05000348/LER-1980-080-03, /03L-0:on 801225,w/pressure Vessel Head Removed for Refueling,Operating B Train RHR Became Inoperable When Loop Suction Valve Closed.Caused by Signal from Pressure Transmitter Loop.Valve Reopened

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/03L-0:on 801225,w/pressure Vessel Head Removed for Refueling,Operating B Train RHR Became Inoperable When Loop Suction Valve Closed.Caused by Signal from Pressure Transmitter Loop.Valve Reopened
ML19341B675
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 01/28/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19341B674 List:
References
LER-80-080-03L, LER-80-80-3L, NUDOCS 8102030618
Download: ML19341B675 (1)


LER-1980-080, /03L-0:on 801225,w/pressure Vessel Head Removed for Refueling,Operating B Train RHR Became Inoperable When Loop Suction Valve Closed.Caused by Signal from Pressure Transmitter Loop.Valve Reopened
Event date:
Report date:
3481980080R03 - NRC Website

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60 Si ooCEET NUMB ER 68 69 EVENT oATC 74 75 RE70RToATE 80 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h

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i Io 121 l At 2350 on 12/25/80, with the pressure vessel head removed for refueling, the loop l

ro T31 I suction valve for B train RHR closed which resulted in the operating 3 train RHR be-l 6

l coming ino,erable. Tech. Spec. 3.9.8 requires at least one RHR loop to be in operationj g l Tech. Spec. 3.9.8 action statement requirements were met.

Health / safety of the public g l were not affected by this occurrence.

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The looo was being de-terminated from its electrical penetr:ition whild L' 1.2_j l energized in order to repair the penetration when the instrument leads were inadver-l

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The valve was reopened and RHR pump - l gl 1B was returned to service at 2355 on 12/25/80.

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