report date:
2981980018R03 - NRC Website

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