05000298/LER-1980-035-03, /03L-0:on 800917,during Surveillance Testing, Gasket in Oil Supply to HPCI Stop Valve Actuator Failed, Causing Shutdown of HPCI Sys.Caused by Gasket of Improper Matl Being Used.Gasket Replaced W/Gasket of Proper Matl

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/03L-0:on 800917,during Surveillance Testing, Gasket in Oil Supply to HPCI Stop Valve Actuator Failed, Causing Shutdown of HPCI Sys.Caused by Gasket of Improper Matl Being Used.Gasket Replaced W/Gasket of Proper Matl
ML19340B205
Person / Time
Site: Cooper Entergy icon.png
Issue date: 10/01/1980
From: Flannigan R
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19340B203 List:
References
LER-80-035-03L, LER-80-35-3L, NUDOCS 8010210649
Download: ML19340B205 (1)


LER-1980-035, /03L-0:on 800917,during Surveillance Testing, Gasket in Oil Supply to HPCI Stop Valve Actuator Failed, Causing Shutdown of HPCI Sys.Caused by Gasket of Improper Matl Being Used.Gasket Replaced W/Gasket of Proper Matl
Event date:
Report date:
2981980035R03 - NRC Website

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1o12l l During routine surveillance testing a gasket in the oil supply to the HPCI stop I

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