05000317/LER-1980-058-03, /03L-0:on 801112,found 4 Kv Bus 11 Normal Break Feeder (152-1115) Opened & 120-volt Ac Vital Bus 11 Voltage Went Low.Cause Undetermined.Diesel Generator 11 re-energized 4 Kv Bus

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/03L-0:on 801112,found 4 Kv Bus 11 Normal Break Feeder (152-1115) Opened & 120-volt Ac Vital Bus 11 Voltage Went Low.Cause Undetermined.Diesel Generator 11 re-energized 4 Kv Bus
ML19343B248
Person / Time
Site: Calvert Cliffs 
Issue date: 12/12/1980
From: Davis S, Rizzo P
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343B247 List:
References
LER-80-058-03L-01, LER-80-58-3L-1, NUDOCS 8012160394
Download: ML19343B248 (1)


LER-1980-058, /03L-0:on 801112,found 4 Kv Bus 11 Normal Break Feeder (152-1115) Opened & 120-volt Ac Vital Bus 11 Voltage Went Low.Cause Undetermined.Diesel Generator 11 re-energized 4 Kv Bus
Event date:
Report date:
3171980058R03 - NRC Website

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69 EV ENT QATE 74 75 REPORT OATE 80 EVENT oESCRIPTioN ANo pro 8ABLE CONSEQUENCES h t o 121 i At 2255 durine coerations,114 KV bus normal feed breaker (152-1115)

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11 diesel cenerator started autcmatically and re-enernized 11 4KV l

io,sil bus restorina normal voltaces. Durina the ensuinc voltace transient i

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